IR 05000255/1990014

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Forwards Safety Insp Rept 50-255/90-14 on 900420-0531.No Violations Noted
ML18155A276
Person / Time
Site: Palisades 
Issue date: 06/14/1990
From: Beverly Clayton
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To: Hoffman D
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.)
Shared Package
ML18155A277 List:
References
NUDOCS 9006210379
Download: ML18155A276 (18)


Text

Docket No. 50-255 Consumers Power Company ATTN:

David P. Hoffman Vice President Nuclear Operations

  • 1945 West Parna 11 Road Jackson, MI 49201 Gentlemen:

'"nm 1 4 1s90 This refers to the routine safety inspection conducted by Messr E. R. Swanson, J. K. Heller and T. J. Kobetz during the period of April 20 through rtiay 31, 1990, of activities at the Palisades Nuclear Generating Plant authorized by NRC Provisionctl Operating License No. DPR-20 and to the-discussion of our findings with Mr. G. B. Slade and others of your staff at the conclusion of the inspectio The enclosed copy of our inspection report identifies areas examined during the inspectio Within these areas, the inspection consisted of a selective examination of procedures and representative records, observations, and interviews with personne No violations of NRC requirements were identified during the course of this inspectio In accordance with 10 CFR 2.790 of the Commission 1 s regulations, a copy of this letter, the enclosed inspection report and your response will be placed in the NRC Public Document Roo We will gladly discuss any questions you have concerning this inspectio

Enclosure:

Inspection Report

No. 50-255/90014(DRP)

See Attached Distribution

RII I

Schweibinz/dp

Sincerely,

Brent Clayton, Chief

Reactor Projects Branch 2

RI II (Zc

Clayton

(//'0D

r*~--

,

Consumers Power Company

Distribution

REGION I I I

F.acility Narrie:

Palisades Nuclear Generating Plant*

Inspection At:

Palisades Site, Covert, MI

Inspection' Conducted: April 20 through May 31

Inspectors:

E. R. Swanson

Approved

J.. K. Heller

T. J. Kobetz

~.

By:. B. L. Burg~ief

Reactor Projects Section 2 DAT License No. DPR-20

  • Inspection Summary

Ins~ection on Apri 1 20 through May 31, 1990

(Report No. 50-255/90014

(DR ))

.

.

Areas Inspected:

Routine unannounced inspectibn by the resident inspectors

of: actions on previously identified items; plant oper~tions; maintenance;

.

surveillance; security; reportable events; bulletins and generic letters; CFR 21 report; and, NRC Regional.& Headquarters requests. Safety Issues

.

Management System (SIMS) item TI 2515/103 (TAC 6'9761) was reviewed and remains

ope.

Results: Of the ten areas inspected, two licensee identified violations were

identified in Paragraph 8, and were found to meet the crite~ia of 10 CFR 2

Appendix C for non-i~suance of a citatio The i~spection disclosed weaknesses i~ the licensee's late identification of

the heat trace problem reported in LER 255/9000 The inspection noted strengths in the lic~nsee's responsiveness to plant

operattonal needs during startup, th~ identification of a potential protected

area breach, the comprehensive actions on the PART 21 issue, and their efforts

to define the goal of "TOP TEN

11 for employees~

No new Open Items and/or Unresolved Items were.identifie DETAILS Persons Contacted

Consumers Power Company

  • G. B. Slade, Plant General Manager
  • R. M. Rice, Plant Operations Manager
  • D. J. VandeWalle, Technical Director
  • R. D. Orosz, Engineering and Maintenance Manager
  • K. M. Haas, Radiological Services Manager

J. L. Hanson, Operations Superintendent

R. B. Kasper, Mechanical Maintenance Superintendent

K. E. Osborne, System Engineering Superintendent

R. M. Brzezinski, I&C Engineering and Maintenance Superintendent

L. J. Kenaga, Health Physics Superintendent

  • R. E. McCaleb, Director of Quality Assurance
  • C. S. Kozup, Technical Engineer

J. R. 'Brunet, Licensing Analyst

R. J. Frigo, Operations Staff Support Supervisor

K. A. Toner, Plant Projects Superintendent

  • Denotes some of thdse present at the Management Interview on June 1,

199 Other members of the Plant staff, and several members of the Contract

Security Force, were also contacted during the inspection perio.

