IR 05000282/1999001

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Insp Repts 50-282/99-01 & 50-306/99-01 on 990115-0225.No Violations Noted:Licensee Operations,Maint,Engineering & Plant Support
ML20204E480
Person / Time
Site: Prairie Island  Xcel Energy icon.png
Issue date: 03/18/1999
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20204E470 List:
References
50-282-99-01, 50-282-99-1, 50-306-99-01, 50-306-99-1, NUDOCS 9903250043
Download: ML20204E480 (24)


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U.S. NUCLEAR REGULATORY COMMISSION REGIONlil Docket Nos: 50-282,50-306 License Nos: DPR-42, DPR-60 i

Report No: 50-282/99001(DRP); 50-306/99001(DRP)

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l Licensee:

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Northern States Power Company Facility: Prairie Island Nuclear Generating Plant Location: 1717 Wakonade Drive East Welch, MN 55089 Dates: January 15 through February 25,1999 Inspectors: S. Ray, Senior Resident inspector 1 P. Krohn, Resident inspector S. Thomas, Resident inspector ,

P. Lougheed, Reactor inspector '

Approved by: Roger Lanksbury, Chief Reactor Projects Branch 5 '

Division of heactor Projects 9903250043 990318 PDR ADOCK 05000282 e PM .

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EXECUTIVE SUMMARY Prairie Island Nuclear Generating Plant, Units 1 & 2 Prairie Island Inspection Report 50-282/99001(DRP); 50-306/99001(DRP)

This inspection was performed by the resident inspectors and included aspects of licensee operations, maintenance, engineering, and plant support. A regional engineering inspector also provided some inspection followup suppor Operations

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Conduct of operations was generally good. Licensee management made a conservative decision to shut down Unit 2 to repair a power range nuclear instrument cab!e and small leaks in secondary-side steam generator manways. During the shutdown, good supervisory oversight and prompt response to increasing turbine vibrations were note (Section 01,1)

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Inconsistent control room control board monitoring was illustrated by two opposing examples. Very good monitoring was illustrated by the lead reactor operator noticing, without the benefit of a turbine runback alarm, that turbine power was decreasing because of an actual 2.2-second runback. Weak monitoring occurred when, until pointed out by the inspectors, a number of operators did not notice that an extra reactor protection system control board indication was locked in as the result of removing nuclear instrument system channel 2N44 from service. (Section 01.1)

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Activities of the safety audit (offsite review) committee observed by the inspectors met the requirements of the Technical Specifications. (Section 07.1)

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Licensee management proactivel? commissioned an independent assessment of its readiness for dry cask loading activities. The assessment resulted in several beneficial findings and suggestions. Management's response to the assessment results was appropriate and actions were initiated to resolve the concerns prior to loading the cas (Section O7.2)

Maintenance

- The 12 maintenance and surveillance test activities observed by the inspectors were well planned, used approved maintenance or surveillance test procedures, and involved personnel who exhibited safe work practices. Good coordination and communication between different departments was a strength common to all of the activitie j

(Section M1.1)

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Operators failed to ensure that a required Technical Specification surveillance test of the j source range high neutron flux trip funcFen had been completed prior to closing the reactor trip breakers and withdrawing tae shutdown banks of control rods. The possibility of just s A an error occurring had been identified three months earlier, but a l temporary procedure change issued to prevent the problem was not sufficiently clea The failure to perform the required surveillance test was a non-cited violatio (Section M1.2)

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  • . Based on an inspection of the material condition of about 60 motor-operated valves, the inspectors concluded that adequate preventive maintenance was being accomplishe Some minor oil leakage was noted and was being addressed by the license (Section M2.1) '

+ The inspectors conducted an extensive common-cause failure review of 20 risk-significant, safety-related components. The review included system / component walkdowns and maintenance history searches. No evidence of common-cause failure modes were identified by the inspectors. (Section M2.2)

Enaineerina

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The inspectors identified a minor error in the Updated Safety Analysis Report description of refueling water storage tank levelinstrumentation. The error had no safety significance for actual plant operation and will be corrected by the license (Section E3.1)

Fuel oil consumption calculations for the D1 and D2 emergency diesel generators had I not been updated when anticipated accident loading was changed in the Updated Safety Analysis Report. The licensee determined that the design basis fuel oil storage requirements were still met and initiated actions to update the calculation (Section E3.2) i

Plant Support  !

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The licensee's evaluation of the Notification of Unusual Event associated with the loss of the 1M transformer was insightful and contained several good recommendation (Section P1.1)

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e i Report Details Summarv of Plant Status Unit 1 operated continuously at or near full power for the entire inspection period. Unit 2 operated at or near full power until a voluntary outage on February 6,1999. The unit was taken to hot shutdown to repair the 2N44 power range nuclear instrument system (NIS) detector cable) and manway cover leaks on the 22 steam generator, and to pedorm other miscellaneous work. Unit 2 was restarted on February 7, reached full power on February 8, and operated at or near full power for the remainder of the inspection perio j l. Operations l 01 Conduct of Operations j 01.1 General Comments

inspection Scoce (71707) j The inspectors conducted frequent reviews of plant operations. These reviews included )

observations of control room evolutions, shift turnovers, operability decisions, and logkeeping. Updated Safety Analysis Report (USAR) Section 13, " Plant Operations,"

was reviewed as part of the inspectio l Observations and Findinos

On January 19,1999, the inspectors compared the actual annunciator and bistable status lights received as a result of removing the Unit 2 power range NIS channel 2N44 from service with those described in Instrument Failure Guide,2C51.4, " Power Range Nuclear Instrument N44 - Low," Revision 1 Power range NIS channel 2N44 had been removed from service on January 13, because of intermittent noise problems associated with the lower uncompensated ion chamber detector. Since no procedure existed which explicitly described removing an NIS channel from service, the procedure for nuclear instrument failure,2C51.4, was used. Instrument Failure Guide 2C5 described the steps necessary to realign the reactor protection system for one-out-of-three coincidence logic vice the normal two-out-of-four logi During the comparison, the inspectors noticed that bistable status light 44512-0404,"PWR RNG HI F RATE NC 44 U/K [ Power Range High Flux Rate Instrument Bistables 44U and 44K]," was illuminated but was not discussed in 2C51.4. The inspectors discussed the discrepancy with the Unit 2 reactor operator (RO) who acknowledged the discrepancy and stated that the bistable status light was likely a result of having removed 2N44 from service. Based on the inspectors' observation, the RO submitted Procedure Change l

