| | | Reporting criterion |
|---|
| 05000400/LER-1987-001, :on 870111,alarm Received Indicating That Data B Inputs Failed on Rod Withdrawn from Core.Caused by Mfg Deficiency Leading to Unreliable Rod Position Info.Reactor Trip Breakers Opened |
- on 870111,alarm Received Indicating That Data B Inputs Failed on Rod Withdrawn from Core.Caused by Mfg Deficiency Leading to Unreliable Rod Position Info.Reactor Trip Breakers Opened
| 10 CFR 50.73(a)(2) |
| 05000400/LER-1987-002, :on 870102,discovered That Testing of Reactor Protection Sys Logic,Reactor Trip Breaker & Bypass Breaker Not Staggered Properly Per Tech Spec Table 4.3-1.Caused by Personnel Error.Tests Staggered |
- on 870102,discovered That Testing of Reactor Protection Sys Logic,Reactor Trip Breaker & Bypass Breaker Not Staggered Properly Per Tech Spec Table 4.3-1.Caused by Personnel Error.Tests Staggered
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
| 05000400/LER-1987-003, :on 870113,cooldown Initiated Due to Inoperable motor-driven 1A-SA Auxiliary Feedwater Pump.Caused by Assembly Error During Initial Installation of Pump.Flow Test Frequency Changed & Pump Repaired |
- on 870113,cooldown Initiated Due to Inoperable motor-driven 1A-SA Auxiliary Feedwater Pump.Caused by Assembly Error During Initial Installation of Pump.Flow Test Frequency Changed & Pump Repaired
| 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown |
| 05000400/LER-1987-004, :on 870121,reactor Tripped While Power Level Reduced Due to intermediate-range Channel N-36 Remaining in Trip Condition.Caused by Reset Value Set Too Low.Setpoints Adjusted to Values Based on Data Collected |
- on 870121,reactor Tripped While Power Level Reduced Due to intermediate-range Channel N-36 Remaining in Trip Condition.Caused by Reset Value Set Too Low.Setpoints Adjusted to Values Based on Data Collected
| |
| 05000400/LER-1987-005, :on 870122,reactor Tripped Due to lo-lo Level in Steam Generator A.Caused by Trip of Condensate Pump a & Inability to Restore Feedwater Flow.Control Valve Repaired. Cause of Pump Failure Will Be Determined |
- on 870122,reactor Tripped Due to lo-lo Level in Steam Generator A.Caused by Trip of Condensate Pump a & Inability to Restore Feedwater Flow.Control Valve Repaired. Cause of Pump Failure Will Be Determined
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000400/LER-1987-006, :on 870123,charging/safety Injection Pumps 1B-SB & 1C-SAB Declared Inoperable Due to Failed Attempts to Automatically Start Train 1B-SB Chiller.Caused by Chiller Tripping on Overload.Plant Cooldown Initiated |
- on 870123,charging/safety Injection Pumps 1B-SB & 1C-SAB Declared Inoperable Due to Failed Attempts to Automatically Start Train 1B-SB Chiller.Caused by Chiller Tripping on Overload.Plant Cooldown Initiated
| |
| 05000400/LER-1987-008, :on 870227,loss of Main Feedwater & Automatic Start of Both motor-driven Auxiliary Feedwater Pumps Occurred.Caused by Transient in Turbine Load.Motor Replaced & Tested & Valve Returned to Svc |
- on 870227,loss of Main Feedwater & Automatic Start of Both motor-driven Auxiliary Feedwater Pumps Occurred.Caused by Transient in Turbine Load.Motor Replaced & Tested & Valve Returned to Svc
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000400/LER-1987-009, :on 870224 & 25,containment Leak Detection Radiation Monitor Noble Gas Channel Declared Inoperable. Caused by Procedural Deficiency.Advance Change 1/2, Correcting Deficiency,Approved |
- on 870224 & 25,containment Leak Detection Radiation Monitor Noble Gas Channel Declared Inoperable. Caused by Procedural Deficiency.Advance Change 1/2, Correcting Deficiency,Approved
| |
| 05000400/LER-1987-010, :on 870228,air Supply Fans Automatically Initiated Control Room Isolation Signal & Tripped Normal Supply Fans.Caused by Faulty Detector.Fire Detector Cleaned & Replaced & Ventilation Sys Restored |
