IR 05000413/1987038

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Insp Repts 50-413/87-38 & 50-414/87-38 on 871102-06.No Violations or Deviations Noted.Major Areas Inspected: Inservice Insp Maint Program Implementation,Maint/Mod Welding & NDE & Action on Previous Enforcement Matters
ML20236U064
Person / Time
Site: Catawba  Duke Energy icon.png
Issue date: 11/24/1987
From: Blake J, Crowley B, Newsome R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20236U050 List:
References
50-413-87-38, 50-414-87-38, IEB-87-001, IEB-87-1, IEIN-87-036, IEIN-87-36, NUDOCS 8712020258
Download: ML20236U064 (20)


Text

{{#Wiki_filter:_ _ _ _ _ _ _ _ _ _ _ _ _ UNITED STATES 8 RE00 [5

'o NUCLEAR REGULATORY COMMISSsON [ E REGION 88 - o $ j 101 MARIETTA STREET,W.W.

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  • 's ATLANTA, GEORGift 760373 :

\\...../ s ' \\ , Report Nos.: 50-413/87-38 and 50-414/87-38 Licensee: Duke Power Company 422 South Church Street a Charlotte, NC 28242 Docket Nos.: 50-413 and 50-414 License Nos.: NPF-35 and NPF-52 Facility Name: Catawba 1 and 2 Inspection Conducted: November 2-6, 1987 - Inspectors: M[[ ///i'!PJ

- [^R. Crowley' p Date Signed S* s< L1en-" ll-23 -67 ' _ . W.

<ew o Date Si ned Approved by: ~ // /1 87 J/ J.

Ihke, Section Chief Date Signed fat ials and Processes Section

sion of Reactor Safety SUMMARY Scope: This routine, unannounced inspection was in the areas of inservice inspection (ISI) (Units 1 and 2), maintenance program implementation (Units 1 and 2), maintenance / modification welding and NDE (Unit 1), licensee action on previous enforcement matters (Unit 2), IEB 87-01 (Units 1 and 2), NRC Information Notice 87-36 (Units 1 and 2) and inspector follt;wup items (Units 1 and 2).

( ( i r ' Results: No violations or deviations wcre identified.

'

, 8712O20258 B71124 PDR ADOCK 05000413 G PDR l

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Persons Cantacted

a

. H Licensee Employees v

  • R. F. Yarde11, Superintendent. o( Technical Services
  • J. O. Barbour, QA Manager - Orbrations
  • B. F. Caldwell, Station Servic6 Superintendent
  • T. M. Hilderbrand, QA Sapervisort j

' R G. B. Robinson, Supervising Q1 Engineer - QA Technical ;5upport ' C. M. Sahma, Test Supervisor - Performance '

  • W.. L.. Anfin, Jr.,\\ Mechanical Maintenance Support

" J. A. Kammer, Test Engineer - Unit 2 - Performance, T. G. Self, Station Instructor - Mechanicel Maintenance G. G. Barrett, Training Supervisor . J. B. Beckman, Maintenance Engineer ' J. E. Reeves, Mechanical Maintenance - Production Specialist

  • J. E. Cherry, QA Specialist - ISI

,( ' R.C.Giles,ISICoordjnator-ISI H. D. Mason, QA Engineer.- Technicdl Support - Mechanical T. W. Huffstickler, Welding Engineering Technical - CMD M. A. Cote', Compliance Specialist, QA/QC Personnel Other licensee employees contacted inc'luded QA/QC personnel, construction craftsmen, engineers, secirity forc( membe7, and office personnel.

\\ NRC Resident Inspectors i ' P. K. Van Doorn, Senior Resident Inspector M. Lesser,ResidentIns/stor .

  • Attended exit intervie d

\\ 4' a, 2.

Exit Intervitu; , , The inspection scope hnd firidings were summarized on November 6,1987, 'p with those persons Adicated in paragraph I above.

The inspectors , - described tne areg/ lespected and discussed in detail the inspection r ,d', findings.

No dissenting comments were received from the licensee.

The d licensee dio not identify as proprietary any of the materials provided to or reviewed by the inspectors during this inspection.

3.

