IR 05000266/1993001

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SALP Repts 50-266/93-01 & 50-301/93-01 for 920201-930331
ML20044H245
Person / Time
Site: Point Beach  
Issue date: 03/31/1993
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20044H238 List:
References
50-266-93-01, 50-266-93-1, 50-301-93-01, 50-301-93-1, NUDOCS 9306080107
Download: ML20044H245 (16)


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SALP 10 INITIAL SALP REPORT U.S. flVCLEAR REGULATORY COMMISSION

REGION III

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORPANCE Inspection Report No. 266/93001; 301/93001

Wisconsin Electric Power Company Point Beach Nuclear Plant February 1, 1992, through March 31,-1993 9306080107 930528 PDR ADOCK 05000266

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SUMMARY OF RESULTS The performance of the facility was considered good and in general followed the trends noted during the previous assessment period.

The prior improving

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trends seen in the Radiological Controls and Safety Assessment / Quality

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Verification areas were sustained over the period and resulted in improved

ratings. Actions taken to reverse the previously noted declining trend in

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Plant Operations were not fully successful and resulted in a lower rating for

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the assessment period.

Performance in the areas of Maintenance / Surveillance,

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Emergency Preparedness, Security, and Engineering / Technical Support remained

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consistent with the previous assessment period.

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t The improving trend previously.noted in Radiological Controls continued during this assessment period and resulted in excellent performance.

The total

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station dose decreased for the third consecutive year and a program challenge identified last period was addressed through better participation in exposure

reduction committee meetings.

Solid waste generation was significantly

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reduced by making changes to the routine radiological work practices and a j

marked improvement was noted in the radiological condition of the auxiliary

building.

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The improving trend noted in the Safety Assessment / Quality Verification area continued throughout the period and resulted in good performance. Management'

F emphasi.Ted a high level of safety awareness and nade several organizational i

<nanget to assure tne proper focus on safety by plant and corporate staff.

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Safety reviews, quality assurance aucits and other self assessment programs

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.;ere effectis: in providing insights and identifying safety issues.

However,

-l corrective actions were not always twely because of inconsistent management cversight anc ineffective guidance for prioritizing' issues.

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Actions taken to reverse the previously noted declining trend in Plant

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Operations were not fully successful. While performance was considered good, j

significant personnel errors continued to cause operational problems.

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automatic reactor trip and several contaminated water and chemical spills cccurred because of personnel errors and miscommunication.

Operator error also caused an excessive cooldown of the reactor vessel which led to the j

issuance of a civil penalty. Management oversight of the activities which

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A lead to these personnel errors was not effective. However, operators

responded well to abnormal events and prevented at least one unnecessary

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automatic reactor trip. Daily shutdown risk assessments and utilization of l

extra senior reactor operators were excellent initiatives.

l Mainter.ance/ Surveillance continued to show good performance and demonstrated j

an improving trend.

The maintenance staff remained stable, well trained, and

qualified which helped sustain high equipment reliability and good materiel l

conditions. Strong management oversight was present during the conduct of

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complex and sensitive evolutions. A long-standing weakness continued to be (

the lack of detailed maintenance procedures, consistent in quality and j

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i content. However, recently written procedures were of good quality and the t

ongoing procedure improvement initiative remained on schedule.

Inconsistent l

procedure implementation contributed to the continuing problem of personnel

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errors.

  • Performance in the other three functional areas remained consistent with the

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previous assessment period.

Emergency Preparedness continued to have

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excellent exercise performance and strong management support for the program.

j While security performance remained good with excellent staffing levels and training programs, enforcement history declined and remained a program-

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challenge.

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l Performance in Engineering / Technical Support also remained good.

Resolution of several challenges that were identified in the previous assessment period included increased staffing levels, more proactive engineering staff, and

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improved safety evaluations for modification packages.

However, some problems involving the improper assignment of priorities and poor work process controls continued to persist.

The performance ratings during the previous assessment period and this assessment period according to functional areas are given below:

Rating Last Rating This Functional Area Period Period Trend Plant Operations 1 Declining

Radiological Controls 2 Improving

Maintenance / Surveillance

2 Improving Emergency Preparedness

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Security

2 Engineering / Technical

2 Support Safety Assessment / Quality 3 Mpro, ng i

Verification

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PEPFORMANCE ANALYSE A.

Plant Operatiqns 1.

