IR 05000397/1993006

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Insp Repts 50-397/93-06 & 50-508/93-02 on 930216-0329. Violations Noted But Not Cited.Major Areas Inspected:Cr Operations,Licensee Action on Previous Insp Findings, Operational Safety Verification & Surveillance Program
ML17290A341
Person / Time
Site: Columbia, Satsop  
Issue date: 04/30/1993
From: Johnson P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML17290A339 List:
References
50-397-93-06, 50-397-93-6, 50-508-93-02, 50-508-93-2, NUDOCS 9305240046
Download: ML17290A341 (41)


Text

U.S.

NUCLEAR REGULATORY COMMISSION REGION V

Report Nos:

Docket Nos:

License Nos:

Licensee:

Facility Name:

Inspection at:

Inspection Conducted:

Inspectors:

50-397/93-06, 50-508/93-02 50-397, 50-508 NPF-21, CPPR-154 Washington Public Power Supply System P. 0.

Box 968 Richland, WA 99352 Washington Nuclear Project No.

(WNP-2)

Washington Nuclear Project No.

(WNP-3 WNP-2 site near Richland, Washington WNP-3 site near Elma, Washington I

February 16 March 29, 1993 (WNP-2)

February 24, 1993 (WNP-3)

R.

C. Barr, Senior Resident Inspector D. L. Proulx,'esident Inspector W. L. Johnson, Resident Intern J.

F. Melfi, Resident Inspector Approved by:

~Summa':

P.

H.

o nson, Chief Reacto Projects Section

Date Signed Ins ection on Februar 16 March

1993 Re ort No. 50-397 93-06 Ins ection on Februar

1993 Re ort No. 50-508 93-02 Areas Ins ected:

At WNP-2, a routine inspection by the resident inspectors of control room operations, licensee action on previous inspection findings, operational safety verification, surveillance program, maintenance program, licensee event reports, special inspection topics, and procedure adherence.

During this inspection, Inspection Procedures 61726, 62703, 71707, 71710, 90712, 92700, 92701, 92702 and 93702 were used.

At WNP-3, a routine inspection through the containment, control room, auxiliary building and warehouses and observation of the condition of the licensee's in-place and stored equipment (Paragraph 11).

The inspector used Inspection Procedure 92050 as guidance during the inspection.

Safet Issues Mana ement S stem SIMS Items:

None.

9305240046 930506 PDR ADOCK 05000397

PDR

Results WNP-2

General Conclusions and S ecific Findin s

Si nificant Safet Hatters:

None Summar of Violations and Deviations:

Ten examples of a previous violation were identified involving the fai lure to follow the procedure for tagging hoses containing radioactive material (Paragraph 5.b(6)).

One non-cited violation was also identified involving the failure to maintain a contaminated area barrier (Paragraph S.b(9)).

0 en Items Summar

Six followup items and three LERs were closed.

Five unresolved items were opened.

One non-cited violation was opened and closed during the inspection period.

Results WNP-3

Site inspection acti vities indicated that the WNP-3 site is being appropriately maintained (Paragraph ll).

DETAILS Persons Contacted WNP-2

  • V. Parrish, Assistant Managihg Director for Operations
  • J. Gearhart, Director, guality Assurance
  • J. Baker, Plant Manager G. Smith, Operations Division Manager L. Harrold, Maintenance Division Manager G. Sorensen, Regulatory Programs Manager
  • D. Pisarcik, Radiation Protection Hanager A. Hosier, Licensing Manager
  • S. Davison, guali ty Assurance Manager J. Peters, Administrative Hanager
  • H. Mann, Assistant Operations Manager
  • R. Webring, Technical Services Manager
  • D. Atkinson, Reactor Engi.neering Manager
  • T. Messersmith, Maintenance Support Hanager
  • J. Rhoads, Hanager, Operational Events Analysis and Resolution
  • J. Harmon, Maintenance
  • M. Davidson, Supply System Legal Department
  • C. Fies, Licensing Engineer
  • K. Pisarci k, Licensing Assistant
  • Attended the WNP-2 exit meeting on April 15, 1993.

WNP-3 Para ra h

QC. Butros, WNP 3/5 Site Manager QJ.

Cooper, Project Business Manager QS.

DeLoe, Acting Administration Manager QM. Deboard, Program Support Manager QW. Drinkard, guality Assurance Manager QJ.

Hayes, Warehouse Supervisor QL. Hill, Plant (Operations/Maintenance)

Manager QR. Harzano, Security and Safety Manager J. Perreault, Engineering Manager S. Ratcliff, I&C Supervisor QC. Reid, Preservation Engineering Manager QJ. Rett, Site Support. Services Manager D. Strassburger, Records and Document Control Supervisor QAttended the WNP-3 exit meeting on February 24," 1993.

The inspectors also interviewed various control room operators, shift supervisors and shift managers, maintenance, engineering, quality assurance, and management personne '.

Plant Status At the start of the inspection period, the plant was in Node 1 at 25~

power.

The plant achieved full power on February 20, 1993.

The reactor continued to operate at 100~

power, until the licensee declared the End-of-Cycle (EOC) recirculation pump trip (RPT) inoperable due to a missed surveillance.

After applying more conservative operating limits because the EOC RPT was inoperable, operators reduced reactor power to 99~.

On Narch 19, 1993, the licensee declared the reactor core isolation cooling (RCIC) system inoperable because a design review identified that a poten-tial accident scenario could result in excessive containment leakage.

The licensee received an NRC Notice of Enforcement Discretion since the RCIC system could not be restored to operability prior to the end of its 14-day Technical Specifications action statement.

The reactor continued to operate at 99~ power (except for momentary downpower maneuvers to support control rod exercises and bypass valve testing) until the end of the inspection period.

3.

Previousl Identified NRC Ins ection Items 92701 92702 The inspectors reviewed records, interviewed personnel, and inspected plant conditions relative to licensee actions on previously identified inspection findings:

a.

