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Category:EXAMINATION REPORT
MONTHYEARIR 05000423/19970041997-08-12012 August 1997 Exam Rept 50-423/97-04(OL) on 970707-11.Exam Results:All RO & SRO Applicants Passed All Portions of Exams ML20134K1721997-02-0707 February 1997 NRC Operator Licensing Exam Rept 50-245/96-12 Administered on 961202-06.Exam Results:Six of Seven Applicants Failed Exams & One Passed,But License Was Not Issued Due to Required Plant Manipulations Not Being Completed IR 05000245/19930251993-10-0101 October 1993 Exam Rept 50-245/93-25-OL on 930914-16.Exam Results: Requalification Exams Were Administered to 8 ROs & 7 Sros. All 15 Licensed Operators Passed All Portions of Exam IR 05000336/19920331993-01-27027 January 1993 Requalification Exam Rept 50-336/92-33OL-RQ on 921214-17. Exam results:14 Licensed Operators Passed All Portions of Exam,Including Evaluation of Three Operating Crews. Requalification Program Determined to Be Satisfactory IR 05000423/19920251992-12-21021 December 1992 Exam Rept 50-423/92-25 (OL-RQ) on 921116-19.Exam Results: All Four Operators Passed Exams.Two SROs & ROs Operated Successfully as Crew During Two Simulator Scenarios.Results of Exam Combined W/Results of Previous Requalification Exam IR 05000245/19900101990-10-26026 October 1990 Exam Rept 50-245/90-10OL on 900827-31.Exam Results:Three of Five SROs & Three ROs Passed Operating & Written Tests IR 05000366/19900271990-10-15015 October 1990 Exam Rept 50-366/90-27OL on 901003.Exam Results:Reactor Operator Candidate Passed Written Exam & Issued Reactor Operator License on 901009 IR 05000336/19900101990-07-20020 July 1990 Requalification Program Audit Rept 50-336/90-10OL-RQ on 900618-22.Audit Results:Training Program Rated Satisfactory IR 05000423/19890051989-05-0303 May 1989 Exam Rept 50-423/89-05OL on 890321-23.Exam Results:All Candidates Successfully Completed Both Written & Operating Parts of Respective Exams Except for One Reactor Operator That Failed Section 1 of Written Exam IR 05000245/19880161989-03-17017 March 1989 Exam Rept 50-245/88-16OL on 881107-10.Exam Results:All Reactor Operator Candidates Passed Exams.Six Senior Reactor Operator (SRO) Candidates Passed Written Exam & Operating Test.One SRO Candidate Failed Written Exam IR 05000336/19880171988-09-12012 September 1988 Exam Rept 50-336/88-17OL Administered During Wk of 880718. Exam Results:Written & Operating Exams Administered to Three Senior Reactor Operator Upgrade Candidates.All Three Passed IR 05000336/19870311988-03-25025 March 1988 Exam Rept 50-336/87-31OL on 880111-14.Exam Results:Six Reactor Operators & Two Instant Senior Reactor Operators Passed Exam IR 05000423/19870281988-03-16016 March 1988 Exam Rept 50-423/87-28OL on 871214-18.Exam Results:Three Senior Reactor Operator (SRO) Candidates & Two Reactor Operator (RO) Candidates Passed Written/Operating Exams.One RO Candidate Failed Operating Exam & One SRO Failed Both IR 05000245/19870231987-11-19019 November 1987 Exam Rept 50-245/87-23OL on 870921-25.Exam Results:Five Senior Reactor Operators Passed Exams.Two Senior Reactor Operators Failed.Related Info Encl IR 05000423/19870231987-11-0606 November 1987 Requalification Exam Rept 50-423/87-23OL on 870612,0731 & 0904.Exam Results:All Senior Reactor Operators (Sros) & Reactor Operators (Ros) Passed Operating Portion of Exams. Three SROs & Two ROs Failed Written Exams IR 05000423/19870161987-10-0909 October 1987 Exam Rept 50-423/87-16OL on 870818-20.Exam Results:One Senior Reactor Operator Candidate Failed Written Exam & Two Failed Operating Exam IR 05000245/19860211987-03-12012 March 1987 Exam Rept 50-245/86-21OL on 861215-19.Exam Results:All Candidates Passed Exams.Accuracy of Simulator Cause & Malfunction Book & Number of Errors Found in Training Matl Raised Concern IR 05000336/19860251987-03-0404 March 1987 Requalification Program Audit Rept 50-336/86-25OL on 861113 & 870105-16.Audit Results:Evaluation of Facility Written Exam Grading & Overall Program Evaluation Satisfactory IR 05000423/19860311987-03-0303 March 1987 Exam Rept 50-423/86-31OL on 861215-19.Exam