Analysis Plant operations' performance declined from the two previous assessment periods. While routine activities and coerator response to events remained strong, inconsistent management ef fectiveness and significant personnel errors

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were primary causes of the performance decline.

Management effectiveness in ensuring quality during operations was mixed. On the positive side, management initiatives to minimize shutdown risk were excellent.

For example, management assigned a dedicated extra senior reactor operator (SRO) to oversee reactor coolant system draindown to reduced inventory condition.

However, management was not effective in identifying procedural inadequacies during reviews of a new steam generator crevice flushing procedure, which contributed to a reactor vessel cooldown event and resulted in a civil penalty.

Additionally, management did not recognize these procedural inadequacies until the NRC identified them.

Management did, however, effectively institute corrective actions, including thorough pre-evolution briefings for infrequently performed tests, critical surveillances, inventory reductions, and reactor startups.

Operator response to automatic reactor trips, engineered safeguards feature actuations, and several minor events, demonstrated an ability to respond effectively to plant transients and stabilize plant conditions.

For example, rapid operator action during the loss of a vital direct current (DC)

instrument inverter and during a turbine generator hydrogen pressure decrease averted two potentially unnecessary reactor trips.

Personnel errors, which were a concern during the previous assessment period, continued to occur.

Operator error was a primary cause of the reactor vessel cooldown event and the cause of the only automatic trip of Unit 2.

In addition, operator errors resulted in several minor chemical spills and the simultaneous inoperability

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of both emergency diesel generators. Although these significant personnel

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errors occurred, overall procedural adherence improved from the previous

assessment period.

p Operations personnel were alert, professional, and knowledgeable of plant and equipment status. Communications among operators, _ although informal, was usually effective. Communication between the control room and remote locations during refueling evolutions was excellent. However,

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miscommunication resulted in a contaminated water spill in the auxiliary building and a manual reactor trip while the unit was off line.

The approach to identifying and resolving technical issues was good.

Experienced SR0s were taken off shif t to function as shift outage coordinators r

and to perform both pre-outag' and daily shutdown risk assessments.

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SR0s performed initial operabi ity determinations on condition reports, which was successful in escalating equipment operability issues.

As a result,

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operators have gained a better understanding of operability requirements.

which was an improvement from the previous assessment period.

Individual shifts also have responsibility for oversight of systems assigned to their respective shifts. As such, they coordinate system procedure revisions and maintenance when practical.

Additionally, experienced licensed personnel actively participated in the technical specificEtion upgrade program.

These initiatives provided beneficial operational insights to these programmatic

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efforts.

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Materiel condition of the plant was good as evidenced by high equipment reliability, low forced outage rate, and normal operation with no illuminated control room annunciators.

The operations staff initiated prompt actions to repair malfunctioning alarms and placed a high priority on completing these

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repairs. General plant housekeeping, a weakness in the previous assessment

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period, improved and was good. However, management was not completely effective in alleviating equipment stowage concerns.

Staffing was excellent and overtime use was limited. A policy of having an additional SR0 on each crew was implemented during the assessment period for all but one operating crew. When an additional SRO was needed for an evolution, an SR0 from either an off-shift or other group was utilized.

This enhanced oversight from the additional SR0 was evident during abnormal and infrequent operations.

However, even though an additional SR0 was on shift, a lack of supervisory oversight contributed to the excessive reactor vessel cooldown event.

l The effectiveness of the training and qualification program for licensed

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operators was good.

The pass rates for initial and requalification examinations were 58 percent and 100 percent, respectively.

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Performance Ratinq Performance is rated Category 2 in this area.

Performance was rated Category

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1 with a declining trend during the previous assessment period.

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Recommendations None.

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B.

Radiological Controls 1.

Analysis Radiological controls were characterized by excellent management:and good inter-sectional support, resulting in low dose expenditures and easily.

accessible safety-related equipment. The overall excellent implementation of

the radiological controls program resulted in. few program challenges, and-

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those that occurred were handled effectively.

Management effectiveness in ensuring quality was excellent. Hydrogen peroxide addition, use of remote video monitoring and inspection equipment, and the

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downsizing of reactor coolant filters demonstrated the excellent support..to

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maintain exposure as-low-as-reasonably'-achievable (ALARA). ALARA program j

concerns identified'during the previous assessment period were addressed

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through better participation in exposure reduction committee meetings and each-

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department providing and meeting yearly personnel exposure goals.

