IR 05000321/2018002
ML18222A503 | |
Person / Time | |
---|---|
Site: | Hatch |
Issue date: | 08/10/2018 |
From: | Alan Blamey NRC/RGN-II/DRP/RPB2 |
To: | Vehec T Southern Nuclear Operating Co |
References | |
EA-18-100 IR 2018002 | |
Download: ML18222A503 (24) | |
Text
UNITED STATES NUCLEAR REGULATORY COMMISSION ust 10, 2018
SUBJECT:
EDWIN I. HATCH NUCLEAR PLANT - NUCLEAR REGULATORY COMMISSION INTEGRATED INSPECTION REPORT 05000321/2018002 AND 05000366/2018002 AND EXERCISE OF ENFORCEMENT DISCRETION
Dear Mr. Vehec:
On June 30, 2018, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Edwin I. Hatch Nuclear Plant Units 1 and 2. On July 19, 2018, the NRC inspectors discussed the results of this inspection with Gary Brinson and other members of your staff. The results of this inspection are documented in the enclosed report.
There was one violation for which the NRC has exercised enforcement discretion. A violation of 10 CFR Part 50.48(b) was identified because the Edwin I. Hatch Nuclear Plant failed to use one of the means described in Appendix R,Section III.G2.a, b,or c to ensure redundant trains of equioment necessary to achieve and maintain hot shutdown conditions was protected from fire damage. The inspectors determined the violation was not associated with a finding of high safety significnacne. The enforcement discretion was based on the Enforcement Policy, Section 9.1, Enforcement Discretion for Certain Fire Protection Issues (10 CFR 50.48), a Confirmatory Order (ML16223A467) which extended the period for discretion, and Inspection Manual Chapter 0305. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.
Sincerely,
/RA/
Alan Blamey, Chief Reactor Projects Branch 2 Division of Reactor Projects Docket Nos.: 50-321, 50-366 License Nos.: DPR-57 and NPF-5
Enclosure:
IR 05000321/2018002, 05000366/2018002
Inspection Report
Docket Numbers: 50-321, 50-366 License Numbers: DPR-57, NPF-5 Report Numbers: 05000321/2018002; and 05000366/2018002 Enterprise Identifier: 2018-002-0057 Licensee: Southern Nuclear Operating Company, Inc.
Facility: Edwin I. Hatch Nuclear Plant Location: Baxley, Georgia Inspection Dates: April 1, 2018 to June 30, 2018 Inspectors: C. Jones, Senior Resident Inspector J. Hickman, Resident Inspector N. Peterka, Fuel Facilities Inspector R. Kellner, Senior Health Physicist (71124.06, 71151)
W. Pursley, Health Physicist (71124.07, 71151)
W. Monk, Reactor Inspector (71153)
Approved By: A. Blamey, Chief Reactor Projects Branch 2 Division of Reactor Projects Enclosure
SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring licensees performance by conducting baseline inspections at Edwin I. Hatch, Units 1 and 2 in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. NRC and self-revealed findings, violations, and additional items are summarized in the table below. Licensee-identified non-cited violations are documented in the Inspection Results section of the Report.
List of Findings and Violations No NRC-identified findings or violations were identified.
Additional Tracking Items Type Issue number Title Report Status Section Licensee 05000321, Unanalyzed Conditions for a 71153 Closed Event 366/2017001-00 Postulated Fire Discovered Report During NFPA 805 Transition (LER)
LER 05000321/2018001-00 Condition Prohibited by Tech 71153 Closed Specs Due to Secondary Containment Inoperability LER 05000321/2018002-00 Performance of Operations 71153 Closed with the Potential to Drain the Reactor Vessel (OPDRV)
Without Secondary Containment
PLANT STATUS
Unit 1 began the inspection period at 100 percent rated thermal power (RTP). On April 4, 2018, power was reduced to 65 percent to replace the 8th stage feedwater heater level detectors. The unit returned to 100 percent power on April 5, 2018 and operated at or near 100 percent RTP for the remainder of the inspection period.
Unit 2 began the inspection period at 100 percent RTP. On April 17, 2018, power was reduced to 50 percent RTP to repair a condenser tube leak in the 2C waterbox, and returned to 100 percent power on April 24, 2018. On May 6, 2018, power was reduced to 50 percent RTP to repair a condenser tube leak in the 2B waterbox, and returned to 100 percent power on May 12, 2018. On May 19, 2018, the unit was taken offline due to high drywell temperatures caused by inoperable return air fans. The unit returned to 100 percent RTP on May 26, 2018 and operated at or near 100 percent RTP for the remainder of the inspection period.
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.
REACTOR SAFETY
71111.01 - Adverse Weather Protection Summer Readiness
The inspectors evaluated summer readiness of offsite and alternate alternating current (AC)power systems.
71111.04 - Equipment Alignment Partial Walkdown
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
- (1) Unit 2 - A and B loops of core spray (CS) train while the A loop of residual heat removal (RHR) was out of service for maintenance on April 9, 2018
- (2) Unit 1 - C emergency diesel generator (EDG) alignment was verified after a minor maintenance package was completed on April 23, 2018
- (3) Unit 2 - A EDG alignment after day tank cleaning and limit switch repairs following a failed surveillance on June 1, 2018
71111.05AQ - Fire Protection Annual/Quarterly Quarterly Inspection
The inspectors evaluated fire protection program implementation in the following selected areas:
- (1) Unit 1, A and B Station Battery Rooms
- (2) Unit 1, High Pressure Core Injection (HPCI) Room, Fire Zone 1205Z
- (3) Unit 1, Southeast (SE) Diagonal, Fire Zone 1203B
- (4) Unit 1 Control Rod Drive (CRD) and Drywell Sump, Fire Zone 1205C
- (5) Unit 1 and Unit 2 Reactor Protection System (RPS) Rooms, Fire Zones 2009, 2010, 1009 and 1010
- (6) Unit 1 and Unit 2 Control Room Roof, Fire Zone 0031
71111.06 - Flood Protection Measures Cables
The inspectors evaluated cable submergence protection in PB2-B and PB2-D, Inground Pullbox on May 7, 2018.