Results:Four Senior Reactor Operator (Sro),Seven Reactor Operator & One Instructor Certification Candidate Received Licenses. One SRO Failed Simulator Portion of Operating Exam IR 05000336/19860221987-02-0404 February 1987 Exam Rept 50-336/86-22OL on 861215.Exam Results:One Reactor Operator Candidate & One Senior Reactor Operator Candidate Passed Operating Exam.Both Issued Licenses IR 05000336/19860101986-09-15015 September 1986 Exam Rept 50-336/86-10OL on 860707-11.Exam Results:Seven Senior Reactor & Five Reactor Operator Licenses Issued.Two Candidates Failed Simulator Exam & One Candidate Failed Written Exam.Exam & Answer Key Encl IR 05000423/19860101986-07-0202 July 1986 Exam Rept 50-423/86-10 on 860331-0404.Exam Results:Three Reactor Operator & Six of Nine Senior Reactor Operator Candidates Passed All Portions of Exam.Problem Continues Re Lack of Proper Exam Security IR 05000423/19850451986-01-22022 January 1986 Exam Rept 50-423/85-45 on 851030-31.Exam Results:One Reactor Operator & Seven Senior Reactor Operator Candidates Passed IR 05000245/19850211985-12-0202 December 1985 Exam Rept 50-245/85-21 During Wk of 850812.Exam Results:One of Six Reactor Operator Candidates & One of Four Senior Reactor Operator Candidates Failed Both Written & Oral Exams.Supporting Documentation Encl IR 05000423/19850441985-11-13013 November 1985 Exam Rept 50-423/85-44(OL) on 850903-06 & 09-12.Exam results:11 Out of 14 Senior Reactor Operator & 3 Out of 4 Reactor Operator Candidates Passed All Portions of Exams & Will Be Issued Licenses ML20133M2181985-08-0202 August 1985 Exam Rept 50-423/OL-85-15 on 850514-17 & 21-23.Exam Results: Two Reactor Operators & Nine Senior Reactor Operators Passed.Three Reactor Operators & Seven Senior Reactor Operators Failed 1997-08-12
[Table view] Category:TEXT-INSPECTION & AUDIT & I&E CIRCULARS
MONTHYEARIR 05000245/19990081999-09-14014 September 1999 Insp Repts 50-245/99-08,50-336/99-08 & 50-423/99-08 on 990615-0809.Four Violations Noted & Being Treated as Ncvs. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000423/19990071999-08-27027 August 1999 Insp Rept 50-423/99-07 on 990614-0715.Violations Noted & Being Treated as Ncvs.Major Areas Inspected:Review of C/A Program Using IP 40500, Effectiveness of Licensee Controls in Identifying,Resolving & Preventing Problems IR 05000336/19990061999-07-19019 July 1999 Insp Repts 50-336/99-06 & 50-423/99-06 on 990420-0614.Ten Violations Occurred & Being Treated as non-cited Violations. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000336/19982191999-06-10010 June 1999 Insp Rept 50-336/98-219 on 981214-18,990126-29,0208-19 & 0301-05.Noncited Violations Identified.Major Areas Inspected:Exam of Licensee Corrective Action Implementation IR 05000245/19990051999-06-0404 June 1999 Errata to Insp Repts 50-245/99-05,50-336/99-05 & 50-423/99-05,consisting of Figure 1 ML20207G1211999-06-0303 June 1999 Insp Repts 50-245/99-05,50-336/99-05 & 50-423/99-05 on 990302-0419.No Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support ML20207F1521999-05-25025 May 1999 Notice of Violation from Investigation Rept 1-94-021 on 940506-960329.Violation Noted:Between 740831-910407,licensee Made Changes to Facility Described in Safety Analysis Rept for Refueling Core Offloads Without Performing Evaluation ML20196K2621999-05-24024 May 1999 EN-99-020:on 980525,notice of Violation & Exercise of Enforcement Discretion Will Be Issued to Licensee.Action Based on Severity Level III Problem Consisting of Four Individual Violations Involving Refueling Outage PNO-I-99-022, on 990509,Millstone Unit 2 Established Reactor Criticality.Nrc Staff Providing Augmented Insp Coverage of Restart Activities,Including round-the-clock Observations of Licensee Activities During Key Operational Evolutions1999-05-11011 May 1999 PNO-I-99-022:on 990509,Millstone Unit 2 Established Reactor Criticality.Nrc Staff Providing Augmented Insp Coverage of Restart Activities,Including round-the-clock Observations of Licensee Activities During Key Operational Evolutions IR 05000336/19990031999-05-10010 May 1999 Insp Rept 