Licensee Action on Previous Enforcement Matters (92702)(Unit 2) (Closed) Violation 414/87-04-01, Failure of Installed Equipment to Meet Drawings and Procedures.

Duke Power Company's (DPC) letter of response dated April 8,1987 has been reviewed and determined to be acceptable by . / Region II (RII).

Based on examination of corrective actions as stated in d

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ J

. - _ _.__ ,

j l l the letter of response 'and discussions with responsible licensee l personnel, the inspector concluded that DPC had determined the full extent ! of the subject violation, performed the necessary survey and follow-up i actions to correct the present conditions and developed the necessary L corrective actions to preclude recurrence of similar circumstances.

The j l corrective actions identified in the letter of response have been i implemented.

The ins L Condensate Drain Tank'pectors verified by visual observation that the Support nuts had been tightened.

4.

Unresolved Items Unresolved Items were not discussed during this ir.spection.

5.

Maintenance Program Implementation (62700) (Units 1 and 2) The ir roectors examined the licensee's maintenance program as detailed below w determine whether the program was being implemented in accordance Wu %ulatory requirements.

Requirements are specified in various Regulatory Guides, Section 6 of the Technical Specifications, and ANSI N18,7-1976.

Based on interviews with plant personnel, the two representative maintenance activities identified in paragraphs a. and b. below were selected for review.

Records associated with the two maintenance activities were reviewed to determire whether: Cause of failure was evaluated and adequate corrective action was - taken to reduce probability of recurrence.

Procedure specified in maintenance package is adequate for scope of - maintenance performance Vendor technical manual for equipment under repair is controlled and - kept up-to-date Vendor maintenance recommendations are translated or referenced by - maintenance procedures Limiting conditions for operation is met while equipment removed from - service Approved procedures were used where activity appeared to exceed - normal skills of qualified maintenance personnel Inspections made in accordance with licensee's requirements and - quality control record are complete ' Functional testing and calibrations, as necessary, were completed - before returning equipment to service and personal performing tests properly qualified i L_________

_____ _ _ _

.

Failures are evaluated and reported in accordance with requirements - Corrective and preventative maintenance records are assembled and - stored as part of maintenance history Measuring and test equipment used was identified and in calibration - Parts and materials used were identified and at least met - specifications of the original equipment Special processes were controlled and documented - System lineups were made and verified prior to return to service - Machinery history records are being kept up to date and properly - stored a.

Letdown Heat Exchanger (Unit 1)

! In June 1986, a tube leak occurred in the letdown heat exchanger.

In March 1987, a tube ru The following records associated with repair (tube plugging) ptured.

to the heat exchanger, were reviewed: Maintenance Request (MR) 21452 OPS dated June 2, 1986 - , - Maintenance Request 25020 OPS dated July 3,1987 A sample of completed maintenance procedures for the above MRs - Qualification / training records for three of the maintenance - personnel involved in repair to the heat exchanger Qualification records for three QC personnel involved with - inspection of repair work on the heat exchanger Welding records for plugging tubes, as follows: - MR 25020 OPS Weld Process Control Sheets Pass 3 - - R10-T4, 6-R10-T2, 6-R10-T1, 4-R10-T3, 5-R10-T1, and 5-R10-T2 Welding Procedure L-231-17 - Welder Qualification rec,rds for welder - H21 Material Certification records for - Ht. 464177 of 3/32" ER308 Inspector Certification records for - j inspector HEE l t

_ _ _ _ _ - - _. ~ .

  • MR 21452 OPS

- Weld Process Control sheets INV-HX-10-4 and INV-HX-8-9 Welder Qualification records for - welders J46 and OJ4 - Inspector Certification records for inspector RDB ' Welding Procedure L231-R16 - Calibration records for torque wrenches CNMNT-18133,18051 and - 18046 Vendor Technical Manual CNM-1201-06-083, updated June 4, 1984, - " Auxiliary Heat Exchangers" Station Preblem Report CNPR02722 - Problem Investigation Report 1-C87-0180 -

NSM CN-11091 - Licensee's internal correspondence describing problem and - proposing fix Based on the licensee's investigation, the tube failures were attributed to vibration.

During the current outage, the licensee was in the process of changing out the tube bundle and replacing with a modified design.