Request 19981586 on January 27, to include the bistable status light

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44512-0404 in 2C51.4. The inspectors later interviewed the RO and lead

reactor operator (LRO) who were on duty on January 13. Both operators stated that 2C51.4, although not precisely describing the condition of 2N44 at the time,

, was used to remove the detector from service. When asked explicitly about the

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ext.a bistable status light,44512-0404, both stated that they did not notice it appearing while executing 2C5 The inspectors reviewed 2C51.4 and discussed its contents with an operations support pool shift manager. The inspectors noted that 2C51.4 was adequate in verifying that reactor protection bistables were placed in the correct state and that the unit was lined up for correct reactor protection coincidence logic with 2N44 removed from service. Even though status light 44512-0404 was not in the procedure, two other annunciators,47513-0101,"NIS Power Range Positive i Flux Rate Channel Alert" and 47513-0201,"NIS Power Range Negative Flux l Rate Channel Alett," were included. Those annunciators demonstrated that the bistables associated with the power range flux rate bistables were in the correct state. Status light 44512-0404 was designed to light when either a positive or negative flux rate trip was receiveo and. in terms of bistable states, was a redundant indication to annunciators 4/513-0101 and 47513-020 Discussions were also held with the system engineer responsible for this j system. The inspectors verified that the correct function, operation, and '

indications associated with bistables 44U and 44K were periodically tested in i accordance with surveillance test procedure l Until pointed out by the inspectors, neither the initiating crew nor subsequent crews noticed that an extra reactor protection system control board indicatian was lit that was not described in the procedure used to remove power range NIS channel 2N44 from service on January 13. The safety significance of the inspectors' observation was low since the procedure wntained other steps and verifications to ensure that bistables were placed in the correct tripped state and l

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that proper reactor protection system coincidence logic was satisfie Nevertheless, the inspectors' observation demonstrated a lock of operating c.ew awareness concerning control board reactor protection system indication l l

  • On January 22,1999, the inspectors observed the Unit 2 control room crew l response to a turbine runback signal. The runback occurred during shift turnover. The runback lasted for 2.2 seconds, decreased turb!nc output by approximately 12 megawatts or 2 percent reactor power, and occurred with no audible control board annunciators or alarms to alert the operators of the transien Despite the lack ol audible indications and despite being in the process of conducting a shift turnover, the LRO immediately noticed the drop in turbine load. The LRO notified the RO and shift supervisor who joined in monitoring plant response to the runback. All equipment responded appropriately, with control rods inserting into the core ac expected. Once plant conditions had stabilized, the shift supervisor contacted the system er.gir.cer who responded to the control room to review the even Power range NIS channel 2N44 had been taken out-of-service with the i

associated bistables placed in the trip pcsition. Coincident with 2N44 being l out-of-service, the 8 main feedwater regulating valve was experiencing periodic

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flow oscillations because cf tight valve stem packing. Although not known at the

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time of the event, it was later determined that the runback' signal occurred d Jring one of the feedwater regulating valve oscillations when the two-out-of-four

"over-temperature delta-temperature" turbine runback coincidence logic became satisfied. One runback signal was caused by the feedwater regulating valve oscillations leading to a slightly elevated reactor coolant system average temperature, while the other runback signal was present because of the tripped bistables associated with 2N44 being out-of-service. Since all the annunciators associated with power range protection circuits were already lit and acknowledged because of the 2N44 bistables being tripped, no additional alarm occurred to alert the operators to the runbac *

During the first portion of the inspection period, the licensee was monitoring and investigating two problems with Unit 2. The first problem involved erratic indications on NIS channel 2N44 as discussed above. The second problem involved indications of leakage inside containment. During the first week of February 1999, the I;censee determined that the prcblem with 2N44 was most likely in the cable connected on the top of the detector and that the containment leakage appeared to be coming from secondary-side manways on the 22 steam gererator. Neither problem forced a rapid reactor shutdown, but both required an eventual shutdown to repair. Licensee management made t wnservative decision to conduct a brief outage during the first convenient time perio That convenient time occurred on February 6,1999, and the inspectors observed the Unit 2 shutdown. The shutdown was performed well with no significant discrepancies nr 'ed. Oversight of the evolution by the shift supervisor was excellent. During the turbine coastdown after operators took it offline, increasing vibrations on the number F ~oearing were noted by the operators as the turbine approached a criticca :. peed. Operators promptly responded by breaking vacuum in the concienser to cause the turbine to pass il';ough the critical speed more rapidl Subseonent to entering mode 3, the operators failed to perform a required eveillance test procedure prior to making the rod control system capable of wandrawing rods (see Section M1.2). On February 7, the 2N44 cable and the 22 steam generator manway repairs were completed successfully and the startup of Unit 2 was commenced. Unit 2 returned to full power operation on February 8. The inspectors observed the reactor startup and the placing of the generator online and no'od no discrepancie As part of this inspection, the inspectors reviewed the following procedures:

Operating Procedure 2C1.4, " Unit-2 Power Operation," Revision 17;

  • Operating Procedure 2C1.3, " Unit 2 Shutdown," Revision 43; and

Operating Procedure 2C1.2," Unit 2 Startup Procedure," Revision 1 c. Conclusions i Conduct of operations was generally good. Licensee management made a conservative decision to shut down Unit 2 to repair a power range NIS cable and small

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leaks in secondary-side steam generator manways. During the Unit 2 shutdown, good supervisory oversight and prompt response to increasing turbine vibrations were noted.