Actions on Previously Identified Items (92701, 92702) Mr. D. Danielson, Chief, Material and Processes Section, documented

in a memorandum that Region III has reviewed the Palisades Open Item

list and determined that the items listed below can be closed

because they are duplicative of issues addressed in Generic Letter 89-10,

11Safety-Related Motor-Operated Valve Testing and

Survei llance

11 and Bulletin 85-03,

11Motor Operated Valve Common Mode

Failures During Plant Transients Due To Improper Switch Settings

,

supplement on Generic Letter 89-10 and Bulletin 85-03, supplement

one open at the Palisades Station and will be inspected at a later

dat (1)

(Closed) Open Item 255/87028-01:

Need clarification for

Bulletin 85-03 response concerning use of data base formulated

from their own testing. *

(2)

(Closed) Open Item 255/87028-02:

No test data was available to

assure adequacy of the limitorque open torque switch settin (3)

(Closed) Open Item 255/87028-03:

No documented program or test

data was available to assure adequacy of the limitorque close

torque switch settin (4)

(Closed) Open Item 255/87028-04:

Long term valve operability

program needs development by the license **

{5)

(Closed) Bulletin 87-28:

Entry was in erro Bulletin 87-28

does not ex i_s (Closed) Open Item 255/88026-01:

Spurious opening of Auxiliary

Feedwater (AFW) flow control valves, flow instability on AFW pump

P-8 The spurious opening of CV-0727 and CV-0749 has been noted to

occur during initial testing after maintenance on the syste The

licensee has postulated that air collects on top of the "balanced

plug" design, and when pressure builds up at the valves when a pump

first starts, that they open, and then pressure equalizes and the

valves close. This initial transient phenomena has been mitigated

by venting, and has only occurred during initial testin Venting

is controlled by Standard Operating Procedure SOP-12 "Feedwater System", Attachment In regard to the second issue of AFW pump P-8C instability on

recirculation flow, the pump was disassembled in November 1989 and

found tu have some pitting on the impelle Although acceptable,

the impeller was replaced and the bulk of testing is now performed

with flow (not on recirculation).

Long term plans are to install a

manual bypass line for testin (Closed) Open Item 255/89021-02:

Nuclear Safety Services Department

(NSSD) involvement in the review of audit plans and participation in

audits did not appear adequat NSSD staff involvement in audits

was planned and documented in the October 20, 1989, NSSD staff

meetin Inspector review indicated that ~he plan was being

implemented adequatel (Open) Violation 255/89024-01 (Example A.2.):

Pipe Support JB-14-6

"f-1197.4 and JB..:.14-6 "H197.5).

The licensee response dated April

12, 1990, stated on page 8 of attachment 1 that the stress package

for these supports was currently in final review and will be

complete by April 30, 199 On May 2, 1990, the li_censee informed

the resident inspector that the package was not complete and, in

fact, was not in final revie It appears that the priorities of

the responsible group in the Corporate Office were modified without

knowledge of the commitmen The inspector requested that the

licensee inform the responsible DRS section chief that the

commitment was not met and provide a written revision to reflect the

corrected completion dat At the exit interview the potential

consequences of providing false information was discusse No violations, deviations, unresolved or open items were identifie.

Operational Safety Verification (71707, 71710, 42700)

Routine facility operating activities were observed as conducted in the

plant and from the main control roo Plant startup, steady power

operation, pJant shutdown, and system lineups and operation were observed

as applica_ble.