71111.07 - Heat Sink Performance Heat Sink
The inspectors evaluated the Unit 1 B Emergency Diesel Generator heat exchanger performance on May 8, 2018.
71111.11 - Licensed Operator Requalification Program and Licensed Operator Performance Operator Requalification
The inspectors observed and evaluated a crew of licensed operators in the plants simulator during licensed operator requalification training on April 24, 2018.
Operator Performance (1 Sample)
The inspectors observed and evaluated Unit 1 Reactor Operator performance during load reduction to 65 percent power to replace 8th stage feedwater heater level detectors on April 4, 2018. The inspectors observed and evaluated Unit 2 Reactor Operator performance during the transfer of the RPS Bus from the alternate power supply to the motor generator (MG)
Set, and two load reductions to 50 percent power to complete condenser tube leak repairs on April 3, April 17, and May 6, 2018.
71111.12 - Maintenance Effectiveness Routine Maintenance Effectiveness
The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:
- (2) Unit 2, High fuel oil supply differential pressure resulting in the inoperability of the 2A EDG on May 29, 2018.
71111.13 - Maintenance Risk Assessments and Emergent Work Control
The inspectors evaluated the risk assessments for the following planned and emergent work activities:
- (1) Unit 1 risk assessment for the removal of the 230KV Bus 2 for degraded grid upgrade on April 2, 2018.
- (2) Unit 1 and 2 risk assessment for the removal of the '1C' startup transformer (SUT)outage on April 19, 2018.
- (3) Unit 2 risk assessment for concurrent work on the 2A RHR system and 2C plant service water (PSW) pump on May 3, 2018.
- (4) Unit 1 elevated risk during the 1B EDG maintenance outage on May 8, 2018.
- (5) Unit 1 and 2 elevated risk during 2A EDG inoperability on May 30, 2018.
71111.15 - Operability Determinations and Functionality Assessments
The inspectors evaluated the following operability determinations and functionality assessments:
- (1) Unit 1 - RHR loops had increased pressure and required venting of loops to lower pressure on April 22, 2018
- (2) Unit 1 and Unit 2 - pull boxes discovered with higher than acceptable water levels during weekly inspections on April 26, 2018
- (3) Unit 1 - through wall leak was discovered on Division 1 PSW piping on June 4, 2018
- (5) Unit 2 - 2A EDG declared inoperable due to degraded fuel oil system on June 26, 2018
- (6) Unit 1 - non-conforming breaker settings on ECCS room coolers on June 12, 2018
71111.18 - Plant Modifications
The inspectors evaluated the following temporary or permanent modifications:
- (1) Unit 2 - Drywell return air fan motor replacement with a lower horsepower unit
71111.19 - Post Maintenance Testing
The inspectors evaluated the following post maintenance tests:
- (1) 34SV-E11-001-2, Residual Heat Removal Pump Operability after the B loop maintenance outage on April 8, 2018
- (2) 34SV-R43-006-1, 1C EDG monthly test following a minor maintenance outage on April 18, 2018
- (3) 34SV-C11-003-1, U1 Control rod exercise following repairs to the rod select 30-51 switch replacement on May 2, 2018
- (4) 34SV-C11-003-1, U1 Control rod exercise following repairs to the rod select 34-51 switch on May 1, 2018
- (5) 34SV-R43-005-2, Emergency diesel generator 1B semi-annual test following a maintenance outage on May 15, 2018
- (6) 34SO-B31-001-2, Reactor recirculation system test following the 2B adjustable speed drive (ASD) loss of flow indication on May 29, 2018
- (7) 34SV-R43-011-2, Emergency diesel generator 2A 24 month operability test following high fuel filter differential pressure and limit switch repairs on May 30, 2018
- (8) 34SO-C51-001-0, TIP system operation and LPRM calibration following CMDAS (process computer) failure during TIP run on June 15, 2018
- (9) 34IT-E51-003-1, RCIC speed control test following a Unit 1 RCIC system outage on June 15, 2018
71111.20 - Refueling and Other Outage Activities
The inspectors evaluated the Unit 2 forced outage activities from May 19, 2018 to May 26, 2018.
71111.22 - Surveillance Testing The inspectors evaluated the following surveillance tests: Routine
- (1) 34SV-C1-005-005-2, Turbine Control Valve Fast Closure Instrument Functional Test, Ver.17.0
- (2) 34SV-E11-001-2, Residual Heat Removal Pump Operability, Ver. 19.3
- (3) 34SV-SUV-019-2, Surveillance Checks (Unidentified Leak rate Calculation), Ver. 41.15
- (4) 64CH-SAM-025-0, Reactor Coolant Sampling and Analysis, Ver. 44.2
- (5) 52PM-P41-036-2, Unit 2 Plant Service Water Pump and Motor Major
Inspection/Overhaul, Ver.9.0 In-service (1 Sample)
- (1) 34SV-E21-001-1, Core Spray Pump Operability, Ver. 22.3
71114.06 - Drill Evaluation Emergency Planning Drill
The inspectors evaluated a simulator based emergency scenario on April 24,
RADIATION SAFETY
71124.06 - Radioactive Gaseous and Liquid Effluent Treatment Walk Downs and Observations
The inspectors evaluated the licensees radioactive gaseous and liquid effluent treatment systems during plant walkdowns.
Calibration and Testing Program (Process and Effluent Monitors) (1 Sample)
The inspectors evaluated the licensees gaseous and liquid effluent monitor instrument calibration and testing.
Sampling and Analyses (1 Sample)
The inspectors evaluated radioactive effluent sampling and analysis activities.