I Inconsistent control room control board monitoring was illustrated by two opposing

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exarnples. Very good monitoring was illustrated by the LRO noticing, without the benefit of a turbine runback alarm, that turbine power was decreasing because of an actual 2.2-second runback. Weak monitoring occurred when, until pointed out by the inspectors, a number of operators did not notice that an extra reactor p,otection system control board indication was locked in as the result of removing NIS channel 2N44 from servic O2 Operational Status cf Facilities and Equipment 02.1 Cold Weather Preparations (71714)

The inspectora walked down selected safety-related systems (Section M2.2) during days when the outside ambient temperature was approximately minus 10 degrees Fahrenheit ( F). The intent was to see if inclement weather conditions could contribute to common-cause failure modes of equipment selected for this inspection. All equipment rooms were at normal,60 to 70 F ambient temperatures. Louvers / dampers connecting to outside areas were visually inspected for evidence of binding / seizing due to the cold temperatures and local ice and snow conditions. No interferences with louver or damper operations were noted. Particular attention was focused on the normai makeup source to the AFW pumps, the condensate storage tanks (CSTs). Three cross-connected CSTs were located outside of the Unit 1 and Unit 2 turbine buildings. Each CST had one large outlet pipe which was exposed to the outside environment prior to joining a common AFW pump suction header located beneath the ground floor of the turb ne building. The inspectors looked at specific heat trace systems and ind!"ations associated with the CST outlet piping. All were found to be operating normally, preventing any freezing of the CST outlet piping and subsequent loss of the normal AFW pump suction suppl Quality Assurance in Operations

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0 Safety Audit Committce (SAC) Meetina Inspection Scope (71707)

On January 20,1909, the licensee held its semi-annual SAC (offsite review committee)

meeting as required by Technical Specification 6.2.A. The inspectors observed the meeting, Observations and Findinas The inspectors verified that the membership, qualification, and quorum requirements of TS 6.2.A were met. All of the required subjects listed in the TS were discussed in the meeting. Some of the specific comments and items discussed by the SAC members included:

forming a subcommittee to review the Prairie Island improved Technical Specifications;

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ways the SAC could improve / increase its role in providing quality assurance oversight;

significant plant events since the last SAC meeting, including the recent increase in reactor plant trips;

the fact that there was no formalized process which encompassed all facets of the Prairie Island self-assessment effort and licensee plans for improvements to

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the self-assessment program including increased management oversight; and

an update from Nuclear Analysis and Design (the corporate nuclear engineering group), which included discussions on the status on ongoing efforts to reanalyze the small-break loss-of-coolant accident for Prairie Island, the status of the latest main steamline break accident analysis methodology suomittal, and the status of the development of adjusted axial flux difference models to be used to aid in predicting axial flux transients late in core lif Conclusions Activities of the SAC observed by the inspectors met the requirements of the T .2 Quality Services AssessmNt of Readiness for Drv Cask Loadina Inspection Scope (71707)

The licensee commissioned the performance of an independent assessment of its readiness to load the eighth dry fuel storage cask. Because it had been over two years since the previous cask load activitia, licensee management wanted an assessment of whether the preparations for the next loading were adequate. The inspectors attended the exit meeting for the assessmen Observations and Findinas The assessment was headed by a senior member of the licensee's quality services group and included three experienced employees of other utilities that had recently completed successful dry cask loading activitie In the exit meeting, the assessment group stated that the licensee could probably safely perform the cask loading operations, but it was their opinion that the preparations for the loading were not adequate and that the loading would not be efficient if performed without additional actions. The assessment group stated that preparations for the current cask loading activities had not received the level of management attention that previous activities had. In addition, the number of personnel providing engineering support for the activities was significantly less than in the pas The plant manager acknowledged the findings and ordered that the cask loading schedule be delayed until corrective actions for the assessment issues could be take Additional personnel viere assigned to the project and a formal plan and schedule were developed by the end of the inspection perio , .

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l Conclusions Licensee management proactively commiss' ned an independent assessment of its i readiness for dry cask loading activities. The assessment resulted in several beneficial l findings and suggestions. Management's response to the assessment results was approprNe and actions were initiated to resolve the concerns prior to loading the cas Miscellaneous Operai!ons issues (92700)

0 (Closed) Licensee Event Report (LER) 50-282/99001: 50-306/99001 (1-99-01): Unit 1 Reactor Trip Following Failure of the Station Auxiliary Transformer. The event was previously discussed in Section 01.5 of Inspection Report 50-292/98023(DRP); l 50-306/98023(DRP). Specific corrective actions taken by the licensee to recover from the event and verify that no damage had occurred to other components were extensive and exhaustive. The licensee determined that the cause of the 1M transformer explosion was a phase-to-phase fault on the 20-kilovolt winding. The cause of the fault l was still unknown and root cause analysis efforts were to continue for the next several months. The 1M transformer was scheduled to be replaced during the spring 1999 refueling outage for Unit 1. Plant operations were continuing without the transformer for the remainder of the operating cycle. The inspectors had no remaining safety significant concerns with the even l l

11. Maintenance M1 Conduct of Maintenance M1.1 General Comments inspection Scope (61726. 62707. 92902)

The inspectors observed all or portions of the following maintenance and surveillance test activities. Included in the inspection was a review of the surveillance test procedures (SPs) and work orders (WOs) listed, as well as the appropriate USAR sections regarding the activities. The inspectors verified that the SPs for the activities observed met TS requirements. The following activities and procedures were reviewed by the inspectors:

SP 2006B, "NIS Power Range Axial Offset Calibration Greater than 50% Power,"

Revision 34;

SP 2005, " Unit 2 NIS Power Range Daily Calibration," Revision 27;

SP 1102, "11 Turbine-Driven AFW [ Auxiliary Feedwater] Pump Monthiy Test,"

Revisico 64;

SP 2102, "22 Turbine-Driven AFW Pump Monthly Test," Revision 56;

