Information Notice 2017-04, High Energy Arc Faults in Electrical Equipment Containing Aluminum Components

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High Energy Arc Faults in Electrical Equipment Containing Aluminum Components
ML17058A343
Person / Time
Issue date: 08/21/2017
From: Louise Lund, Mcginty T
Division of Construction Inspection and Operational Programs, Division of Policy and Rulemaking
To:
Harris B, NRR/DPR/PGCB, 301-415-2277
References
TAC MF9285 IN-17-004
Download: ML17058A343 (14)


ML17058A343 UNITED STATES

NUCLEAR REGULATORY COMMISSION

OFFICE OF NUCLEAR REACTOR REGULATION

OFFICE OF NEW REACTORS

WASHINGTON, DC 20555-0001

August 21, 2017

NRC INFORMATION NOTICE 2017-04: HIGH ENERGY ARCING FAULTS IN ELECTRICAL

EQUIPMENT CONTAINING ALUMINUM

COMPONENTS

ADDRESSEES

All holders of an operating license or construction permit for a nuclear power reactor under

Title 10 of the Code of Federal Regulations (10 CFR) Part 50, Domestic Licensing of

Production and Utilization Facilities, except those who have permanently ceased operations

and have certified that fuel has been permanently removed from the reactor vessel.

All holders of an operating license for a non-power reactor (research reactor, test reactor, or

critical assembly) under 10 CFR Part 50, Domestic Licensing of Production and Utilization

Facilities, except those who have permanently ceased operations.

All holders of and applicants for a combined license under 10 CFR Part 52, Licenses, Certifications, and Approvals for Nuclear Power Plants.

PURPOSE

The U.S. Nuclear Regulatory Commission (NRC) is issuing this information notice (IN) to inform

addressees of operating experience and recent NRC testing results pertaining to the magnitude

of arc fault hazards in electrical equipment containing aluminum components. The NRC

expects that recipients will review the information for applicability to their facilities and consider

actions, as appropriate. The suggestions in this information notice are not NRC requirements;

therefore, the NRC requires no specific action or written response.

DESCRIPTION OF CIRCUMSTANCES

NRC-Led International Testing Program Insights

From 2014 to 2016, the Office of Nuclear Regulatory Research (RES) collaborated in a testing

program with the Nuclear Energy Agency (NEA), the National Institute of Standards and

Technology, and various international partners through the Organization for Economic and

Cooperative Development (OECD). The purpose of the testing program was to confirm the

zone of influence (ZOI) for high energy arcing fault (HEAF) events that was specified in

NUREG/CR-6850 EPRI 1011989 EPRI/NRC-RES Fire PRA Methodology for Nuclear Power

Facilities, Volume 2: Detailed Methodology (Agencywide Documents Access and Management

System (ADAMS) Accession No. ML15167A411). RES initiated the testing program after

reviewing international HEAF events documented in the OECD Fire Project - Topical Report

No.1, Analysis of High Energy Arcing Fault (HEAF) Fire Events, published in June 2013 (https://www.oecd-nea.org/nsd/docs/2013/csni-r2013-6.pdf). The testing protocol initiated the arc by installing a bare copper wire across the three phases of

power in accordance with IEEE C37.20.7-2007/Cor 1-2010, Guide for Testing Metal-Enclosed

Switchgear Rated up to 38 kV for Internal Arcing Faults Corrigendum 1. No accelerants were

used to initiate the fault or ensuing fire conditions. The testing was performed using actual

electrical equipment from nuclear power plants. There were four primary controlled parameters

that were varied as part of the testing programarc location, fault current, voltage and fault

duration:

1. Arc location - operating experience from HEAF events was used to select representative

arc locations within the enclosure. Typically the arc locations were across breaker

stabs, at enclosure power supply entry locations, or along bolted connections within the

enclosure that could be subject to fatigue failures.

2. Fault current - the arc fault currents were selected to replicate fault capacities of typical

electrical distribution systems within nuclear power plants.

3. Voltage - The voltages were selected from typical voltages used in nuclear power

plants power distribution systems. The program tested both low and medium voltage

equipment.

4. Arc duration - The duration selected for the HEAF tests was a controlled parameter and

based on a review of operating experience where arc duration information was readily

available from fault recording devices, or could be determined from post arc fault

investigation.

This program has shown that HEAF tests involving aluminum resulted in a significantly larger

release of energy than HEAF tests involving copper. This aluminum involvement includes

components, subcomponents, or parts that form part of the normal current-carrying pathway

(such as bus bars, breaker armatures, contacts, cable, etc.), or components, subcomponents, or parts that could become involved in the fault current pathway as a result of a ground fault

(housings, structural framework, adapters, cradles, wireways, conduits, draw-out or racking

mechanisms, etc.). In addition to larger energy release during the HEAF event when aluminum

is involved, RES staff also observed dispersal of electrically conductive aluminum byproducts

throughout the area. This byproduct was conductive and caused short circuiting and grounding

of electrical equipment in the area. Through the testing program, RES staff observed that HEAF

tests involving aluminum damaged test measurement and recording equipment and the

electrical supply of the test facility well beyond the damage limits approximated in

NUREG/CR-6850 (EPRI 1011989).