The same modification is planned for Unit 2.

b.

Centrifugal Charging Pump Seal (Units 1 and 2) Leaking seals on the centrifugal charging pumps has been a recurring problem.

The following records associated with replacement of pump seals were reviewed.

MR 508809S (Unit 1 Pump 1A) dated 5/27/83 - MR 46870PS (Unit 1 Pump 1A) dated 4/17/83 - MR 86780PS (Unit 1 Pump 1A) dated 3/22/84 - MR 330220PS (Unit 2 Pump 28) dated 3/6/86 - MR 362460PS (Units 2 Pump 28) dated 3/31/87 - A sample of completed maintenance procedures for the above MRs - Qualification / training records for six of the maintenance - personnel involved in change out of the seals _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ - -

- _ - _______-_

( . D Qualification records for eight QC personnel involved with - inspection of seal change out Calibration records for torque wrenches CNMT-18064,, 18049, - l 18059, and 18138 and dial indicator CNMT-18652 - Vender Technical Manuals CNM-1201.05-203-001 updated 7/20/87-493-001 updated 5/20/86 and -0025-001 updated 7/22/87 Completed performance tests PT/2/A/4200/07B dated 4/24/86 and - 4/3/87 Qualification / training records for the two test technicians in - charge of the above two performance tests - Calibration records for the following instruments used in the above performance tests: CNPRF 20401 OP Cell CNPRF 20277 Pressure gauge CNPRF 20301 Pressure gauge CNPRF 20604 Vibration Instrument CNPRF 20020 Pyrometer The licensee has been studying the seal failures to try to determine the reason for the failures.

At this time, it appears that vibration may be a factor.

c.

The following maintenance procadures associated with the maintenance activities of paragraph a. above were reviewed: MP/0/A/7650/56 Heat Exchanger Corrective Maintenance - MP/0/A/7650/01, Flange Gasket Removal and Replacement - The procedures were reviewed in the areas of: Conformance to licensee's administrative requirements - - Post-maintenance testing appropriate for repairs made Inspection and hold points identified - Supplementary reference material adequate and controlled j - - Activity described in sufficient detail Consideration given to radiological and environmental hazards as - appropriate - Provisions for fire protectin., cleanliness and housekeeping

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-. _ - _ _ _

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i - Provisions for obtaining approval for operations Within the areas inspected, no violations or deviations were identified.

6.

Maintenance / Modification Welding and NDE (Unit 1) The inspectors examined the welding and NDE activities described below relative to maintenance / modification to determine whether applicable code and regulatory requirements were being met.

In general, the governing code is the ASME Boiler and Pressure Vessel Code (B&PV), Section XI, 1980 Edition, W81 Addenda. The general controls are specified in the following sections of the Catawba Nuclear Station Maintenance Welding Manual: Section I, Revision 6, Identification and Control of Class A, B, C, E and F Piping Section III, Revision 4, Welding of Nuclear Structure (Containment and Canal Liner Plate, Structural and Miscellaneous QA Condition Steel) and Non-QA Structures Section I identifies the ASME B&PV Code Section III,1974 Edition, S74 Addenda as the applicable code for pipe welding.

In addition, various editions and addenda of the following codes are being used: ASME B&PV Code Section V ASME B&PV Code Section IX AWS Structural Welding Code D1,1 In addition to the abcve documents, the following administrative and QC inspection procedures are applicable: QCL-8, Revision 12, Procedure for the Inspection of QA Condition 2, 3, and 4 Field Fabricated Pipe Welds QCL-9, Revision 4, Procedure for the Inspection of Containment Plate, and Spent Fuel Pool Liner Plate (McGuire and Catawba Nuclear Stations only) t QCL-10, Revision 9, Procedure for the Examination of Structural and Miscellaneous Steel Welds QCL-11, Revision 4, Procedure for the Inspection of Temporary Attachment Welds MM Procedure 1.0, Revision 20 Work Request Preparation _ ____ ______

_-__

l .

a.

Welding (55050 and 55100) (1) -Welder Performance Qualification The inspectors reviewed tr.a qualification status records for the below listed welders relative to the field welds listed in paragraph (2) below: 8A1 H37 549 H95 P64 (2) Production Welding I (a) The inspectors observed in process welding and reviewed in process records for welds 17 and 18 on ISO 1CA-123 and repair weld 27 on ISO ICA-90.

