IR 05000313/1989017

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Insp Repts 50-313/89-17 & 50-368/89-17 on 890417-21.No Violations or Deviations Noted.Major Areas Inspected: Licensee Implementation of Integrated Corrective Action & Followup Actions Re Unit 2 Extraction Steam Line Break
ML20247D098
Person / Time
Site: Arkansas Nuclear  Entergy icon.png
Issue date: 05/10/1989
From: Barnes I, Gilbert L, Murphy M, Wagner P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20247D097 List:
References
50-313-89-17, 50-368-89-17, NUDOCS 8905250165
Download: ML20247D098 (15)


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.i APPENDIX-I U.S. NUCLEAR REGULATORY COMMISSION.

REGION IV

NRC Inspection Report:- 50-313/89-17 Operating Licenses: DPR-51 50-368/89-17 NPF-6-Docket's:

50-313

'50-368.

Licensee: Arkansas Power & Light Company (AP&L)

P.O. Box 551 Little Rock, Arkansas 72203 Facility Name: Arkansas. Nuclear One -(ANO), Units 1 and 2

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Inspection At: Russellville, Arkansas Inspection Conducted:

April 17-21,1989'

Inspectors:

h. C. NMW b[9/01 P. C. Wagner, Reactor Inspector, Plant Systems Date Section. Division of Reactor Safety

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L. 'D. Mlbert, Reactor Inspector, Materials Ddte '

and Quality Programs Section, Division of Reactor Safety 9A W%

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M. E. Murphy, Reactor Inspector, Test Programs Date

- Section, Division of Reactor Safety l

Na.,so r/ MP'7 Approved:

I. Barnes, Chief, Materials and Quality Date Programs Section, Division of Reactor Safety

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Inspection Summary

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Inspection' Conducted April 17-21,1989(Report 50-313/89-17; 50-368/89-17)

Areas Inspected:' Routine, unannounced inspection of the licensee's

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- implementation of an: integrated corrective action program, and a special-(

inspection'of the followup action's in response to the Unit.2 extraction steam line break which occurred on April 18, 1989. During the currective ' action program inspection,'the NRC inspectors reviewed germane procedures, QA audits, and documentation packages. The special inspection included physically

' checking the portion of extraction steam line that failed and discussing the.

licensee's planned corrective actions.

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,

Results: During th'e inspection, no violations or deviations were identified.

The NRC inspectors determined that there was a timeliness problem with the implementation'of the new corrective action program and noted some problems

.with the completion of the controlling procedures. The NRC inspectors also

- discussed the advisability of implementing an aggressive trending program for identified problems and their resolution.

The NRC inspectors found the licensee's actions in response to the extraction steam line break to be acceptable and had no questions in that area.

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DETAILS ~

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- Persons' Contacted

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Y AP&L.

  • C.' Anderson, In-House Events Analysis Supervisor

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  • *B. Daker, Plant Modification Manager

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  • T. Baker, Technical Support Manager

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  • W. Converse,L.0perations' Assessment Superintendent

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  • E. Ewing, General. Manager.1 Plant Support
  • H..Greene, QA Superintendent

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  • R. Lane, Manager,- ANO Engineering -
  • J. < Levine,' Executive Director, Nuclear Operations
  • D Lomax, Plant Licensing Supervisor

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'+ S. McGregor, Superintendent, Engineer.ng Services

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  • J. McWilliams, Manager, Maintenance

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L+*P. Michalk', Licensing Engineer

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C. Turk, Superintendent, Nuclear Engineering

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NRC Personnel.

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. L.--J. Callan, Director, Division of Reactor Projects, RegioriLIV.

+*R. Haag, Resident ~ Inspector, ANO

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  • A. Howell, Project Engineer, Region IV g

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+ Denotes personnel who attended the exit meeting.on April-20,:1989'.

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  • Denotes-personnel who attended the exit meeting on April.21, 1989.

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The NRC inspectors; also contacted and interviewed other AP&L operations, M'

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maintenance, and engineering personnel during the course of the.