A total of 26 tests were performed, consisting mostly of electrical equipment that contained

copper conductors. The equipment with copper components exhibited similar damage states to

those postulated in the current methodology presented in NUREG/CR-6850, Appendix M.

However, results obtained for equipment containing aluminum components exhibited damage

states well beyond current HEAF damage models. These results are summarized as follows:

Test 23 of the HEAF experimental series consisted of a low-voltage, 480 VAC

switchgear cabinet that contained an aluminum bus bar. The test resulted in failure of

the cabinet walls such that the plasma created by the arcing fault was expelled a

significant distance out of the cabinet. Inconel temperature sensors located

approximately 0.9 m (3 ft.) from the enclosure (which is the NUREG/CR-6850 horizontal

ZOI limit) were melted and destroyed during the test. The vapor/plasma cloud migrated

well beyond the current limit of 0.9 m (3 ft.) horizontal and 1.5 m (5 ft.) vertical distance

for the ZOI. In addition to the physical damage caused by the HEAF event, there was a

layer of aluminum byproducts that coated structures and components within the test cell. This aluminum byproduct layer caused shorting problems in the test facility electrical

power system and required major repair. This test is an outlier from the other

low-voltage tests performed as part of the experimental program. It was the only low

voltage experimental test to exhibit a level of damage beyond the NUREG/CR-6850,

Appendix M, ZOI methodology. In all other low-voltage tests, the temperature sensors

located 0.9 m (3 ft.) horizontally from the cabinet were not damaged, recorded data, and

were able to be used in subsequent experimental tests.

Test 26 of the HEAF experimental series involved a 4.16 kV bus duct section removed

from a decommissioned United States nuclear plant. The bus duct section consisted of

non-segregated copper bus bars enclosed within an aluminum duct. The bus duct

section was secured to the floor of the test enclosure using wooden structural members

and the open ends were secured with a sheet of electrically insulating fiber board. This

piece of fiber board was installed to create a pressure boundary within the bus duct unit

and limit the free release of energy once the fault was initiated. Immediately upon

initiating the HEAF event, the hot gas mixture forced the fiber board away, allowing the

arc and associated hot gas/plasma mixture to jet out of the bus duct, blowing hot

gas/molten metal linearly from the bus duct opening. The hot gases/plasma extended

approximately 9 m (30 ft.) horizontally. The instruments associated with temperature

and heat flux, located approximately 0.9 m (3 ft.) away from the duct, were damaged.

The test facility was coated with an electrically conductive aluminum byproduct and

several electrical components in the test cell required replacement.

The increased physical damage to the test specimens, measurement devices, and the testing

facility observed during tests 23 and 26 can be attributed to the involvement of aluminum during

the HEAF. The presence of aluminum in the components, subcomponents, or parts that form

part of the normal current carrying pathway causes a more energetic plasma development when

consumed during the arcing process. The increased energetic plasma causes a larger amount

of cabinet damage and/or the transport of gaseous high energy particles/plasma farther than

previously assumed. These two tests included aluminum components which resulted in

exceeding the ZOI documented in NUREG/CR-6850 and its Supplement 1. In both tests, a

major impact from the HEAF was a layer of aluminum byproducts that plated out on most

surfaces within the test enclosure, including electrical equipment. This aluminum byproduct

layer caused shorting problems in the test facility electrical power supply and required a major

repair and cleanup activity. The extent of damage observed from tests 23 and 26, which

contained aluminum components, far exceeded the damage observed from other tests which

did not contain aluminum components.

The OECD/NEA test report is publically available and can be downloaded at

https://www.oecd-nea.org/nsd/docs/indexcsni.html NEA/CSNI/R (2017) 7-Report on the Testing

Phase (2014-2016) of the High Energy Arcing Fault Events (HEAF) Project: Experimental

Results from the International Energy Arcing Fault Research Programme.

NRC Generic Issue Program

On May 6, 2016, RES submitted a possible generic issue involving an identified vulnerability of

electrical equipment containing aluminum components during a HEAF event (ADAMS

Accession No. ML16126A091). The issue was entered into the generic issue process on May

12, 2016, (ADAMS Accession No. ML16132A116) and an initial evaluation was performed

(ADAMS Accession No. ML16064A250). On May 20, 2016, a generic issue review panel was

formed (ADAMS Accession No. ML16209A007). The committee is currently in the screening phase, in

accordance with the NRCs Management Directive 6.4, Generic Issues Program (ADAMS

Accession No. ML14245A048).