The performance of licensed Reactor Operators and Senior Reactor

Operators, and Shift Engineers, and of Auxiliary Equipment Operators was

observed and evaluated including procedure use and adherence, records and

logs, communications, shift/duty turnover, and the degree of

professionalism of control room activitie Evaluation, corrective action, and response to _off normal conditions or

events, if any, were examine This included compliance to any reporting

requirement Observations of the control room monitors, indicators, and recorders were

made to verify the operability of emergency systems, radiation monitoring

systems and nuclear reactor protection systems, as applicabl Reviews

of surveillance, equipment condition, and tagout logs were conducte Proper return to service of selected components was verifie Periodic verification of Engineered Safety Features status was conducted

by the resident inspecto Equipment alignment was verified against

plant pro~edures and drawings and detailed walk downs selectively

verified: equipment labeling, the absence of leaks, housekeeping, freeze

protection, calibration dates, operability of support systems, breaker

and switch alignment as appropriat~. Walkdowns during this inspection

period focused on the shutdown cooling syste General

The unit began the reporting period in a preplanned maintenance

outage and was returned to service on May 1 During the outage the

licensee performed: steam generator replacement engineering

activities; safety related restraint reverifications.; Post Accident

Sampling System modifications; installation of motor operated

disconnects for off-site power modifications; cooling tower

modifications; Auxiliary Feedwater Turbine driven pump overhaul;

repair to the leaking Safety Injection Tank outlet check valve; and

completed numerous open outage work order Before the turbine was put on line, four unexplained atmospheric

steam dump openings occurred, two of them causing actuation of the

auxiliary feedwater (AFVJ) syste The AFW actuations were

explained to be a result of the pressure transient causing the AFW

actuation channels (which are very quick acting) to sense a spurious

low steam generator level, depending on the initial steam generator

leve The root cause for the atmo~pheric steam dump openings was

determined to be electronic noise on the temperature circuit which

inputs to the steam dump controlle The noise source has not been

specifically identified, but circuit modifications have been made to

reduce the nois Current limiting capacitors were added and a fast

acting current switch was rep-laced with a similar, but slower

devic A final calibration check was performed on the circuits and

a demonstration test was satisfactorily performed to confirm the

adequacy of the circuit modification A LER is planned by the

license CFR 50.72 Reports

( 1)

On April 25, the licensee informed the NRC that a Local

Leakrate Test (LLRT) of containment penetration 26 determined

that leakage limits exceeded allowable Technical Specification

limits. It was determined that a containment nitrogen supply

line check valve would not close because of machining marks on

the piston. After resurfacing, a LLRT was performed

satisfactory and the penetration returned to service. Generic

implications of the failure were considered and the licensee

concluded that further immediate action was not warrante Additional NRC review will be performed during close out of the

associated LE (2)

On April 25 the licensee informed the NRC that the analysis for

a main steam line break transient described in their FSAR was

not limiting for containment pressur In their original

analysis they had analyzed for a guillotine-type steam line

break as the bounding case for peak containment pressur Feedwater isolation currently occurs on a low steam generator

pressur A followup analysis was performed on a small break

which would allow a slower blowdown_ of the faulted steam

generato This resulted in a delayed isolation of the

feedwater which would allow more steam to be released into

containment for a longer period of time, resulting in a higher

peak containment pressure than previously analyze The peak

pressures analyzed exceeded the containment design pressure of

55 psig by approximately 20 psi This pressure does not

exceed the capability of the containment, how.eve The identification of this oversjght was a result of analytical

work being performed for the upcoming steam generator

replacemen Since the results were determined to have an

immediate operational safety impact, the licensee modified the

feedwater isolation actuation circuitry to include input from

containment high pressur Additional NRC review will be performed during close out of the

associated LE (3)

On April 25 the licensee informed the NRC of gross deformation

of pipe supports (H-747, 765) associated with two of the four

Safety Injection Tank outlet line The two hangers'

supporting "I" beams had buckled and the riser clamps were

ben Calculations performed by the licensee's vendor

regarding operability of the hangers in the as-found

configuration supported the conclusion that the supports were

"'capable of carrying the imposed design loads and qualified for

the operability criteria" (Interim Operability Criteria).

The

calculation evaluated the "worst case" loads including dead,

thermal, and Safe Shutdown Earthquake load The hangers were

repaire..

The remaining two (H-735, 756) were inspected on April 26 and

found to have sli~ht deformation that didn't require repai A region III structural specialist reviewed the licensee repair

activities and calculatio The inspection results will be

documented in Inspection Report No. 50-255/90015(DRP).