The welding was observed and the records reviewed to determine whether: Work was conducted in accordance with a document which - coordinates and sequences operations, references, procedures, establishes hold points, and provides for production and inspection approval Weld identification and location were as specified - Procedures, drawings, and other instructions were at - the work station and readily available WPS assignment was in accordance with applicable code - requirements Welding technique and sequence were specified and - adhered to Welding filler materials were the specified type and I - traceable to certifications ' Weld joint geometry was in accordance with applicable - procedure and was inspected Alignment of parts was as specified - Preheat and interpass temperature were in accordance - with procedures Electrodes were used in positions and with electrical - characteristics specified Shielding gas was in accordance with the welding - procedure _ _ - _ _ _ _ - _ _ _ _

- _ _ _ _ _ _ _ _

..

Weldir] equipment was in good condition - Interpass cleaning was in accordance with applicable - procedures Temporary attachments were removed in accordance with - applicable procedures Gas purging, if specified, was used in accordance with - applicable procedu.'es Process control system had provisions for repairs - Welders were qualified - No peening performea on root and surface layers - Weld inspection pers: nel were qualified - (b) Completed welds 1, 2, , and 4 on ISO INC286 were examined . to verify by visual inspection that the characteristics listed below ccnformed to ASME Code and applicable procedures.

These welds are Class A welds.

Weld surface finish and appearance - Transition between components of different diameter , - and thicknesses

Shape and size of fillet and socket welds - Weld reinforcement - Removal of temporary attachments, arc strikes and wald - spatter Fit,ish grinding - absence of wall thinning - Absence of surface defects - In addition, the completed weld process control sheets for the welds were reviewed.

(3) Welding Mateiial Control l The inspectors verified that required ASME Code tests were performed on each lot of welding material by reviewing the receiving inspection and material certification documentation for the following materials used in the wclds identified in paragraph (2) above: .035" [R308 - Ht. X4311T308 5/32" Insert - Ht. E4252T308 l ____-_ _ -__ _ _ _ _ - - - _ _ _ _ -

_ _ - - - _ - ' .

1/8" E705-2 - Ht. 97403 . (4) Inspection Personnel Certifications

Inspection personnel certification records for the following examiners who inspected the welds listed in paragraph (2) above,- were reviewed: BC - Welding, VT, PT RDB - PT, VT, Welding HEE - Welding CEF - Welding b.

Upper Head Injection Piping Deletion Radiography Unit 1 (57090) Radiography activities associated with the welds generated by the deletion of. piping in the upper head injection system were reviewed as documented below.

(1) The inspectors reviewed radiogryhy procedure NDE-10 Rev.16 " General Radiography Procedure, to determine whether it . contained sufficient. information to assure that the following - parameters - were specified. and controlled within the limits permitted by the applicable code, or any additional specification requirement: type of material to be radiographer; material and weld surface condition requirements;. type of radiation source, effective focal _ spot or effective source size;

film brand or type; number of films in cassette; minimum source - to film distance; type and thickness of intensifying screens and filters; quality of radiographs; film density and contrast for-single and composite viewing; use of densitometers for assuring compliance with film density requirements; system of radiograph identifications; use of location markers; methods of reducing and testing for back-scatter; selection of penetrameters including penetrometer placement; number of penetrameters; shims under penetrameters; radiographic technique of double wall viewing; and, evaluation and disposition of radiographs.

(2) The inspectors performed an independent evaluation of the below ) listed finally accepted welds to determine if radiographic film quality was in accordance with the applicable procedure and Code requirements and to specifically verify the following: penetrometer type, size, and placement; penetrometer sensitivity; film density and density variation; film identification; film quality; and weld coverage.

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Weld ID Drawing No.

Film View Evaluated INC286-3 CNM1201.01.424-001 0-1, 1-2, 2-3, 3-4, 4-5, 5-0 INC286-1 CNM1201.01.424-001 0-1, 1-2, 2-3, 3-4, 4-5, 5-0 1NC286-2 CNM1201.01.424-001 0-1, 1-2, 2-3, 3-4, 4-5, 5-0 (3) The inspectors reviewed the examination records for the above , listed welds to determine compliance with procedure requirements ! - for examination records and to determine if the reported I disposition of the welds was consistent with the independent evaluation and in compliance with the applicable Code and specification requirements.