United States Nuclear Power Plant Operating Experience

Fort Calhoun Station, Unit 1

On June 7, 2011, a switchgear fire occurred at the Fort Calhoun Station while the plant was

shut down for a planned refueling outage. The fire resulted in a loss of power to six of nine

safety-related 480 VAC electrical distribution buses, one of two safety-related 4160 VAC buses

and one of two non-safety related 4160 VAC buses. The event resulted in the loss of the spent

fuel pool cooling function and could have resulted in the loss of a safety function or multiple

failures in systems used to mitigate a situation had the event occurred at power. Significant

unexpected system interactions also occurred. Specifically, combustion products from the fire

caused a fault across an open bus-tie breaker on an island bus; as a result a feeder breaker

tripped unexpectedly resulting in loss of power to the opposite train bus. Also, the event

resulted in grounds on both trains of safety-related direct current (DC) power used for breaker

operation and electrical protection.

Fort Calhoun Station originally used General Electric AKD-5 Powermaster Low Voltage Drawout

Switchgear, with a welded aluminum bus bar structure that transitioned to copper bus stabs in

each breaker cell. The original AK-50 circuit breakers connected directly to the silver-plated

areas on the line and load stabs. The new Nuclear Logistics Incorporated/Square-D circuit

breaker design was an integrated unit consisting of a circuit breaker and cradle assembly. The

cradle assembly converted the internal vertical breaker connectors in the new breaker to top

and bottom spring-loaded horizontal finger assemblies which connected to the original

switchgear bus stabs.

The fire was caused by the catastrophic failure of the feeder breaker for 480 VAC load center

1B4A in the west switchgear room. A large quantity of soot and smoke was produced by the fire

which migrated into the conducting connections associated with the non-segregated bus duct (a

metal enclosure containing the bus bars for all three electrical phases) connecting to island bus

1B3A-4A, even though the bus-tie breaker was open. The smoke and soot were sufficiently

conductive that arcing occurred between the bus bars such that island bus 1B3A-4A was

affected and the other connected train load center, 1B3A, was affected by incorrect breaker

sequencing.

The licensee's root cause investigation concluded that the initial fire in the load center was the

result of high resistance connections on the line side of the feeder breaker cubicle, which

caused overheating and failure of the cradle finger clusters, resulting in bus grounding and

phase-to-phase shorting. The investigation also determined that combustion products from the

fire caused a fault on the island bus side of the bus-tie breaker (BT-1B4A), which resulted in an

overcurrent condition through two breakers (feeder breaker 1B3A and bus tie breaker BT-

1B3A). The licensees initial investigation determined that breaker 1B3A tripped prematurely on

a short-time overcurrent fault and concluded that since the breaker protection scheme did not

operate as designed, bus 1B3A de-energizing resulted in the loss of multiple electrical power

distribution system trains from a single fire. Appropriate breaker coordination was required by

the licensees fire protection program to ensure that the plant could achieve and maintain safe

shutdown conditions following a fire. The maximum conditional core damage probability for the event was estimated to be

3.4 x 10-4. At the time of the fire, Fort Calhoun Station was experiencing impacts from flooding

of the Missouri River and had declared a Notice of Unusual Event on June 6, 2011. Additional

information is available in Licensee Event Report (LER) 2011-008, Revision 1, for the Fort

Calhoun Station, Fire in Safety Related 480 Volt Electrical Bus (ADAMS Accession

No. ML113010208), and Fort Calhoun Station - NRC Special Inspection Report 05000285/2011014; Finding of Preliminary High Safety Significance (ADAMS Accession

No. ML12072A128).

Columbia Generating Station

On August 5, 2009, at 7:49 a.m., while operating at 100 percent rated thermal power, the main

generator experienced a differential current lockout. This resulted in a main generator overall

differential lockout trip, causing a turbine trip and a fast transfer from the output of the main

generator to the startup transformer (normal breakers opened and start up breakers closed). As

a result of the turbine trip with reactor power above 30 percent, an automatic reactor scram

occurred.

At 7:51 a.m., the control room received a report from the turbine building of a fire in the electrical

bus duct above switchgear SM-3. This resulted from a fault on the non-segregated 6900 VAC

bus that supplies power from the normal auxiliary transformer to switchgears SH-5 and SH-6.

The bus catastrophically failed and vaporized all three phases of the conductor in the location of

a flexible bus connection link. The faulted bus section was located above switchgear SM-3.

Operators notified the fire brigade to respond. At 7:53 a.m., operators closed the inboard main

steam isolation valves to halt the reactor vessel depressurization and cooldown, however, the

technical specification cooldown limit of 100°F was exceeded. Operators called the offsite fire

department for assistance due to heavy smoke in the turbine building.

The licensees root cause evaluation determined that the fault was located on the

non-safety-related, non-segregated, 6900 VAC N2/X bus. The bus catastrophically failed, melting all three phases of conductor in the location of a flexible link. The bus bars are

completely enclosed in aluminum ducts, with all three phases in the same duct

(non-segregated). The bars were a combination of aluminum square hollow tubing and copper

connection plates and were mounted on porcelain insulators with spring washers. The bars

were assembled together using a series of rigid and flexible connections.