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significant improvement in the radiological condition of tne auxiliary

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building and the requirements of the revised 10 CFR Part 20 were implemented

on January 1,1993, a year prior to its required implementation.

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The approach to the identification and resolution of technical issues from a-safety standpoint was excellent.

The total station dose in 1991, including

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the contribution from two refueling outages, was low at 265 person-rem.

Total

station dose for 1992, also with two refueling outages, decreased to 256 j

person-rem.

This was the third consecutive decline in yearly dose expenditure and is indicative of effective planning and execution of work activities.

Although doses were already low, a source-term reduction program to further

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reduce dose was being developed at-the end of the assessment period.. The q

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number of personnel contamination events was low.

Several long standing

contaminated areas containing safety-related equipment were decontaminated

during the assessment period providing for easy operator accessibility.

Gaseous and liquid radioactive effluent releases continued to remain well within technical specification limits.

Solid waste generation declined significantly due to the elimination of protective clothing routinely used in the auxiliary building and implementation of a clean waste program.. Vendor-supplied volume reduction techniques were effectively used, compensating for.

the somewhat limited onsite volume reduction capability. No radwaste shipping or transportation problems were experienced in this period. The radiological environmental monitoring program was appropriately implemented and'the equipment was well maintained.

Performance in the NRC nonradiological confirmatory measurements program was excellent with 30 agreements in 32 comparisons.

Staffing, training, and qualification of personnel in the radiation protection

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and chemistry departments were excellent. The staffs were knowledgeable and experienced and maintained a low turnover rate. An excellent training. program was implemented on the revised 10 CFR Part 20 for all plant personnel.

2.

performance Ratin_g

Performance is rated Category 1 in this area.

Performance was rated Category 2 with an improving trend during the previous assessment period.

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Recommendations None.

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Maintenance / Surveillance 1.

Analysis Performance in this area was characterized by effective management working with an experienced and qualified staff to sustain high equipment availability and good materiel condition. The overall excellent level of performance was detracted from by continued personnel errors.

Management was effective in ensuring quality as evidenced oy the continued high equipment availability, low forced outage rate, and good materiel condition of the plant.

Strong management oversight was cresent during the conduct of such complex evolutions as the extensive ere.en:ive main:enance on safeguards ouses, restructuring of the DC cistribution system. and resetting of degrade: grid voltage relays.

Establisnment of an cutage managcr position, an expanded maintenance planning group, and shift outage coordinators enhanced outage planning. Timely and safe completion of two ren.eiing outages was directly attributable to effective management oversight. as was an emergency replacem nt of a residual heat removal pump seal which prevented the need for a plant shutdown. A long-standing weakness continued to be the lack of detailed maintenance procedures, consistent in quality and content, to control work.

Procedure implementation was inconsistent.

For example, a main steam isolation valve test failure resulted from a maintenance crew not initiating a needed procedure change. However, procedural inadecuacies were identified and corrected during diesel generator maintenance which descnstrated increased

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procedure acceptance.

Recently written procedures were of good quality and the ongoing procedure improvement initiative remained on schedule.

i The approach to identification and resolution of technical issues was good.

Inservice inspection activities were suitably planned and prioritized. The maintenance work backlog, consisting primarily of low priority items, was j

high. However, a decreasing trend was evident toward the end of the assessment period. Additionally, the number of priority categories was i

increased from three to four to improve prioritization. Although the maintenance group primarily used the computer data base for reactive reviews of performance history, its employment for proactive maintenance analysis increased. The instrument and control group utilized this database for proactive analysis.

Results of surveillance testing and preventive and corrective maintenance were reviewed to determine failure trends and to re-evaluate testing periodicity.

The plant continued to manage and successfully implement the technical specification surveillance program with surveillances routinely completed on time and in a professional manner. Most surveillance procedures were well written with clear directions provided.

Technicians appropriately stopped performing surveillances on several occasions when they discovered errors in procedures.

Unexpected equipment response was brought to the attention of supervision for evaluation and resolution.

Instrument and control technicians maintained good communications with operations personnel during the performance of tests, thereby allowing operators to remain cognizant of test status.

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Personnel errors continued as a weakness from the previous assessment period.-

These included two instances of safeguards buses being de-energized, violation of the equipment isolation procedure,-and improper turbine testing that caused an automatic reactor trip. These various errors were primarily attributable to workers failing to perform adequate self-checking while performing the evolution. Management recognized this deficiency and conducted a Human Performance Enhancement System evaluation so that appropriate corrective action could be developed.