SP 1112 " Steam Exclusion Damper Test," Revision 34;

  • SP 2091, " Containment Fan Coil Units Surveillance Test," Revision 20; i

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SP 1075, "TN-40 Fuel Selection and Identification," Revision 6; l

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SP 1024, " Refueling Water Storage Tank Level Functional Test," Revision 10;

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SP 2024, " Refueling Water Storage Tank Level Functional Test," Revisicn 14;

WO 9900448, "2N44 Delta I is Reading Erratic"; l

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WO 9901103, "D2 Diesel Generator Engine Jacket Coolant Pump Tripped"' and ,

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WO 9900635," Bypass 2N44 Trips to Allow Performance of SPs."

b. Observations and Findings

On January 13,1999, power range NIS channel 2N44 was declared inoperable because of spiking on its lower detector. As required by TS Table 3.5-2A, 1 Action 2a, the reactor protection bistables associated with 2N44 were placed in a tripped condition. On January 21, the inspectors observed the licensee perform an axial offset calibration in accordance with SP 2006B. Since that surveillance test included generating trip signals from the other power range NIS channels, the bistables assv. 4ted with 2N44 first needed to be bypassed. That action was allowed for up to 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> in accordance with TS Table 3.5-2A, Action 2 Prior to the test, the system engineer, instrument and controls (l&C) supervisor, and the l&C technicians performing the test, met to go over SP 2006B in detail and develop the temporary procedure changes that would be sequired to complete the test with an inoperable 2N44 channel. The system engineer then explained the plan to the shift supervisor who approved the temporary change The I&C technicians then bypassed the trip bistables per WO 990063 The entire surveillance test, including a post-test calorimetric calibration in !

accordance with SP 2005, was completed in about 3% hours with no problems '

observed. The l&C technicians performed the work in a careful but expeditious manne *

The inspectors observed surveillance testing of the 11 and 22 turbine-driven AFW pumps in accordance with SP 1102 and SP 2102. During both surveillance tests, the equipment performed as expected and all observed parameters were within specifications. The system engineer was present throughout both surveiliance tests and carefully monitored turbine governor response during startup and overall equipment operation. Lccal operators maintained formal communications with the control room operators during all portions of the test During SP 1102, Step 7.26, the local operator was required to record the 11 auxiliary feedwater pump suction strainer outlet pressure on gauge PI-1105 This was a compound gauge providing a pressure indication in three units of measurement: inches of mercury vacuum, feet of water pressure, and pounds per square inch - gauge (psig). The operator initially recorded the suction strainer outlet pressure as 18 psig. The system engineer observed the value

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The inspectors observed the performance testing of steam exclusion dampers in i accordance with SP 1112. Although there was no formal pre-job briefing, there I was a thorough discussion between the control room operator and the I&C l technician. performing the testing, covering the details of the procedure. During the testing, the inspectors noted that the I&C technician used good verification practices when setting up individual circuits for testing and while installing and removing test equipment required for testin l

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The inspectors observed containment fan coil testing in accordance with SP 2091. The purpose of the testing was to obtain nominal current and voltage values for containment fan coil units 21,22,23, and 24 while operating in slow speed. The inspectors noted that appropriate electrical precautions $nere taken by the electrician while working near energized motor control centers. The data obtained was within expected values and the surveillance test was successfully '

complete The inspectors observed portions of spent fuel operations in accordance with SP 1075. The purpose of the activity was to identify and inspect spent fuel assemblies to be loaded into the next dry fuel storage casks. The nuclear engineer coordinating the activities demonstrated good control of the evolution and provided good insights and training to the RO on the specialized tools used to move thimble plugs and older fuel cells. Good component identification techniques, careful handling of fuel cells, and formal communications were observed throughout the activitie +

The inspectors observed refueling water storage tank level testing in accordance with SP 1024 and SP 2024. The tests were performed by a relatively inexperienced l&C technician under the supervision of an experienced technician. The testing was performed well with no discrepancies noted. Near the beginning of the procedure, the RO reminded the new technician that the operators expected the technicians to use three-way communication techniques when contacting the control room to confirm annunciator status. The technician used acceptable communications techniques from that point forwar + The inspectors observed both the mechanical and electrical portions of work associated with WO 9901103 for replacemer;t of the D2 emergency diesel generator (EDG) jacket cooling water pump. The work was accomplished in a very safe and careful manner. During the planning for the job, the maintenance supervisor realized that a small amount of chromated water would have to be drained from the system as the piping was disconnected from the pump. The supervisor assigned a second mechanic to the job so that one mechanic could

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disconnect the piping while the other collected the drainage. The mechanics I

were careful to follow the appropriate safety precautions for handling and disposal of the c' romated water.

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l Conclusions The 12 maintenance and surveillance test activities observed by the inspectors were well planned, used approved maintenance or surveillance test procedures, and involved i personnel who exhibited safe work practices. Good coordination and communications 1 between different departments was a strength common to all of the activitie M1.2 Failure to Perform Surveillance Test before Withdrawina Control Rods Inspection Scoce (92902)

On February 6,1999, the licensee identified and informed the NRC that it had failed to perform a required Technical Specification surveillance test prior to withdrawing control rods while Unit 2 was in hot shutdown conditions. The inspectors reviewed the circumstances of the event and the licensee's corrective actions, Observations and Findinas In early November 1998, the licensee identified that a deficiency existed in the surveillance testing program in that no test of the source range high flux reactor trip logic was specified by procedure or schedule prior to making the control rod drive system capable of rod withdrawal when the reactor was only taken to hot shutdown or cold shutdown instead of refueling mode. No actual occurrences of a failure to perform the surveillance test was identified. Such a test was required by TS Table 4.1-1 A. The licensee reported the finding in LER 50-282/98017; 50-306/98017 (1-98-17) on ,