The faulted bus section was located above the medium voltage switchgear SM-3 and damage

from the molten metal produced by the fault included another high voltage bus and other cables

in the area of switchgears SH-5 and SH-6. The licensee inspected the damage and noted the

explosion melted and removed approximately 1.2 m (4 ft.) of each of the three buses and 2.4 m

(8 ft.) of the bus duct enclosure. Both the bus and the bus duct enclosure were made of

aluminum. This bus duct was located at approximately 4.6 m (15 ft.) above finished floor. The

molten aluminum and debris was thrown in the general vicinity. Photographs revealed that a

circular pattern of material remained. The licensee evaluation concluded that the fault likely

originated on the center flexible link of the bus connection. However, the licensee concluded

that the root cause of the failure was indeterminate, because the catastrophic failure of the bus

destroyed any evidence that would have provided an indication as to the cause. The remaining

bus duct showed signs of high heat exposure. Observed from the ground were smoke streaks at all metal joints and covers for a distance of 6 m (20 ft.) south and about 3 m (10 ft.) north of

the missing section.

The licensee determined that the most probable cause of the event was the

relaxation/loosening of a bolted connection on the flexible link from repeated thermal cycles

over time. The relaxation/loosening of the bolted connection resulted in degradation and

overheating of the connection. The insulation continued to degrade to the point where a short

occurred between two phases of the bus. The short destroyed the bus and the surrounding bus

enclosure. The molten aluminum and copper splattered nearby switchgear cabinets but did not

cause any internal damage. A possible contributor to the non-segregated bus failure was

attributed to running the bus near its original rating of 2500 amps. The nominal bus loading at

90 percent capacity was closer to the rating than the other four buses, and, therefore, could

have caused higher temperatures and connection degradation. The licensee performed a bus

uprate analysis in 1994 and increased the rating to 2806 amps to account for the worst case

loading of 2610 amps.

Additional information is available in LER 2009-004-00, for Columbia Generating Station, 6.9 kV Non-Segregated Electrical Bus Failure (ADAMS Accession No. ML092870468), and

Columbia Generating Station - NRC Special Inspection Report 05000397/2009010 (ADAMS

Accession No. ML093280158).

Diablo Canyon Nuclear Power Plant, Unit 1

On May 15, 2000, at 12:25 a.m., at 100 percent power, Diablo Canyon, Unit 1 experienced a

turbine/reactor trip. The cause of the unit trip was an electrical phase-to-phase fault on the

12 kV bus in an overhead bus duct supplied by auxiliary transformer 1-1. The switchyard and

main generator field breaker opened immediately following the unit trip; however, coast down of

the main generator continued to feed the arc fault. The fault and subsequent arcing damaged a

4 kV startup bus duct located immediately above the faulted 12 kV bus. Damage to the 4 kV

bus induced a second arcing fault in the 4 kV bus duct resulting in a differential trip of startup

transformer 1-2 that occurred 11 seconds after the initial fault. The loss of both offsite sources

of power to all 4 kV loads resulted in an undervoltage condition that caused the emergency

diesel generators to start and load successfully.

The cause of the bus failure could not be conclusively determined due to the absence of

physical evidence. The immediate cause was postulated to be a thermal failure of the bolted

connection of the center conductor of the 12 kV bus. The faulted nonsegregated bus duct

consisted of three conductors of aluminum in a sealed bus duct enclosure. The bus

connections consist of silver-plated splice plates bolted to the silver-plated bus bars and

insulated with polyvinyl chloride (PVC) boots or Raychem tape. It is postulated that the PVC

boot failed due to the excessive heat and created smoke. The radiant heat from the center

conductor caused the insulation to fail on adjacent conductors. The smoke provided an ionized

environment for a phase-to-phase arc from the center conductor to the south conductor.

Subsequently, there was arcing between all conductors.

Prior to returning Unit 1 to service, the licensee performed extensive inspections, tests, maintenance and repairs, including an effort to increase the capacity by replacing the 12 kV

aluminum bus conductors inside the turbine building with copper, from where the bus entered to

pass the damaged section. The licensee upgraded buses with little design margin from

aluminum to copper and installed large copper splice plates in select locations. Corrective

actions included a new preventative maintenance program and upgrades to the 4 kV and 12 kV nonsegregated buses on both units. Additional information is available in LER 1-2000-004-00,

Unit 1 Unusual Event Due to a 12 kV Bus Fault (ADAMS Accession No. ML003725220).

Zion Nuclear Power Station, Units 1 and 2

On April 3, 1994, at 4:30 a.m., Zion Nuclear Power Station, Unit 1 was synchronized to the

electrical distribution system after the completion of refueling outage Z1R13. The unit was

stabilized at 25 percent reactor power at 5:11 a.m. At 6:13 a.m., a 3 percent load increase was

initiated as required by fuel conditioning guidelines. At 6:18 a.m., a loud noise emanating from

the vicinity of the main generator was heard in the control room. Almost simultaneously, a main

generator lockout trip and subsequent turbine and reactor trips occurred with the main

generator tripping on differential current.