The inspectors found no discrepancies.

(4) A review of qualification records for two radiographic examination personnel was accomplish to determine whether the qualification records reflect the employer's name, person certified, activity qualified to perform, level of qualification, effective period of qualification, effective period of certification, basis used for certification, and annual visual acuity.

j (5) The inspectors confirmed the calibration status for denistometer 1788.

(6) The inspectors reviewed the weld process control sheets for welds 1NC286-1, INC286-02, and INC6-3 to ascertain if the documents were complete and accurate.

Within the areas examined, no violations or deviations were identified.

7.

Inservice Inspection (ISI) and Preservice Inspection (PSI) The inspectors examined documents, activities, and records as indicated below to determine whether PSI /ISI was being conducted in accordance with applicable procedures, regulatory requirements and ifcensee commitments.

The applicable code for ISI is American Society of Mechanical Engineers ! Boiler and Pressure Vessel (ASME B&PV) Code, Section XI, 1980 edition with ! eddenda through Winter 1981.

Duke Power nondestructive examination (NDE) personnel are performing the liquid penetrant (PT), magnetic particle (MT), and visual (VT) examinations while Babcock and Wilcox (B&W) personnel are performing the ultrasonic (UT) and eddy current (ECT) examinations for Duke Power.

a.

Review of Procedures Units 1 and 2 (73052) (1) The inspectors reviewed the Duke Power (DP) and Babcock and Wilcox (B&W) procedures indicated below to determine whether the procedures were consistent with regulatory requirements and licensee commitments.

The procedures were also reviewed in the areas of procedure approval, requirements for qualification of ' L____-_ _ __

______ ___ __ _.. _ ~ .

NDE personnel, and compilation of required records; and if applicable, division of responsibility between the licensee and contractor personnel if contractor personnel are involved in the ISI effort.

Procedure ID Title i NDE-40 R8 Ultrasonic Examination Procedure and Technique A Techniques for Thickness Measurements, Lamination Detection, and Stud Location ISI-130 R23 Ultrasonic Examination of Vessel Welds and Nozzle Inside Radius Sections NDE-12 R5 General Radiography Procedure for Preservice and Inservice Inspection i i ISI-120 R25 Utrasonic Examination of Piping and Vessel Welds Joining Similar and Dissimilar Materials ISI-424 R10 Multifrequency Eddy Current Examination of.750-inch OD x.044-inch Wall RSG tubing for Detection of Tube Wear at Support Plate ISI-464 R4 Technical Procedure for the Evaluation of Eddy Current Data of Nuclear Grade Steam Generator Tubing for Wear Fretting 151-460 R14 Technical Procedure for the Evaluation of Eddy Current Data of Nuclear Grade Steam Generator Tubing All procedures listed above had been previously reviewed by NRC during previous outages.

During the current inspection, only changes to previously reviewed c3cuments were reviewed.

(2) The inspectors reviewed ultrason.'c procedures NDE-40, ISI-130, and 151-120 to ascertain whether they had been reviewed and approved in accordance with the licensee's established QA procedures.

The above procedures were reviewed for technical adequacy and conformance with ASME, Section V Article 5 and other license commitments / requirements in the below listed areas: type of apparatus used; extent of coverage of weldment; calibration requirements; search units; beam angles; DAC curves; reference level for monitoring discontinuities; method for demonstrating penetration; limits for evaluating and recording indications; recording significant indications; and, acceptance limits.

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-_ __. _ ___ . _ ' .-

1 (3) The inspectors reviewed eddy current procedures ISI-424, ! ISI-464, and 15I-460 for technical content relative to: j multichannel examination unit, multichannel examination i indication equipment is specified, examination sensitivity, l material permeability, method of examination, method of calibration and calibration sequence, and acceptance criteria.