50-336/99-03 on 990322-26.No Violations Noted. Major Areas Inspected:Review of Actions Taken by Util to Resolve Significant Issues List Item 21,fire Protection ML20206F4601999-04-30030 April 1999 Insp Rept 50-336/99-04 on 990315-31.Violation Noted.Major Areas Inspected:Monitored Licensee Activities During Plant Transition Between Operational Modes,Both During Normal & off-normal Working Hours PNO-I-99-016, on 990406,operators Initiated Plant Cooldown from Normal Operating Pressure & Temp in Mode 3,hot Standby. Cooldown Was Necessary to Minimize Further Degradation of Bonnet Pressure Seal for Valve 2-SI-652 & to Repair Valve1999-04-0707 April 1999 PNO-I-99-016:on 990406,operators Initiated Plant Cooldown from Normal Operating Pressure & Temp in Mode 3,hot Standby. Cooldown Was Necessary to Minimize Further Degradation of Bonnet Pressure Seal for Valve 2-SI-652 & to Repair Valve ML20205M7201999-04-0606 April 1999 Notice of Violation from NRC OI Case 1-96-002 & Conclusions of Millstone Independent Review Team.Violation Noted. E Debarba,Deliberately Discriminated Against Supervisor in Performance Engineering Group at Millstone Station ML20205M7351999-04-0606 April 1999 Notice of Violation from Investigation in Case Numbers 1-96-002 & 1-97-007.Violation Noted:Licensee Discriminated Against Supervisor in Performance Engineering Group at Plant Due to Involvement in Protected Activities IR 05000245/19990021999-04-0202 April 1999 Insp Repts 50-245/99-02,50-336/99-02 & 50-423/99-02 on 990112-0301.Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support IR 05000336/19990011999-03-29029 March 1999 Insp Rept 50-336/99-01 on 990117-0217.Violations Noted.Major Areas Inspected:Licensee C/A Program Implementation Using Guidance of NRC IP 40500, Effectiveness of Licensee Controls in Identifying,Resolving & Preventing Problems ML20205J0941999-03-12012 March 1999 Rept of Review of Millstone Units 1,2 & 3:Allegations of Discrimination in NRC Ofc of Investigations Cases 1-96-002, 1-96-007,1-97-007 & Associated Lessons Learned ML20207M1131999-03-0909 March 1999 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $88,000.Violation Noted:Employment of Two Contractor Employees Terminated in Aug 1997,in Part Because Individuals Raised Concerns Re MOV Program Manual ML20205G6161999-03-0909 March 1999 EN-99-010:on 990309,notice of Proposed Imposition of Civil Penalty in Amount of $88,000 Issued to Licensee.Action Based Upon Severity Level II Problem Involving Discrimination Against Two Contractor Employees at Millstone MOV Dept IR 05000245/19980061999-03-0101 March 1999 Insp Repts 50-245/98-06,50-336/98-06 & 50-423/98-06 on 981123-990111.No Violations Noted.Major Areas Inspected: Operations,Maintenance,Engineering & Plant Support PNO-I-99-006, on 990128,operators Inadvertently Reduced Spent Fuel Pool Water Level by Two Inches When Purification of Spent Fuel Pool Water Initiated.Operators Held Shift Briefing to Discuss Realigning Purification Sys1999-01-29029 January 1999 PNO-I-99-006:on 990128,operators Inadvertently Reduced Spent Fuel Pool Water Level by Two Inches When Purification of Spent Fuel Pool Water Initiated.Operators Held Shift Briefing to Discuss Realigning Purification Sys IR 05000245/19982171999-01-22022 January 1999 Evaluation Repts 50-245/98-217,50-336/98-217 & 50-423/98-217 Conducted on 981026-30.Areas Evaluated:Whether NNECO Has Improved Sufficiently & Has Demonstrated Sustained Performance in Maintaining safety-conscious Work Environ PNO-I-99-004, on 990115,carbon Dioxide Was Inadvertently Discharged Into Unit 3 Cable Spreading Room,Containing Electrical Wiring.Ambulance Reported to Site as Precautionary Measure.Licensee Assembled Event Review1999-01-20020 January 1999 PNO-I-99-004:on 990115,carbon Dioxide Was Inadvertently Discharged Into Unit 3 Cable Spreading Room,Containing Electrical Wiring.Ambulance Reported to Site as Precautionary Measure.Licensee Assembled Event Review IR 05000336/19980051999-01-0707 January 1999 Insp Repts 50-336/98-05 & 50-423/98-05 on 981006-1123. Violations Noted.Major Areas Inspected:Operations, Maintenance,Engineering & Plant Support ML20199C6381999-01-0707 January 1999 Notice of Violation from Insp on 981006-1123.Violation Noted:On or Before 981120,conduit 9-15,in Fire Area A-24,not Sealed & Tested in Accordance with Astme E-119,fire Endurance Test PNO-I-99-001, on 981231,Millstone Unit 2 Began Reloading Fuel Into Reactor After Extended Shutdown.Millstone Unit 3 Went Critical on 981230,after Forced Outage Due to Inadvertent MSIV Closure During Surveillance Testing at Power1999-01-0404 January 1999 PNO-I-99-001:on 981231,Millstone Unit 2 Began Reloading Fuel Into Reactor After Extended Shutdown.Millstone Unit 3 Went Critical on 981230,after Forced Outage Due to Inadvertent MSIV Closure During Surveillance Testing at Power PNO-I-98-062, on 981211,Millstone Unit 3 Tripped from 100% Reactor Power During MSIV Partial Stroke Testing.Solenoid Valve Integral to MSIV Failed to Reopen When Licensed Operator Released Test Switch1998-12-15015 December 1998 PNO-I-98-062:on 981211,Millstone Unit 3 Tripped from 100% Reactor Power During MSIV Partial Stroke Testing.Solenoid Valve Integral to MSIV Failed to Reopen When Licensed Operator Released Test Switch ML20195H6901998-11-18018 November 1998 Notice of Violation from Insp on 980818-1005.Violation Noted:Engineering Evaluations Not Performed When RCS Heatup Rate Limit Exceeded on 951217 & When RCS Cooldown Rate Limit Exceeded on Three occasions,940424,0728 & 951215 IR 05000245/19982161998-11-18018 November 1998 Insp Repts 50-245/98-216,50-336/98-216 & 50-423/98-216 on 980818-1005.Violations Noted.Major Areas Inspected: Operations,Maintenance,Engineering & Plant Support IR 05000336/19982031998-11-0505 November 1998 Insp Rept 50-336/98-203 on 980824-0904.No Violations Noted. Major Areas Inspected:Effectiveness of Configuration Mgt Plan ML20155B1521998-10-23023 October 1998 Notice of Violation from Insp on 980810-0903.Violation Noted:Design Basis,As Described in FSAR Chapter 14,Accident Analyses Had Not Been Correctly Translated Into Plant Procedures & Acceptance Criteria IR 05000336/19982131998-10-23023 October 1998 Insp Rept 50-336/98-213 on 980810-0903.Violations Noted. Major Areas Inspected:Certain Aspects of Accident Mitigation Sys IR 05000245/19982151998-10-14014 October 1998 Evaluation Repts 50-245/98-215,50-336/98-215 & 50-423/98-215 on 980824-28.Major Areas Evaluated:Whether Licensee Has Improved Sufficiently & Has Demonstrated Sustained Performance in Maintaining safety-conscious Work Environ IR 05000336/19980041998-10-0101 October 1998 Insp Rept 50-336/98-04 on 980914-18.No Violations Noted. Major Areas Inspected:Mov Program Associated with GL 89-10 IR 05000245/19982121998-09-25025 September 1998 Insp Repts 50-245/98-212,50-336/98-212 & 50-423/98-212 on 980630-0817.No Violations Noted.Major Areas Inspected: Operations,Maintenance,Engineering & Plant Support IR 05000423/19982111998-09-11011 September 1998 Insp Rept 50-423/98-211 on 980413-24,0511-15,27-29,0609-11 & 23-25.Violation Noted.Major Areas Inspected:Evaluation of Licensee C/As & Other ICAVP Process Activities ML20154D1151998-09-11011 September 1998 Notice of Violation from Insp on 980413-24-0511-15,27-29, 0609-11 & 23-25.Violation Noted:Program Implemented TS 6.8.4.a,failed to Include Provisions to Reduce Leakage from RSS Heat Exchangers to SW Sys IR 05000424/19980061998-09-10010 September 1998 Insp Repts 50-424/98-06 & 50-425/98-06 on 980628-0815.No Violations Noted.Major Areas Inspected:Aspects of Licensee Operations,Engineering,Maint & Plant Support PNO-I-98-039, 980812,Millstone Unit 3 Was Shutdown to Repair Small Leak on Afws Discharge Noted.Current Leakage Does Not Exceed Regulatory Requirements & Shutdown Not Required by Tech Specs.Licensee Issued Press Release on 9808111998-08-12012 August 1998 PNO-I-98-039:980812,Millstone Unit 3 Was Shutdown to Repair Small Leak on Afws Discharge Noted.Current Leakage Does Not Exceed Regulatory Requirements & Shutdown Not Required by Tech Specs.Licensee Issued Press Release on 980811 ML20237D3041998-08-12012 August 1998 Notice of Violation from Insp on 980413-0508.Violations Noted:Two Examples Identified Where Licensee Not Performing Leakage Testing of safety-related Valves in Sys That Could Contain Highly Radioactive Fluids During Accident IR 05000245/19982081998-08-12012 August 1998 Insp Repts 50-245/98-208,50-336/98-208 & 50-423/98-208 on 980428-0629.Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support ML20237B0741998-08-12012 August 1998 Notice of Violation from Insp on 980428-0629.Violation Noted:Licensee Failed to Direct Test Personnel to Close & Lock RHR Outboard Drain Valve IR 05000336/19982011998-08-12012 August 1998 Insp Rept 50-336/98-201 on 980413-0508.Violations Noted. Major Areas Inspected:Licensee Ability to Identify & Resolve Deficiencies Focusing,But Not Limited To,Period of CMP Implementation & ICAVP at Parsons Power Group,Inc PNO-I-98-026, on 980701,Millstone Unit 3 Criticality Update Made.Nrc Staff Continues to Provide Augmented Insp of Unit 3 Restart Activities,Including round-the-clock Coverage of Key Operational.Licensee Plans No Press Release1998-07-0101 July 1998 PNO-I-98-026:on 980701,Millstone Unit 3 Criticality Update Made.Nrc Staff Continues to Provide Augmented Insp of Unit 3 Restart Activities,Including round-the-clock Coverage of Key Operational.Licensee Plans No Press Release PNO-I-98-025, on 980630,unit 3 Established Reactor Criticality,However Reactor Was Shut Down When Control Room Operator Noticed Spiking Intermediate Range Monitor.Licensee Troubleshooting1998-06-30030 June 1998 PNO-I-98-025:on 980630,unit 3 Established Reactor Criticality,However Reactor Was Shut Down When Control Room Operator Noticed Spiking Intermediate Range Monitor.Licensee Troubleshooting IR 05000245/19982071998-06-19019 June 1998 Insp Repts 50-245/98-207,50-336/98-207 & 50-423/98-207 on 980301-0427.Violations Noted.Major Areas Inspected:Maint, Operations,Engineering & Plant Support ML20249C6931998-06-19019 June 1998 Notice of Violations from Combined Insp on 980301-0427. Violations Noted:Prior to 980424,instrument Min Accuracy of Wind Speed Channels Were Not Measured as Required by Table 3.3-8 of Unit 2 TS 3/4.3.3.4 IR 05000423/19970831998-06-12012 June 1998 Insp Rept 50-423/97-83 on 980413-24.Violations Noted. Major Areas Inspected:Readiness of Plant Hardware,Staff & Mgt Programs to Support Safe Restart & Continued Operation of Plant Unit 3 ML20249B0421998-06-12012 June 1998 Notice of Violations from Insp on 980413-24.Violations Noted:Only 1 RCS Loop Operable W/Plant in Mode 4 on 980407 IR 05000423/19970821998-06-11011 June 1998 Insp Rept 50-423/97-82 on 980209-20.Violations Noted.Major Areas Inspected:Corrective Actions Processes 1999-09-14
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. U.S. NUCLEAR REGULATORY COMMISSION. REGION I OPERATOR-LICENSING REQUALIFICATION PROGRAM EVALUATION REPORT
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_ EVALUATION REPORT NO. 50-336/90-10 (0L-RQ)
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. . . FACILITY DOCKET NO. 50-336 FACILITY LICENSE.NO. DPR-65 LICENSEE: Northeast Nuclear Energy Company l P. O. Bo'x 270 l
_ Hartford, Connecticut 06141-0270-i FACILITY: Millstone Nuclear Power Station, Unit 2 ,
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EXAMINATION DATES: June 18-22,-1990 4 CHIEF EXAMINER: / //// [ eth tarrg. Briggs, SMior Operations Engineer
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APPROVED BY:
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Peter Eselgroth, Chief, PWR section 6dd/7A
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Operations Branch, Division of Reactor Safety
- SUMMARY: The licensed operator requalification' training progrcm was rated as satisfactory. .Written requalification examinations and operating tests were .
administered to seven_ senior reactor _ operators (SR0s) and six reactor '
operators (R0s). The examina'tions were graded concurrently and independently.
by the NRC and'the facility training staff. As graded by the NRC, all SR0s and R0s passed all portions of-the examinati_on. Facility. grading paralleled that of the NRC in all aspects of the. examination.