At 6:19 a.m., the operating personnel received a report of a fire emanating from the generator

lead box. The station fire alarm was sounded and the fire brigade was dispatched to extinguish

the fire. The shift engineer was notified at 6:30 a.m. that the fire brigade could not contain the

fire. The plant then requested offsite fire department assistance.

After the termination of the fire, the licensee performed an assessment of the damage to the

main generator and associated bus ducts. The A and B phase isophase bus ducts showed

signs of excessive arcing. The corners of the 90-degree turns on both phase housings were

blown outward, and aluminum spatter covered the general area of the fault. Large amounts of

white powder were also found in the A and B phase duct work (later determined to be aluminum

oxide). The conductors on both phases were also damaged. The bus duct cooling boundaries

for the A and B phases at the insulator penetration on the generator end were blown inward.

The retaining clamps for the A and B phase housings, located at the generator end, appeared to

have separated. One broken and several damaged stand-off insulators were also found. The C

phase bus duct sustained only minor damage in this event. An internal inspection of the

C phase bus duct, conducted by the licensee, found an oil film on the first and second standoff

insulators from the generator end.

The licensee also inspected the generator lead box and surrounding areas. The licensee

determined that the C phase bushing was severely damaged at the isophase shorting plate and

internal to the lead box. The A and B phase bushings sustained damage external to the lead

box. Molten metal was found in the area where the C phase bushing exits the lead box. The

micarta cleats which separate the generator from the lead box were blown upward into the

generator. Evidence of arcing between the top flange of the C phase bushing and the structural

ribbing of the lead box was discovered. Soot covered the inside of the lead box and appeared

to cover the lower third of the generator stator. The licensee also found evidence of arcing on

the neutral bus enclosure in the vicinity of the generator lead box.

The licensee determined that the root cause of the electrical fault was a main generator phase

C bushing failure. The licensee investigation found that the inner ceramic surface inside the

bushing insulator had been contaminated with an oily substance, and this contamination lead to

the failure. The high current arc from the C phase to the lead box resulted in the rupture of the

bushing internal and external to the lead box. This allowed hydrogen to escape into the

atmosphere. The hydrogen was ignited by the flashover and started to burn. The fault currents

generated were significant enough in magnitude to cause the fault damage observed on the

A phase winding of the west main power transformer. Although this scenario provides an

explanation for the high side neutral residual current recorded during the event, the physical damage observed during the internal inspection of the transformer is not of the magnitude seen

on other documented failures of this nature.

Samples of molten metal and fire residue obtained from the A and B phase bus ducts and the

C phase lead box were analyzed. The intent of this examination was to identify the presence of

any conductive foreign material which may have contributed to the flashover of the A and B

phases. Nothing out of the ordinary was found in this investigation. The majority of the material

examined was identified as aluminum. The white powder found in the ducts was identified as

aluminum oxide. The aluminum deposits were a result of the arcing that occurred on the A and

B phases, which are fabricated from aluminum. Additional information is available in LER

94-005-01 Unit 1 Main Reactor Trip and Subsequent Start of 1A Auxiliary Feedwater Pump

Following a Generator Fire and Isophase Bus Duct Fault (Legacy ADAMS Accession

No. 9801210070).

Shearon Harris Nuclear Power Plant, Unit 1

On October 9, 1989, at 11:05 p.m., with the plant at full power, a turbine/reactor trip occurred at

Shearon Harris Nuclear Power Plant, Unit 1, due to an electrical fault. The reactor was

stabilized in hot standby. The licensee determined that the initiating cause of the turbine/reactor

trip was multiple ground faults. The ground faults destroyed the neutral grounding bus and

caused three fires: (1) an oil fire at the B main power transformer; (2) a hydrogen fire

underneath the main generator; and (3) a small oil fire in the generator housing. The licensee

declared an alert and the site fire brigade responded to the fires. The site fire brigade was later

assisted by offsite fire departments.

The licensee determined that the ground faults were caused by aluminum debris carried down

the bus duct by the forced air cooling system. The aluminum debris entered the bus duct as a

result of previous damper failures in the bus duct cooling system in 1988 and 1989. Arcing

between the conductor and the enclosure occurred over a 15 m (50 ft.) length of the A phase

bus immediately upstream of the B main power transformer. Ionization from this arcing reduced

the dielectric strength of the cooling air which was carried into the bushing box of the B main

power transformer. This caused an A phase to ground flashover in the bushing box, which

immediately propagated to the B phase bushing. The fault cracked both low voltage bushings, causing oil to leak from the bushings and ignited the leaking oil.