Instrumentation and Equipment (1 Sample)
The inspectors evaluated radioactive effluent instrumentation and equipment.
Dose Calculations (1 Sample)
The inspectors evaluated dose calculations.
71124.07 - Radiological Environmental Monitoring Program Site Inspection
The inspectors evaluated the licensees radiological environmental monitoring program.
Groundwater Protection Initiative Implementation (1 Sample)
The inspectors evaluated the licensees groundwater monitoring program.
OTHER ACTIVITIES - BASELINE
71151 - Performance Indicator Verification The inspectors verified licensee performance indicators submittals listed below for the period from April 2017 through March 2018
- (1) Reactor coolant system (RCS) specific activity, BI01, both units (2 Samples)
- (2) RCS leakage, BI02, both units (2 Samples)
- (3) Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual Radiological Effluent Occurrences (RETS/ODCM) Radiological Effluent Occurrences, PR01 (1 Sample)
- (4) Occupational Exposure Control Effectiveness Sample, OR01 (1 Sample)
71152 - Problem Identification and Resolution Semiannual Trend Review
The inspectors reviewed the licensees corrective action program for trends that might be indicative of a more significant safety issue.
- (1) Unit 1 PSW seismic restraints (CRs 10238732, 10319598, 10328432, 10458271)
Annual Follow-up of Selected Issues (1 Sample)
The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:
- (1) Unit 2 Control Rod 34-23 Mispositioned, CR 10492356
71153 - Follow-up of Events and Notices of Enforcement Discretion Licensee Event Reports
The inspectors evaluated the following licensee event reports which can be accessed at https://lersearch.inl.gov/LERSearchCriteria.aspx:
- (1) LER 05000321, 366/2017-001-00: Unanalyzed Conditions for a Postulated Fire Discovered During NFPA 805 Transition
- (2) LER 05000321/2018-001-00, Condition Prohibited by Tech Specs Due to Secondary Containment Inoperability, on Jan. 20, 2018
- (3) LER 05000321/2018-002-00, Performance of Operations with the Potential to Drain the Reactor Vessel (OPDRV) Without Secondary Containment, on Feb. 9,
INSPECTION RESULTS
Observation
71124.07 - Radiological Environmental
Monitoring Program NEI 07-07 Groundwater Protection Initiative (GPI) Implementation No violations of regulatory requirements were identified. During performance of Inspection Procedure 71124.07, Radiological Environmental Monitoring Program (REMP), inspectors noted three examples where the licensee failed to provide timely communication to State/Local officials when elevated tritium levels in ground water samples indicated a new onsite leak or spill had occurred. Per NEI 07-07, Industry Ground Water Protection Initiative
- Final Guidance Document, Objective 2.2, a licensee shall make informal communication as soon as practicable to appropriate State/Local officials, with follow-up notification to the NRC, as appropriate, regarding significant (> 100 gallon) onsite leaks/spills or ground water well sample results, from sources that could be used as drinking water, that exceed the reporting criteria in the REMP. These reports should be made before the end of the next business day.
Contrary to this, in January 2016, January 2017, and February 2018, ground water samples from monitoring well T-12 , located inside the protected area of the plant in close proximity to the Unit One Condensate Storage Tank (CST), showed anomalous tritium spikes of 400,000 pCi/L, 120,000 pCi/L, and 400,000 pCi/L respectively, yet informal reports to State and Local officials were not made before the end of the next business day and, for the leak in 2017, was not reported at all. Due to historical leaks in the area around the CSTs, the licensee had created reporting criteria for T-12 sample results that were higher than the 20,000 pCi/L threshold specified in the REMP. The communication protocol in NEI 07-07 is meant to drive the reporting of new spills and leaks, not to require multiple reports for the same historical tritium plume as it moves through the subsurface. However, in this case, the licensee had created a reporting threshold that was too high to allow for timely recognition of new leaks.
NEI 07-07 also states that any changes to the reporting thresholds need to be agreed upon by State and Local stakeholders and that such agreements shall be documented. The inspectors noted that no such stakeholder agreements to substantially increase reporting thresholds had been made. Also, monitoring well T-12 is not a source of site or public drinking water.
In addition, NEI 07-07, Objective 2.4, requires licensees to include any voluntary communications performed under Objective 2.2 in either the Annual Radiological Environmental Operating Report (AREOR) or Annual Radioactive Effluent Release Report (ARERR). Contrary to this, the voluntary communication made in 2016 was not included in either of the 2016 annual reports.
Observation
71152 - Problem Identification and
Resolution Semi-Annual Trend Review: Unit 1 PSW seismic restraints No findings of significance were identified. The inspectors did observe that there continued to be material problems with the seismic restraints on the Unit 1 Plant Service Water suction piping as documented in CRs during this period. The licensee completed their 2018 annual structural monitoring program for both units and as documented in CRs, it was noted that the seismic restraints continued to degrade on the Unit 1 Plant Service Water piping, specifically the seismic restraint studs and bolts. The licensee first documented degradation on the restraints in 2016 and in the following years, it had been noted that the corrosion of the studs, bolts and degradation of the protective coating had steadily progressed. After reviewing associated CRs, performing a walkdown of the affected seismic restraints, and interviewing the structural engineer, it was determined that the licensee identified the issues, evaluated the root causes, and have taken appropriate corrective actions. The inspectors however, noted a weakness in the monitoring program for the plant service water seismic restraints. As defined in the structural monitoring program procedure, there is no deterministic or testing criteria for when a structures integrity would be considered degraded to such a condition that it would not be able to perform its safety function. Currently, the corrosion and coating degradation on the seismic restraints is evaluated visually only and based on a licensed engineers professional judgement. No measurements or mechanical tests are performed to determine if the corrosion has affected the seismic restraints beyond what is visible on the surface. No similar issues were identified on the Unit 2 seismic restraints because they are of a different design.