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a DETAILS ;
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( TYPE OF EXAMINATIONS: Requalification ]
L ' EXAMINATION RESULTS: J NRC l R0 E SRO l TOTAL l
._ Grading- l Pass / Fail SPass/ Fail GPan/4il l l L* -
g E E E 'l R l Written l 6/0 l 7/0 l_ 13/0 l I I I I I l Simulator l- 6/0 5 7/0 l 13/0 l E I E E E ;
-l Walk-through I 6/0 3 7/0 E 13/0 l
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I E I E I E l Overall l 6/0 E 7/0 l 13/0 l ,
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E SR0 g TOTAL E Grading 5. Pass / Fail EPass/ Fail l Pass / Fail l l E E E E !
l Written- l 6/0 3 7/0 l 13/0 l l l;
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E= E E E E L 5 Simulator- l 6/0 5 7/0 E 13/0 l l L I- E E I I
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l 6/0 -g 7/0 g- 13/0- .g E E E E~ E l_Overall 3 6/0 5 7/0 l 13/0 5 <
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1.0 PERSONNEL CONTACTED DURING THE EVALUATION CHIEF EXAMINER AT SITE: '
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L. Briggs, Senior Operations Engineer (1,2,3)
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l: OTHER NRC PERSONNEL:
P. Habighorst, Resident Inspector, Millstone Unit 2 (3)
J. Hanek, Principle Nuclear Operations Engineer, EG&G (1,2,3)
.F. Jagger, Principle Nuclear Operations Engineer, EG&G (1,2,3)
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LICENSEE PERSONNEL: ,
. S. Brinkman, Operations Engineer, Millstone Unit 2 -(3)
J. Keenan, Unit 2 Director (3)
J. Smith, Unit 2 Operations Manager (2,3)
R. Spurr, Senior Operator Instructor (Requal. Coord.)- (1,2,3)
R. Stotts, Operator Training Manager. (Acting)- (3)
M. Wilson, Supervisor of Operator Training, Unit 2 (1,2,3)
LEGEND:
(1). Participated in examination development-(2) Participated in examination administration (3) Attended exit meeting on June 8, 1990 at the Northeast Utilities Training Center 2.0 PROGRAM EVALUATION RESULTS Overall rating: Satisfactory
=The program for licensed operator requalification training at Millstone Point Unit 2-(MP2) was rated as satisfactory in accordance with the criteria established in the revision 5 of NUREG-1021, ES-601. Those criteria are:
p a. A pass / fail decision agreement between the NRC and facility grading
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of.90% for the written and operating examinations, with the licensee
'not being penalized for holding a higher standard of operator performance.
NRC grading resulted in thirteen operators passing.the written exami-nation. Facility grading also resulted in thirteen operators passing the written examination. This satisfies criterion a.
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NRC grading resulted in thirteen operators passing the job perform- i ance measures of the examination. Facility grading resulted in ;
thirteen operators passing the job performance measures of the exami- :!
nation. This also satisfies criterion a.
NRC grading resulted in thirteen operators passing the simulator portion of the examination. Facility grading resulted in thirteen i' operators passing the simulator examination. This also satisfies '
criterion a.
b. At least 75% of all operators pass the examination.
NRC grading is the only consideration for this criterion. All !
thirteen operators passed the examination overall. This satisfies criterion b.
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c.- Failure of no more than one crew during the simulator portion of the operating examination.
Again, NRC grading is the only consideratio.n for this. criterion.
Three crews were evaluated and all three crews passed the simulator portion of the operating examination. This satisfies criterion c.
3.0 SCENARIO EVALUATION The.'following concern was noted during the scenario portion of the operat-ing examinations. '
Scenario RQ2-900-42 was performed by two different operatino crews with different results. The major event in the scenario is a stwr, generator tube rupture (SGTR) with a stuck open stmospheric steam dump valve (ADV).