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inspection.

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Corrective ~ Actions-- Units-1 and 2- (92720)

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The NRC identified-weaknesses with the corrective action program being

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4 implemented at ANO during late 1987.

These weaknesses were' documented in

NRC Inspection Reports 50-313/87-20; 50-368/87-20 ands 50-313/87-26;.

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50-368/87-26.' As a result of those findings ~, and NRC management concerns, AP&LevaluatedtheANOcorrectiveactionprogram(CAP)andcommittedto

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program improvements in the areas of condition identification, timeliness.

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of review and corrective action, root cause analysis, and trending. Thec

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licensee ~ presented the program improvements to the NRC during a. management S

, meeting which was held in the NRC Region IV offices on February 4,1988.

This inspection was performed in an effort to evaluate the effectiveness'

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.j of the CAP that was. presented to the NRC.

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In order to ensure that the " improved" CAP would resolve the earlier NRC concerns, the NRC inspectors reviewed pertinent procedures, Quality j

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Assurance ~(QA) Audits, and a sample of both completed and in-process-documentation packages.

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Procedure Reviews J

.

The NRC inspectors reviewed Station Administrative Procedure 1000.104, " Condition Reporting and Corrective Actions,"

Revision 3, dated January _21,1989. This procedure provided guidance to all pesonnel on how to document " undesirable conditions at ANO,"

and on how the improved CAP was to be implemented. The procedure also provided instructions on determining operability and deportability, establishing significance and priority, and in closing the documentation package when the corrective actions were completed.

The procedure included the various forms which made up the Condition Report (CR)-documentation (Forms 1000.104A through K).

The NRC inspectors found the above procedure to be adequate in providing the framework for the CAP, but discussed the apparent need for additional guidance in the areas of determining deportability, operability, and cause/ root cause. The NRC inspectors were informed that additional guidance in determining operability was being provided by a new procedure which was to become effective on April 30, 1989.

Because timeliness in making operability determinations had been a problem, the new procedure (1000.116 " Operability Determination")

required the Shift Technical Advisor (STA) to make a determination within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> of the request for such a determination from the Shift Operations Supervisor (50S).

If the STA concluded that an engineering evaluation was needed, a documented interim determination by the STA that the system or component would remain fully functional during the time required for the evaluation was required.

The NRC inspectors determined that these provisions would help to preclude long-term conditions during which no documented basis existed for continued operations with systems or components which were being evaluated for operability.

The NRC inspectors noted that trending of identified conditions was not delineated by the above procedures and questioned how this was being accomplished. The NRC inspectors were informed that the In-House Events Analysis Group (IHEA) was trending the CRs and providing a periodic report to AP&L management. The NRC inspectors reviewed existing IHEA reports and found them to be acceptable; however, the NRC inspectors remained concerned that the trending program was not required by procedure.

The NRC inspectors discussed their concerns over the CAP implementation with the involved AP&L personnel and reiterated their concerns during the April 21, 1989, exit meeting.

The NRC inspectors determined that the new procedures provided an improved method of identifying, reporting, and correcting undesirable

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-5-conditions at ANO. ThenewCAhwasalsofoundtoprovidean acceptable framework for resolving previously identified NRC concerns.

Problems-identified with the implementation of the CAP are

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discussed in subparagraph c, belex.

No violations or deviations were identified, b.

QA Audits The NRC inspectors reviewed QA Audits QAP-10-88, " Corrective Action,"

first half dated August 19, 1988, and second half dated March 29, 1989.- Since the first half audit was conducted shortly after the initiation of the new CAP, the findings were inconclusive.

The second audit was more productive and concluded that:' " Management attention has not been adequately given to the timely completion of:

Condition report corrective actions

"*

'For further evaluation'. operability / deportability concerns

"

Managers and IHEA root cause determinations

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Transmittal of completed records to ANO DCC

"

Transmittal of CR's from security to IHEA"

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The report went on to identify the most significant weakness of the new CAP,.as "The failure to complete assigned corrective actions within the assigned time frames." The NRC inspectors review of selected condition report packages substantiated the QA audit findings.