Closed Followu Item 397 91-39-02

Verification and Validation V&V not erformed for EOP-Referenced Procedures During the referenced inspection period, the inspector found that V&V had not been performed for several procedures called out by the Emergency Operating Procedures (EOPs).

The inspector was concerned that there may have been undetected errors in these procedures.

During development of the

"Phase II" EOPs, the licensee performed V&V of these procedures and approved appropriate deviations.

The inspector reviewed the licensee's documentation, and considered the actions and the records to be satisfactory.

This item is closed.

b.

Closed A

arent Violation 397 92-37-02

Desi n and 0 eration of Core not in Accordance with General Desi n Criteria GDC 12.

During followup inspection after the Augmented Inspection Team (AIT)

assessment of the August 15, 1992, power oscillation event, the inspector noted that the licensee's basic design and operation of the core did not. appear to adhere to GDC 12.

The inspector questioned whether operators could readily and reliably detect and suppress regional core power oscillations.

Further NRC evaluation and analysis of licensee procedures indicated that the licensee's procedures were adequate to detect and suppress this condition.

This item is closed.

C.

Closed A

arent Violation 397 92-37-03

Inade uate 50.59 Review for C cle 8 Core.

During followup inspection after the core power oscillation AIT of the August 15, 1992, power oscillation event, the inspector

questioned whether the licensee's safety evaluation per

CFR 50.59 was adequate, in that, it did not ',dentify the reduced margin to stability.

Further NRC evaluation of the licensee's methodology indicated that the

CFR 50.59 review was adequate despite this concern.

The Supply System used technical information and computer codes licensed for.use for the Cycle 8 core.

Therefore, the licensee did not violate

CFR 50.59.

This item is closed.

d.

Closed Part 21 Notification 397 92-004-P21 Im ro er Desi n of Anchor Darlin Motor 0 crated Valve MOV Yoke Clam s.

e.

The licensee submitted a

CFR Part 21 notification of potential defects in safety-related equipment concerning the improper design of Anchor/Darling MOV yoke clamps.

Three MOVs in the high pressure core spray system had undersized yoke clamps that could potentially fail, due to cyclic fatigue, during the valve's closure.

The licensee performed non-destructive examination (NDE) on each of

'hese valve's yoke clamps to determine if the valves were previously inoperable.

The licensee found no degradation of the valves, and determined that HPCS was previously operable, and that an LER was not required.

After performing the NDE, WNP-2 replaced the undersized yoke clamps with the proper size.

This item is closed.

Closed Part 21 Notification 397 92-005-P21 Limitor ue Model SMB-000 MOV Ca screws.

The licensee submitted a

CFR Part 21 notification of potential defects in safety-related equipment concerning the use of commercial-grade fasteners in Limitorque Model SMB-000 HOV capscrews.

The vendor had provided WNP-2 with seven Limitorque Model SMB-000 motor operators which had grade 1 or 2 capscrews instead of grade 5.

Licensee testing of the actual material properties of the capscrews indicated that they were acceptable for the applied loads.

This item is closed.

Closed Part 21 Notification 397 92-006-P21 Siemens Power Cor oration SPC Minimum Critical Power Ratio MCPR Calculations The licensee submitted a

CFR Part 21 notification of a poten-tially defective analysis provided by SPC.

SPC found that errors in the computer code for calculating HCPR during a loss of feedwater transient resulted in a non-conservative analysis late in the fuel cycle.

SPC corrected these errors and resubmitted the analysis.

No loss of feedwater events challenged the HCPR limit at WNP-2.

The inspector reviewed the second submittal with respect to the loss of feedwater transient and it appeared to be satisfactory.

This item

>s closed.

4.

Event Followu 93702 a ~

Reactor Core Isolation Coolin RCIC S stem Ino erabi lit On March 19, 1993, the licensee identified that if a small break loss of coolant accident (LOCA) were to occur simultaneously with a

ff

)t

loss of Division 1 direct current (DC) power, primary containment integrity through the RCIC system could be compromised.

For this scenario, the licensee assumed RCIC to be aligned to the suppression pool.

The loss of DC power, which causes DC motor-operated valves to fai 1 in the as-.is condition and the loss of the vacuum tank drain pump, results in a 5-10 gpm flow path through the RCIC suction valve, the lube oil cooling water supply valve, the barometric condenser, the vacuum tank, and vacuum tank relief valve.

Mith the loss of the vacuum tank drain pump, the static head of water from the suppression pool is sufficient to fill the vacuum tank and lift the relief valve.

Mater from the suppression pool would then flow from the relief valve to the equipment drain in secondary containment.

The licensee took compensatory action to prevent this flow path by opening the breaker that allows transfer of the RCIC suction from the condensate storage tank (CST) to the suppression pool.

Because the TS require the RCIC system to be capable of taking a suction from the suppression pool, the licensee declared the RCIC system inoperable.

At the end of the inspection period, the RCIC system was in the 13th day of the action statement.

Subsequently, the NRC issued a Notice of Enforcement Discretion to allow the licensee to continue to operate in this condition until the refueling outage.

Shortly thereafter, WNP-2 received a TS amendment that allowed operation until the upcoming refueling outage.

Among other items in the Noti'ce of Enforcement Discretion, the inspectors verified that the licensee completed the compensatory actions to which they had committed, and verified that no work was performed on the HPCS system.

In addition, the inspectors interviewed operators to confirm t$at the operators understood the reasons for RCIC inoperability, and the actions necessary in the unlikely event of a LOCA.

The licensee intends to submit an LER for this event.

Until the NRC revi ews the LER to determine if the root cause and effective corrective actions were identified, this is an

. unresolved item.

(Unresolved Item 397/93-06-01)

End-of-C cle EOC Recirculation Pum Tri RPT Ino erabilit On March 4, 1993, the licensee, found that the EOC RPT breakers had not been properly tested.