.(4) The inspectors reviewed radiographic procedure NDE-12 to determine whether it contained sufficient information to assure that the following parameters were specified and controlled within the limits permitted by the applicable code, or any additional specification requirement: type of material to be radiographer; material and weld surface condition requirements; type of radiation source, effective focal spot or effective source size; film brand or type; number of films in cassette; minimum source to film. distance; type and thickness of intensifying screens and filters; quality of radiographs; film density and contrast for single and composite viewing; use of densitometers for assuring compliance with film density requirements; system of radiograph identification; use of location markers; methods of reducing and testing for back-scatter; selection of penetrameters including penetrometer placement; number of penetrameters; shims under penetrameters; radiographic technique for double wall viewing; and, evaluation and disposition of radiographs.

b.

Observation of Work and Work Activities Unit 1 (73753B) The inspectors observed work activities and reviewed certification ! records of aquipment, materials, and NDE personnel which had been and will be utilized during the required ISI/ PSI examinations during this outage.

The reviews conducted by the inspectors are documented below.

I (1) ExaminerQualification i The inspectors reviewed the qualification documentation for the below listed Duke Power (DP) and B&W examiners in the following areas: employer's name; person certified; activity qualified to perform; effective period of certification; signature of employer's designated representative; basis used for certification; and annual visual acuity, color vision examination and periodic decertification.

I

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m_--- _ _ _ _ _... _ _. _ _ _. _ _ _

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Method - Level l VT Company Examiner UT PT MT EC

2

4 DP TMB II - - - - - - - DP KLW II - - - - - - - DR GEH II - - - - - - - l OP WMM I - - - - - - - LP BW - - - - II II II - DP PS II - - - - - - - DP KD II - - - - - - - DP JKT II - - - - - - - DP TJW II II - - - - - - DP HLM II II - - - - - - DP MM - - - - - - II II B&W ACG IIA - - - - - - - B&W RJP II - - - - - - - B&W CBW IIA - - - - - - - B&W WJP II - - - - - - - B&W MJK IIA - - - - - - - (2) The inspectors observed calibration activities and the in process ultrasonic examinations being conducted on the welds indicated below.

The observations were compared with the applicable procedures and the Code in the following areas: availability of and compliance with approved Nondestructive Examination (NDE) procedure; use of knowledgeable NDE personnel; use of NDE personnel qualified to the proper level; type of apparatus used; extent of coverage of weldment; calibration requirements; search units; beam angles; DAC curves; reference level for monitoring discontinuities; method of demonstrating penetration; limits of evaluating and recording indications; recording significant indications; and, acceptance limits.

Item No.

Weld No.

' B01.021.002 1RPV-WO9 801.040.001 1RPV-WO8 805.010.009 1RPV-W51-01-SE B05.010.012 1RPV-W51-04-SE The following listed ultrasonic equipment and materials certification records were reviewed: Ultrasonic Instruments Manufacturer /Model Serial No.

T-K/SM-100 1344 KK/USK-7 5161

! ! ____

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.

The inspectors observed spectrum analysis being performed on ultrasonic transducers with serial numbers 184278 and M18416.

Ultrasonic Couplant Batch No. 8552 and 8558.

Ultrasonic Calibration Block 50360 (3) The inspectors conducted an ultrasonic verification examination using licensee equipment, on portions of weld 1RPV-WO9, The examination was performed in order to evaluate the technical adequacy of the ultrasonic examination procedure being used by the licensee's contractor to perform ultrasonic examinations and to assess the validity of the information being reported by the ultrasonic examiners.

(4) The inspectors reviewed the below listed liquid penetrant materials certification records to ascertain if the sulfur and halogen content of the material was within acceptable content limits.

Materials Batch Number Liquid Penetrant 78E084 Cleaner / Remover 86J005 Developer 83G033 (5) The inspectors reviewed documentation indicating that a current lift test had been performed on magnetic particle AC yoke CN026 and a review of magnetic particle material certification records for batch number 84K005 indicated the sulfur and halogen content of the material was within acceptable content limits.

(6) The inspectors observed the Eddy Current activities indicated , below.

The observations were compared with the applicable procedures and the Code in the following areas: method for maximum sensitivity is applied; method for determining material { permeability; method of examination has.been recorded; l examination equipment has been calibrated in accordance with the applicable performance reference; amplitude and phase has been calibrated with the proper applicable calibration reference and is recalibrates at predetermined frequency; required coverage of steam generator tubes occurs during the examination; acceptance criteria is specified or referenced.