The NRC inspectors found.the QA Audit to be effective in meeting the objectives of the QA program and in providing insight to the licensee management on areas requiring improvement.

No violations or deviations were identified, c.

Documentation Package Reviews The NRC inspectors selected a number of CRs from the licensee provided tabulation which listed approximately 850 CRs for Unit 1, 525 CRs for Unit 2, and~100 CRs common to both Units.

Some of the CRs were closed while others remained open for various reasons. The NRC inspectors also selected some Reports of Abnormal Conditions (RACs) which remained open from the previous corrective action systems. A partial listing of the RACs and CRs that were reviewed is contained in the attachment to this report.

The NRC inspectors noted that frequent delays in documenting both

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' operability and deportability determinations were being made while

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waiting for "further evaluation." The NRC inspectors also noted that the CR Forms were not always properly completed, especially in the

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area of cause/ root cause. The CR procedure required a cause for each condition and a root cause for those conditions judged to be L

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significant;.a root cause was not always provided for conditions.that-had been determined to be significant. The NRC inspectors discussed'

these observations with licensee personnel and also discussed questions they. had on the reviewed RACs and CRs. The following are examples of problems observed:

(1) RAC-2-86112 This RAC was initiated on June 24, 1986, to document discrepancies between the ANO-2 Technical Specification required protective system and safeguards system setpoints and the values calculated to be appropriate by Combustion Engineering Corporation (CE). The NRC inspectors, on April 19, 1989, were unable to determine from the available information if the

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condition had ever been evaluated. A telephone conference call was conducted on April 21, 1989, at which AP&i. personnel explained that CE engineers had utilized an inappropriate

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containment pressure transmitter error value in their calculation.

(These' transmitters had been replaced at ANO-2 with a different brand which had lower errors.) AP&L personnel explained that the proper transmitter error values had been substituted into the CE calculation for the high containment pressure trip setpoint when the CE error was detected and that

- the resulting setpoint was consistent with the implemented value. The RAC hed remained open pending a determination of its deportability..

The AP&L personnel also informed the NRC inspectors that the implemented high-high containment pressure setpoint was verified

.to be appropriate on April 20, 1989, by using a method similar to that used earlier for the high pressure setpoint.

This RAC was transferred to the new CAP system by the initiation of CR-2-89-161 on April 19, 1989.

The NRC inspectors found the processing of this RAC to be an additional example of the NRC concerns with the previous corrective action systems at ANO and were troubled that these old issues (RACs) had not all been' incorporated into the new

'

CAP.

(A few of the old RACs had been transferred to new CRs in the weeks preceding the inspection, but numerous other RACs remained without actions being finalized.)

(2) CR-1-88-239 This CR documented a wiring error that was discovered on September 21, 1988, during the licensee's "as-building" of the essential 4160 volt switchgear-A4. The wiring error caused one of the trip paths for the emergency diesel generator (EDG)

output circuit breaker to be inoperable. This condition could have caused an overload and loss of the EDG if it was being Y

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-2-Inspection Summary Inspection Conducted April 17-21, 1989 (Report 50-313/89-17; 50-368/89-17)

Areas Inspected:

Routine, unannounced inspection of the licensee's implementation of an integrated corrective action program, and a special-inspection of the followup actions in response to the Unit ? extraction steam line break which occurred on April 18, 1989. During the corrective action program inspection, the NRC inspectors reviewed germane procedures, OA audits, and documentation packages. The special inspection included physically checking the portion of extraction steam line that failed and discussing the licensee's planned corrective actions.

!

Results:

During the inspection, no violations or deviations were identified.

The NRC inspectors determined that there was a timeliness problem with the implementation of the new corrective action program and noted some problems with the completion of the controlling procedures. The NRC inspectors also discussed the advisability of implementing an aggressive trending program for identified problems and their resolution.