In general, the licensee has identified trends and has addressed the trends with their corrective action program. No new adverse trends were identified this period that had not already been identified by the licensee.
Observation
71152 - Problem Identification and
Resolution Annual Follow-up of Selected Issues: Unit 2 Control Rod 34-23 Mispositioned The inspectors performed a review regarding the licensees assessments and corrective actions associated with CR 10492356, Control Rod 34-23 Mispositioned. Specifically, on May 11, 2018, operations, while performing rod pattern adjustments in accordance with the reactivity plan, withdrew rod 38-27 and received a rod block annunciator. The operator selected control rod 34-23 in order to clear the rod block alarm and noticed that rod 34-23 had inserted one notch from 48 to 46. The shift entered 34AB-C11-004-2S, Mispositioned Control Rods Version 4.3, and rod 34-23 was returned to position 48. Troubleshooting revealed no equipment issues and rod pattern adjustments were completed on May 12, 2018. Further investigation revealed that that the operator did not wait the required 5 seconds to allow the relay to reposition as required by 34GO-OPS-065-0, Control Rod Movement. A Stand Down for each shift was performed to review this event and procedural guidance. The assigned corrective actions taken by the licensee identified issues with verification practices and procedure use and adherence. The inspectors determined that the corrective actions developed as a result of the condition reports were reasonably commensurate with the safety significance of the control rod drive system.
Enforcement Enforcement Action (EA)-18-100: Unanalyzed 71153(1) - Follow-up of Discretion Conditions for a Postulated Fire Discovered Events and Notices of During NFPA 805 Transition Enforcement Discretion
Description:
On April 3, 2017, the licensee submitted Licensee Event Report (LER)05000321, 366/2017-001-00: Unanalyzed Conditions for a Postulated Fire Discovered During NFPA 805 Transition documenting the discovery of a condition of non-compliance with the sites fire protection program (FPP). In preparation for transiting the fire protection licensing basis from 10 CFR 50.48(b) (Appendix R) to 10 CFR 50.48(c) (NFPA 805), a weak-link and operator manual action analysis was completed for Information Notice 92-18 type hot shorts on motor operated valves (MOV). The licensees examination of their Appendix R Safe Shutdown Analysis identified circuit configurations in multiple fire areas where an Appendix R postulated fire could impact the ability to achieve safe shutdown conditions. The licensee failed to protect MOV cables associated with the RHR and RCIC emergency cooling systems in fire areas 0024 (Main Control Room), 1203F (Unit 1 Reactor Building), 1205F (Unit 1 Reactor Building), and 2203F (Unit 2 Reactor Building). Specifically, the licensee failed to ensure that fire induced cable impacts cannot bypass the limit and torque switches and result in physical damage to the MOVs, thus preventing the MOVs from being operated from the Main Control Room, Remote Shutdown Panel, or locally. This condition could prevent operators from achieving and maintaining safe shutdown (SSD) of the plant in the case of a postulated fire.
A licensee-identified non-compliance with 10 CFR Part 50, Appendix R, Section III.G.2, was identified for the licensees failure to protect one of the redundant trains of equipment needed to achieve post-fire SSD from fire damage. Specifically, the licensee failed to use one of the means described in Appendix R,Section III.G.2.a, b, or c to ensure that one of the redundant trains of equipment necessary to achieve and maintain hot shutdown conditions was protected from fire damage.
The inspectors performed a detailed review of the information and documents related to the LER and discussed the condition with the licensee to assess the adequacy of the licensees compensatory measures and corrective actions.
Corrective Action(s): Hourly fire watches and Fire Action Statements were initiated to address the postulated condition for the identified MOVs. Additionally, the licensee committed to completing physical plant modifications to the impacted MOVs during the next Unit 1 and Unit 2 plant refueling outages to rectify the issue of potential spurious operation of the associated MOVs associated with this LER.
Corrective Action Reference(s): The licensee entered this issue into their Corrective Action Program (CAP) as condition reports (CRs) 10326399, 10326401, 10326402, 10326404, and 10326405.
Enforcement:
Violation: 10 CFR Part 50.48(b)(1) requires that all nuclear power plants licensed to operate prior to January 1, 1979, must satisfy the applicable requirements of 10 CFR Part 50, Appendix R, Section III.G. 10 CFR 50, Appendix R, Section III.G.2, states, in part, that where cables or equipment, that could prevent operation or cause mal-operation due to hot shorts, open circuits, or shorts to ground, of redundant trains of systems necessary to achieve and maintain hot shutdown conditions are located within the same fire area outside of primary containment, one of the following means of ensuring that one of the redundant trains is free of fire damage shall be provided:
- (a) separation of cables and equipment by a fire barrier having a 3-hour rating,
- (b) separation of cables and equipment by a horizontal distance of more than 20 feet with no intervening combustibles or fire hazards and with fire detectors and an automatic fire suppression system in the fire area, or
- (c) enclosure of cables and equipment in a fire barrier having a 1-hour rating and with fire detectors and an automatic fire suppression system in the fire area.
Contrary to the above, the licensee failed to use one of the means described in Appendix R,Section III.G.2.a, b, or c to ensure that one of the redundant trains of equipment necessary to achieve and maintain hot shutdown conditions was protected from fire damage. Specifically from October 1974 to April 2017, the licensee had not met the requirements of 10 CFR Part 50.48(b) to identify and protect cabling of 51 Unit 1 and Unit 2 RHR and RCIC emergency cooling system MOVs in fire areas 0024 (Main Control Room), 1203F (Unit 1 Reactor Building), 1205F (Unit 1 Reactor Building), and 2203F (Unit 2 Reactor Building). On April 3, 2017, the licensee identified the failure to protect equipment that was required to mitigate fire events and determined that fire damage could cause mal-operation of the affected MOVs, potentially leading to fire induced cable impacts which bypass the limit and torque switches and result in physical damage to the MOVs, thus preventing the MOVs from being operated from the Main Control Room, Remote Shutdown Panel, or locally. A fire-induced failure could have caused the loss of the required Safe Shutdown components.