TS 4.3.4.2.3 requires that the RPT breakers be tested every 60 months to verify that the arc suppression time is less than or equal to 83 milliseconds.

Plant Procedures Hanual (PPN) 7.4.3.2.3.3A and PPN 7.4.3.2.3.3B perform this surveillance for the RPT 3-and 4-series breakers.

The tests are conducted by recording the amount of time between actuation of a trip coil in the breaker and the time when the breaker arc has been interrupted.

The procedures used to conduct these tests initiate the trip through actuation of a different trip coil (TC-1) than the trip coil which performs the safety function for the breaker (TC-2).

The licensee stated that if TC-1 and TC-2 have only slightly different characteristics the response time for the breaker would be inaccurate.

These inadequate response time tests existed for RPT breakers 3A, 3B, 4A, and 4 I(

'

Ce Subsequent to this discovery, the licensee declared both EOC-RPT systems inoperable.

The licensee's Core Operating Limits Report (COLR) requires operators to increase the limit for the Hinimum Critical Power Ratio (HCPR) if the EOC-RPT is inoperable.

The licensee inserted these new limits into the plant computer, which resulted in the licensee restricting operation of the plant to 99~

power.

The inspectors verified that the licensee took the proper actions, and that the correct limits were being used.

The licensee had not determined if the HCPR limits had been exceeded prior to discovery that the EOC-RPT had been inoperable.

The licensee intends to properly test the EOC RPT breakers during. the RB

'efueling outage.

Because the licensee had not yet determined through testing whether the EOC RPT could have performed its intended safety function, the inspectors will perform additional followup when the licensee submits their LER for this event, and after proper testing of the TC-2 coil.

This is an unresolved item.

(Unresolved Item 397/93-06-02)

Hain Turbine B

ass S stem Set oint Discre anc On Harch 4, 1993, the licensee found that the turbine bypass system setpoint that enables the system above 25~ power was set improperly.

The licensee had set the enabling relays based on 25~ of rated electrical power.

However, TS 3.7.9 states that the main turbine bypass system shall be operable when thermal power is greater than 25~ of rated thermal power.

At low power levels, plant efficiency is lower than at full power due to reduced feedwater heating.

Therefore, 25~ electrical power does not correlate well with 25~0 thermal power.

The licensee determined that the reactor produces 33~ thermal power when generator output is 25~ electrical power.

Therefore, the licensee determined that their design and setpoint violated the TS.

The licensee stated that the main turbine bypass system would be declared inoperable when reactor power is less than 35'hermal power.

- The action statement for this condition requires the reactor to be less than 25~ power within four hours.

Licensee management stated that they will reset the arming relays for the bypass system during the R8 refueling outage, and the new setpoint will conserva-tively correlate to 25~0 thermal power.

The licensee intends to submit an LER for this event.

Until the HRC reviews the LER to determine if the root causes and corrective actions have been iden-tifieded, this is an unresolved item.

(Unresolved Item 397/93-06-03)

No violations or deviations were identified.

5.

0 eratiooal Safet Veri ficati o~7r1707 a

~

Plant Tours The inspectors toured the following plant areas:

Reactor Building e

Control Room

Diesel Generator Building Radwaste Building Service Water Buildings Technical Support Center Turbine Generator Building Yard Area and Perimeter b.

The inspectors observed the following items during the tours:

0 eratin Lo s and Records.

The inspectors reviewed records against Technical Specification and administrative control procedure requirements.

(2)

(3)

Monitorin Instrumentation.

The inspectors observed process instruments for correlation between channels and for conform-ance with Technical Specification requirements.

~Ehif N

i

.

Tl i

p t b

d

d hfdf manning for conformance with 10 CFR 50.54(k), Technical Speci-fications, and administrative procedures.

The inspectors also observed the attentiveness of the operators in the execution of their duties and the control room was observed to be free of distractions such as non-work related radios and reading materials.

(4)

(5)

E ui ment Lineu s.

The inspectors verified valves and electrical breakers to be in the position or condition required by Technical Specifications and administrative procedures for the applicable plant mode.

This verification included routine control board indication reviews and conduct of partial system lineups.

Technical Specification limiting condi tions for operation were verified by direct observation.

E ui ment Ta in

.

Selected equipment, for which tagging requests had been initiated, was observed to verify that tags were in place and the equipment was in the condition specified.

General Plant E ui ment Conditions.

Plant equipment was observed for indications of system leakage, improper lubr ica-tion, or other conditions that would prevent the system from fulfillingits functional requirements.

Annunciators were observed to ascertain their status and operability.

During a tour of the Reactor Building on March 22, 1993, the inspector noted several instances in which the licensee did not appear to be following their procedure for the tagging of temporary hoses and electrical lines in the plant.

Paragraph 4.2. 11 of PPM 1.3. 19, "Plant Material Condition Inspection Program," requires that all rubber and tygon hoses used in the power block to route equipment drains, vents, leaks, pump from sump to sump, etc. shall be tagged with a

'Work in Progress'ag.

The tag shall show the procedure number for performing the vent or drain operation, or in cases of hoses used in conjunction with a Maintenance Work Request (MWR) or equipment

lj

deficiency identification, the MWR number or equipment deficiency tag number shall be used.

For hoses used to route leakage from leaking valves or other components to a drain or catch basin the equipment piece number (EPN) of the leaking equipment, the date the drain was installed, and the name of the individual authorizing installation of the drain will be recorded on the 'ta'g.

The number of the hose, if applicable,

.

will be recorded on the tag.

In addition, licensee management interpreted this procedure to also require tagging of temporary electrical cables.

During the tour, the inspector observed the following examples of personnel not following PPM 1.3. 19:

A tag attached to a hose in the 8 residual heat removal (RHR)

pump. room was missing a signature for the individual authorizing the hose installation.

A tag attached to a hose in the B reactor feedwater pump room was missing the signature for the individual authorizing the hose installation.