Staffing was sufficient to accomplish required maintenance and surveillance activities without excessive overtime. Maintenance craft workers were well qualified and highly experienced and had a low turnover rate. Retirenents and-a maintenance group reorganization resulted in significant personnel changes in first line maintenance supervision starting late in the previous assessment-period and continuing into the early part of this period..Although the'new supervisors were skilled in their maintenance craft area, they recaired time to acclimate to their new responsibilities.

Their effectiveness " proved toward the end of this period.

Effectiveness of the training and qualification program was excellent.

Maintenance personnel consistently demonstrated excellent skill.in the conduct of work.

The balance between formal training and on-the-job training was appropriate and provided assurance that techr.icians were qualifiec.

Non-destructive examination training and qualification programs complied with applicable code requirements.

2.

Performance Ratinq

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Performance is rated Category 2 with an improving trend in this area.

Performance was rated Category 2 during the previous assessment period.

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Recommendations None.

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Emeroency Preparedness 1.

Analysis Performance was characterized by strong management support for the program and excellent exercise performance.

Management effectiveness in ensuring quality was excellent.

Enhancements continue to be made to the emergency response facilities (ERFs) including relocation of the joint public. information center to Manitowoc, Wisconsin.

The dedicated ERFs and their equipment continued to'be maintained at an excellent level of operational readiness.

The approach to resolution of technical issues from a safety standpoint remained excellent.

The operability 'of the public alert and notification system following system malfunctions was aggressively addressed.

The 1992 evaluated exercise was successful, and all significant aspects of the emergency plan were effectively exercised.

Overall performance was excellent, and no exercise weaknesses were identified. Challenging aspects of the 1992

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exercise included the first use of the control room simulator, evacuation of the technical support center and the operational support center, and responses to separate releases of radioactivity.

The 1992 routine inspection indicated excellent program maintenance with no significant problem areas.

One activation of the emergency plan occurred during the assessment period and was appropriately classified.

The station's emergency planning unit continued to be staffed with excellent personnel.

Initiatives have been implemented to keep the emergency preparedness program active and visible.

The onsite emergency response organization (ERO) staffing also remained good, with at least three individuals assigned to each key emergency response position.

The emergency preparedness training program continued to be excellent. A conscious effort was being made to keep staff training current, varied, and interesting. The training program was effective in maintaining qualified ERO pe r son r.el in supervisory ar'd s cort positions.

Training was effective as cemonstratea through exercise performance ard interviews.

2.

Perforr:ance Rat inq Perfora nce is rated Category '. in this area.

Performance was rated Category i during the previous assessmera period.

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Recorrendat ions None.

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Security

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Analysis Performance in this functional area was charecterized by a decline in enforcement history, mixed management effectiveness, good support relating to resolving technical issues and operational events, and excellent performance in staffing and training.

Enforcement history declined from the previous assessment period and was weak.

Five violations were identified this period compared to three violations during the previous period.

The violations involved both the security and the special nuclear material control and accountability programs.

Management effectiveness in ensuring quality was mixed.

Plant and corporate support for improvements was excellent as evidenced by new security equipment upgrades and the continuing implementation of a goals and objectives program.

Management was not effective in ensuring consistency in day-to-day operations.

Management corrected weaknesses involving strained security management

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resources and specific overview deficiencies noted during the previous assessment period.

However, during this assessment, weak management controls were identified in the followup of a fitness-for-duty issue, personnel access control, and the control of special nuclear material.

Specific corrective actions were taken once these issues were identified.

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The approach to the' identification and resolution of technical issues.was good.

Excellent action by engineering and security resulted in significant

. improvement of vital area door control and the effectiveness and reliability

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of perimeter cameras.

Tracking and trending programs.were good and continued to improve. These programs increased site awareness and resulted in a reduction of personnel errors. The volume of security maintenance requests and the timeliness of completing these activities improved and was ' good.

Engineering and security support was weak in the modification process of an alarm upgrade.

Evaluation and reporting of events was good, except for the failure-to identify and report the potential loss of a small quantity of special nuclear material.

Required security reports-and logs _were accurate and timely.

Staffing levels were excellent.

Licensee and contractor resources were effectively utilized to support operational security program requirements.

Contractor support was increased at the end of the assessment period to monitor the effectiveness of security maintenance activities. An effective working relationship continued between local law enforcement agencies and'

security management.