Severity/Significance:
Failure to protect one train of cables and equipment necessary to achieve post-fire SSD from fire damage for fire areas designated in the Fire Protection Program (FPP) as meeting Appendix R,Section III.G.2, was a performance deficiency. This finding was more than minor because it was associated with the reactor safety mitigating system cornerstone attribute of protection against external events (i.e., fire). Specifically, failure to protect safe shutdown cables and equipment from fire damage negatively affected the reactor safety mitigating systems cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Because this issue relates to fire protection and this non-compliance was identified as a part of the sites transition to NFPA 805, this issue is being dispositioned in accordance with Section 9.1, Enforcement Discretion for Certain Fire Protection Issues (10 CFR 50.48) of the NRC Enforcement Policy.
The significance of this licensee-identified non-compliance with 10 CFR Part 50, Appendix R, Section III.G.2, was determined by the results of the IMC 0609, Appendix F, Fire Protection Significance Determination Process, Phase III Quantitative Screening Approach. The quantitative screening approach performed by a Region II Senior Risk Analyst resulted in a calculated delta core damage frequency (CDF) of less than 1E-04, which screens this non-compliance to less-than-red significance. Additionally, in order to verify that this non-compliance was not associated with a finding of high safety significance (Red), inspectors reviewed qualitative and quantitative risk analyses performed by the licensee. These risk evaluations took ignition source and target information from the ongoing HNP fire PRA to demonstrate that the significance of the non-compliances were less-than-red (i.e. CDF less than 1E-4/year). The inspectors also performed walk-downs to verify key assumptions were applicable. Based on the ignition frequency of fire sources in the affected areas, inspectors determined that the significance of this non-compliance was less-than-red. The inspectors also noted that the values in the licensees quantitative analysis were conservative, in that they used screening values instead of more detailed values. This provided additional confidence that this non-compliance was not associated with a finding of high safety significance (Red).
The inspectors determined that no cross cutting aspect was applicable to this performance deficiency because this finding was not indicative of current licensee performance.
Basis for Discretion:
The NRC exercised enforcement discretion in accordance with Enforcement Policy, Section 9.1, Enforcement Discretion for Certain Fire Protection Issues (10 CFR 50.48), a Confirmatory Order (ML16223A467) which extended the period for discretion, and Inspection Manual Chapter 0305. On April 4, 2018 (ML18096A955), the licensee submitted a license amendment request to adopt NFPA 805 and change their fire protection licensing bases to comply with 10 CFR 50.48(c). The inspectors reached this conclusion due to the fact that this issue was licensee-identified and will be addressed during the licensees transition to NFPA 805, it was entered into the licensees corrective action program, immediate corrective action and compensatory measures were taken, it was not likely to have been previously identified by routine licensee efforts, it was not willful, and it was not associated with a finding of high safety significance (Red).
EXIT MEETINGS AND DEBRIEFS
The inspectors verified no proprietary information was retained or documented in this report.
- On July 19, 2018, the inspectors presented the quarterly baseline inspection results to Gary Brinson, and other members of the licensee staff.
DOCUMENTS REVIEWED
71111.01: Adverse Weather Protection
Procedures:
34AB-S11-001-0, Operation with Degraded System Voltage, Ver. 4.1
NMP-OS-020, Station Response to Southern Company Alert Conditions, Ver. 1.2
71111.04: Equipment Alignment
Procedures:
34SO-R43-001-1, Attachment 3, Diesel Generator 1A and 1C Valve Lineup, Ver. 28.1
34SO-E21-001-2, Attachment 3, Core Spray System Valve Lineup, Ver. 25.11
34SO-R43-001-2, Attachment 3, Diesel Generator 2A and 2C Valve Lineup, Ver. 29
Drawings:
H-11631 Sht. 1, Diesel Generator 1A & 1C P&ID Sheet 1, Unit 1, Ver. 31.0
H-11600 Sht. 2, P&ID for Service Water at Diesel Generator, Unit 1, Ver. 37.0
H-21074, Diesel Engine & Fuel Oil System P&ID, Unit 2, Ver. 55.0
Documents:
Unit 1 Technical Specifications, Amendment 288
Unit 2 Technical Specifications, Amendment 234
Condition Reports:
10498152
71111.05AQ: Fire Protection Annual/Quarterly
Drawings:
A-43965 Sht. 54B, CRD and Drywell Sump Room, Fire Zone 1205C, Ver. 2.0
A-43966 Sht. 50B, Control Room Roof, Fire Zone 0031, Ver. 1.0
A-43965 Sht. 51B, South East Residual Heat Removal and Core Spray Room Unit 1, Fire Zone
203B, Ver. 2.0
A-43965 Sht. 22B, RPS Battery Room 2B, Fire Zone 2010, Ver. 4.0
A-43965 Sht. 14B, RPS Battery Room 1B, Fire Zone 1009, Ver. 2.0
A-43965 Sht. 15B, RPS Battery Room 1A, Fire Zone 1010, Ver. 4.0
A-43965 Sht. 21B, RPS Battery Room 2A, Fire Zone 2009, Ver. 3.0
A-43965 Sht. 55B, Unit 1 HPCI Pump Room, Fire Zone 1205Z, Ver. 2.0
Documents:
Fire Protection Fire Hazards Analysis (FHA), Rev. 36.0
Condition Reports (*NRC Identified):