A tag attached to a hose in the auxiliary condensate pump room was missing a signature for the individual installing the hose, and for the person authorizing the hose installation.

A tag attached to a hose in RHR A pump room was missing the EPN, hose number, date, and signatures for installing and authorizing the hose.

A tag attached to a hose in the reactor core isolation cooling (RCIC)

pump room was missing the EPN, hose number, date, and signatures for installing and authorizing the hose.

A tag attached to a hose in the fuel pool cooling pump room was missing the EPN, hose number, date, and signatures for installing and authorizing the hose.

A hose connected to a drain on CMS-SR-13 was missing the Work in Progress tag.

On the 572-foot level of the reactor building, near the reactor building ventilation units, a tag attached to a hose going to a barrel

.was missing the EPN, hose number, date, and signatures for ".nstalling and authorizing the hose.

A tag attached to a hose coming out of the traversing incore probe (TIP) room was missing the EPN, the hose number, date, and signatures for installing and authorizing the hos H

,(

t f

~

A tag attached to a hose connected to a drain line from DW-V-100-60 was missing the procedure number, estimated completion date, and authorizing signatures.

In addition, the inspector found 6 instances in which temporary power cables were not tagged.

PPM 1.3. 19, Revision 13, was signed by the Plant, Manager on January 28, 1993, and issued on January 29, 1993.

This procedure was issued pursuant to a Supply System commitment in, their response to the Notice of. Violation (NOV) issued with NRC

Inspection Report

No. 50-397/92-35,

to establish

a hose control

program by February

1,

1993.

The procedure

had

been

approved.

by the Plant Operating

Committee

(POC) in December

1992,

and

.

placed

on administrative hold to allow time for personnel

training on the

new procedure

requirements.

However,

as noted

by licensee

management

in a subsequent

NOV response,

personnel

training and compliance verification by plant supervision

were

inadequate

for implementation of Revision

13 of PPM 1.3. 19.

During an

NRC inspection

conducted

on February

16 through

22,

1993 (refer to

NRC Inspection

Report

No. 50-397/93-07),

the

inspector identified a violation of PPM 1.3. 19, Revision

13,

involving four instances

of failure to properly tag hoses

containing radioactive liquids.

This was cited in a Notice of

Violation issued

on March 25,

1993.

On February

24,

1993, in response

to the NRC-identified

violation, line management

was directed to conduct walkdowns to

ensure

compliance with Revision

13 of PPM 1.3. 19.

On

February

26,

1993,

a procedure deviation

was approved in an

attempt to make it less restrictive.

On March 2,

1993,

gA

initiated

a Problem Evaluation

Request

(PER) to address their

findings that approximately ten percent of the hoses

in the

'lant were not properly tagged.

Licensee

management

stated that lack of effective supervision

in the plant was

a partial

cause of these

problems,

and that

more frequent plant tours

and work observation

would be

undertaken

to ensure that personnel

understood

and followed

PPM 1.3. 19.

However,

based

on the additional discrepancies

identified by the inspector

on March 22,. 1993,

as noted above,

it appeared 'that the licensee

had not taken effective steps

to

ensure

proper implementation of PPM 1.3. 19.

Because

the Notice of Violation for this violation was not

forwarded unti l March 25,

1993,

and

%ho licensee's

corrective

actions for the violation of PPM 1.3. 19 had not been in effect

for very long, these

occurrences

were not cited as

a new

violation.

However, the inspector

was concerned that these

new

examples

indicate that the actions for the previous violation

have not been effective in preventing recurrence

of this

problem.

The effective implementation of the corrective

if,

actions for this violation will be followed in a future

inspection

as

a review of Violation 50-397/93-07-01.

The inspector also noted that the licensee's

April 23,

1993;

response

to the Notice of Violation issued

on March 25,

1993,

included

an apparently incorrect statement.

Item 5 under

"Corrective Steps

Taken/ Results

Achieved" in Appendix A

incorrectly stated that

PER 293-318

was initiated on March 22,

1993, to address

PPM 1.3. 19 discrepancies

identified during

management

housekeeping

tours.

These discrepancies

were

actually identified by the

NRC inspector,,as

discussed

above.

This incorrect statement

was identified to licensee

management

in a telephone call

on May 4,

1993.

The licensee

committed to

provide by May 14,

1993,

a letter correcting

and explaining

this error.

The inspectors will determine during the next

inspection period whether this incorrect statement violated

NRC

requirements.

(Unresolved

Item 397/93-06-04)

Fire Protection.

The inspectors

observed fire fighting

equipment

and controls for conformance with administrative

procedures.

Plant Chemistr

.

The inspectors

reviewed chemical

analyses

and'rend

results for conformance with Technical Specifications

and

administrative control procedures.

Radiation Protection Controls.

The inspectors periodically

observed radiological protection practices

to determine

whether

the licensee's

program

was being implemented in conformance

with facility policies

and procedures

and in compliance with

regulatory requirements.

The inspectors

also observed

compliance with Radiation

Work Permits,

proper wearing of

protective

equipment

and personnel

monitoring devices,

and

personnel

frisking practices.

Radiation monitoring equipment

was frequently monitored to verify operability and adherence

to

calibration frequency.

On February

11,

1993, during the previous inspection period,

the inspector

found

a contamination

area

boundary sign and rope

down on the

422 foot level of the reactor building. 'everal

licensee

employees

were in the room at the time; however,

none

of these

employees

were aware that the boundary

was

down, or

had

been in the contaminated

area.

Section

3. 1.7.4.3 of the

WNP-2 Health Physics

Program Description states

that "an area

shall

be posted

as

a contaminated

area

when loose surface

contamination exists

above

100 dpm/100

cm~ alpha and/or

1000

dpm/100cm~

beta-gamma

as determined

by smear tests.

Posting of

such

an area shall include

a sign reading

CAUTION

CONTAMINATED

AREA."