The effectiveness of the training and qualification program ' improved and was excellent. Upgraded tactical response contingency training improved response capabilities.

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The fitness-for-duty program met the objectives of 10 CFR'Part 26. Program strengths included management support, and a canine program to. aid in the identification of controlled substances.

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Performance Ratina_

Performance is rated Category 2 in this area.

Performance was rated Category 2 during the previous assessment period.

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Recommendations None.

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Enqineerino/ Technical Support 1.

Analysis Engineering and technical support performance remained mixed.

In most instances engineering support of the plant was good, showed. a conservative approach, and was timely.

However,-there were several instances of poor work-process controls that resulted in personnel errors and a spill of contaminated water. A major reorganization of engineering took place too close to the end -

of the assessment period to be evaluated.

Management effectiveness in ensuring quality remained mixed. On the positive side, there was ample evidence of prior planning and assignment of priorities during the extensive preventive maintenance of the electrical safeguards l

buses, the replacement of a DC distribution bus, and motor operated valve j

(MOV) work in response to Generic Letter 89-10. Aspects of'the M0V program, j

such as the innovative techniques developed for test performance, were good.

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i However, the MOV program was excessively dependent on the knowledge of a

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single engineer. This approach lacked backup expertise and was vulnerable to

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the loss of the individual. The effective self-initiated system evaluation programs instituted over the last few years continued.to uncover numerous deficiencies in original plant design.

Safety evaluations for modification

packages, a weakness during the last SALP period, improved.

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On the other hand, some engineering calculations were not properly documented.

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An example was the absence of a basis for calculating the maximum differential

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pressure at which MOVs must operate. At times, engineering involvement with

work in progress was not evident.

Examples included the lack of test procedure acceptance criteria, a problem during the previous SALP period, and incomplete walkdowns of design and design verification packages.

l Comprehensive reviews and corrective action for NRC and industry information

applicable to the station were sometimes untimely.

This appeared to be caused l

by the improper assignment of priorities, a weakness identified during the

last S'LP period.

n example was the delay in resolving the degraded grid

voltage issue.

The continuing nigh number of initial license examination

failures and the large number of simulator discrepancies during 1992 indicated

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a lack of effective management involvement.

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Enforcement history remained weak. A Severity Level III violation was issued i

for inadequate foreign material control during a modification and weak site l

contractor oversight.

In addition, several Severity Level IV violations were

issued reflecting some of the weaknesses discussed in this functional area.

The identification and resolution of technical issues remained mixed.

On the'

l positive side, most evaluations and corrective actions were technically sound-l and displayed an understanding of the safety implications.

One' example j

ta included the resolution to a problem with a leaking inter-system loss-of i

coolant accident (Event V) check valve.

Four other similar valves also were i

modified even though they were not leaking. Additional examples included the installation of a fifth safety-related battery and two nonsafety-related

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batteries to enhance the capability of the DC electrical distribution system, and the actions taken after. finding a visual defect in a fuel assembly.

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On the other hand, the identification and resolution of problems were not

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always appropriate.

For example,. weaknesses included the incorrect use of l

inservice testing acceptance criteria, the practice of deferring operability j

determinations on test results until instrumentation accuracy was confirmed, i

and the improper use of stall efficiency to predict MOV capability.

l Weaknesses in the control of work also resulted in plant problems. One j

example was the use of inappropriate plastic tubing for a leak test of a

charging system check valve, which resulted in a spill of contaminated water.

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Although the number of reportable events increased during this period, most were the result of long standing design deficiencies.

The remaining event

reports were for isolated events and none were indicative of programmatic i

weaknesses.

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Staffing was increased in response to previous concerns; however, the allocation of resources was not changed significantly. As a result, the i

backlog of open design changes and of completed modifications waiting for l

engineering post-installation review remained high.

The engineering and l

technical support staff was competent and more proactive, the latter an

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improvement over the last assessment period. The effectiveness of the major

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engineering reorganization could not be evaluated because it took place late

in the assessment period. A good staffing level was maintained within.the

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training organization.

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The operator training and requalification program was mixed.

While the

requalification program experienced a high degree of success, the passing rate for initial operators continued to be low.

The training and qualification of engineers was good. The corporate engineering staff had the necessary technical expertise to evaluate problems and to provide oversight of

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contractors.

The technical support staff was knowledgeable of their assigned f

systems or components.