One crew followed the Emergency Operating Procedure (EOP) and allowed _the ADV.to remain open during cooldown. This crew also classified the event as an ALERT CHARLIE-ONE based on the symptom description in the emergency action level table which statec " leakage in excess of normal makeup AND air ejector or steam gen,erator blowdown radiation monitor alarm." These were the' plant indications at the time. 'The next higher classification symptom required the Main Steam Line (MSL) radiation monitor to be in alarm; it was not. In the condition column of the hioher classification level, it noted rapid SGTR failure with a radioacti u steam release to atmosphere which.was taking place through the ADV. Ouring subsequent- i discussion with the SRO, he did not classify the event as an SITE AREA EMERGENCY CHARLIE-TWO because the symptom column required the'MSL radia-tion monitor alarm, and it was not in alarm, and he did not consider the SGTR to be a rapid failure. Further discussion with the licensee staff indicates that what is being looked for when " rapid" is used is a large leak rate (gallons per minute value) not a'. rate of failure as implied by the word rapid. The EAL classification table is also currently being revised to make it easier to use. In the naw revision, the SGTR will not have an ALERT level, it will start at the SITE AREA EMERGENCY level.
Based on the conflicting information in the EAL classification table and the SR0s reasoning, the NRC examination team-decided that'aithough the SRO failed to classify the event at the predetermined level, he did not fail the overall operating portion (dynamic simulator) of the requalification examination.
The second operating crew to perform the same scenario took action to close the ADV and preclude the release of radioactive steam (via the SGTR). This action, isolating the faulted steam generator by closing the ADV is not in strict compliance with the direction contained within the E0P, which does not instruct the operator to close the valve. Further research'of by the examination team indicates that CEN-152, Revision 3, Page 6-46, allows the faulted steam generator to be isolated if there is forced reactor coolant system flow. During this scenario there was forced coolant flow. The examination team determined that the SR0 had taken action that was more conservative than that directed by the E0P and m
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, ' change to the E0P to allow isolation of a' ruptured and faulted steam b generator if . forced coolant flow is available. ,
The Supervisor of _0perator Training 'noted that both SR0s would receive ,]
additional training to address the need for conservative.EAL classific- ;
ation-and procedural adherence matters. l
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4.0 WRITTEN EXAMINATION EVALUATION j No problems were noted with section A or B of the written-examination. i The overall average grade for all thirteen operators was 95.2 percent. !
5.0 JOB PERFORMANCE MEASURES (JPM) EVALUATION JPM #012-500-01-018 I t
This JPM required the operator to manually calculate a shutdown margin.
It was performed incorrectly two of the four times it was conducted. This j
.I indicates a possible need for increased training in this subject area.
S JPM #123-727-01-01 .
!
This was a common JPM (performed by all 13 operators) and required the restoration of bus 24C from emergency diesel generator operation, Three of the 13 operators conducting this JPM failed to properly perform the required task. This indicates a possible need for further training in .
this subject area also.
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No-other areas-of possible generic weakness were identified.
-6.0 SUMMARY OF COMMENTS MADE AT EXIT MEETING ON JUNE 8, 1990 i
.i a. The NRC expressed appreciation for the level of effort expended by 1
' the training department representatives in accommodating the NRC ]
examination team. This level of effort helped in expediting the ;
review process and the conduct of the exam. Appreciation was also !
expressed for the cooperation and level of-effort expended by all those_ involved in the process, including the operators that were examined, and especially the facility examination team members who j
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administered the examination.
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b. The NRC discussed the topics addressed in Paragraphs 2 thru 5 above.
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> c. Examination scheduling was excellent. The length of examination days ,
were reasonable and no undue delays were experienced. i Attachinent: Northeast Nuclear Energy Compny Summary of NRC Requalification 1 Examination d
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MM General Offices * Selden St'reet, Berlin, Connecticut
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P.o. BOX 470
' HARTFORD. CONNECTICUT OS141-0270-
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k ' J CUCSY5%~, J203) 665-5000 RE: NUREG 1021, ES-601-July 12, 1990
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'Mr. Robert Gal'lo Chief,. Operations Branch .
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U.-S. Nuclear Regulatory. Commission, Region 1 475 Allendale' Road
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King of Prussia, PA 19406 I
REFERENCE: Facility Operating License No. DPR-65 s Docket No. 50-336 NRC Requalification Examination Summary L r l Dear Mr. Gallo E
During the. Week of June 18, 1990, Licensed Operator Requalifi-cation Examinations were administered to thirteen Millstone Unit.2 Licensed ~ Operators and Senior Licensed Operators. These examinations were conducted in accordance with.NUREG 1021,.
Operator Licensing Examiner Standards, section ES-601.
Accordingly, the' examinations were prepared, administered, and
, ' evaluated by both NRC and facility examiners.
Preliminary-results of the facility evaluations for all portions of the examination were provided to Larry Briggs, NRC Chief
. Examiner, on June ~22, 1990. Based on our review of the exam grading, these preliminary results can be considered final.