(4)

On May 5 the licensee informed the NRC that a LLRT of

containment penetration 49 indicated that leakage limits

exceeded the allowable Technical Specification limit Additional _review determined that only administrative limit was

exceede Based on this information the 50.72 notification was

retracted and no LER will be issue The inspector reviewed

the associated work request, retest of penetration 49 and the

DR associated with the test failur The inspector does not

have additional questions at this tim Oe_erational Readiness of the Spent Fuel Pool Crane

The inspector received a telephone inquiry from an individual who

had concerns about operational readiness of the spent fuel pool crane

and the integrity of the container vans used to transport material

to/from the corttainment equipment hatc This inquiry was discussed

with Region III and the on-shift outage manage It appears that the crane was very 'noisy while moving or lifting a

load and had control problem In addition, the container vans were

rusty on the botto The outage manager ~tated that: crane control problems were

experienced at the beginning of the outage but were resolved by

replacing control circuit cards; the crane was noisy, however, the

noise was characteristic of the crane and did not indicate an

operational problem; and, the integrity of the safety brakes was

satisfactory. The contractor who owned the vans, Bechtel, was asked

to confirm the integrity of the container van The inspector observed several lifts/movements of container vans and

did not notice any unusual noises or control problem The

inspector interviewed a crane operator who stated that control

problems have not reappeared si~ce the circuit cards were replace The inspector also interviewed the area coordinator who stated that

he had observed a number of 1 if ts and had not noticed any unusua 1

noise During one lift, the Bechtel engineer performed an

inspection of the container van botto The inspection did not

identify any problem Subsequently, the inspector contacted the

individual who initiated the inquiry and the concerns were

resolved.

  • Plant Startup

During the May 17, 18 and 19 startup the inspector observed the

fo 11 owing:

(1)

Portions of the plant heatup from cold shutdown to hot ~hutdowri

(GOP 2).

(2)

Portions of the mode change from hot shutdown to hot standby

(GOP 3).

(3)

Control rod withdrawal (SOP 6)

(4)

Inverse multiplication plot (GOP 3, attachment 2).

(5)

Licensee response to potential control rod group sequencing

problem caused by a faulty control rod position car (6)

Operations management routinely visited the control roo (7)

Support from other plant departments was available when

required and promptly supplied when requeste Isotopic Analysis for Iodine of the Primary Coolant

On May 20, 1990, a required isotopic analysis.for iodine of the

primary coolant was not completed within the specified two to six

hour time perio Reactor power was increased from 3.3 percent to

23.6 percent in an hour which exceeds the 15 percent change which

invokes the sampling requirement under Technical Specification

4. Samples analyzed before the power increase and the following

day indicated normal levels of iodine, and the licensee concluded

that the event had no safety significanc The air ejector off

gas monitor was monitored periodically during the startup and would

have given an indication of any unusual increase in iodine level A Human Performance Evaluation.will be conducted by the license Further review of this event will be done after the LER is submitted

to the NR No violations, deviations, unresolved or open items were identifie.

Maintenance (62703, 42700)-

Maintenance activities in the plant were routinely inspected, including

both corrective and preventive maintenanc Mechanical, electrical, and

instrument and control group maintenance activities were included as

availabl The focus of the inspection was to assure the maintenance activities

reviewed were conducted i11 accordance with approved procedures,

regulatory guides and industry codes or standards and in conformance with

Technical Specification The following items were considered during

    • *

this review: the Limiting Conditions for Operation were met while

components or systems were removed from service; approvals were obtained

prior to initiating the work; activities were accomplished using approved

procedures; and post maintenance testing was performed as applicabl The following activities were inspected: Boric Acid Pipe Heater Circuit 4358 Failure (Work Order (WO)

24001878).

Initially, this work request was written to resolve a

circuit failure alarm believed caused by a loose fuse holde The

Work Order instructions stated troubleshoot, repair, and adjust as

necessary for proper operatio During the troubleshooting, the

inoperability of circuit 4358 was discovere The inspector noted

that an inherent weakness exists with instructions that state

"troubleshoot, repair and adjust as necessary for proper operation."

In this case no limitations or precautions were included pe~taining

to LCO time limit Which may have contributed to the licensee

exceeding an LC Paragraph 8.g of the report discusses the

enforcement aspect of this work activit Modification of the fuel oil pump suction and discharge piping to

repair fuel oil leaks (WO 24001300).