The fault at the B main power transformer created magnetic forces in the main section of the

isolated phase bus that damaged insulators in A and B phase. The 58 cm (23 in.) diameter

tubular conductor is suspended in the middle of the 104 cm (41 in.) diameter aluminum

enclosure by the ceramic insulators. In the A bus duct, five insulators pulled apart, allowing the

conductor to come in contact with the grounded enclosure, creating a phase-to-ground fault.

As part of the corrective actions, the licensee evaluated the design of the isolated phase bus

duct bus supports and found it to be adequate. However, the sections in which the conductor

supports failed were rotated 180 degrees to place the supports underneath the conductor as a

prudent design measure. The licensee also revised the design of the isolated phase bus duct

cooling system to preclude debris intrusion into the ducts. The licensee has replaced the

damaged duct. Additional information is available in the Shearon Harris Nuclear Power Plant

LER 89-017-01, Electrical Fault on Main Generator Output Bus Causing Plant Trip and Fire

Damage in Turbine Building (Legacy ADAMS Accession No. 8912130259). Kewaunee Power Station

On July 10, 1987, at 11:43 a.m., with the plant at full power, a reactor/turbine trip occurred due

to an undervoltage transient on the 4160-volt electrical buses, which supply the reactor coolant

pumps and main feedwater pumps.

The control room operators received an unexpected reactor/turbine trip. Following normal

practice, the plant dispatched an equipment operator to verify that the auxiliary feedwater

pumps and diesel generators had started and were operating normally. Upon investigation, the

equipment operator noticed smoke and fire coming from the vicinity of the electrical bus bar

located on the eastern end of the turbine building, and immediately notified the shift supervisor.

The bus fire terminated once the transformer was de-energized. A smaller fire occurred on a

maintenance cart involving rags and rubber goods ignited by falling aluminum slag. The

equipment operator quickly extinguished this fire. At 11:46 a.m., the equipment operator

reported to the control room that the fire had been extinguished.

The licensee determined that the event was caused by a phase-to-ground fault which occurred

on the bus bar (1.3 cm by 10.2 cm [0.5-inch by 4-inch] flat aluminum bus bar rated at

3000 amps) routed from the main auxiliary transformer to buses 1-3, 1-4, 1-5 and 1-6. The fault

caused an undervoltage condition resulting in a reactor trip and subsequent turbine trip. The

bus undervoltage reactor trip is set at less than 77 percent of the rated bus voltage for greater

than 0.1 second. Plant systems performed as designed. The fast transfer prevented the

reactor coolant pumps from tripping on the undervoltage condition because of the time delay of

approximately 5 seconds in the pump breaker trip logic. A time delay relay of approximately

5 seconds is designed in the reactor coolant pump logic to prevent tripping of the pumps before

fast transfer to an offsite power supply.

The licensee determined that the root cause of the event was an insulation failure on the bus

bar compounded by accumulation of particulate debris. The bus bar runs perpendicular to

turbine building ventilation fans mounted in the turbine building exterior wall. Suction from the

fan pulled dust-filled air through the bus duct. Dust and metallic powder debris collected on the

outside of the bus bar insulation. The insulation failure combined with the accumulated dirt

provided a tracking path from phase to ground. The phase-to-ground fault progressed to a

phase-to-phase fault which accounted for the extensive bus damage. The event damaged a

9 meter (30 ft.) section of the bus bar from the main auxiliary transformer to buses 1-3, 1-4, 1-5 and 1-6. The equipment operator quickly extinguished the related fire. There was no other

equipment damage as a result of this event.

The damaged section of bus bar was isolated. The bus bar and main auxiliary transformer were

inspected to determine the extent of damage, and a temporary change request was

implemented to supply electrical buses 1-3 and 1-4 from the reserve auxiliary transformer. The

main auxiliary transformer supplied buses 1-1 and 1-2. Safeguards buses 1-5 and 1-6 remained in their normal lineup. In addition to the immediate corrective actions taken to replace

damaged components, the licensee inspected and cleaned various sections of the bus bar

ducting. The licensee implemented a triennial inspection procedure covering all bus bar

ducting. Additional information is available in LER 87-009-00, Electrical Bus Bar Failure

Causes Undervoltage on RXCP Buses and Reactor Trip (ADAMS Accession

No. ML111661536).

BACKGROUND

HEAF events have occurred in both United States and foreign nuclear power plants. HEAFs

are energetic and explosive faults in electrical equipment characterized by a rapid release of

energy in the form of heat, light, vaporized metal, and pressure increase due to high current

arcs between energized electrical conductors or energized conductors and ground or neutral.

HEAFs have the potential to cause extensive damage to the failed electrical components and

distribution systems along with adjacent equipment and cables. Furthermore, the significant

energy released during a HEAF event can act as an ignition source of nearby combustibles

resulting in an ensuing fire, which could potentially affect the performance of nearby structures, systems, and components (SSCs) important to safety.

