IR 05000280/1981008
| ML18139B274 | |
| Person / Time | |
|---|---|
| Site: | Surry |
| Issue date: | 03/16/1981 |
| From: | Burke D, Dance H NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML18139B273 | List: |
| References | |
| 50-280-81-08, 50-280-81-8, 50-281-81-08, 50-281-81-8, NUDOCS 8104300391 | |
| Download: ML18139B274 (5) | |
Text
UNITED STATES NUCLEAR REGULATORY COMMISSION
REGION II
101 MARIETTA ST., N.W., SUITE 3100 ATLANTA, GEORGIA30303 Report Nos. 50-280/81-08 and 50-281/81-08 Licensee: Virginia Electric and Power Company Richmond, VA 23261 Facility Name: Surry Uni ts 1 and 2 Docket Nos:. 50~280 and 50-:-*281 License-Nos., DPR-32 and DPR-3T Inspection at Surry site ea,r Surry, SUMMARY Inspection on February 2-27, 1981
- Area's< fosp.ected, *.
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This inspectfon. involved 90 resident inspector-hours, on site* in the' a.rea's of* :
plant opera-tions* and' operating records, plant maintenance and: testing:, followup on previous fi'ndi ngs, and plant securit Results Within the four areas inspected, no violations were identified.
DETAILS Persons Contacted Licensee Employee *J:; L. Wilson,. Station-Manager
- G. Kane,Superintendent, Operations
- R. F. Saunders*, Acting Superintendent of T~chnical Services J. Patrick, Acting Superintendent, Maintenance S. P. Sarve*r-, Heal th Physics Supervisor*
- F. L. Rentz, Resident QC Engineer Other licensee employees contacted during this inspection included control room operators, shift supervisors, QC, _HP,_ plant maintenance,. security, engineering:, chemistry, administrative, records and contractor personne * * *At:tended\\exJt: interview~: ' - Management Interviews The inspection scope and findings were summarized on-a biweekly basis with those:. persons indicated in Paragraph 1 above*.
- . 3, Licens~e-Actfon* on* Previous Ffndi ngs
- (Closed) Noncompliance (280/80-39'-01). Improper-ly installed. containment escape hatch/metal flange-during refuelin Refueling. was stopped until the seal was repaired and refueling procedures were revised and personnel rei nstructed to assure. that the hatch is properly seal e prior-to fuel movemen b*.
(Closed) Non comp Ti ance ( 281/80-43.-0l) I"nadequate documentation for th installation of a Jumper hose on valve 2-DA-43 which led to the diversion of containment sump water into the Safeguards Buildini valve-pi The water was processed* through the liquid waste *system; personnel were rei ns.tructed on-the use. of jumpers, including doc-umentation requ:i rement '.
Unreso l :ved Items Unresolved item_s were* not identified during this inspectio s~
Unit 1 SGRP Unit I is. shutdown for the Steam Generator Replacement Project (SGRP), the outage is currently expected to last some 10 month During the reporting period~ the inspector routinely toured the Unit 1 control room and other plant areas to,,verify that the plant testing, maintenance, and repairs were
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being conducted in accordance with the technica~ s_pe<;ification and facility procedure Within the areas inspected, no violatfons or deviations were identifie Specific. areas of inspection included:
.. Routine inspect.fan of the repair work, modifications, and maintenance during* the outage*.* Procedures and work were 0 reviewed on the Service Water System*modifications (DC 8Q~S42) to the charging pump and chiller cooling systems, which affect both uni"ts ( common-system}. - SJnce: silt, was observed, in the six inch'" service-water lines to these systems, the-1 icensee* stated that the-pipelines will be,- cleaned-during,* the-Un*it 2 April, 1981, outag (Item 280/81-08-01). The Service Water Systems has adequate f~ows and pressure~. Review of the February. 23, 1980, radiography identification o-f linear indications *on the 30 inch A main steamline: on Unit 1;~ simi"lar* indic:-.
ati ons were: subsequent.ly found on the B. and C steaml i ne Further exami natfons* revealed~ ro* pittJng.. f-n: *the* bottom' circumference-: of; the pipin Metallurgical inspections and results are detafled* in IE Inspection Report 50:-280/81-07; Code requirements for the piping and welds: do not appear to have been violated, however, repairs are. in progress~
Hot UT's-were performed on the operating Unit 2, and no indicatidnswere detected; additional examinations will be performed on the. Unit 2*.pi pi ng,-duri ng the, Ap.ri 1., 1981,. outag * Unit 2 Operattons Unit 2. operated* at power during February, 1981.. During this-ttme*,. the inspector routinely toured the Unit 2 control.room and other plant areas to verify that the. plant operations, testing and maintenance were being con-
.ducted in. accordance with the. facility technical specifications and pro-cedure Within the areas inspected, no violations were identifie Specific areas.of inspection and review included the following: Review of* annunciated alarms in the control room and inspection of safety related valve-and pump alignments on the consoles and. in the p 1 ant..
b*.
Observation of certain Periodic: Test ( PT) performance; such as PT 15.1c*
on-the, Unit 2 steam driven auxiliary feedwater pump, and tests on protect.iv.e instrumentation.. * FolTowup on the-power reduction on February 24, 1981, during per-formance of 2;..PT-1.2, 11 Nuclear Instrumentation Trip Channel Test During Power Operation.