TS 6.8. I.k requires

procedures

to be established,

implemented,

and maintained for the Health Physics/Chemistry

Support Program.

The failure to post

a contaminated

area is

a

violation of TS 6.8. 1 which requires

the licensee

to follow

health physics procedure,

I

-10-

(Io)

The licensee

conducted

an incident review board

and found that

personnel

error was the cause of the event.

Because

of this

event,

and previous instances

in which

HP boundaries

were not

restored

during personnel

passage,

HP supervision

toured the

plant and installed swing gates

in place of rope boundaries

to

preclude

any further instances

of roper boundaries

not being

restored.

In addition,

the licensee

employed assistance

from

INPO for additional

improvements in radiological postings.

Due to the low safety significance,

and because

the criteria of

Section VII.B(l) of the

NRC Enforcement Policy were satisfied,

this violation was not cited.

(NCV 397/93-06-05,

Closed)

Plant Housekee

in

.

The inspectors

observed plant conditions

and material/equipment

storage to determine

the general

state

of cleanliness

and housekeeping.

Housekeeping

in the radio-

logically controlled area

was evaluated with respect

to

controlling the spread of surface

and airborne contamination.

During tours performed

on February

22-23 and March 22, the

inspector

found a number of items which indicated that

housekeeping

and plant material condition problems

may be

increasing.

The inspectot

discussed

the following items with

licensee

management:

N

~

A 24-inch flanged elbow stored

near safety-related

instrument tubing.

~

Four valves in the

RCIC missing

handwheels

~

Unrestrained

tool boxes in the

RHR A and

B pump rooms.

A loose fire extinguisher

on the floor of the

RHR A pump

room.

~

All lights burned out in the

RHR

B heat exchanger

room,

and four of five lights burned out in the

RHR A heat

exchanger

room.

~

Temporary

power cables

wrapped

around Division I and

Division 2 power cable.

~

A personnel

safety chain attached

to safety-related

cabling.

In addition, the inspector

found loose rags

and unsecured

ladders

throughout the reactor building.

The inspector discussed

the above observations

with the

maintenance

Division Nanager,

who stated that these

problems

did not meet.his

expectations

and corrected

them in a timely

manner.

The inspector will continue to monitor plant

housekeeping

in future inspection r

I

- 11

(ll) ~Securit

.

The inspectors periodically observed security

practices

to determine if the licensee

followed the security

plan per site procedures,

search

equipment at the access

control points

was operational, vital area portals

were kept

locked and alarmed,

personnel

allowed access

to the protected

,area

were badged

and monitored,

and the monitoring equipment

was functional.

c.

En ineered Safet

Features

Walkdown

The inspectors

walked

down selected

engineered

safety features

(and

systems

important to safety)

to confirm that the systems

were

aligned in accordance

with plant procedures.

During walkdown of the

systems,

items

such

as hangers,

supports,

electrical

power. supplies,

cabinets,

and cables. were inspected

to determine that they were

operable

and in a condition to perform their required functions.

The inspectors

checked major components

for adequate

lubrication and

cooling.

The inspectors

also verified that certain

system valves

were in the required position by both local

and remote position

indication,

as applicable.

The inspectors

walked

down accessible

portions of the following

systems

on the indicated dates:

.

~Sstem

Diesel

Generator

Systems,

Divisions 1,

2, and 3.

Hydrogen Recombiners

Low Pressure

Coolant Injection (LPCI)

Trains "A"j "B", and

"C"

Low Pressure

Core Spray

(LPCS)

Reactor

Core Isolation Cooling

(RCIC)

Residual

Heat Removal

(RHR), Trains

"A" and "B"

Scram Discharge

Volume System

Standby Liquid Control

(SLC) System

Standby Service Water System

125V

DC Electrical Distribution,

Divisions

1 and

250V

DC Electrical Distribution

No violations or deviations

were identified.

Dates

March

March

Harch

18,

March 18,

March

March

March

Harch

March

March

March 18,

rJ

e

-12-

6.

Survei l 1 ance

Tes tin

61726

The inspectors

reviewed

a sampling of Technical Specifications

(TS)

surveillance tests verify that:

(1)

a technically adequate

procedure

existed for performance of the surveillance tests;

(2) the surveillance

tests

had been performed at the frequency specified in the

TS and in

accordance

with the

TS surveillance

requirements;

and

(3) test results

satisfied

acceptance

criteria or were properly dispositioned.

The inspectors

observed

portions of the following surveillance

on the

dates

shown:

Procedure

PPM

Descri tion

Dates

Performed

.

7.4.8.2.1.20

7.1. 1-

7.1.2

7.4.5.1.9

12.13.34

Meekly Surveillance for

Battery E-Bl-1

Health Physics Shiftly

Channel

Checks

Chemistry Daily Channel

and Source

Checks

RHR

B System Operability

Stack Monitor Daily

Monitoring Data

March

March

March

March 25

March

On March 25,

1993, during the performance of PPM 7.4.5. 1.9, the inspector

noted that the licensee

obtained

7423 gallons per minute

(gpm) while

operating

RHR loop

B in the suppression

pool cooling mode

(SPCM).

However,

paragraph

7.2, step

20, allows the operator to augment the flow

for suppression

pool cooling by opening

RHR-V-27B, the wetwell spray

valve.

Operators

opened

RHR-V-278 and flow increased

to 7500 gpm.

Operators

recorded

7500

gpm in the procedure

and signed off the step

as

satisfactory.

TS 4.6.2.3.b states,

"The suppression

pool cooling mode of the

RHR system

shall

be demonstrated

operable

by verifying that each of the required

RHR

pumps develops at least

7450

gpm on recirculation flow through the

RHR

heat exchanger

and the suppression

pool

when tested

pursuant to 4.0.5."

The inspector questioned

the licensee's

practice of augmenting

SPCM with

spray flow because it'id not appear to meet the intent of this TS.

