05000400/LER-2004-004

From kanterella
Jump to navigation Jump to search
LER-2004-004, Unanalyzed Condition Due to Inadequate Separation of Associated Circuits
Docket Number Sequential Revmonth Day Year Year Month Day Yearnumber No. N/A 05000
Event date: 09-27-2004
Report date: 11-26-2004
Reporting criterion: 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition
4002004004R00 - NRC Website

I.� DESCRIPTION OF EVENT On September 27, 2004, with the Unit in Mode 1 at 100% power, HNP identified that certain cables for redundant components credited by the Safe Shutdown Analysis (SSA) lack the required degree of separation in one fire area. This discovery was identified during a comprehensive review and validation of the HNP SSA. This review and validation were being performed as part of the corrective actions for previously reported conditions (reference HNP LER 2002-004-05 submitted November 15, 2004).

HNP identified that spurious opening of multiple valves M in the Reactor Coolant System (RCS) [AB] could potentially result in the transfer of some coolant inventory to containment. For a postulated fire in SSA fire area 1-A-CSRB, located in the Reactor Auxiliary Building (RAB) elevation 261', certain cabling [CBL3] for the RCS High Point Vent System Valves (1RC-901, 1RC-903, and 1RC-905) [AB-FSV] were not protected from spurious actuation in accordance with the requirements of NUREG 0800, Attachment 1 (Branch Technical Position CMEB 9.5-1) Section C.5.b. Specifically, the control power cables for RCS solenoid operated valve (SOV) 1RC-905 are routed in cable trays with no fire barrier within five feet of the conduit with no fire barrier which contains the control power cables for RCS SOVs 1RC-901 and 1RC-903 in SSA fire area 1-A-CSRB. Therefore, the cables for these SOVs could be vulnerable to fire-induced hot shorts.

During normal plant operation, these RCS vent valves are closed and the valves' control power is removed via a pull-to-lock switch in the main control room. However, a postulated fire in this area could result in spurious opening of multiple valves 1RC-905, Combined Head Vent and Steam Space Vent Valve, and either 1RC-901, Reactor Vessel [RPV] Head Vent Valve, or 1RC-903, Pressurizer [PZR] Steam Space Vent Valve, and thus could potentially create a pathway from the RCS to the containment atmosphere. At the time of this discovery, a roving fire watch was already posted in the fire area of concern as interim compensatory action for previously reported conditions, and the fire watch remains posted.

Based on a review of historical plant documents, this condition was previously identified during plant construction and was considered to have been resolved at that time. However, the drawing change requiring these cables to be protected by fire barrier material was apparently never issued during plant construction. Subsequently, the fire barrier material was never installed as required by the SSA. No other condition similar to this historical one has been identified during the comprehensive review and validation of the HNP SSA.

The RCS High Point Vent System is designed to remove non-condensible gases from the primary system to assist core cooling during natural circulation. The system is designed with one-inch (nominal size) piping to provide adequate venting capacity white ensuring that any transfer of coolant inventory is less than the make-up capacity of one charging pump in the event of a Safety Class 2 pipe break or inadvertent valve actuations. In addition, the path from the reactor vessel head utilizes a 3/8-inch diameter orifice [OR]. This orifice also limits flow to less than the make-up capacity of one charging pump in the event of a Safety Class 2 pipe break or inadvertent valve actuations.

This finding of an unanalyzed condition is being reported pursuant to 10 CFR 50.73(a)(2)(ii)(B). No systems, structures, or components were inoperable at the time of discovery that significantly contributed to the event.

Energy Industry Identification System (EIIS) codes are identified in the text within brackets [ ].

II. CAUSE OF EVENT

The most probable cause of this historical condition is that the drawing change requiring these cables to be protected by fire barrier material was apparently never issued during plant construction. Subsequently, the fire barrier material was never installed as required by the SSA. No other condition similar to this historical one has been identified during the comprehensive review and validation of the HNP SSA.

III. SAFETY SIGNIFICANCE

All of the findings are based on scenarios that have not actually occurred. Therefore, there are no actual adverse safety consequences.

The potential safety consequence for a postulated fire in fire area 1-A-CSRB (261' elevation) that also results in spurious opening of multiple SSA SOVs may include:

  • Transfer of some RCS inventory to containment atmosphere. However, the system is designed to ensure that any transfer of coolant inventory is less than the make-up capacity of one charging pump in the event of a Safety Class 2 pipe break or inadvertent valve actuations. In addition, the path from the reactor vessel head utilizes a 3/8-inch diameter orifice, which also limits flow to less than the make-up capacity of one charging pump in the event of a Safety Class 2 pipe break or inadvertent valve actuations.

In addition, the defense-in-depth provided by the fire protection program mitigates this potential safety consequence by:

  • Prevention of fire initiation,
  • Prompt detection of fires or incipient fire conditions by installed automatic detection systems,
  • Effective suppression of fires by installed automatic fire suppression systems with fire brigade backup.

IV.�CORRECTIVE ACTIONS At the time of this discovery, a roving fire watch was already posted in the fire area of concern as interim compensatory actions to minimize the impact of a postulated fire for previously reported conditions, and the fire watch remains posted.

Complete a validation of the HNP safe shutdown analysis.

Restore the identified conditions of this LER to compliance by design changes or other methods approved by the NRC.

These actions are scheduled to be completed by refueling outage (RFO) 13 (Currently scheduled for May 13, 2006).

No corrective actions are associated with the cause of this historical condition since it is the only condition of its type identified during the comprehensive review and validation of the HNP SSA.