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Performance Ratina t

Performance is rated Category 2 in this area.

Performance was rated Category.

2 during the previous assessment period.

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Recommendations i

None.

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Safet'. Assessment /Ouality Verification

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Analvsis Management's effectiveness in improving the quality of work and an awareness

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of the importance of safety improved and was good.

The timeliness and

prioritization of corrective actions continued to be a concern.

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Management took steps to convey the expectation that plant personnel must maintain a high level of safety awareness.

Organizational changes were made j

to focus on plant and corporate staff resources to more efficiently support

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the safe operation of the plant.

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Management involvement in ensuring quality and plant safety was evident in i

outage safety reviews (OSRs).

The safety evaluation group (SEG)' performed an

OSR before each refueling outage. Outage containment. closure drills to verify -

the effectiveness of procedures were performed as recommended by the SEG. The.

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SEG did not, however, consider the negative effects of performing routine

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surveillance during refueling outages, particularly during reduced inventory.

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. operations or when grid stability could be an issue.

For example, a j

surveillance performed during reduced inventory conditions in the Fall 1992

Unit 2 refueling outage resulted in the temporary de-energization of one train j

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of safety-related electrical buses requiring operators to start' the other

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residual heat removal pump.

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Management's commitment to perform effective-and independent safety ~ reviews

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was evident.

The SEG offsite and onsite review committees typically: conducted

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thorough reviews and provided valuable insight into plant operations.

However, the onsite review committee Managers Supervisory Staff (MSS) had a

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tendency to occasionally allow details to detract from the focus on the -

overall safety-issue.

Some improvement in the MSS focus was noted toward the i

end of the assessment period.

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a Further, the positions of shift outage manager and shift outage coordinators

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were created as part of a program to minimize shutdown risk. The

responsibilities of these positions, in addition to assessing plant safety, included presenting daily risk assessment briefings and maintaining the risk status charts within the plant. Risk assessment briefings were beneficial to the continued conduct of safe cperations. Senior plant management wa_s t

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successful in heightening the level of plant safety awareness among both plant operators and mid-level managers, particularly during reduced inventory operation.

Management's commitment to improve plant safety was also demonstrated by a

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number of plant improvements. These included the installation of new and

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additional station batteries and the scheduled installation of two new safety-

related emergency diesel generators.

Further, the quality assurance (QA)

i organization identified a number of significant deficiencies through the performance of quality " vertical slice" audits including the reactor protection and service water systems.

Sound program _ audits were also

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conducted in the security and emergency plannir.; areas.

The identification and resolution of technical issues improved and was good.

For example, following a failed leak test on an Event V check valve, plant

management demonstrated a clear focus en plant safety.

This was evident in

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the decision to extend the refueling outage to.odify additional Event V check.

i valves. Management also demonstrated a commitcent to resolve technical issues

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by revising the corrective action and commitment tracking precedures.

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example, the corrective action process was revised to include a requirement for an SR0 to assess equipment operability and reportability during the first

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24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> of writing a condition report, ano a requirement for the plant j

manager to document a review of all Prio ity 1 and 2 condition reports.

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identification and resolution of issues documented in condition reports

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originating from the vendor technical information program, quality assurance i

audits, and the licensee component failure analysis reports were considered

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program strengths.

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Timeliness of corrective actions occasionally suffered due to inconsistent

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assignment of priority and plant resources.

Examples include the resolution i

of degraded voltage issues and combustion turbine generator deficiencies.

Several findings involving corrective actico program deficiencies, identified

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during a QA audit early in the reporting period, were addressed through procedure revisions.

However, inconsistent management involvement and a lack i

of employee support in the condition reporting system continued to limit the o

effectiveness of these efforts.

Further management oversight techniques continue to be developed, but were not fully successful.

For example, a lack'

of management involvement resulted in scheduling delays of a test plan to I

assess potential safety injection pump cavitation problems.

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Performance Ratino Performance is rated Category 2 in this area.

Performance was rated Category 3 with an improving trend in the previous period.

3.

Recommendations None.

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IV.

SUPPORTING DATA AND SUMMARIES A.

hjor licensee Activities During steam generator crevice flushingUnit I refueling ou rough June 12, 1992.

cooled down at a higher than allowed rate., the reactor vessel was inadve An inspection of the gas station blackout purposes) turbine generator (used for fire protection and in April 1992, revealed significant degradati wear of internal components, requiring an extensi were completed in October 1992, with reliability t on and ve overheul.