The

inspector considered

that the intent of the

TS was to test the

SPCM as in

actual plant operations

to meet the surveillance requirement.

The

inspector also questioned

the ability to trend degraded

flow conditions

in SPCM in a manner which would be possible if the operators

only

recorded

flow through the test return line (RHR-V-24B).

The inspector also noted that neither the Emergency Operating

Procedures

(EOPs)

nor the system operating procedure

(PPM 2.4.2) recognize

the

practice of augmenting

SPCM with wetwell spray flow.

The

EOPs only allow

spraying the wetwell when certain containment

parameters

exist,

due to

. differential pressure

considerations

.

Also,

FSAR Section 7.3. 1. 1. 5

I'

f

f

e

(

t

provides

a valve-by-valve'description

of the

SPCM flow path of RHR.

This

flow path

does not include

RHR-V-27B.

In addition,

FSAR Section 6.2.2.1

states

that the

RHR system is capable of obtaining the full flow of 7450

gpm through the test return line.

The licensee

responded

by stating that because all flow went through the

RHR heat

exchanger

and eventually returned to the suppression

pool, the

RHR flow path complied with the

TS requirement.

Furthermore,

preliminary

licensee

calculations

indicated that only 7000

gpm were required,

and

that the system

was operable.

The inspector did not agree with the

licensee's

logic for compliance with the TS,

and questioned

the

licensee's

methodology for determining if adequate

flow was available for

SPCM.

The licensee's

calculation

assumed

that the design

basis

heat load

for SPCN was the decay heat

20 hours2.314815e-4 days <br />0.00556 hours <br />3.306878e-5 weeks <br />7.61e-6 months <br /> after shutdown.

However,

FSAR

Section 5.4.7. 1. 1.3 states,

"The functional design basis for the

suppression

pool cooling mode is that it shall

have the capacity to

ensure

that the suppression

pool temperature

immediately after a blowdown

shall not exceed

170 degrees."

Therefore, it appears

that incorrect

assumptions

were

used in the preliminary calculations.

The licensee

stated that neither the

A or

B SPCN loop could meet the

required

SPCM flow rate of 7450

gpm during startup testing in 1983,

and

that

PPM 7.4.5. 1.9 was changed

to include augmenting with wetwell spray

flow at that time.

The licensee

plans to submit a

FSAR amendment

to

provide the actual

flow rate of SPCN,

and the actual

system design basis.

In addi tion, the licensee

changed

PPN 7.4.5. 1.9 to include

an extra data

block for recording

SPCN flow prior to augmentation with wetwell spray

flow.

The

NRC must complete further evaluation to determine

whether the

licensee

complied with TS 4.6.2.3.b,

and whether or not the system is

within its design basis.

This is an unresolved

item (Unresolved

Item

397/93-06-06).

One unresolved

item was identified,

as discussed

above.

Plant Maintenance

62703

During the inspection period,

the inspector

observed

and reviewed

documentation

associated

with maintenance

and problem investigation

activities to verify compliance with regulatory requirements

and with

administrative

and maintenance

procedures,

required

OA/gC involvement,

proper

use of clearance

tags,

proper equipment alignment

and use of

jumpers,

personnel

qualifications,

and proper retesting.

The inspector

verified that reportabi lity for these

maintenance activi ties

was correct.

The inspector witnessed

portions of the following maintenance activities:

Dates

Performed

PPN 1.6.63,

Replace

Cell

on Battery

E-BI-I

March

-14-

AP 3030,

Repair

OG-RF-20B

(Offgas Chiller)

AR9492, Fabricate

and Install Anchor

Bolts and Seismic Supports for Stack

Radiation Monitor

AP2141, Install

New Stack Radiation

Monitor Panel

March

March

March

No violations or deviations

were identified.

8.

L'icensee

Event

Re ort

LER

Fol lowu

90712

92700

The inspector

reviewed the following LERs associated

with operating

events.,

Based

on the information provided,

the

NRC concluded that

reporting requirements

had been met, root causes

had

been identified,

and

corrective actions

were appropriate.

The below LERs are considered

closed.

LER NUMBER

DESCRIPTION

50-397/88-05-01

50-397/91-05-01

50-397/91-06-01

B Control

Room Emergency Filtration System

Bypass

Flow Exceeded

Technical Specifications

Wetwell Oxygen Concentration

Not Measured

per.

Technical Specification Surveillance

requirements

EDG

1 Inoperable

Due to High Particulate

in the

Generator

Lubricating Oil

In addition, the corrective actions for the following LER were evaluated.

0 en

50-397 92-044

"Hi h Pressure

Core

S ra

S stem

HPCS

Pum

Suction Valve Automatic Switchover Actuation"

This

LER described

an automatic switchover, that occurred

on December

8,

1992, of the

HPCS suction valve from the condensate

storage

tank

(CST) to

the 'suppression

pool

(SP)

when the conditions required for the switchover

did not exit.

The licensee

concluded that the root cause of the switch-

over was indeterminate,

but suspected

the cause of the switchover

was

spurious actuation of'either one or both of the

CST pipe break detectors,

since the detectors

had been

found to have excessive

setpoint drift.

As

immediate corrective action,

the license

changed

the calibration interval

of those detectors

from every

18 months to every month.

Longer term

corrective actions included evaluating

replacement of the detectors

and

investigating the susceptibility of the detectors

to radio frequency

emissions.

The licensee

did not expect to submit a supplemental

report.

The inspectors

made the following observations

during review of this

LER:

The licensee

investigation of the event found that from September

8,

1991,

to April 7,

1992,

the detectors

had drifted; however,

the

}

t

~

licensee's

investigation did not determine

why the calibration

frequency

had not been previously increased.

In subsequent

discussion with the licensee,

the inspector

learned

the licensee

believed it was inappropriate

to change calibration frequency

based

on

a single set of drift values.

The inspector also noted the

system engineer for the system

had not been

aware that the

instruments

had previously exhibited drift.