December 3,1998. Corrective actions included issuing Temporary Change Notices l (TCNs) 1999-0151, " Unit 1 Shutdown," and 1999-0153, " Unit 2 Shutdown," which added a step to each unit's shutdown procedure with instructions to perform the source range test immediately prior to the step that directed the operator to withdraw the shutdown banks of control rods if a cooldown was not planne A pen-and-ink change was inserted prior to the appropriate step in each unit's shutdown procedure to indicate the existence of the TCN. However, the pen-and-ink change did not make it exactly clear to which step it applied. On February 6,1999, when the ROs reached the step in the Unit 2 shutdown procedure which directed them to withdraw the shutdown banks, it appeared to them that the TCN applied to the previous step which discussed actions needed if a cooldown was planned. That step had been marked as not applicable since a cooldown was not planned. The ROs apparently believed that the TCN was also not applicable, closed the reactor trip breakers, and withdrew the shutdown banks of control rods without the source range trip test having been complete The ROs soon noted the mistake, reinserted the shutdown banks, and opened the reactor trip breakers to make the rods incapable of being withdrawn. Rods had been withdrawn or capable of being withdrawn for a total of about 30 minutes. The licensee initially reported the event to the NRC under 10 CFR 50.72 but later retracted the notification when they confirmed that an immediate notification was not required. The license intended to issue an LER (2-99-01) within 30 days as required by 10 CFR 50.73.

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A surveillance test of the source range trip function was successfully completed about four hours later. Thus, failure to perform the test prior to making the control rods capable of withdrawal had minimal safety significanc Closure of the reactor trip breakers and withdrawal of the shutdown banks of control rods on February 6,1999, prior to performing a surveillance te.st on the source range high neutron flux trip, was a violation of TS Tabla 4.1-1 A, Item 6.b, which required that the trip be verified to be operable prior to entering a condition in hot shutdown, intermediate shutdown, or cold shutdown where the reactor trip breakers were closed and the control rod drive system was capable of rod withdrawal. This nonrepetitive, licensee-identified and corrected violation is being treated as a non-cited violation, consistent with Section Vll.B.1 of the NRC Enforcement Policy  ;

(NCV 50-306/99001-01(DRP)). l The LER associated with this event (2-99-01) will be considered open when issued I pending the inspectors verification that appropriate corrective action commitments have been entered into the licensees corrective action system. Licensee Event Report 1-9817 is closed in Section M l Conclusions l

Operators failed to ensure that a required Technical Specification surveillance test of the source range high neutron flux trip function had been completed prior to closing the reactor trip breakers and withdrawing the shutdown banks of control rods. The possibility of just such an error occurring had been identified three months earlier, but a i temporary procedure change issued to prevent the problem was not sufficiently clea The failure to perform the required surveillance test was a non-cited violatio M2 Maintenance and Material Condition of Facilities and Equipment M2.1 Unit 1 Motor-Operated Valve Inspection Inspection Scope (92902)

The inspectors examined the physical condition of a large number c,r motor-operated ;

valves associated with Unit I Observations and Findinas

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The inspectors examined approximately sixty motor-operated valves. The valves were located in a number of safety and nonsafety-related systems which included cooling water, component cooling, safety injection, main steam, containment spray, auxiliary i feedwater, and feedwate '

Generally, the material condition of the valves was good as evidenced by clean and well lubricated valve stems, tight packing glands, no excessive buildup of grime or dirt on the valves or motors, protected electrical connections, and minimal corrosion observed on or near the valves. The following material discrepancies were noted by the inspectors:

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  • MV32095 had packing leakage as evidenced by a buildup of chromate residue on and around the packing gland follower and a buildup of grime on the valve actuator threads;
  • MV32094 had packing leakage as evidenced by a buildup of chromate residue on and around the packing gland follower;
  • MV32093 had packing leakage as evidenced by a buildup of chromate residue on and around the packing gland follower; and
  • Oil leaks were noted on the operators for MV32058, MV32089, MV32090, MV32091, MV32092, MV32093, MV32378, MV32139, MV32133, MV32034, and MV3203 The inspectors noted that work request stickers had been placed on MV32091 and MV32093. The inspectors discussed all of the noted deficiencies with the system engineer responsible for the motor-operated valve program at Prairie Island. The system engineer informed the inspectors that each would be evaluated and repaired as require Conclusions Based on an inspection of the material condition of about 60 motor-operated valves, the inspectors concluded that adequate preventive maintenance was being accomplishe Some minor oil leakage was noted and was being addressed by the license M2.2 Review of Selected Systems / Components Based on Probabilistic Risk Assessment Common-Cause Failure Analysis Inspection Scope (92902)

Based on common cause failure information obtained from the licensee's probabilistic risk assessment team leader, the inspectors performed walkdowns and maintenance history reviews of the following systems / components:

  • 11,12,21, and 22 AFW pumos;
  • 15,16,25, and 26 safeguards bus sequencer programmable logic controllers;
  • 11 and 21 safeguards screenhouse roof exhaust fans;
  • 121 and 122 fuel oil transfer pumps;
  • 12 and 22 diesel-driven cooling water pumps (DDCLPs);
  • 15 and 16 safeguards bus switchgear room unit coolers; i
  • DS and D6 EDG .

l The systems / components were chosen based on a combination of risk achievement worth and Fussel-Vesely rankings obtained from the Prairie Island Nuclear Generating Plant Individual Plant Examination, NSPLMI-94001, Revision 0. Risk achievement worth measures the factor by which core damage frequency increased if the equipment was removed from service. Fussel-Vesely measured the overall contribution of an event towards the core damage frequency. The combination of both rankings allowed the inspectors to examine systems / components that had both large risk effects when ,

removed from service and were significant contributors to overall core damage l frequenc Observations and Findings