The NRC inspectors found the licensee's actions in response to the extraction steam line break to be acceptable and had no questions in that area.

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-3-DETAILS

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Persons Contacted AP&L-

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  • C. Anderson, In-House Events Analysis Supervisor-
  • B. Baker, Plant Modification Manager
  • T. Baker, Technical Support Manager
  • W.' Converse Operations Assessment Superintendent
  • E. Ewing, General Manager,2 Plant Support
  • H. Greene. QA Superintendent
  • R. Lane, Manager, AN0 Engineering
  • J. Levine, Executive Director, Nuclear. Operations
  • D. Lomax, Plant Licensing Supervisor

+ S. McGregor, Superintendent, Engineering Services

  • J. McWilliams, Manager, Maintenance

+*P. Michalk, Licensing Engineer C. Turk, Superintendent, Nuclear Engineering NRC Personnel

- L. J. Callan, Director, Division of Reactor Projects, Region IV=

.

+*R. Haag, Resident Inspector, ANO

  • A. Howell, Project Engineer, Region IV

+ Denotes personnel who attended the exit meeting on April 20, 1989.

The NRC inspectors also. contacted and interviewed other AP&L operations, maintenance, and engineering personnel during the course'of the inspection..

-

2.

Corrective Actions - Units 1 and 2 (9272k)),

The' NRC identified weaknesses with the correctivo action program being implemented at ANO during late 1987.

These weaknesses were documented in NRC Inspection Reports 50-313/87-20; 50-368/87-20 and 50-313/87-26; 50-368/87-26. As a result of those findings, and NRC management concerns, AP&L evaluated the ANO corrective action program (CAP) and committed to program improvements in the areas of condition identification, timeliness-of review and corrective action, root cause analysis, and trending. The licensee presented the program improvements to the NRC during a management meeting which was held in the NRC Region IV offices on February 4; 1988.

This inspection was performed in an effort to evaluate the effectiveness of the CAP'that"was presented to the NRC.

,

In order to ensure that the " improved" CAP would resolve the earlier NRC concerns, the NRC inspectors reviewed pertinent procedures, Quality

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Assurance (QA) Audits, and a sample of both completed and in-process documentation packages.

a.

Procedure Reviews The NRC inspectors reviewed Station Administrative Procedure 1000.104, " Condition Reporting and Corrective Actions,"

Revision 3, dated January 21, 1989. This procedure provided guidance to all personnel on how to document " undesirable conditions at ANO,"

and on'how the improved CAP was to be implemented.

The procedure also provided instructions on determining operability and deportability, establishing significance end priority, and in closing the documentation package when the corrective actions were completed.

The procedure included the various forms which made up the Condition Report (CR) documentation (Forms 1000.104A through K).

The NRC inspectors found the above procedure to be adequate in providing the framework for the CAP, but discussed the apparent need for additional guidance in the~ areas of determining deportability, operability, and cause/ root cause. The NRC inspectors were informed that additional guidance in determining operability was being provided by a new procedure which was to become effective on April 30, 1989.

Because timeliness in making operability determinations had been a problem,.the new procedure (1000.116. " Operability Determination")

required the Shift Technical Advisor (STA) to make a determination within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> of the request for such a determination from the

.

Shift Operations Supervisor (505).

If the STA concluded that an

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engineering evaluation was needed, a documented interim determination by the STA that the system or component would remain fully functional during the time required for the evaluation was required.

The NRC inspectors determined that these provisions would help to preclude long-term conditions during which no documented basis existed for continued operations with systems or components which were being evaluated for operability.

The NRC inspectors noted that trending of identified conditions was not delineated by the above procedures and questioned how this was being accomplished. The NRC inspectors were informed that the In-House Events Analysis Group (IHEA) was trending the CRs and providing a periodic report to AP&L management. The NRC inspectors reviewed existing IHEA reports and found them to be acceptable; however, the NRC inspectors remained concerned that the trending program was not required by procedure.