The current method for estimating the damage from a HEAF for electrical enclosures is

contained in an industry/NRC fire probabilistic risk assessment methodology document, EPRI

1011989/NUREG/CR-6850 Appendix M. This method is based on a single well-documented

event that occurred at San Onofre Unit 3 in 2001. NUREG/CR-6850 Supplement 1 FAQ

07-0035 provides the current methodology for estimating damage specific to bus duct failures.

Recent international HEAF testing has been performed to better characterize the damage

potential and modes of failure. RES initiated this testing project after investigating international

HEAF events documented in the OECD Fire Project - Topical Report No.1, Analysis of High

Energy Arcing Fault (HEAF) Fire Events, NEA/CSNI/R (2013) published in June 2013 (https://www.oecd-nea.org/nsd/docs/2013/csni-r2013-6.pdf). The experimental test program

identified that the presence of aluminum can cause a more energetic plasma arc and

subsequent metal fire. Under some circumstances this may cause a larger amount of cabinet

damage and/or cause the transport of conductive aluminum byproducts further than previously

assumed.

Each operating nuclear power plant is required to have a fire protection plan that satisfies

General Design Criteria (GDC) 3 in Appendix A of 10 CFR Part 50. This is to ensure that SSCs

important to safety are designed and located to minimize the probability and effects of fires and

explosions. Licensees who have chosen to voluntarily adopt a risk-informed, performance-based fire protection program in accordance with 10 CFR 50.48(c) have typically

evaluated the hazard posed by HEAF events through the use of the EPRI/NRC-RES fire

Probabilistic Risk Assessment document, EPRI 1011989/NUREG/CR-6850. Licensees

adhering to a deterministic fire protection program either meet the prescriptive requirements of

Section III.G in Appendix R of 10.CFR 50.48(b) (or corresponding NRC staff guidance in

NUREG-0800) and approved exemptions, or have a NRC staff-approved safety evaluation

report on the fire protection program.

Related NRC Generic Communications and Documents:

The following NRC generic communications contains additional operating experience

addressing general electrical distribution equipment complications (non-aluminum related):

IN 1999-13, Insights from NRC Inspections of Low- and Medium-Voltage Circuit

Breaker Maintenance Programs,dated April 29, 1999 (ADAMS Accession

No. ML031040447).

IN 2000-14, Non-Vital Bus Fault Leads to Fire and Loss of Offsite Power, dated

September 27, 2000 (ADAMS Accession No. ML003748744). *

IN 2002-01, Metalclad Switchgear Failures and Consequent Losses of Offsite Power, dated January 8, 2002 (ADAMS Accession No. ML013540193).

IN 2002-27, Recent Fires at Commercial Nuclear Power Plants in the United States, dated September 20, 2002 (ADAMS Accession No. ML022630147).

IN 2005-21, Plant Trip and Loss of Preferred AC Power from Inadequate Switchyard

Maintenance, dated July 21, 2005 (ADAMS Accession No. ML051740051).

IN 2005-15, Three-Unit Trip and Loss of Offsite Power at Palo Verde Nuclear

Generating Station, dated June 1, 2005 (ADAMS Accession No. ML050490364).

IN 2006-18, Supplement 1, Significant Loss of Safety-Related Electrical Power at

Forsmark Unit 1 in Sweden, August 10, 2007 (ADAMS Accession No. ML071900368).

IN 2006-31, Inadequate Fault Interrupting Rating of Breakers, dated

December 26, 2006 (ADAMS Accession No. ML063000104).

IN 2007-14, Loss of Offsite Power and Dual-Unit Trip at Catawba Nuclear Generating

Station, dated March 30, 2007(ADAMS Accession No. ML070610424).

NUREG/IA-0470, Volume 1 Nuclear Regulatory Authority Experimental Program to

Characterize and Understand High Energy Arcing Fault (HEAF) Phenomena, dated

August 2016 (ADAMS Accession No. ML16235A163).

DISCUSSION

Title 10 CFR Part 50, Appendix A, GDC 3, Fire Protection states, in part, Structures, systems

and components important to safety shall be designed and located to minimize, consistent with

other safety requirements, the probability and effect of fires and explosions

Improper operation and maintenance practices represent the most significant contributors to

HEAF events. Additional contributing causes include the use of improper tools and equipment

during maintenance, introduction of conductive foreign material, insulation breakdown due to

aging, failure of tripping mechanisms, loose bolted connections due to vibrations or inadequate

maintenance practices, corrosion, improper work practices due to inadequate training, and a

lack of preventative maintenance. Any of these contributors could lead to the development of a

low resistance path between conductors or between conductors and ground, creating a HEAF

event.

For plants that have transitioned to a performance-based fire protection program under

10 CFR 50.48(c) and National Fire Protection Association Standard 805, HEAF events

constitute some of the high-risk scenarios. Recent testing suggests HEAFs involving aluminum

components may exceed the ZOI methodology presented in NUREG/CR-6850.