~

The inspector

found that the setpoint of the instrument

had recently

been

changed

as

a result of the licensee's

setpoint program.

The

change in setpoint,

which required the instrument to respond faster

to

a pipe break,

caused

the instrument to be at the limits of its

reproducible

response

band.

In reviewing licensee

documentation

associated

with the

LER, the inspector

found that, prior to

implementing the setpoint

change,

the licensee

had not evaluated

the

instrument's

performance characteristics.

The inspector

found the

licensee's

investigation of the event recognized that

a= setpoint

change

had occur red, but considered this not to be

a contributing

cause of the event.

The potential implication of the effect of the

setpoint

change

was not described

in the

LER.

The licensee's

corrective actions did not include further evaluation of the

implementation of the setpoint

program to determine if reviews of

setpoint

changes

are of appropriate detail.

The inspectors

concluded that the licensee's

documentation of events that

led to the switchover of the

HPCS suction valves

was poor.

As a result,

the licensee's ability to effectively determine root cause for this event

was documented

as indeterminate

and could potentially result in

additional

events

due to inappropriate setpoint

change

implementation.

The licensee

stated

they would evaluate

the inspectors

concerns with

respect

to out-of-calibration reviews

and the implementation of setpoint

changes.

This

LER remains

open for further evaluation of these

issues.

No violations or deviations

were identified.

9.

1993 Refuelin

Outa

e

R-8

Pre arations

The R-8 Outage,

which includes major work items

such

as refueling, motor

operated

valve testing, ventilation

system modifications,

and jet pump

cleaning,

was scheduled

to begin

on April 15,

1993,

and take

approximately

45 days.

At the request of Bonneville Power Administration

(BPA), the Supply System deferred

the beginning of R-8 until Hay 1,

due

to regional

power demand.

Outage duration is still planned for 45 days.

The inspectors

discussed

preparations,

in progress for the

WNP-2 R-8

Outage,

with the Outage

t1anager

and other members of the plant staff.

The discussions

included topics

such

as

ALARA planning,

maintenance

work

package

preparation,

and work coordinators.

The inspectors

also

examined

a limited number of the work packages

that had

been completely planned

for the Outage.

From the discussions

and work package

reviews the

inspectors

made the following observations:

Planning for the R-8 Outage,

as

compared to the R-7 Outage,

was

improved.

On Harch

18,

1993,

the inspectors

found that about

25'. of

I

H

-16-

the approximately

1300 work packages

were fully planned;

however,

according to the Outage

Manager, at the

same

time last year only

about

15~ of the work was completely planned.

Most of the remaining

work packages

were in the planning process.

~

A significant amount of the ALARA planning rema'ined to be completed.

~

Most of the parts required for the worked planned to begin early in

the outage

were available.

The licensee

plans to assign

area coordinators for specific areas

within the plant to control work activities within those areas.

In

addition,

the licensee

plans to use work control field managers

to

identify and resolve

emergent

work restraints that occur during the

course of daily activities.

t

The licensee

plans to evaluate

the daily schedule for shutdown risk

to ensure

the number of available safety systems

remains

high and

never gets

below the minimum required

by technical specifications.

No violations or deviations

were identified.

10.

En ineered

Safet

Feature

S stem Malkdown

71710

The inspectors

performed

a detailed

walkdown of accessible

portions of

the high pressure

core spray

(HPCS)

system.

The inspectors

made the

following observations:

The

HPCS lineup procedures

matched plant drawings

and the as-built

configuration.

Generally,

HPCS equipment

and components

were in acceptable

condition.

However,

several

equipment deficiencies

were noted to be

greater

than 24-months old.

The inspectors

noted several

housekeeping

discrepancies

and

a poor

work practice.

Several

T-handles

on small

HPCS globe valves were

loose

and

one

had

no retaining nut.

During the repair of a

fluorescent light fixture on the mezzanine

level of the

HPCS

pump

room, the craftsmen left the area with the light suspended

from its

power cord and the fluorescent

tubes upright on

a grated floor.

The

inspectors

referred these

observations

to the licensee

and the

deficiencies

were corrected.

The inspectors

found that

HPCS component labeling was generally

satisfactory.

They observed that the components

located in the

higher areas of the

HPCS

pump room were labeled with small metal

tags

and that those

components

were especially difficult to identify

from the grating level..

Some of those valves were

on the facility

locked-valve list.

The inspectors

noted that many of the doors in areas

that contained

HPCS components

or support equipment

had fire impairments.

Some of

the impairments

were greater

than

12-months old.

The impaired doors

fl

were veri fied to be part of periodic fire tours.

Upon further

facility touring, the inspectors

observed that

a very high

percentage

of facility fire doors

had impairments,

some of which

were greater

than

18-months old.

The inspectors

discussed

this

observation with the licensee at the exit meeting.

~

The inspectors

observed that

HPCS instruments

were within their

calibration periodicity

and that process

parameters

were within the

expected

band for the operational

state of the system.

~

The inspectors

observed

proper electrical

breaker position at the

local distribution panel

and at remote locations.

In general,

the inspectors

found that the

HPCS system

was maintained

adequately.

The discrepancies

the inspectors

observed

suggest that the

quality and attention to detai

1 of operator

and supervisory tours require

strengthening.

No violations or deviations

were identified.

11.

WNP-3 Ins ection

92050

On February

24,

1993,

an inspector visited the

WNP-3 site.

The

WNP-3

site is in an extended construction

delay status.

The inspector toured

the containment,

control

room, auxiliary building and warehouses,

observi ng the condition of the licensee's

in-place

and stored equipment.

The condition of the equipment

was satisfactory.

Instrumentation

monitoring the temperature

and humidity was in-place, in calibration,

and

operating.

The inspector

concluded that the plant equipment

was

satisfactorily maintained.

a ~

Back round and Plant Status

WNP-3 is in a construction

delay status

and is approximately

76~

completed.