Walkdowns of AFW pumps and associated critical piping noted no abnormalitie I Suction and discharge valve lineups, trip mechanism settings, cooling water supplies, i and goverhor, motor, and pump oil levels were correct. Local and remote selector l switches were aligned to ensure required automatic safeguards functions. Safeguards programmable logic controller eouipment was also found to be operating correctly as evidenced by the absence of er;or messages and the periodic illumination of status lights on the front of the load sequencers. Safeguards screenhouse roof exhaust fan electrical lineups, louver / damper condition and position, safety train separation, and louver / damper actuators and associated air supplies were visually inspected. No abnormalities were note Fuel oil transfer pump disconnect switches and circuit breaker electrical lineups, local l and remote selector switch positions, and principal valve lineups for the EDGs were verified. During the walkdown, the inspectors noticed that there was little discernable difference between the ON and TRIPPED positions of 480-volt General Electric 8000 model circuit breakers associated with the D5 and D6 EDG fuel oil transfer pumps on motor control centers 2TA1 and 2TA2. This made it difficult to determine if the breaker was in the tripped status, which would have rendered the associated pump inoperabl The inspectors contacted the system engineer and questioned the status of the luel oil transfer pump circuit breakers. The engineer stated that this difficulty had been previously noted by the operators and declared as operator work around 19960857 in July 1996. The inspectors verified that the observation was included in the current list of open work around issues and was targeted for correction by July 1 ~99. During the D1 and D2 EDG fuel oil transfer system walkdown, the inspectors noticed that the engine fuel oil suction lines exited from the top of the day tank rather than the bottom. This prompted the inspectors to further examine the D1 and D2 fuel oil day tank configurations. Results of that investigation are discussed in Section E The D1 and D2 EDGs, D5 and D6 EDGs, and 12 and 22 DDCLPs were inspected for satisfactory standby air, lubricating oil, fuel oil, jacket cooling water, and raw cooling water levels, temperatures and pressures. Room ventilat.bn configurations, control panel switch positions and indications, and electricallineups of support equipment and output power were also reviewed. No discrepancies were noted. A visual inspection of the 15 and 16 safeguards bus switchgear room unit coolers noted no abnormalitie Both coolers were running satisfactorily, maintaining the bus rooms at approximately 70 F.

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The inspectors reviewed the maintenance histories of the risk significant systems / components identified above. A total of 315 WOs and 50 nonconformance reports (NCRs) associated with the system / components were screened of which 31 WOs and 25 NCRs were selected for a detailed review. Emphasis was placed on identifying any commonalities in equipment problems or failures over the life of the systems / components to date. System engineers were contacted to better understand the root cause of several equipment failures and problems. The inspectors'

investigations revealed no instances where prior maintenance histories indicated common-cause failures that had been overlooked by licensee maintenance, engineering, or operating personne Conclusicas The Inspectors conducted an extensive common-cause failure review of 20 risk-slgnificant, safety-related components. The review included system / component walkdowns and maintenance history searches. No evidence of common-cause failure modes were identified by the inspector M8 Miscallaneous Maintenance issues (92700)

M8.1 (Closed) LER 50-306/98006 (2-98-06): Unplanned Actuation of Unit 2 Engineered Safety Feature Equipment During Performance of a Sur Mance Test Procedure Due to Personnel Error. This event was originally discussed in Section M1.2 of Inspection Report 50-282/98023(DRP); 50-306/98023(DRP) and was considered a minor violatio The licensee identified the main causes of the event were an inadequate pre-job brief and inadequate self-checking techniques used by the electrician operating the relay Two commitments have been entered into the licensee corrective action program which addressed those issues. Per commitment 19990132, the licensee will conduct refresher pre-job brief training for personnel tasked with conducting pre-job briefs. Per commitment 19990133, the licensee will conduct self-checking simulator training for appropriate work group M8.2 (Closed) LER 50 282/98017: 50-306/98017 (1-98-17): Failure to Test Source Range High Flux Trip Functions During Non-Refueling Outages as Required by Technical Specification 4.1-1 A. This licensee finding was discussed in Section M1.2 of this repor The inspectors verified that commitment 19983344 had been entered into the licensee's corrective action system to develop the appropriate test procedures. As discussed in )

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Section M1.2, the licensee issued TCNs as an interim measure. The licensee was unable to find an actual case where they had failed to perform the required testing in the l

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past, so the issue was not considered a violation of regulatory requirements. However, during this inspection period, the licensee failed to perform the test and the event was considered a non-cited violation, as discussed in Section M1.2. The LER for that event was pending and will be reviewed when issue M8.3 (Closed) LER 50-282/98004 (1-98-04): Engineered Safety Feature Equipment in Alternate Train Inoperable During Diesel Generator Monthly Surveillance Test Ru This event was previously discussed in inspection Report 50-282/98005(DRP);

50-306/98005(DRP), Section M3.1, and was considered an NCV, 50-282/98005-03(DRP). The inspectors verified that all corrective actions discussed in the LER had been cornpleted or entered into the licensee's corrective action program as commitments 19980600,19980601, and 1998060 . _ _ _ _ _ _ . -- _ _ _ _ _ __ . _ __ __ _ _

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! E3 Engineering Procedures and Documentation E USAR Discrepancy for Refuelina Water Storaae Tank (RWST) Level Instrumentation Jtspection Scoce (92903)

During surveillance test observations, the inspectors reviewed the applicable USAR i sections to verify that the USAR descriptions of the instrumentation involved in the tests

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i During a review of USAR Section 7.4.2.2.2," Refueling Water Storage Tank Level,"

Revision 14, associated with a surveillance test observation for the RWST instrumentation, the inspectors identified a USAR discrepancy. Section 7.4.2.2.2 ot :he USAR stated that only one of the two channels of RWST level provided remote indication on the control board and a low-low level alarm. Actually, both RWST channels on each unit provided a control board indication and low and low-low level alarms. The instrumentation was installed as designed and the USAR error had no safety significance for actual plant operatio The inspectors checked with the licensee's USAR review group and were informed that the licensee had not yet identified the discrepancy. However, the licensee had not completed the Phase il portion of the USAR review project. Part of Phase ll was to be a physical comparison of the USAR descriptions to the physical plant. The inspectors i determined, based on the relatively obvious nature of the discrepancy and the thoroughness of the review project to date, that the licensee probably would have i identified the discrepancy during Phase 11. When informed of the discrepancy by the inspectors, a member of the USAR review team provided the information to the individual assigned to the Phase ll review of the applicabla USAR section so that the discrepancy would be correcte Conclusions The inspectors identified a minor error in the USAR description of RWST level instrumentation. The error had no safety significance for actual plant operation and will be corrected by the license E3.2 Investiaation into EDG Fuel Oil Day Tank Confiaurations. Desian Basis Information. and Associated Calculations Inspection Scope (92903)