The NRC inspectors discussed their concerns over the CAP implementation with the involved AP&L personnel and reiterated their concerns during the April 21, 1989, exit meeting.

The NRC inspectors determined that the new procedures provided an improved method of identifying, reporting, and correcting undesirable

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-5-conditions'at ANO. The new CAP was also found to provide an-acceptable framework for resolving previously identified NRC concerns.

Problems identified with the implementation of the CAP are discussed in subparagraph c, below.

No violations or deviations were identified.

b.

0A Audits The NRC inspectors reviewed QA Audits QAP-10-88, " Corrective Action,"

first half dated August 19, 1988, and second half dated March 29-1989. Since the first half audit was conducted shortly after the initiation of'the new CAP,'the findings were inconclusive. The

,

second audit was more productive and concluded that:

" Management

,

attention has not been adequately given to the timely completion of:

'

Condition report corrective actions

"

'For further evaluation' operability / deportability concerns

"*

Managers and IHEA root cause determinations

"*

Transmittal of completed records to ANO DCC

"*

Transmittal'of_CR's from security to IHEA"

"*

The report went on'to identify the most significant weakness of the-new CAP as "The failure to complete assigned corrective actions within the assigned time frames." The NRC inspectors review of selected condition report packages substantiated the QA audit findings.

The' NRC inspectors found the QA Audit to be effective in meeting the objectives of the QA program and in providing insight to the licensee management on areas requiring improvement.

No violations or deviations were identified.

c.

Documentation Package Reviews The NRC inspectors selected a number of CRs from the licensee provided tabulation which listed approximately 850 CRs for Unit 1, 525 CRs for Unit 2, and 100 CRs common to both Units.

Sone of the CRs were closed while others remained open for various reasons. The NRC inspectors also selected some Reports of Abnormal Conditions (RACs) which remained open from the previous corrective action systems. A partial listing of the RACs and CRs that were reviewed is contained in the attachment to this report.

The NPC inspectors noted that frequent delays in documenting both operability and deportability determinations were being made while waiting for "further evaluation." The NRC inspectors also noted that the CR Forms were not always properly completed, especially in the area of cause/ root cause. The CR procedure required a cause for each condition and a root cause for those conditions judged to be

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-6-significant; a root cause was not always provided for conditions that had been determined to be significant. The NRC inspectors discussed these observations with licensee personnel and also discussed questions they had on the reviewed RACs and CRs. The following are examples of problems observed:

(1) RAC-2-86112 This RAC was' initiated on June 24, 1986, to document discrepancies between the ANO-2 Technical Specification required protective system and safeguards system setpoints and the values calculated to be appropriate by Con.bustion Engineering Corporation (CE). The NRC inspectors, on April 19, 1989, were unable to determine from the available information if the condition had ever been evaluated. A telephone conference call

.was conducted on April 21, 1989, at which AP&L personnel explained that CE engineers had utilized an inappropriate containment pressure transmitter error value in their calculation.

(These transmitters had been replaced at ANO-2 with a different brand which had lower errors.) AP&L personnel explained that the proper transmitter error values had been substituted into the CE calculation for the high containment pressure trip setpoint when the CE error was detected and that the resulting setpoint was consistent with the implemented value. The RAC had remained open pending a determination of its deportability.

The AP&L personnel also informed the NRC inspectors that the implemented high-high containment pressure setpoint was verified to be appropriate on April 20, 1989, by using a method similar to that used earlier for the high pressure setpoint.

This RAC was transferred to the new CAP system by the initiation of CR-2-89-161 on April 19, 1989.

The NRC inspectors found the processing of this RAC to be an additional example of the NRC concerns with the previous corrective action systems at ANO and were troubled that these old issues (RACs) had not all been incorp:vated into the new CAP.

(A few of the old RACs had been transferred to new CRs in the weeks preceding the inspection, but numercus other RACs remained without actions being finalized.)