This modification required the

installation and welding of additional piping and flange The

welders were interviewed to determine _if they were cognizant of weld

buildup requirement The welders interviewed were able to discuss

a recent problem that resulted from insufficient weld buildup and

the corrective action implemente Installation of fasteners for the Auxiliary Feedwater pump equipment

hatches (WO 24906149).

This work order required the drilling of

holes in the floor to facilitate the installation of anchor The

inspector found that the workers understood the restrictions

pertaining to cutting of rebar and appeared to properly use

equipment that would prevent cutting of reba VOTES testing on PORV block valves M0-1042A and -1043A (WO 2400709,

2400711). Check valve CK 3101 *resurfacing of seat (WO 24903760,

RWP 900419).

..

No violations, deviations, unresolved or open items were identifie Surveillance (61726, 42700)

The inspector reviewed Technical Specifications required surveillance

testing as described below and verified that testing was performed in

accordance with adequate procedures, that test instrumentation was

calibrated, that Limiting Conditions for Operation were met, that removal

and restoration of the affected components were properly accomplished,

that test results conformed with Technical Specifications and procedure

requirements and were reviewed by personnel other than the individual

directing the test, and that deficiencies identified during the testing

were properly reviewed and resolved by appropriate management personne **

The following activities were inspected or reviewed: RI-3

High Pressurizer Channel Calibratio DW-13

Local Leak Rate Test for Inner and Outer Personnel Air

Lock Door Seal Q0-18

Inservice Test Procedure - Concentrated Boric Acid

Pump R0-32-49

Local Leak test for penetration 4 S0-48

Escape lock penetration tes T-232

Nitrogen Backup Supply Test for Auxiliary Feedwater

System (performed November 88). DW0-1

Daily Control Room Surveillanc SH0-1

Operators Shift Surveillanc No violations, deviations, unresolved or open items were identifie.

Security (71707) Routine facility security measures, including control of access for

vehicles, packages and personnel, were observe Performance of

dedicate.d physica 1 security equipment was verified during inspections in

various plant area The activities of the professional security rorce

in maintaining faciTity security protection were occasionally examined or

reviewed, and interviews were occasionally conducted with security force

member During tours of the plant the inspector observed that contractor personnel

challenged visitors and their escorts when it appeared that a security

violation was about-to occu This was highlighted in the exit meeting

as a strength of their security training progra The licensee reported that the underwater integrity of the m1xrng basin

may have been compromised by a shifting sand bar and natural wave actio The method of discovery is significant in that plant personnel noted

large fish in the mixing basin and pursued their method of ingres The

discovery, repair and reporting were prompt and professional, indicating

a good knowledge of unique plant design feature No violations, deviations, unresolved or open items were identifie Safety Jl.ssessment/Qua l ity Verif i ca ti on ( 35502, 40500)

The effectiveness of management controls, verification and oversight

activities, in the conduct of jobs observed during this inspection, was

evaluated.

The inspector frequently attended management and supervisory meetings

involving plant status and plans and focusing on proper co-ordination

among Department The results of licensee auditing and corrective action programs were

routinely monitored by attendance at Corrective Action Review Board

(CARB) meetings and by review of Deviation Reports, Event Reports,

  • Radiological Incident Reports, and Security Incident Report As

applicable, corrective action program documents were forwarded to NRC

Region III technical specialists for in.formation and possible followup

evaluatio As part of the licensee

1 s efforts to communicate expectations to

employees, the licensee is using their "Weekly Bulletin

11 to describe the

characteristics of a

11Top Ten" performing plant. Four indicators were

chosen to measure overall plant performanc These are:

(1) reliability

(measured by capacity factor), (2) regulatory performance (measured by

violation points and SALP ratings), (3) ALARA (measured by radiation

exposure), and (4) cost effectiveness (measured by generation cost).

No violations, deviations, unresolved or open items were identifie.