Attached is a summary of our-grades.
An evaluation of.the examination results was performed to identify strengths and weaknesses, both individual and crew,.and l. to: identify necessary remediation and enhancements to the MP2 Licensed Operator Requalification Program content.
'
The following ;
is a summary,.by examination environment, of the evaluation:.
SIMULATOR EXAMINATIONS STRENGTHS (CREW):
o In general, teamwork and communications were-good. Where appropriate, team members were involved in decision-making and shared with each other information concerning event strategy and inter-watchstation operations.
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o Use of Abnormal Operating Procedures (AOP's). The.
appropriate AOP's were referenced in aLtimely fashion and
:the actions carried.out showed good familiarity with the affected systems and procedural content.
o 'The fifth, or " spare", cperator, when available, was efficiently used to asstst the teams' efforts.
WEAKNESS (CREW):-
o The use of Plant Procents Computer . (PPC) displays to more effectively trend important process variables needs general improvement. 'tisparities among the shifts was noted; some were excellent; some poor.
WEAKNESSES (INDIVIDUAL):.
o Operator r:
- -Properly referencing and logging applicable Technical l Specification action statements o Operator J:
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Use of the Emergency Action Level (EAL) tables to arrive at the most conservative event classification l
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Proper sequencing of actions within EOP 2540, runctional Recovery o Operators A and B:
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Strict compliance with the requirements of Emergency ;
Operating Procedure steps l
o Operator E:
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General lack of aggressiveness-and contribution.
Communications were not always-complete; actions were tentative.
l o Operator M
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Knowledge of integrated plant response associated with the development of natural circulation (tripping of RCP's)
L Remedial programs will~be implemented for operators r, J, E, and-M.
E Counseling by Operations = Management has been conducted for Opera-Ia tors A and B with respect to EOP step deviations, Ld The. effective'use of PPC displays will be stressed in future simulator training sessions.
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h WALKTHROUGH' EXAMINATION
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a In. general', the operators demonstratediexcellent proficiency and knowledge for-the-tasks examined.
ThreeJJPM's were performed unsatisfactorily by more than one examineek These JPM's are:
o Restore Bus 24C from EDG Operations
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o Calculate SDM Ak o Local, Manual Operation of the FRV
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! Deficiencies noted during the performance of these JPM's will be addressed in upcoming Licensed Operator Requalification T.aining.
WRITTEN EXAMINATION
I Examinee performance _on the written examination was excellent, L . showing a sound mastery of the learning objectives examined. I u
" A high percentage of examinees lost credit on four questions.
Two.of these questions, #2116 and #1939, warrant modification ir such that the questions elicit a complete, correct response. Two u questions,.#2313 and #2037 indicate deficiencies which will be
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corrected ~in the Licensed Operator-Requalification Training Program.
,
Yours truly,
.
u NORTHEAST NUCLEAR ENERGY COMPANY L Fort Stephen E. Scace Station Director i,
Millstone Nuclear Power Station By: S li MP1 Unit Director j.; Millstone Nuclear Power Station Attachment SES/MJW/rg i i
c: Document Control Desk, US NRC L , B. W. Ruth, Manager, Operator Training, NU L R..M. Kacich, Generation Facilities Licensing, NU L. Briggs, US-NRC l
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ATTACHMENT LORT EXAMINATION SUMMARY WEEK OF JUNE'18,- 1990 -
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MILLSTONE UNIT 2L l-Simulator Static . Static Open Written JPM's JPM Questions Name P/F- 10 3 04- Reference Total No. Sat. No. Correct OPERATOR A P 24.2 22.1 49.45 95.75 9 19 OPERATOR B P' 21.95 22.1 47.8 91.85 9 20-OPERATOR C P 25 21.65 44.05
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90.7- 9 -19 OPERATOR D P 25 25 49.79- 99.79 10 20 OPERATOR E P 25 22.1 49.015- 96.115 '8 20 OPERATOR F P '22.6 25 45.62 93.22 '10 20
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OPERATOR G P. 25 22.1 49.66 96.76 9 l 20 OPERATOR H P '21.8 25 47.06 93.86 9 20 OPERATOR I P 25 24.55 49.52 99.07' 10- '"
OPERATOR J P 24.2 24.6 50 98.8 10- ~19 OPERATOR K P 25 20.6 45.19 90.79 10 16 OPERATOR L P 22.5 20.6 47.29 90.19 10 19 OPERATOR M P 25 22.1 50 97.1 9- 20
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