A blown control power fuse on Channel N43 caused a runback on Unit 2 from one hundred percent to.some fifty-seven percent of full power~ The inspector reviewed computer logs and charts. for the period following the transient to verify that axial flux difference limits were not exceeded during rod insertio While the axial flux difference deviated from the~ 5% target rang~ for a total of 14
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minutes cumulative penalty time, the axial flux difference did not enter the region of unacceptable operation on Figure 3.12-10 of Technical* Specification Observatiun of portions of the concrete drilli~g*and repair work in the auxiliary building to service building wan for conduit penetration Adequate procedures, work permits, and fire watches were es tab 1 i shed durfng th~ inspectors observati ans..
e:
Inspection of the-common process. vent system. fi 1 ters. and, instrument'."""
atio The filter de.lta; P1 s(pressures)- were we:ll below* setpo:i*n.t:.
va 1 ues*, however* the-* roughing filter appeared somewha-t. dust The*,
filter (GW-FL~2)wa 0s. replaced:
The inspector also reviewed certa-.in
- process vent (ga*seous* waste) system instrumentation calibration data and determined.that* certain pressure or DP instruments,-
such as_ *
PI-GW-TOR and PDI-GW-100,- are not periodically calibrated and are not
- routinely read. to assure. that. the process. vent filters-and cha;rcoal *
remain fully* operable:: and. effec.ti v.e*..
The, 1 i censee is revising pro-cedures~ to': rout.tneJy.., check and,, perfodJcaJlY caJibrate. the, i.ns.t.ru~- -
mentat,ion. * ( Item.. 281/81-08-01). General Items The. inspector reviewed the: licensee-* s * response to IE Bulletin -80:--2.4,.
_- -Preventi*on,,, of* _Damag~,- due, *t*o _, Water* Le.akage* Ins-i de Canta foment,,- and:
discussed: c:erta:hr BuJJetirl-:and; response. i terns wi'th*,. thei lic.ens.ee:-~. Siirry, has: no no.rmal ly-open:- water *system-s; i'ns:i de, conta.i nmen The Service
- . Water *sy.stem which cools: the, Reci rcu,i'ation* Spray. Heat. Exchangers-i*nsdde:::
c.onta i nment. is a', closed. system, i"nsi de-containment during:. power opera.--
ti on, and is isolated by motor operated valves (MOV 1s) outside contain-men The MOV 1 s. open during accident* conditions. on high containmen pressure-.. Historically, the.only 1 eaks. inside containment: which led to, overfn 1 ed.*, conta,i nment sumps-were, from the-*-feedwater. systems, which are,
. quite 1 arge-, 11c.l osed~r-systems:. The norma 1 containment, sump, ha-s a. vo.lume~
of some 92 gallons', level indication in* the control room* which annunciates (a.larms) at 80% (L-DA-200), and sump pumps which automati-cally control sump. level between 20 and 80%.
The sump overflows (over a baffle plate) into the adjacent recirculation sump which has a volume of some 915 ga*ll an The-recirculation sump has two* safety grade level instruments (L:-RS-251 A&B for-Unit 2) which display in the-control room and are: read, logged; and reviewed twice per shif L-DA-100 and L:-DA-200 for Unit. 1 and.: 2 sumps. are: al s.o on. PT 36 to. assure. that al 1 containment * sump 1 eve 1 s are recorded and reviewed* twice per 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> shift*. All of the* leve.l instruments (L:-DA-100" and. 200, L-RS-151 A&B, and 25I A&B} are periodically tested and calibrated by procedures (eg -
PT-2.20). Significant changes in fl~w f~om the sump:would be observed by level observations, annunciator alarms, PT 36, and reduction of volume available in the liquid waste syste Due to recent problems with the installed containment sump pumps, the licensee removed the pumps and is utilizing portabla submersible pumps in the sumps; the portable pumps require less maintenance and therefore reduce contain-
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ment entries and stay times. The inspector observed that the installe p.iping from the sump does not appear to be properly restrained at the poi n-ts of flange disconnection from the ori gi na 1 pump The licensee stated that the piping would. be inspected and properly restrained on both units;..
The incore* room** sump pump* automatical Ty. controls sump level, has*
control and'. ru~ indication in the control room, and discharges. to. the containment sum Although the sump has no level indication instrument..
in the control room,. the,, high level alarm'. (18 inches): annuncia-tes in*
the-control roo The incore room, contains-no open water* systems and*
fs-i so 1 ated from conta.i nment fl oar wate *The.inspector had no further questions at this time; IE Bulletin 80-24 is close The-inspector observed i ncreas.i ng storage of paten ti ally combusti b*l e HP supp:l i es in the' CCW, surge tank room in the auxi 1 iary bu.i Tdfog; the licensee" removed(the-, supp'li:e-s,- and>stored* items, from, the,roo c:.
The inspector verified the following by observation: Gates and doors in protected and vital area, barriers were closed and~Tocked-when not attende ' * IsoTatton, ZOJleSsf described.' fn:* the-physkal se~uri t~:; p,l ~n*s were not coinpromi:sed0 or obstructed*.
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3*.
Personnel were* properly i den ti fi ed, searched*, authorized,- badged:
anc:r escorted as necessary for plant access control.