Reportable Events (92700, 92720)

The inspector reviewed the following Licerisee Event Reports (LERs) by

means of direct observation, discussions with licensee personnel, and

review of record The review addressed compliance to reporting

requirements and, as applicable, that immediate corrective action and

appropriate action to prevent recurrence had been accomplishe (Closed) LER 255/89006-Revision 1: Component cooling water

availability following a high energy line brea (Closed) LER 255/89009: Loose valve operator stem coupling results

in inoperable containment isolation valv (Closed) LER 255/89021: Single failure potential within CR HVAC

circuitr (Closed) LER 255/89021 Revision 1: Single failure potential within

CR HVAC circuitr (Closed) LER 255/89TS1 (255/8999-LL): Radiation monitor inoperable

for greater than seven day (Closed) LER 255/90003: Inadvertent auxiliary feedwater actuation

during logic testin The inspector reviewed the revised procedures

and licensee training program and concluded the corrective action

was taken as stated in the LER.

    • (Closed) LER 255/90004: Failed heater cable results in inoperability

of a concentrated Boric Acid Heat Trace Channel for a period greater

than allowed by Technical Specification Initially, it was

believed that a fuse holder was the problem that caused a circuit

failur However, during the maintenance activity the inoperability

of circuit 4358 was identified. A time line of the repair is

provided below:

3/29/90 - Secondary heat trace channel TICA-4358 was found ope This is the first indication that the heat trace was

inoperabl The time was not documented on the Work Order

log sheet. A check of the security logs for auxiliary

building entries shows that the individual identified on

the work request made three entries between 8:30 p.m. and

Midnigh /30/90 - 1:00 The Deviation Report identifies that

the need to replace secondary heat trace channel

TICA-4358 was discussed at the daily maintenance

meetin /31/90 - 11:17 The heat circuit was declared

inoperable and the plant entered a LCO, requiring

the plant be in hot shutdown within the next 36

hours if the circuit was not returned to servic :44 The heat trace circuit was repaired

and the plant exited the LC The licensee concluded that the inoperability determination should

have been made at 1:00 p.m. on April 3 Using this time the

licensee complied with the LCO time limi However, sufficient

information was available on March 29, 1990 at midnight, to

determine that the equipment was inoperabl Using this time the

licensee did not comply with the LCO time limi The inspector

reviewed this item to determine if enforcement action was

appropriate using March 29, 1990 (midnight) as the time of

inoperabilit If this time is used, then the licensee exceeded the

LCO time limi This would be a less significant vio*lation of a

Technical Specification and categorized as a Severity IV or V

violatio CFR Part 2, Appendix C.V.G. states that the NRC may

refrain from issuing Notices of Violation that: were identified by

the licensee; can be classified as a Severity Level IV or V

violation; was reported; was not a willful violation; and will be

corrected; including measures to prevent recurrence, within a

reasonable period of tim Based on this, e~forcement action was

not appropriate. (Closed Violation (NV6) 255/90014-0l(DRP)) (Closed) LER 255/90005:

Inoperability of Auxiliary Feedwater (AFW)

System as the r~su1t of a valving error during restoration of the

Backup Nitrogen System fol lowing bottle replacemen ** *

The valves that supply steam to the Turbine Driven AFW Pump and the

valves that regulate AFW to both steam generators are air operated

valve The principle air source is instrument air (regulated at

80-100 psi) and the backup is compressed air (nitrogen) supplied by

two manifold The compressed air is regulated at 60 ps Installation of the manifold was discussed in NRR Safety Evaluation

dated May 26, 1983, to address alternate safe shutdown capability,

sections III.G.3. and III.1 of Appendix R to 10 CFR 5 In that

Safety Evaluation the licensee committed to provide a standby 12

hour source of compressed gas to pperate certain critical valve During auxiliary operator training, the licensee found bottles to

each manifold valved out-of-service. Since the Technical

Specifications do not specifically address either the instrument air

or compressed air systems, the licensee requires operability of both

and considers loss of either air supply cause for entry into the

Limiting Condition for Operatio Upon discovery of the valving

errors the licensee evaluated operability and determined that the

manifold for the AFW flow control valves was operable, with one of

four bottles valved out-of-servic The licensee determined that

the manifold for the steam supply valves to the turbine driven AFW

pump was inoperable with four of eight bottles valved out-of-service

because, under worst case conditions the compressed gas was only

available for six hours versus the 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> identified in the Safety