V.� PREVIOUS SIMILAR EVENTS NRC Inspection Report 50-400/00-09 (dated February 3, 2000) This inspection identified two unresolved items (URIs) concerning adequacy of a Thermo-Lag fire barrier to meet plant licensing basis requirements and the adequacy of the 10 CFR 50.59 for changes made to the FSAR to revise the fire rating of selected Thermo-Lag fire barriers. The identified fire barrier serves as the fire area separation barrier between the "B" Train Switchgear Room/Auxiliary Control Panel (ACP) Room and the "A" Train Cable Spreading Room. Based on Thermo-Lag barrier fire resistance tests conducted in 1994 and 1995, this fire barrier did not have the required three-hour fire resistance rating. Therefore, a single fire in the "B" Train Switchgear Room, of significant intensity and duration, could breach the Thermo-Lag fire barrier assembly and damage certain redundant "A" train cables and their associated functions of safe shutdown systems. The final significance determination for these two items was one notice of violation (White finding). The root cause was inadequate fire testing of the installed fire barrier. The corrective actions included modifications to the affected rooms and establishing review criteria to ensure that future fire barrier modifications do not invalidate test results. The root cause for this previous event is not significant in relation to the subject event, therefore, the previous corrective actions would not be expected to identify or prevent the deficiency identified by this LER.

HNP LER 97-006-00 (reported 4/17/97) This LER reported that an undocumented breach was identified in the thermo-lag wall while sealing penetrations through the Thermo-Lag Wall in the 286' Cable Spreading Room "A." Follow-up investigation revealed an additional thermo-lag fire barrier deficiency in a floor drain assembly in the cable spread room.

These conditions do not comply with the 3-hour fire-rated barrier requirements specified in the HNP FSAR.

The root cause was identified to be incomplete design, incomplete construction, and incomplete final construction walkdown. The penetration was modified per ESR 95-00715. The root cause investigation (CR 97-01123) stated, "Nothing indicates a common trend to the fact of an area of a Thermo-lag panel being missed both in design and in the final construction walkdown." The root cause for this previous event is not significant in relation to the subject event, therefore, the previous corrective actions would not be expected to identify or prevent the deficiency identified by this LER.

HNP LER 97-020-00 (reported 9/12/97) This LER reported that design discrepancies were identified during an Engineering review of the Safe Shutdown Analysis in Case of Fire. These discrepancies pertain to safety-related electrical cables in 261' elevation of the RAB for the EDG Fuel Oil Transfer Pumps "A" and"B". These cables did not comply with separation requirements to maintain safe shutdown capability. These deficiencies were caused by engineering oversight and inadequate design verification during initial plant construction. A plant modification was installed to provide the required protection for the cited cables. The root cause investigation (CR 97-03861) stated, "A review of the safe shutdown cables in the unit 2 areas north of column line 43 was performed and no additional cable protection discrepancies were found. Also, an in­ depth review of an additional fire area (1-A-EPB) was performed . . . and no similar deficiencies were identified." The root cause for this previous event is not significant in relation to the subject event, therefore, the previous corrective actions would not be expected to identify or prevent the deficiency identified by this LER.

V.�PREVIOUS SIMILAR EVENTS (Continued) HNP LER 2002-004-00 through -05 (reported February 18, 2003, March 26, 2003, September 19, 2003, April 12, 2004, and November 15, 2004, respectively) This LER and its associated revisions reported that unanalyzed conditions exist due to inadequate separation of associated circuits. HNP identified postulated fires that could cause spurious actions of multiple valves and components that could also result in some of the following potential conditions:

  • Spurious opening of multiple valves in the safety injection system or the containment spray system could result in transfer of Reactor Water Storage Tank (RWST) inventory to the containment recirculation sump. However, this water inventory would still be available for use, if needed, from the containment recirculation sump.
  • Spurious opening of multiple valves in the safety injection system could result in damage to the Charging/Safety Injection Pump (CSIP) in service due to run out conditions.
  • Spurious closure of valves in the charging system could result in loss of flow and subsequent damage to the running CSIP credited by the Safe Shutdown Analysis (SSA).
  • Spurious closure of valves in the Component Cooling Water (CCW) System could result in loss of CCW flow credited by the SSA for Reactor Coolant Pump (RCP) seal cooling.
  • Spurious closure of multiple valves in the charging and CCW systems could result in loss of RCP seal cooling and subsequent degradation of the RCP seals, possibly leading to an RCP seal LOCA without credited CSIPs.
  • Loss of RCS pressure and level indication credited by the SSA which could potentially impact pressure and level monitoring.

The cause of these conditions was inadequate original Safe Shutdown Analysis. Specifically, certain conductor-to-conductor interactions (i.e., hot shorts) were not adequately evaluated in the initial Safe Shutdown Analysis. The root cause for LER 2002-004-00 through -05 was an old design deficiency (i.e., certain conductor-to-conductor interactions such as hot shorts were not adequately evaluated in the initial SSA) and is not significant in relation to the current event. However, the corrective actions for this previous event would be expected to identify or prevent the deficiency identified by the current LER, and, in fact, did identify this deficiency during the ongoing comprehensive review and validation of the HNP SSA. This review and validation are being performed as part of the corrective actions for the previously reported conditions.

VI.�COMMITMENTS The actions committed to by Carolina Power & Light Company doing business as Progress Energy Carolinas, Inc. (PEC) in this document are identified below. Any other actions discussed in this submittal represent intended or planned actions by PEC. They are described for the NRC's information and are not regulatory commitments.

Scheduled Commitment(s) Completion Date 1. Complete a validation of the HNP safe shutdown analysis. June 20, 2005 2. Restore the identified conditions of this LER to compliance by design Refueling Outage 13 changes or other methods approved by the NRC. (Current schedule May 13, 2006)