IR 05000389/1981001
| ML17209A829 | |
| Person / Time | |
|---|---|
| Site: | Saint Lucie |
| Issue date: | 02/11/1981 |
| From: | Conlon T, Harris J NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML17209A828 | List: |
| References | |
| 50-389-81-01, 50-389-81-1, NUDOCS 8103190045 | |
| Download: ML17209A829 (5) | |
Text
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+g qP W**yW UNITED STATES NUCLEAR REGULATORY COMMISSION
REGION II
101 MARIETTAST., N.W., SUITE 3100 ATLANTA,GEORGIA 30303 Docket/Report No.
50-389/81-1 Licensee:
Florida Power and Light Company 9250 West Flagler Street Miami, FL 33101 Facility Name:
St. Lucie License No.
CPPR-144 Inspection at:
St. Lucie site near Ft. Pierce, Florida Inspector:
J.
R.
arris
/'pproved by:
T. E. Conlon, Section Chief, RCES Branch Date of Inspection:
January 20-23, 1981 Areas Inspected Da e
igned
~ -o-F/
Date Signed This routine, unannounced insp'ection involved 28 inspector-hours onsite in the areas of structural concrete, earthfill and previously identified items.
Results Of the 3 areas inspected, no apparent items of noncompliance or deviation were identifie DETAILS 1.
Persons Contacted Licensee Employees
"B. J.
Escue, Project Manager W. Hayward, QA Construction Supervisor E. Sherman, QA Engineer 0. Karch, QA Engineer
"J. Parker, Project Quality Control Supervisor C. Carlos, Civil QC Supervisor
"D. Cooper, Supervising QA Engineer Other licensee employees contacted included three construction craftsmen, three technicians, and two office personnel.
Other Organizations R. Garramore, Senior Resident Engineer, EBASCO
"Attended exit interview.
2.
Exit Interview
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~
3.
The inspection scope and findings were summarized on January 23, 1981 with those persons indicated in Paragraph 1 above.
t Licensee Action on Previous Inspection Findings (Closed) Infraction (389/80-08-01)
Inadequate procedural controls on sand-cement fill.
The inspector reviewed the licensee's response and implemen-tation of that response presented in the licensee's letter dated July 24, 1980.
Design change number 518.822 was issued to clarify procedural con-trols and to document testing showing that sand cement fill met design requirements.
This item is closed.
Unresolved Items Unresolved items were not identified during this inspection.
5.
Independent Inspection The inspector examined the following areas:
a.
b.
Construction status Concrete and soils testing laboratory C.
Backfill operations adjacent to the reactor control building and component cooling buildin d.
Ongoing concrete curing controls.
e.
Installation of reinforcing steel in shield walls around the steam generator and pressurizer.
Concrete test cylinder strength data from January 3,
1980 to January 5,
1981.
No deviations or violations were identified.
6.
Containment (Structural Concrete II) Observation of Work and Work Acti-vities The inspector performed a followup inspection of structural concrete activi-ties.
The inspector observed placement of pour number 77-85 in the Fuel Building exterior wall.
Acceptance criteria examined by the inspector appear in the following documents:
a.
PSAR, Section 3.8. 1 and 3.8.3 b.
gI's 10.2, 10.3, 10.6, 10.70, 10.71 and 15.1 c.
Flo-2998.473, EBASCO Specification Concrete Forms were tight, clean and level; rebar was properly installed and clean.
Placement activities pertaining to delivery time, free fall, flow distance, layer thickness and consolidation conformed to specifications.
In-process tests for slump, air content, and cylinder molding were performed in accord-ance with procedure requirements.
Batch plant forms indicated the specified mix was being delivered, Activities were continuously monitored by gC personnel.
An examination of the batch plant indicated materials were being controlled and accurate batch re'cords were being generated.
No deviations or violations were identified.