(a) In process tube data acquisition was observed for the following system generator tubes: I ! , L____---_----------_---

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1 , i Tube I.D.

j Steam Generator-B Steam Generator-C Row Column Row Column

38

63

35

63 '

35

62

34

62

35

61

34

61

34

61' (b) In process eddy current (ET) inspection data evaluation including calibration checks were observed for the following steam generator (SG) tubes: SG - C Tube I.D.

SG - C Tube I.D.

T<ow Column Row Column

108

51

102

51

10-

52

27

54

29

50

17

44

16

43

43

30

45

73

49

73

72 SG - B Tube I.D.

Row Column

77 i Certification records for eddy current reference standard Z1579 was reviewed and eddy current equipment calibration was confirmed.

' (c) Discussions with B&W and licensee personnel indicated that , the current data and analysis procedure employed did not require that the data be evaluated by more than one analyst.

B&W indicated that their contract did not include provisions for them to have the examination data analyzed by more than one analyst and, therefore, no second analysis of the data was accomplished by them.

The inspectors pointed out to the licensee that although there is not a L - - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

-__ , ~ .

requirement to conduct a second evaluation of the data, that the economical consequences associated with a missed

leaking tube through the use of a single analyst could be very expensive.

The probability of this occurring is documented in IE Information Notice 84-49.

Further discussions with the licensee indicated that Duke Power was in the process of qualifying some of their personnel to perform eddy current data analysis and will be utilizing these examiners once the program is established.

The NRC inspectors indicated to the licensee, that unless these examiners were going to be re-evaluating 100% of the data, that it still would only amount to a sampling and that provisions for a second evaluation of all data should be l included as part of their eddy current examination program as this has become common practice through out most of the industry.

The inspectors strongly recommended that the in-house data analysis program be given high priority and that a second analysis of the examination data be accomplished commencing with the next required eddy current examinations, c.

ISI/ PSI Data Review and Evaluation, Unit 1 (73755)(73055) (1) Records of completed nondestructive examinations were selected

and reviewed to ascertain whether: the method (s), technique and extent of the examination complied with the ISI plan and applicable NDE procedure; findings were properly recorded and i evaluated by qualified personnel; programmatic deviations were recorded as required; personnel, instruments, calibration l blocks, and NDE materials (penetrants, couplants) were designated.

Records selected for this review are listed below.

. ISI/PST Item No.

Item / Weld I.D.

NDE Method B05.040.002A IPZR-W2SE PT B05.040.003A 1PZR-W3SE PT B06.180.001 1RCP-1A-F UT B07.060.005 1RCP-1A-H (12 Bolts) VT B07.070.020 IND-18 (8 studs) VT B08.020.002 1PZR-W10A MT B08.020.003 1PZR-V10B MT . B09.011.053A 1NC173.01 PT I B09.011.054A INC190.19 PT F1.01.635 RNV1489 VT F1.02.055 1RCA 1082 VT l F1.02.427 1RND0546 VT F1.03.397A 1RKC1093 VT F1.03.418 1RKC1017 VT l l E --

. _ _ _ _ L ' . ,

, ' (cont'd) ISI/ PSI Item No.

Item / Weld I.D.

NDE Method 805.010.009 1RPV-W51-01-SE UT B05.010.010 1RPV-W51-02-SE UT , 805.010.011 1RPV-W51-03-SE UT ' B05.010.012 1RPV-W51-04-S2 UT B09.011.068

  • 1NC286-01 UT B09.011.069
  • 1NC286-02 UT B09.011.C70
  • 1NC286-03 UT B09.011.071
  • INC286-04 UT l

801.040.001 1RPV-WO8 UT i 801.021.002 1RPV-WO9 UT

  • Denotes examinations for PSI purposes.

(2) Eddy Current Examination of Steam Generator Tubing (a) The inspectors reviewed records of the eddy current examinations indicated below.

The reviews were compared with the applicable procedures and the Code in the following areas: the multichannel eddy current examination equipment has been identified; material permeability has been recorded; method of examination has been recorded; and, results are consistent with acceptance criteria.