There is no fuel

on site.

Plant equipment is maintained

according to WMC-051,

"WNP-3 Preventive

Maintenance

Program."

These

documents

describe

the equipment

storage

requirements

that have

been

implemented,

and specify periodic equipment preservation

maintenance.

Personnel

assignments

at the site has

been stable.

WNP-3 management

consists of both Supply System

and

Ebasco

employees.

Events that occurred at WNP-3 in 1992 include:

~

The licensee

sold

WNP-5 components

and these

components

were

removed

from site.

The licensee

combined several

WNP-3

warehouse

items into this space.

~

The licensee is doing an extensive

re-lamping effort, replacing

incandescent

fixtures with high efficiency florescent fixtures.

This reduces

the energy

used

on site.

In order to maintain the status

and material condition of the site

equipment,

the licensee

has designated

four levels of equipment

warehouse

storage,

Levels A, B,

C,

and

D, which are consistent with

ANSI/ASME N45.2.2-1973 classifications.

The inspector

observed that

equipment

storage within areas

A,

B and

C appeared

proper and

appropriate for each classification level.

Work Observation at

WNP-3

The inspector

observed part of a non-routine maintenance activity at

WNP-3.

This activity was

a flush of a

pump filled with Vaportec,

an

additive the licensee

previously used to inhibit corrosion

and

preserve

internals of plant equipment.

The addition of the Vaportec

degraded

some elastomeric

components

and caused sticking of

internals,

making them difficult to rotate.

The licensee

reported

this to the

NRC as

a potential

CFR 50.55(e) report

on April 21,

1989, which the

NRC will continue to followup until the issue

concerning

Vaportec is fully dispositioned.

The licensee is

investigating different ways to remove the Vaportec without

disassembly of equipment.

The inspector

observed that the licensee

tested

an approach

by using citric acid to flush some

pump internals

that were difficult to rotate.

After the flush, the licensee

inspected

the

pump internals.

The Vaportec

had substantially

dissolved,

but some remained

(where the flowrates were lower).

The

licensee is continuing to resolve

the Vaportec problem and will

inform the

NRC if this approach will be used.

Plant

E ui ment and Material

Ins ection at

WNP-3

The inspector

conducted

a walk-through inspection of equipment

and

material

storage

areas.

These storage

areas

included the

containment,

control

room, reactor auxiliary building (RAB), and

Warehouse

Nos.

1, 2, 3, 4,

6 and 7.

These

areas

contained

Levels A,

B and

C storage.

Naterial storage

and use of dunnage

appeared

adequate

and in accordance

with the licensee's

procedures.

Dunnage

for pipes stored in outside

areas

appeared

adequate.

The licensee's

Level

A and

B storage

areas

had operable

automatic fire protection

systems.

No evidence of water or abnormal

material

corrosion

was observed in

any of the inside storage

areas.

Cleanliness,

preservation,

and

protection

o'f equipment,

including housekeeping,

were satisfactory.

Corrosion

coupons

or bare metal

surfaces

in the containment

and

auxiliary bui ldiggs did not show any significant deterioration.

Hygrothermographs

(instruments monitoring humidity and temperature)

inside these

storage

areas

were in calibration, in operation,

and

reading in specification.

Heasurin

and Test

E ui ment

HSTE

The inspector observed that the.licensee

had replaced

the previous

hygrothermographs

with a newer model.

These

hygrothermographs

monitor the temperature

and humidity within the storage

areas,

and

provide the

gA record that the ANSI storage

requirements

are

maintained.

Since this was

a newer model,

the inspector

reviewed

the calibration procedure,

10.700.76,

"Calibration of Hygrothermo-

l

't

I

t)

'

-19-

graphs, All Hakes

All Hodels," to assess

the adequacy of the

procedure.

After reviewing calibration procedure

10.700.76,

the inspector

questioned

whether this procedure

was adequate

for calibrating the

instruments,

since only two points

(approximately

32% and

75%

humidity) were checked.

The licensee

stated that their calibration

procedure is based

on the vendor's

manual.

The inspector's

concern

was assuring

the linearity of the humidity instrument,

since this

was not a standard five-point calibration.

In further discussions,

the licensee

showed that the instrument

was

accurate

to within 3~ for a humidity between

20~ and 90~.

Based

on

this information and discussions

with the licensee,

this concern is

resolved.

The licensee further stated that the humidity readings

correlate well when checked against different humidity instruments.

No violations or deviations

were identified.

12-.

Unresolved

Items

Unresolved

items are matters

about which the

NRC requires

more infor-

mation to determine whether they are acceptable

items, violations, or

deviations.

Paragraphs

4.a, 4.b, 4.c, 5.b(6),

and

6 of this report

discuss

unresolved

items addressed

during this inspection.

i3.

~Ei

The inspectors

met with licensee

management

representatives

periodically

during the report period to discuss

inspection status.

An exit meeting

was conducted with the indicated personnel

(refer to Paragraph

1)

on

April 15,

1993.

The inspectors

discussed

the scope of the inspection

and

the inspection findings with licensee

management.

Licensee

representatives

acknowledged

the inspectors'indings.

An exit meeting

was held with the licensee's

staff (refer to Paragraph

1)

at WNP-3 on February

24,

1993.

The inspection

scope

and findings of

.

Paragraph

11 were discussed.

The licensee did'not identify as proprietary any of the information

reviewed

by or discussed

with the inspectors

during the inspectio I

I]

bcc w/copy of enclosure:

Docket File

Project Inspector

Resident

Inspector

B. Faulkenberry

J. Martin

R.

Huey

C. VanDenburgh

P. Johnson

J. Clifford, NRR

G.

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S. Richards

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Docket File

Project Inspector

Resident

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B. Faulkenberry

J. Hartin

R.

Huey

C. VanDenburgh

P. Johnson

J. Clifford, NRR

G.

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