The inspectors reviewed the physical configuration, design basis information, and l

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engineering calculations associated with Unit 1 and Unit 2 sal sty-related diesel engine fuel oil day tanks. The review inc;uded the day tanks associated with the D1, D2, DS, l and D6 EDGs as well as 12 and 22 DDCLPs. The following documents were reviewed

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as part of this inspection:

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Design Basis Document SYS-38A, " Emergency Diesel Generator System,"

Revision 2;

USAR Section 2.4.3.5, " Floods," Revision 14;

USAR Section 8.4.2, " Plant Standby Diesel Generator Systems / Description,"

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USAR Section 10.4.1.2, " Plant Cooling System / Description," Revision 14;

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NCR 19990307, "D1/D2 Fuel Oil Day Tank Setpoint Calculation Versus the USAR",

Calculation Namber ENG-ME-020, "D1/D2 and DDCLP Fuel Oil Storage Capacity," dated April 3,1993;

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Calculation Number SPC-EG-0011, "D1/D2 Emergency Diesel Generators' Fuel Oil Day Tank Level Switch Setpoints," Revision 0;  :

  • Preventative Maintenance Procedure ICPM 1-031 D1, "D1 Diesel Generator Fuel Oil Day Tank Level Switch Calibration," Revision 2;

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Preventative Maintenance Procedure ICPM 1-031 D2, "D2 Diesel Generator Fuel l

Oil Day Tank Level Switch Calibration," Revision 2; '

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Procedure H12, " Plant Check Valve Program," Revision 3; l

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Tank Book, " Diesel Generator Fuel Oil Day Tank (D1 & D2)," dated July 1,1 ~93; I

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Design Change 98EB02, "Repower Cooling Water System Common Unit Motcr Valves," Revision 0; l

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Drawing X-HIAW-2815, " Tank - Fuel Oil - 500 Gallon Nominal - Above Ground,"

Revision A;

Drawing X-HIAW-48-12, "500 Gallon Fuel Oil Day Tank for #2 Diesel Fuel,"

Revision 3;

  • Drawing NF-39255-1, " Diesel Generators D1 & D2 Units 1 and 2 Flow Diagram,"

Revision X;

Drawing NF-39232, " Flow Diagram Units 1 & 2 Fuel & Diesel Oil System,"

Revision AC;

  • Drawing NF-40323-1, " Interlock Logic Diagram Fuel & Diesel Oil System -

Units 1 and 2," Revision J:

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Drawing NF-4032533-1, " Interlock Logic Diagram Diesel Generator System j Unit 1 and 2," Revision V; and

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Drawing X HIAW-106-1158," Isometric Engine Fuel Pump Suction," Revision 74.

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I Observations and Findinas After reviewing the actualinstallation of the fuel oil systems for the EDGs and diesel ,

driven cooling pumps and comparing the as found installation to plant drawings and USAR descriptions, the inspectors noted the following; .

l Check valves that were located at the bottom of the fuel oil suction lines from the l D1 and D2 fuel oil day were not included in tne check valve program as

described in procedure H12. " Plant Check Valve Program." Discussions

! between the inspectors and the superintendent of mechanical systems revealed i that the valves did not meet the requirements for inclusion in program per l procedure H12. He also stated that, although the valves were not specifically tested, they were exercised and verified operable by performing the monthly emergency diesel generator testing.

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The USAR description of the day tank for D1 and D2 EDGs stated that they held enough fuel oil for the engine to run up to two hours. The inspectors noted that ,

the special consideratior section of preventativo maintenance procedure ICPM 1-031-D2 stated that there was approximately four hours of engine operating time availabl *

The inspectors noted that the fuel oil consumption calculation for the D1 and D2 EDG day tanks (SPC-EG-0011) did not use the latest EDG loading numbers found in the USAR. When the D1 and D2 EDG loads were changed in the past, the calculation was not updated to ensure the design value for available fuel oil was still met. The licensee issued NCR 199C3307 to record its evaluation of the finding. The licensee determined that the design basis of the day tanks was still met but that the calculations and USAR would need to be revised. As part of Design Change 98EB02, the diesel loading calculations, the Oland D2 fuel c;l storage calculation (ENG ME-020), and the fuel oil day tank calculation (SPC-EG-011) were to be revised based on changes to the dieselloading. The design change was scheduled to be completed during the Unit 1 Spring 1999 refueling outag * The inspectors also looked at 12 and 22 DDCLP and DS and D6 EDG fuel oil day tank configurations and did not note any issues, Conclusions Fuel oil consumption calculations for the D1 and D2 EDGs had not been updated when anticipated accident loading was changed in the USAR. The licensee determined that the design basis fuel oil storage requirements were still met and initiated actions to ,

update the calculations, t E8 Miscellaneous Engineering issues (92903)

E8.1 LClosed) Violation (VIO) 50-282/96015 01(DRS): 50 306/96015-01(DRS) (EA 96-402): i Unreviewed Safety Question Regarding Emergency intake Line. On November 8,1998, t the NHC Office of Nuclear Reactor Regulation issued License Amendment 140/131 j crediting the use of the intake canal during seismic events to ensure adequate suction for the cooling water pumps. This resolved the concern in the violatio I