SG - B Tube I.D.

SG - C Tube I.D.

Row Column Row Column

4

34

9

53

20

64

29

50 l

34

54 .

57

61 (b) At the conclusion of the NRC inspection all examinations had not been completed.

The inspectors discussed the program and status with the licensee and the preliminary examination status for steam generators B and C are listed below.

Examination of steam generators A and D had not yet started.

SG-8 SG-C Tubes Scheduled 491 570 Tubes examined 389 474 Tubes with >20% TW indications

4 No violations or deviations were identified in this area of inspection.

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8.

IE Bulletin 87-10, Thinning of Pipe Walls in Nuclear Power Plants (Units 1 and 2) . The licensee has officially responded to the requirements of Bulletin 87-01; however, a final review of the response has not yet been completed within the NRC.

The inspectors conducted a review of documentation and.

data relative to the actions being generated as a result of this bulletin.

The inspectors also observed work being performed as a result of actions being taken by the licensee.

The documentation reviews and observations conducted by the inspectors are documented in the following subparagraphs.

a.

Plan Review

The inspectors reviewed the below listed documents relating to the inspection plan in the areas of: plan approval; general QA requirements; examination procedures; control of examinations and examination equipment; quality records, personnel qualifications; and, NDE records.

PT/0/8/4600/18 - Periodic Inspection of Piping Wall Thickness

Pipe Erosion Control Program Manual (second draft) b.

The inspectors reviewed Ultrasonic Procedure NDE-40 R8.

This procedure is being utilized to obtain the thickness readings required by the licensee inspection plan.

The procedure was reviewed in the areas of procedure approval, requirements for qualification of NDE , personnel, and compilation of raquired records, i c.

The inspectors observed approximately 400 thickness readings being taken on the items listed below.

The inspectors also reviewed certification records of equipment, materials, and NDE personnel being utilized during the examination of these items.

Test Location Drawing No.

CF-02 CN-1CF-41 CM-56 CN-1CM-37 < CM-4 CN-1CM-37 I d.

The inspectors conducted an independent verification on several of the thickness readings taken on the above test locations.

The verification readings were made following the completion of the ' examinations conducted by licensee personnel and with the use of the licensee's equipment, couplant, and calibration block.

The verification readings obtained were within an acceptable tolerance range although minor deviations were noted that could be attributed to transducer placement.

e.

The inspectors reviewed the thickness data and associated records for the Unit 1 test locations indicated below.

The data was reviewed to determine whether the reported thickness was consistent with the data __- -_______ ,

___.

" .

being obtained in the field.

The data was also reviewed to determine compliance with requirements for examination records.

Test Location System ICM10 Condensate ICM36 Condensate 15C14 Turbine Crossover ISC19 Turbine Crossover ICF05 Main Feedwater ICF14 Main Feedwater f.

Discussions with licensee personnel and a review of the complete dcta from Unit 1 indicate that no significant pipe wall thinning has occurred.

The scheduled examinations for Unit 2 have not yet started.

In this area of inspection, no violations or deviations were identified.

9.

NRC Information Notice 87-36, Significant Unexpected Erosion of Feedwater Lines (Units 1 and 2) IE Bulletin 87-01 requests written response from licensees concerning their programs for monitoring the thickness of pipe walls in high-energy single-phase and two-phase carbon steel piping systems.

As noted in paragraph 8 above, DPC has responded to the Bulletin and has an extensive inspection program.

Information Notice 87-36 notifies licensees that a l thinning problem has been identified ir feedwater piping inside the I containment.

Although the feedwater piping inside the containment is ir.cluded in the Catawba inspection program, the sample selected for the current Unit 1 outage did not include any inspection points inside the containment.

After discussion of the Information Notice with the licensee, site r,rsonnel stated that inspection points on feedwater piping inside the cor,ainment would be selected as soon as feasible probably for inspectir, during the next outage.

10.

Inspector ollowup Items (IFIs)(927018)(Units 1 and 2) (Close',IFI 413/86-34-01, 414/86-37-01, Clarification of Responsibilities , for T.aluation of ISI Results.

QA procedure QA-516 has been issued to

more clearly cover responsibilities for evaluation of ISI results.

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