- 10480359 *10486412 *10487128 *10488339 *10491165 *10491167
71111.06: Flood Protection Measures
Procedures:
2PM-Y46-001-0, Inground Pullbox Debris Removal/Inspection, Ver. 10.0
Documents:
Hatch Final Safety Analysis Report, Section 2.4, Rev. 36.0
Condition Reports:
10490488
71111.07: Heat Sink Performance
Procedures:
NMP-ES-012, Heat Exchanger Program, Ver. 11.0
NMP-ES-024-701, Eddy Current Testing of Heat Exchanger Tubing, Ver. 3.1
NMP-MA-027, Heat Exchanger Tube Plugging, Ver. 3.0
2IT-TET-012-1, Plant Service Water and RHR Service Water Piping Inspection Procedure,
Ver. 2.14
2SV-R43-001-0, Diesel, Alternator, and Accessories Inspection, Ver. 30.4
Work Orders:
SNC600263
Condition Reports:
10491516
71111.11: Licensed Operator Requalification Program
Procedures:
34SO-C71-001-2, 120 VAC RPS Supply System, Ver. 15.0
34GO-OPS-005-1, Power Changes, Ver. 29.1
34GO-OPS-005-2, Power Changes, Ver. 30
Documents:
Plant Hatch Emergency Preparedness 2018 Plant Drill 01, dated April 24, 2018
Condition Reports (*NRC Identified):
- 10484362 *10488628 *10487777
71111.12: Maintenance Effectiveness
Procedures:
NUMARC 93-01, Industry Guideline for Monitoring the Effectiveness of Maintenance at Nuclear
Power Plants, Rev. 4A
NMP-ES-027, Maintenance Rule Program, Ver. 7.0
NEI 99-02, Regulatory Assessment Performance Indicator Guideline. Rev. 7
Documents:
Maintenance Rule Unavailability Hours - 1R28 Outage
(A)(1) Evaluation for 1B Reactor Feed Pump
Maintenance Rule Expert Panel Meeting Minutes, 2018-04
2A EDG (2R43-S001A) Past Operability Review, 2018-06
R43-01: Stand-by A/C Power Maintenance Rule Evaluation, 2018-06
Condition Reports:
10468179 10480228 10489583 10498152
71111.13: Maintenance Risk Assessments and Emergent Work Evaluation
Procedures:
NMP-OS-010-002, Hatch Protected Equipment Logs, Ver. 11.0
Documents:
Equipment Out of Service Calculations 4/02/2018
Equipment Out of Service Calculations 4/18/2018
Equipment Out of Service Calculations 5/3/2018
Equipment Out of Service Calculations 5/8/2018
Equipment Out of Service Calculations 5/30/2018
Drawings:
01-10-00 Sht.09-100, Georgia Integrated Transmission System Substation Diagram, Hatch
500/230KV, Revised 04/16/2018
01-10-00 Sht.09-101, Georgia Integrated Transmission System Substation Diagram, Hatch Unit
1, Revised 04/03/2018
71111.15: Operability Determinations and Functionality Assessments
Procedures:
NMP-AD-012, Operability Determinations and Functionality Assessments, Ver. 13.3
NMP-AD-012-GL02, Functionality Assessment Guideline, Ver. 6.0
NMP-AD-012-GL03, Immediate Determination of Operability Guidelines, Ver. 3.0
Documents:
Unit 1 Technical Specifications, Amendment 288
Unit 2 Technical Specifications, Amendment 234
Past Operability Review, 2A EDG
Prompt Determination of Operability (PDO), Containment Spray (CS) and Residual Heat
Removal (RHR) Room coolers, Rev. 1-18-004
PDO, Unit 1 Division 1 Plant Service Water (PSW) Supply Header, Rev. 1-18-003/1.0
Troubleshooting Log, Unit 1 RHR Increased Loop Pressure, Dated May 15, 2018
Condition Reports:
10484768 10485173 10486169 10486859 10492952 10493644
10497648 10498152 10498463 10498509 10498527 10502759
10504784 10505033
71111.18: Plant Modifications
Procedures:
NMP-ES-054, Temporary Modifications, Ver. 3.1
NMP-ES-054-001, Temporary Modification Processing, Ver. 3.2
Documents:
SNC947269, 2T47C001A Drywell Return Air Fan Motor Replacement, Rev. 1.0
Condition Reports:
- 10490986 10494186 10496217 10496360 10496486
71111.19: Post Maintenance Testing
Procedures:
NMP-MA-009-001, Foreign Material Exclusion Program Requirements, Ver. 10.0
NMP-MA-014-001, Post Maintenance Testing Guidance, Ver. 4.3
34IT-E51-003-1, RCIC Turbine Speed Control Test, Ver. 5.4
34SO-B31-001-2, Reactor Recirculation System, Ver. 46.8
34SO-C51-001-0, TIP System Operation and LPRM Calibration, Ver. 19.1
34SV-C11-003-1, Rod Control Exercise, Ver. 17.3
34SV-R43-006-1, Diesel Generator 1C Monthly Test, Ver. 14.1
34SV-R43-005-2, Diesel Generator 1B Semi-annual Test, Ver. 20.0
34SV-R43-011-2, Diesel Generator 2A 24 Month Operability Test, Ver. 5.2
Work Orders:
SNC690520 SNC858864 SNC907093 SNC947513
Condition Reports:
10436719 10480898 10498527 10501621
71111.20: Refueling and Other Outage Activities
Condition Reports:
10497957 10497975
Procedures:
34GO-OPS-001-2, Plant Startup, Ver. 49.1
34GO-OPS-013-2, Normal Plant Shutdown, Ver. 32.2
71111.22: Surveillance Testing
Procedures:
34SV-C1-005-005-2, Turbine Control Valve Fast Closure Instrument Functional Test, Ver.17.0
34SV-E11-001-2, Residual Heat Removal Pump Operability, Ver. 19.3
34SV-E21-001-1, Core Spray Pump Operability, Ver. 22.3
34SV-SUV-019-2, Surveillance Checks (Unidentified Leak rate Calculation), Ver. 41.15
2PM-P41-036-2, Unit 2 Plant Service Water Pump and Motor Major Inspection/Overhaul,
Ver.9.0
64CH-SAM-025-0, Reactor Coolant Sampling and Analysis, Ver. 44.2
Work Orders:
SNC889958 SNC889964
Condition Reports (*NRC Identified):
- 10484161 *10489655
71114.06: Drill/Training Evaluation
Documents:
Plant Hatch Emergency Preparedness 2018 Plant Drill 01, dated April 24, 2018
Section 71124.06 - Radioactive Gaseous and Liquid Effluent Treatment
Procedures, Guidance Documents, and Manuals
64CH-RPT-006-0, Liquid Effluent Reports, Ver. 22.1
64CH-RPT-007-06, Gaseous Effluent Reports, Ver. 9.1
64CH-SAM-028-0, Releases via Planned and Unplanned Routes: Sampling and Analysis, Ver.