Evaluatio The iicensee has determined that the valving error was the result of

personnel error during changeout of empty bottles. Corrective

action, in the form of instruction on bottle replacement (formally

considered skill-of-the-craft) including valve verification upon

restoration and modification of system checklist to include the

valves that were operated, has been implemente The inspector has reviewed the enforcement policy and determined

that this LER identifies a deviation from a commitment which fits

the severity level IV or V categor In addition this LER was

evaluated for enforcement action and the determination made that

enforcement action was not necessary because the provisions of

Appendix 10 CFR 2. Appendix C, V.G,

11 Exercise Enforcement

Discretion

11 were me These provisions include the following

criteria. It was: identified and reported by the licensee;

corrected in a reasonable period of time; not a willful violation;

and, classified as a severity level IV violatio (Closed Violation

(NV6) 255/90014-02(DRP))

Two licensee identified violations and no deviations, unresolved or open

items were identifie NRC Compliance Bulletins (92703)

The inspector reviewed the NRC communications listed below and verified

that: the licensee has received the correspondence; the correspondence

was revie0ed by appropriate management representatives; a written

response was submitted if required; and, plant-specific actions were

taken as described iri the licensee's respons *

(Open)Bulletin 89-03 (255/89003-BB):

Potential Loss of Required

Shutdown Margin During-Refueling Operation The licensee responded to

the Bulletin on November 21, 1989, outlining their intended actions prior

to refueling in the fall of 199 The NRC acknowledged their response by

letter dated May 10, 1990, and requested written confirmation of

completion of the action No violations, deviations, unresolved or open items were identifie.

NRC Generic Letter (92703)

The inspector reviewed the NRC communications listed below and verified

that: the licensee has received the correspondence; the correspondence

was reviewed by appropriate management representatives; a written

response was submitted if required; and, plant-specific actions were

taken as described in the licensee

1 s respons (Closed) Generic Letter 88-11 (255J88011-GL):

NRC Position on Radiation

Embrittlen1ent of Reactor Vessel Materials and it

1 s Impact on Plant

Operation The licensee responded by letter dated November 21, 198 In this letter, they predicted that use of Regulatory Guide 1.99 Revision

2 methodology for determining when Palisades would exceed 10 CFR.50.61

screening criteria, would result in exceeding this criteria iri 199 The

licensee implemented the revised methodology which was reviewed and

approved by the NRC, as part of Technical Specification Amendment Number

13 No violations, deviations, unresolved or open items were identifie.

10 CFR 21 Report (36100, 92701)

Consumers Power received notification of potential misapplication and

improper installation of Patel/EGS conduit seals through notification

from the vendor and by NRC Information Notice 90-2 The licensee

reviewed all four modification pack~ges where Patel conduit seals had

been used and verified either by physical verification or record review

that appropriately sized grommets had been used for each applicatio In

one case, the vendor specified wire size tolerance was.002 inches

smaller than acceptable for the grommet use Wire from the same spool

was found to be of an acceptable diameter but to make sure, the licensee

~1ill physically verify the wire size during the next outag The second issue raised was the possible loosening of the union nuts due

to inadequate torquin The licensee checked about 35 percent of the

seals and found all of them properly torque No further action on this

is planne This issue is closed for Palisades (Part 21

255/90014-03(DRP)).

1 Inspection of Regional and Headquarters Requests (255103/TAC #69761)

(Open) Temporary Instruction (TI) 2515/103 - Loss of Decay Heat Removal (Generic

Letter No. 88-17) Programmed Enhancements Revie An inspection of the

subject matter was performed to verify the licensee preparation for

non-power operation in accordance with the long term actions of Generic

Letter 88-1 Provisions described in Consumers Power Company letter

. dated January 31, 1989 were reviewe NRC has not yet completed its

Safety Evaluation Report of the six programmed enhancements described in

the licensee's letter, and therefore, this inspection cannot be

complete Instrumentation

In addition to the existing loop level instrument, a new independent

level instrument will be installed during the 1990 refueling outag This instrument will have a range span of 100 percent of the loop 2

hot le The licensee intends to continue using the installed sight

glass for once per shift calibration check Qualified core exit

thermocoupl~s (CETs) will continue to be relied upon for temperature

measurement while the reactor vessel head is installed. These can

be read from several different sources (plant computer, critical

function monitor, or cooling instrumentation).