(2) g-1-88-239 l

This CR documerited a wiring error that was discovered on September 21, 1988, during the licensee's "as-building" of the esrential 4160 volt switchgear-A4. The wiring error caused one of the trip paths for the emergency diesel generator (EDG)

output circuit breaker to be inoperable. This condition could have caused an overload and loss of the EDG if it was being

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tested when a loss of offsite power occurred, concurrent with an engineered safety features actuation signal.

The condition was..

determined to be. reportable by the SOS and the Department Manager, but to be not reportable by the Licensing Department.

The Plant Safety Comittee (PSC) recommended that the condition not be reported. The condition was judged to have existed since the initial construction installation.

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. Although the condition was deterrrined to be not significant'

because only one EDG was affected, end the appropriate "cause" box had been checked on Form 1000.104F, a "rcot cause" was provided. This root cause stated that "the condition can be attributed to insufficient procedures to ensure operability. of electrical equipment controis."

A Job Order (J.0. 00768226) was completed on October 29, 1988, to correct and test the wiring for the circuit breaker. The CR remained open for completion of the additional corrective action to " develop procedures to verify operability of all 4160 and 6900 switchgear controls."

The NRC inspectors expressed their concern over the appropriateness of the determination to not report the above condition, especially in light of the additional wiring error detected in Switchgear A4 (CR-1-88-251) and the wiring error detected in Switchgear A3 (CR-1-88-324).

In addition, four termination problems were-detected during the "as-building" of the A3 and A4 switchgear, each of which could have lead to failure of the associated

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device. The NRC inspectors also discussed their observations about the appropriate cause/ root cause determinations being.

provided for a condition, and the adequacy of those determinations, s

(3)-RAC-2-88074

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This RAC, dated March 25, 1988, reported hanger and pipe deformation due to thermal growth. This RAC was marked for further evaluation to determine deportability. As of this inspection, the deportability determination had not been made and the RAC had not been converted to the CR system.

(4) CR-2-88-0015 This CR was written to document a long-term problem with the loss of the volume control tank (VCT) level indication wtthout an accompanying low level alarm. This had caused, on various occasions, the loss of the charging pumps due to air. binding.

The root cause was identified in 1983 as a design problem with the level detectors having a common reference leg so that a loss of reference leg caused both detectors to sense an erroneous normal level when the VCT was actually empty. To correct this t

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problem the l_icensee has issued a DCP which is scheduled to be accomplished during the next refueling.

(5) CR-2-88-0027 and CR-2-88-0069 These CRs were written in June 1988 to document the lift of one pressurizer code safety relief valve on June 6 and the lift of the second valve on June 23. The plant was at normal operating pressure and-temperature and at 100 percent power. On CR-0069, the event was marked "significant" but only "cause" was marked on Form 1000.104F. On CR-0027, the event was marked

"significant" but no mark was made on Form 1000.104F. What was apparently a root cause was written up on this form, but since no conclusion was drawn, there was no identified corrective action. The NRC inspectors were told that these CRs are still

'open and are being reevaluated.

The NRC inspectors concluded that this area warrants further evaluation and recommended to NRC management that additional i

inspection activity be conducted as the CAP implementation progresses.

l 3.

Steam Extraction Line Rupture Event - Unit 2 (93702)

The NRC inspector observed the high pressure turbine extraction steam line that ruptured on April 18, 1989. The steam line rupture was approximately 180 degrees around the 14-inch diameter. pipe ud 2 inches below the turbine nozzle to pipe weld. The original thickness of the pipe was 3/8-inch nominal wall and had been eroded to less than 1/32 inch in the area where failure occurred. The cause for the preferential erosion has been determined to be a step on the internal diameter of the pipe which resulted from a pipe to nozzle mismatch. The high pressure turbine has four extraction steam lines of which two are 14-inch diameter and two are 10-inch diameter. The three lines which did not rupture were inspected for wall thinning using ultrasonic thickness measuring equipment. The other 14-inch line was measured at less than 0.100-inch remaining wall thickness and will be replaced.since the minimum design wall thickness required was 0.267-inch. The two 10-inch lines were measured and determined to have sufficient wall thickness; however, the licensee was also considering replacing them.