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E8.2 (Closed) VIO 50-282198098 01(DRS): 50-306/98098-01(DRS) (Office of Investiaation 3-97-034): Inaccurate information in Amendment Request. This violation was written following an investigation by the NRC Oifice of Investigation which found that a licensee amendment request submittal contained inaccurate information. The licensee trained its staff on the importance of ensuring that information submitted to the NRC was complete and accurate. An improvement in the quality of license submittal has been noted by the Office of Nuclear Reactor Regulatio IV. Plant Support R1 Radiological Protection and Chemistry Controls (71750,92904)

During the normal resident inspection activities, routine observations were conducted in the area of radiological protection and chemistry controls. No discrepancies were note P1 Conduct of Emergency Preparedness Activities P Review of Licensee Evaluation of Emeraency Response Activities Inspection Scoce (92904)

During this inspection period, the inspectors reviewed licensee evaluations of the emergency response associated with the Notice of Unusual Event (NUE) for the explosion of the 1M transformer on January 5,1999. Evaluations were contained in Error Reduction Task Force Report 99-01," Unit 1 Turbine Trip / Reactor Trip Following Failure of Unit 1 Main Transformer," and "E-Plan Activation Evaluation - January 5, 1999 NUE," dated January 19,1999 (and reviewed by the operations committee on Feb uary 2).

I Observations and Findinas  ;

l The evaluations were insightful and contained several good recommendations. One evaluation noted that the plant manager decided to use the Technical Suppor' Center to coordinate the support group responses during the NUE. The evaluation contained a suggestion that the licensee consider revising the emergency plan implementing procedures to direct the person in command to consider using the Technical Support Center at the NUE level. Presently, it is not directed to be activated below the Alert level. Another example of a good recommendation was that during the NUE the licensee noted that the radiation monitor multiplexer in the control room was powered from a nonsafeguards power supply so that the data was not available after the transformer loss. The evaluation contained a recommendation to establish a noninterruptible power source for the multiplexe Conclusions The licensee's evaluation of the NUE associated with the loss of the 1M trar. stormer was insightful and contained several good recommendation ;. _ . _ = _ _ - _ - .- - _ _ . . . _ . _ . _ . . - . . - , _ - .

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S1 Conduct of Security and Safeguards Activities (71750,92904)

During normal resident inspection activities, routine observations were conducted in the areas of security and safeguards activities. No discrepancies were note .

i V. Manaaement Meetinas X1 Exit Meeting Summary The inspectors presented the inspection results to members of the licensee management at the conclusion of the inspection on February 25,1999. The licensee acknowledged the findings presented. The inspectors asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identifie _ _ . _ . _ . _ . __ . . . _ _ _ - _ ._.. _ _ _ _ _ __ . _ _ . _ - .

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PARTIAL LIST OF PERSONS CONTACTED

. Licensee K. Albrecht, General Superintendent Engineering, Electrical / instrumentation & Controls  ;

T. Amundson, General Superintendent Engineering, Mechanical J. Goldsmith, General Superintendent Engineering, Generation Services  :

J. Hill, Nuclear Performance Assessment Manager 1 G. Lenertz, General Superintendern Plant Maintenance J. Maki, Outage Manager D. Schuelke, General Superintendent Radiation Protection and Chemistry T. Silverberg, General Superintendent Plant Operations M. Sleigh, Superintendent Security J. Sorensen, Plant Manager ,

INSPECTION PROCEDURES USED IP 37551: Engineering IP 61726: Surveillance Observations t IP 62707: Maintenance Observations I IP 71707: Plant Operations IP 71750: Plant Support Activities IP 92700: Onsite Follow-up of Written Reports of Nonroutine Events at Power Reactor Facilities IP 92901: Follow up - Operations IP 92902: Follow up - Maintenance IP 92903: Follow up - Engineering IP 92904: Follow up - Plant Support i

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ITEMS OPENED, CLOSED, AND DISCUSSED

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Opened 50-282/99001-01(DRP) NCV Failure to Perform Surveillance Test Before Withdrawi19 Control Reds  ;

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50-282/99001-01(DRP) NCV Failure to Perform Surveillance Test Before l Withdrawing Control Rods 50-282/99001; LER Reactor Trip Following Failure of the Station Auxiliary 50-306/99001 (1 99-01) Transformer

50-306/98006(2-98-06) LER Unplanned Actuation of Unit 2 ESF Equipment During l Performance of a Surveillance Test Procedure Due iu Personnel Ebor 50-282/98017; LER Failure to Test Source Range High Flux Trip 50-306/98017 (1 98-17) Functions During Non-Refueling Outages as Required by Technical Specification 4.1-1 A I 50-282/98004 (1 98-04) LER Engineered Safety Feature Equipment in Alternate Train Inoperable During Diesel Generator Monthly Surveillance Test Run I 50-282/96015-01(DRS); VIO Unreviewed Safety Question Regarding Emergency 50-306/96015-01(DRS) Intake Line l (EA 96-402)

50-282/98098-01(DRS); VIO Inaccurate Information in Amendment Request 50-306/98098-01(DRS)

(Office of Investigation 3 97-034)

Discussed Non _ __

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I LIST OF ACRONYMS USED l

l t AFW Auxiliary Feedwater l CFR Code of Federal Regulations l

! CST Condensate Storage Tank

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l DDCLP Diesel Driven Cooling Water Pump DRP Division of Reactor Projects DRS Division of Reactor Safety EA Enforcement Action EDG Emergency Diesel Generator l

ESF Engineered Safety Feature 1

'F Degrees Fahrenheit I&C Instrument and Controls IP Inspection Procedure I LER Licensee Event Report LRO Lead Reactor Operator NCR Nonconformance Report NCV Noncited Violation NIS Nuclear Instrument System  :

NRC Nuclear Regulatory Commission l NUE Notice of Unusual Event psig pounds per square inch - gauge PDR Public Document Room RO Reactor Operator RWST Refueling Water Storage Tank SAC Safety Audit Committee l SP Surveillance Procedure '

TCN Temporary Change Notice TS Technical Specification USAR Updated Safety Analysis Report VIO Violation WO Work Order

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