10.2
64CI-OCB-001-0, Main Stack Radiation Monitoring, Ver. 13.1
64CI-OCB-002-1, Unit One Reactor Building Vent Radiation Monitoring, Ver. 12.1
64CI-OCB-002-2, Unit Two Reactor Building Vent Radiation Monitoring, Ver. 16.2
64CI-OCB-003-1, Recombiner Building Vent Radiation Monitoring, Ver. 14.2
HNP-ODCM, Offsite Dose Calculation Manual for Edwin
- I. Hatch Nuclear Plant, Ver. 24
Records and Data
Calibration Record, Source Calibration of Main Stack Radiation Monitor 1D11-K600A per
Procedure 64CI-OCB-001-0, 01/25/2016
Calibration Record, Source Calibration of Main Stack Radiation Monitor 1D11-K600B per
Procedure 64CI-OCB-001-0, 01/25/2016
Calibration Record, Source Calibration of Unit 2 Reactor Building Vent (Normal Range)
Radiation Monitor 2D11-K636A per Procedure 64CI-OCB-002-2, 09/07/2016
Calibration Record, Source Calibration of Unit 2 Reactor Building Vent (Normal Range)
Radiation Monitor 2D11-K636B per Procedure 64CI-OCB-002-2, 09/07/2016
Calibration Record, Source Calibration of Unit 1 Recombiner Building Vent Radiation Monitor
1D11-K763B per Procedure 64CI-OCB-003-1, 04/25/2017
Certificate of Calibration, Standard Radionuclide Source, S/N 93549F [HNP source ID # Cd-
109-147], 06/23/2013
Certificate of Calibration, Standard Radionuclide Source, S/N 73715-06 [HNP source ID # Co-
60-146], 09/18/2006
Certificate of Calibration, Standard Radionuclide Source, S/N 73713-06 [HNP source ID # Cs-
137-284], 09/18/2006
Interlaboratory Cross-Check Results, First and Third Quarters 2017, Various Dates
Waste Stream Characterization (10 CFR Part 61 Analysis Data) Data, Dry Active Waste (DAW),
U-1 and U-2 CPS Resin, U1 and U-2 Primary Resin, 02/02/2018 thru 02/05/2018
Work Order (WO) SNC523180, Calibration of U-1 Main Vent Stack and Reactor Building Vent
Stack Accident Range Radiation Monitors 1D11-P007 [after detector replacement],
11/21/2014
WO SNC534541 and SNC730521, Calibration of U-2 Reactor Building Vent Stack Accident
Range Radiation Monitors 2D11P601, 08/25/2014 and 08/07/2017
WOs SNC562755 and SNC754124, Calibration of U-2 Drywell High Range Radiation Monitor
2D11K621A and B, 01/03/2015 and 01/26/2017
WO SNC 617713, Control Room Habitability Filter Testing, Train Z41-D004A [Filter DOP Test
and Charcoal Sample Analysis], 10/19/2016
WO SNC 617716, Control Room Habitability Filter Testing, Train Z41-D004B [Filter DOP Test
and Charcoal Sample Analysis], 11/29/2016
WOs SNC643031 and SNC821119, Calibration of U-1 Drywell High Range Radiation Monitors
1D11K621A and B, 12/27/2015 and 09/27/2017
WO SNC754510, Calibration of U-1 Main Vent Stack and Reactor Building Vent Stack Accident
Range Radiation Monitors 1D11-P007 and 1D11-P601, 03/11/2017
Hatch Annual Radiological Environmental Operating Report (AREOR) for 2016 and 2017,
5/15/2017 and 5/14/2018
Hatch Annual Radioactive Effluent Release Report (ARERR) for 2016 and 2017, 4/26/2017 and
4/25/2018
Corrective Action Program (CAP) Documents
CR 10255887
CR 10278613
CR 10338211
CR 10339649
CR 10410370
CR 10425479
NMP-GM-002, Corrective Action Program, Ver. 14.1
NMP-GM-002-001, Corrective Action Program Instructions, Ver. 36.2
Section 71124.07 - Radiological Environmental Monitoring Program
Procedures, Guidance Documents, and Manuals
57IT-Y33-001-0, Climatronics Instruments, Ver. 7.4
64EV-ENV-001-0, Airborne Dust and Gaseous Iodine Air Sampling Flow Calibration, Ver. 1.0
64EV-ENV-002-0, Airborne Dust and Gaseous Iodine Sampling, Ver. 1.2
64EV-ENV-009-0, River Water Sampling, Ver. 1.0
NMP-EN-002, Radiological Groundwater Protection Program, Ver. 7.0
NMP-EN-002-GL02, HNP Groundwater Monitoring Plan for Radionuclides, Ver.1.0
NMP-EN-002-GL04, Radiological Groundwater Protection Program Technical Bases, Ver. 1.0
Records and Data
Edwin I. Hatch Nuclear Generating Plant Environmental OSLD Data for 2016 and 2017
Edwin I. Hatch Nuclear Generating Plant 2016 Annual Groundwater Monitoring Report
Edwin
- I. Hatch Nuclear Power Plant EPRI Priority Index Worksheet, October 2017 Revision
Georgia Power Environmental Radiochemistry - 2016 Performance Evaluation Samples
Georgia Power Environmental Radiochemistry - 2017 Performance Evaluation Samples
Gamma Spectrum Analysis U1 CST for 2016, 2017 and 2018 to date, APEX Numbers 72515,
73802, 74947, 75741, 76388, 77318, 78001, 78586, 79588, 80446, 81293, 81308, 82015,
2889, 84365, 85647, 86388, 87032, 87855, 88526, 89151, 89886,90397, 91096,91698,
271, 92483, 92484, 93321, 94071, 94650 and 95344
Gamma Spectrum Analysis U2 CST for 2016, 2017 and 2018 to date, APEX Numbers 72516,
73382, 74950, 75742, 76389, 77317, 78002, 78587, 79589, 80483, 81292, 82049,82890,
84366, 85648, 86389, 87033, 87035, 87856, 88527,88564, 89152, 89821, 90398, 91097,
91699, 92272, 93309, 94639 and 95270,
Georgia Power Environmental Lab Radiochemistry Gamma Isotopic Result for Sample Number
1-2018-03-02-12-2018.