For plants that have not transitioned to a performance-based fire protection program, fire hazard

analyses performed to satisfy 10 CFR Part 50, Appendix A, GDC 3, may not have considered

HEAFs as potential failure modes, including explosions or the dispersion of aluminum

byproducts. These regulations include 10 CFR 50.48(a) and (b) and Appendix R to

10 CFR Part 50, Section III.G (or corresponding NRC staff guidance in NUREG-0800) and/or exemptions/deviations from these requirements granted in accordance with 10 CFR 50.12 or

established in the licensing basis.

The operating experience and recent testing presented in this information notice demonstrates

that the hazards from a HEAF may be substantially greater for electrical equipment that

contains aluminum components than for those with copper components. Additionally, the

operating experience and testing highlights the spread of an electrically conductive coating of

aluminum byproducts which could lead to additional failures. A summary of the aluminum

impact from operational experience is stated below:

The Fort Calhoun event illustrates the adverse effects caused by large quantities of

conductive aluminum byproducts in the smoke produced by HEAF events involving

aluminum which can adversely affect adjacent equipment. The event further resulted in

significant unexpected system interactions. Specifically, loss of power to both train A

and train B buses occurred. Also, the event resulted in grounds on both trains of

safety-related DC power used for breaker operation and electrical protection.

The Columbia event involved aluminum bus bars completely enclosed in aluminum

ducts. The event vaporized approximately 1.2 m (4 ft.) of each of the three buses and

2.4 m (8 ft.) of the bus duct enclosure and smoke and heat effects were observed at all

metal joints and covers for a distance of 6 m (20 ft.) south, and about 3 m (10 ft.) north of

the missing section.

The Diablo Canyon HEAF event damaged both the 12 kV bus duct and the 4 kV bus

duct. Both bus duct conductors were made of aluminum. The event led to the loss of

both offsite electrical sources and the reliance on emergency diesel generators.

The Zion HEAF event initiated a fire that the onsite fire brigade could not control. The

bus duct was made of aluminum and the A and B phase isophase bus ducts showed

signs of excessive arcing. The licensee found extensive aluminum spatter in the general

area of the fault as well as large amounts of white powder that were later determined to

be aluminum oxide. Additionally, the licensee stated that the physical damage observed

during inspections was greater than other documented failures of this nature.

The Shearon Harris event damaged over a 15.2 m (50 ft.) section of the phase A bus.

The bus duct enclosure was made of aluminum. The event also destroyed the neutral

grounding bus and caused three fires: (1) an oil fire at the B main power transformer, (2)

a hydrogen fire underneath the main generator, and (3) a third small oil fire in the

generator housing.

The Kewaunee Power Station HEAF event damaged a 9.1 m (30 ft.) section of the bus

bar and the licensee observed the spread of a metallic dust. The bus bar conductor was

made of aluminum.

As previously discussed, the NRC has entered the issue of high-energy arc faults involving

aluminum into the generic issue process. As part of this process, the NRC staff will obtain

additional data and will perform additional evaluations to inform future agency actions, as

appropriate. As described in a memorandum dated March 4, 2016, the NRC staff had also

performed an initial evaluation and determined that there was no immediate safety concern

(ADAMS Accession No. ML16064A250). Although not explicitly required, the NRC encourages addressees to review the information in

this information notice for applicability and consider actions, as appropriate. Suggestions

contained in this information notice are not NRC requirements; therefore, the agency requires

no specific action or written response.

CONTACT

S

Please direct any questions about this matter to the technical contact(s) listed below or the

appropriate Office of Nuclear Reactor Regulation (NRR) or Office of New Reactors (NRO)

project manager.

/RA/ (Paul G. Krohn for)

/RA/

Timothy J. McGinty, Director

Louise Lund, Director

Division of Construction Inspection

Division of Policy and Rulemaking

and Operational Programs

Office of Nuclear Reactor Regulation

Office of New Reactors

Technical Contact:

Nicholas Melly, RES/DRA

Mark Henry Salley RES/DRA

301-415-2392

301-415-2474

E-mail: Nicholas.Melly@nrc.gov

E-mail- MarkHenry.Salley@nrc.gov

ML17058A343

TAC No. MF9285 OFFICE

NRR/DPR/PGCB/LA

RES/DRA/FXHAB

QTE

NRO/DCIP/QVIB-1*

NRR/DRA/APLB

NRR/DRA/D

NAME

ELee

NMelly

CHsu

TJackson

JRobinson

JGiitter

DATE

03/09/2017

04/03/2017

03/16/2017

06/06/2017

06/13/2017

06/13/2017 OFFICE

RES/DRA/FXHAB

RES/DRA/D*

NRR/DPR/PGCB/PM*

NRR/DPR/PGCB/LA*

NRR/DPR/PGCB/BC

NRO/DCIP/D

NAME

MSalley

MCheok

BHarris

ELee

AGarmoe

TMcGinty

(PKrohn for)

DATE

06/14/2017

07/21/2017

07/25/2017

07/26/2017

08/01/2017

08/02/2017 OFFICE

NRR/DPR/D

NAME

LLund

DATE

08/21/2017