While the head is

off, loop RTDs can be used, but due to location they are not

expected to be useful for other than trending purpose No plant

procedures exist governing the use of RTOs in this condition. Alarm

capability for increasing temperature while on shutdown cooling has

not been provide Monitoring of the shutdown cooling (SOC) system

performance is provided by flow indications (both total and

individual loop), a trend recording of the temperature outlet and

return to the primary coolant system, pump breaker indication and a

pump trip alar An alarm is also provided on low pump discharge

pressure of about 80 percent of normal flo The viability of this

alarm in monitoring pump performance has been demonstrated during

prior events and is considered by the licensee to be equivalent to

pump motor amp trending or acoustical monitorin Trending of the

SOC parameters is provided only for temperatur Level trending has

been added to the plants Critical Function Monitor (CFM) during the

last few outages, but no procedural requirement for the capability

exist The future loop level instrument will have a permanently

assigned data point on the CF Procedures

Procedures have been developed to govern operation of the NSSS,

containment and supporting systems for reduced i,riventory coo 1 i n General Operating Procedure (GOP) 14 "Shutdown Cooling (SOC)

Operations", Standard Operating Procedure (SOP) 3 "Safety Injection*

arid Shutdown Cooling", and Off Normal Procedure (ONP) 17 "Loss of

Shutdown Cooling" contain adequate instructions to govern the

operation of the SOC system during normal and off normal conditions

including loss of flow, cooling, or coolant inventor The GOP,

SOP, and ONP do not reference the Emergency Operating Procedures

(EOPs) if significant core damage is expected or indicate However, operator training and the symptom based EOPs provide

adequate confidence that mitigating actions (such as containment

hydrogen control) will be carried out.

  • Containment closure provisions are contained in GOP-14 with

Operations normally responsible for clearing lines from the

equipment hatch and Maintenance responsible for positioning the

hatch and installing/tightening four clamp Four bolts maintain

the hatch adequately sealed to permit any containment pressure to

further seat the hatc GOP-14 also contains pretautions meeting

the intent of the guidance for avoidance of perturbations while in a

reduced inventory conditio Equipment

In addition to proceduralized equipment operability requirements,

the licensee has developed an excellent method of keeping the

control room operators informed of equipment availability and their

preferential us The Operations Scheduling Supervisor (an SRO)

prepares a status sheet with limits for each plant parameter while

on shutdown cooling reflecting: primary coolant system (PCS) state

of fi 11, S/G tubes covered or not, temperature and' level bands

(assumed in containment closure response time calculation),

operability of core cooling paths, inventory addition paths,

electric power requirements, preferred core exit thermocouples,

level instruments, and Containment Status, closure time and

res pons i bi 1 i t ONP-17 contains three methods for core cooling when the PCS

integrity is not maintaine In order of preference, containment

spray pumps, Spent Fuel Pool Cooling, and PCS boil off and makeup

methods are outlined. A HPSI pump may be used under the provisions

of 10 CFR 50.54(X).

Flow paths have been evaluated and tested as

necessar Adequacy of vent paths for cooling flow have been

evaluated when necessar Reliable communication methods have been

provided for the conduct of activities under accident condition Analyses

The inspector verified that analyses exist to support the procedures

including the PCS vent sizin Technical Specifications

The licensee submitted a Technical Specification Change Request on

June 28, 198 NRR has not completed their action on the amendmen PCS Perturbations

The inspector verified the adequacy of the 12 month training

provided to operators, procedures and controls concerning PCS

perturbations. Additional precautions are required to be considered

for both monitoring and preventing a loss of shutdown cooling during

activities of jeopard No violations, deviations, unresolved or open items were identified.

.,.

1 Management Interview (30703)

Th~ inspectors met with licensee representatives (denoted in Paragraph 1)

on June 1, 1990 to discuss the scope and findings of the inspectio In

addition, the inspector also discussed_ the likely informational content

of the inspection report with regard to documents or processes.reviewed

by the inspector during the inspectio The licensee did not identify

any such documents/processes as proprietar