Hatch Nuclear Plant Work Practices Risk Assessment, 2017
HNP Air Sampler Calibration Field Sheets for Sample Station #s 103, 107, 112, 116 & 304,
dated 10/14/2016 and 04/10/2017
ODCM for Edwin
- I. Hatch Nuclear Plant, Version 24.0
R-2744291H-006, Plant Hatch Annual Meteorological Report 2016, Rev 0
R-2744291H-007, Plant Hatch Annual Meteorological Report 2017, Rev 0
Work Order (W/O) # SNC793044, 57IT-Y33-001-0, Climatronic Instruments Calibration,
06/12/2017
W/O # SNC812349, Yard Structures Meteorological, 03/16/2017
W/O # SNC831764, 57IT-Y33-001-0, Climatronic Instruments Calibration, 12/20/2017
2016 and 2017 Annual Radiological Environmental Operating Report
Corrective Action Program (CAP) Documents
CR 10181436
CR 10233673
CR 10340817
CR 10427749
CR 10431394
CR 10434336
CR 10459149
CR 10461270
CR 10476929
CR 10494018
CR 10505088
NMP-GM-002, Corrective Action Program, Ver. 14.1
NMP-GM-002-001, Corrective Action Program Instructions, Ver. 36.2
71151: Performance Indicator Verification
Procedures:
NMP-AD-029, Preparation and Reporting of Regulatory Assessment Performance Indicator
Data and the Monthly Operating Report, Ver. 1.1
NMP-DP-001-GL01, Risk Assessment Worksheets, Ver. 11.1
NMP-HP-206, Issuance, Use, and Control of Radiation Work Permits, Ver. 4.3
Documents:
NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Rev. 7.0
Records and Data
Gamma Spectrum Analysis Report 27Feb18-007, Main Stack Particulate, 02/27/2018
Gamma Spectrum Analysis Report 27Feb18-002, Main Stack Charcoal, 02/27/2018
Gamma Spectrum Analysis Report 28Feb18-004, U2 RBV Particulate, 02/28/2018
Gamma Spectrum Analysis Report 28Feb18-005, U2 RBV Charcoal, 02/28/2018
Gaseous Release Permit G-20180220-030-C, Main Stack, 02/27/2018
Gaseous Release Permit G-20180221-032-C, Reactor Building Vent, Unit One, 02/28/2018
Hatch Key Performance Indicators, January 2017 through February 2018
Liquid Release Permit L-20180217-021-B, Waste Sample Tank B, Unit One, 02/18/2018
ALARA Briefing Sheet - Replacement of the Transfer Canal Gate Seal, 03/14/2018
Electronic Dosimeter Dose and Dose Rate Alarms, February 2017 to March 2018
Hatch Key Performance Indicators - February 2017 to February 2018, 03/19/2018
Self-Assessment High, Locked and Very High Radiation Area Access Control, 08/03/2017
Survey #155733, Plant Hatch RF Cask Pit (2RX228), 03/04/2018
Survey #155728, Plant Hatch RF Cask Pit (2RX228), 03/04/2018
CAP Documents
CR 02197169
CR 02204181
CR 10324140
CR 10328406
CR 10333129
CR 10439725
CR 10461882
CR 10472292
71152: Problem Identification and Resolution
Procedures:
34AB-C11-004-2S, Mispositioned Control Rods, Version 4.3
34GO-OPS-065-0, Control Rod Movement, Version 14.0
NMP-ES-021, Structural Monitoring Program for the Maintenance Rule, Ver. 10.0
NMP-GM-002, Corrective Action Program, Version 14.4
Documents:
SNC-843238-01, Hatch Unit 2 Structural Maintenance Inspection Report 2017
Condition Reports (*NRC Identified):
238732 10319598 10328432 10458271 10485050 10486201
- 10486751 10489906 10490691 10490702 *10496723 10492356
10493675 10493676 10493682 10493836 10495981 10498306
- 10505037 10505214 2001000891
71153: Follow-up of Events and Notices of Enforcement Discretion
Documents:
0380-0042-MO-01, U1 MOVs in Pressure Boundary Evaluation Scope Calculation, Rev. 2
0380-0042-MO-02, U2 MOVs in Pressure Boundary Evaluation Scope Calculation, Rev. 2
Information Notice No. 92-18, Potential for Loss of Remote Shutdown Capability During a
Control Room Fire, February 28, 1992
RBA-18-002-H, IN 92-18 VALVE RISK ASSESSMENT, March 21, 2018
RBA-18-003-H, IN 92-18 VALVE RISK ASSESSMENT UPDATE, April 11, 2018
21