These efforts the end of the assessment period.

esting contir.uing through Unit 2 refueling outage took place from Septe b

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1992.

leading to one train of contairsent spray andA foreign materia Me ; lug had been s a fe t,ered in me suction piping surveillance testing.

this section of piping inoperableafter a codification perfor ed du

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us cutage a :

1: re :ered batteries was complete: Installation of a fif th safety-related battery

.n Cecember 1992.

and wo nce-cife:.-rel2ted B.

fialor_ln_spect ion Activit ies february 1,1992, an? MarchThis assessment period consisted of the in listed below under " Inspection Data "

ons conducted te:weer.

31. 1993 listed below under "Special Inspection Summary "nt, and docu

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Significa inspect':-

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Jrtspestion Data

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activities are 1.

l U_ nit 1, Docket 50-266 l

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Inspection Reports:

92027, 92028 and 93002 - 93007.92003, 92007 - 92019, 9202),

92023 through 92025, t

Unit 2, Docket 50-301 i

l Inspection Reports:

I 92028, and 93002 - 9300792003, 92007 - 92010, 92012 - 92019

, 92021 through 2.

Special_lnsjyection Summary s

Significant inspections conducted during the SALP j

listed below:

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10 assessment period are An inspection was performed on March 16 301/92003). emergency preparedness exercise (Inspection Repo t1992, of the a

- 20, r s 266/92003; An inspection was conducted from April 20 (Inspection Reportsinservice inspection program delineated in Gene i-May 2 266/92008; 301/92008)

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SUPPORTING DATA AND SUMMARIES

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A.

Major Licensee Activities

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' Unit I refueling outage took place from April 11 through June 12, 1992.

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During steam generator crevice flushing, the reactor-vessel was inadvertently cooled down at a higher than allowed rate.

An inspection of the gas turbine generator (used for fire protection and station blackout purposes) in April 1992, revealed significant degradation and

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wear of internal components, requiring an extensive overhaul.

These efforts were completed in October 1992, with reliability testing continuing through

the end of the assessment period.

Unit 2 refueling outage took place from September 26 through November 16,.

1992.

A foreign material exclusion plug was discovered in :ne sucticn pipine

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leading to one train of contairment spray and safety injec:':n = ring rcutine..

surveillance testing.

The plug had been inadvertently le#: " :.E pi;ng after a modification perforned during the previous cutage r: "a: re :' seed

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this section of piping inoperable.

Installation of a fif th safety-related battery and two non-sifety-reisted

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batteries was completed in December 1992.

B.

Maior Inspection Activities

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This assessment period consisted of the inspections conducted betweer.

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February 1, 1992, and March 31, 1993, and documented in the inspection reports

.l listed below under " Inspection Data." Significant inspectic activities,are listed below under "Special Inspection Summary,"

a 1.

Inspection Data

Unit 1. Docket 50-266

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Inspection Reports: 92003, 92007 - 92019, 92021, 92023 through 92025,

92027, 92028 and 93002 - 93007.

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Unit 2. Docket 50-301

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Inspection Reports: 92003, 92007 - 92010, 92012.- 92019, 92021 through 92028, and 93002 - 93007

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2.

Special Inspection Summary i

Significant inspections conducted during the SALP 10 assessment period are l

listed below:

i An inspection was performed on March 16 - 20, 1992, of the annual I

emergency preparedness exercise (Inspection Reports 266/92003;

,

301/92003).

An inspection was conducted from April 20 - May 27, 1992, to review the inservice inspection program delineated in Generic Letter 89-04

.(Inspection Reports 266/92008; 301/92008).

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A special inspection of the reactor cooldown event.on May 27, 1992, was

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conducted through June 14, 1992 (Inspection Reports 266/92014; 301/92014).

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A safety inspection was performed from October 5 - 22, 1992, on_the licensee's response to Generic Letter 89-10 for motor-operated valves (Inspection-Reports 266/92021; 301/92021).

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.

A team inspection was conducted from October ~ 13, 1992, - February 4,

,

1993, to review the-quality and effectiveness of engineering involvement-in plant activities (Inspection Reports 266/92024; 301/92024).

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A physical security and reactive material control inspection was performed from flovember 30 - December 4,1992, to' review the loss of a small quantity of special nuclear material (Inspection Reports 266/92028; 301/92028).

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