The original material for the extraction steam system was a carbon steel material while the replacement material was a low alloy steel. The licensee had a wall thickness monitoring program for systems susceptible to erosion / corrosion. Although much of the pipe downstream of the rupture had been replaced because of wall thinning which had been detected during the previous outage, the area which ruptured was neither suspected of wall thinning nor measured. The monitoring program for wall thinning of pipe was based on calculated flow rates, piping geometries, and past experience. The licensee also used the EPRI "CHEC" computer program to assist in determining which areas in

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single-phase piping systems were most susceptible to erosion and/or corrosion. The licensee was also working with EPRI to utilize the newly developed "CHECMATE" computer program for two-phase piping systems.. The

' licensee's wall thinning monitoring program had included the steam'

-extraction lines in the selection for_ the next outage. The selection also included, for the first time, components in safety-related piping systems, i

E such as. the main steam and nmin feedwater piping systems.

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No violations or deviations were identified.

4.

Exit Meeting (30703)

Exit _ meetings were conducted April 20 and 21, 1989, with the licensee representatives identified in paregraph 1 of this report. No written material was provided to the licensee by the NRC inspectors during this i

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reporting period. This licensee did not identify, as proprietary,'any of:

the materials provided to, or reviewed by, the NRC inspectors during this inspection.

During these neetings, tta NRC inspectors summarized the scope and findings of the inspection.

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ATTACHMENT

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LIST OF DOCUMENTS REVIEWED

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e Number

- iiubject RAC-2-85200, NQ Power Supply RAC-2-86112, PPS Limits Not Per Calculation.

RAC-2-86201, Incorrect Electrical Splices

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CR-1-88-191, Ser'vice Water Flow Rates low

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CR-1-88-239, Jumper Not Installed in.Switchgear A4 CR-1-88-245,-Loose Wire in Switchgear Cubicle A-408 CR-1-88 282 Motor Feeder Cable Failure CR-1-88-284, Motor Feeder Cable' Failure CR-1-88-305, Wrong Overcurrent Relay Taps CR-1-88-324 Wiring Not Per Drawing

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' CR-1-88-337, Bad' Crimp..on Terminal Lug

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CR-1-88-344, Cracks,in EFW Pump Impeller

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.CR-1-89-089,' Solenoid Coil Age Over Qualified Lifetime

,CR-1-89-137, 480 Volt Circuit Breaker Would Not Close.

CR-1-89-151, 480 Volt Circuit Breaker Would Not Close CR-1-89-228, Drmper Seal Age Over Qualified Lifetime:

y.

CR-2-88-0011; Charging Pump ~ "C" - Air Bound

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'CR-2-88-0015, Loss of VCT Level c

CR-2-88-0018... Sporadic Vibration & Loose Parts Monitor Alarms

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CR-2-88-0021, Cherging Pumps - Packing Leaks

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CR-2-88-0023, Fuel Element Leakage Indicated

' CR-2-88-0027, Pressurizer Relief Valve Lift

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CR-2-88-0069, Pressurizer Relief Valve Lift

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CR-2-88-0115, Potential Failure of Kapton Diaphragm (Part 21)

CR-2-88-0149, RCP Breaker Failed to Close CR-2-88-0166, Air System Moisture Test Failed CR-2-88-0167, Spare Cards Not Available CR-2-88-0175, Charging Pump Air Binding CR-2-88-0244, Missed Surveillance Test CR-2-88-0335, Reactor Trip From ESFAS Surveillance Test CR-2-88-0343, MSSV Response During Reactor Trip CR-C-88-007 Fire Water Pump' Diesel Without Coolant CR-C-88-029, SPDS Computer Cooler Failures CR-C-88-039, Jumper for Connecting Offsite Power CR-C-88-048, Problems with HFA Relays CR-C-88-049, Inoperable Fire Door in October 31, 1986

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