- on 870228,air Supply Fans Automatically Initiated Control Room Isolation Signal & Tripped Normal Supply Fans.Caused by Faulty Detector.Fire Detector Cleaned & Replaced & Ventilation Sys Restored
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
| 05000400/LER-1987-011, :on 870307,breaker Tripped Open Causing de-energization of Auxiliary Bus 1E.Caused by Procedural Inadequacy.Defective PIC Card in Power Supply to LT-112 Relay Replaced & Procedure Revised |
- on 870307,breaker Tripped Open Causing de-energization of Auxiliary Bus 1E.Caused by Procedural Inadequacy.Defective PIC Card in Power Supply to LT-112 Relay Replaced & Procedure Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(e)(2) |
| 05000400/LER-1987-012, :on 870311,turbine & Reactor Trips Occurred During Troubleshooting at Main Turbine Supervisory Control Panel.Turbine Trip Caused by Depressing Test Push Button on Turbine Supervisory Control Panel |
- on 870311,turbine & Reactor Trips Occurred During Troubleshooting at Main Turbine Supervisory Control Panel.Turbine Trip Caused by Depressing Test Push Button on Turbine Supervisory Control Panel
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(e)(2)(viii) |
| 05000400/LER-1987-013, :on 870313,plant Manually Tripped at 49% Power Due to Loss of Main Feedwater.Caused by High Discharge Pressure Spike of Condensate Booster Pumps.Feedwater Regulating Valves Stroked |
- on 870313,plant Manually Tripped at 49% Power Due to Loss of Main Feedwater.Caused by High Discharge Pressure Spike of Condensate Booster Pumps.Feedwater Regulating Valves Stroked
| 10 CFR 50.73(e)(2) |
| 05000400/LER-1987-014, :on 870314,three Pressure Gauges Installed, Placed in Svc & Opened on Three Drain Lines Whose Isolation Valves Considered Containment Isolation Valves in Violation of Tech Specs.Caused by Personnel Error |
- on 870314,three Pressure Gauges Installed, Placed in Svc & Opened on Three Drain Lines Whose Isolation Valves Considered Containment Isolation Valves in Violation of Tech Specs.Caused by Personnel Error
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
| 05000400/LER-1987-015, :on 870325,noble Gas Grab Sample Not Taken. Caused by Personnel Error.Grab Sample Taken on 870326.Event Reviewed W/Staff & Personnel Counseled |
- on 870325,noble Gas Grab Sample Not Taken. Caused by Personnel Error.Grab Sample Taken on 870326.Event Reviewed W/Staff & Personnel Counseled
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
| 05000400/LER-1987-016, :on 870323 & 26,turbine Bldg Vent Stack Monitor Declared Inoperable Due to Problems W/Water in Monitor.On 870327,monitor Declared Operable & Lined Up to Sample Stack. Turbine Bldg Vent Stack Reinstated |
- on 870323 & 26,turbine Bldg Vent Stack Monitor Declared Inoperable Due to Problems W/Water in Monitor.On 870327,monitor Declared Operable & Lined Up to Sample Stack. Turbine Bldg Vent Stack Reinstated
| 10 CFR 50.73(e)(2) |
| 05000400/LER-1987-017, :on 870331,reactor Trip Occurred Due to Steam Flow/Feedwater Flow Mismatch.Caused by Feedwater Control Valve Oscillation.Main Feedwater Regulating Valves Placed in Manual Control |
- on 870331,reactor Trip Occurred Due to Steam Flow/Feedwater Flow Mismatch.Caused by Feedwater Control Valve Oscillation.Main Feedwater Regulating Valves Placed in Manual Control
| |
| 05000400/LER-1987-018, :on 870403,manual Reactor Trip Initiated Due to Loss of Both Main Feedwater Pumps.Caused by Inadvertent Short of Test Leads in Process Instrumentation Cabinet & Incorrect Setpoint.Undocumented Leads Removed |
- on 870403,manual Reactor Trip Initiated Due to Loss of Both Main Feedwater Pumps.Caused by Inadvertent Short of Test Leads in Process Instrumentation Cabinet & Incorrect Setpoint.Undocumented Leads Removed
| 10 CFR 50.73(e)(2) |
| 05000400/LER-1987-019, :on 870412,manual Plant Trip Initiated Due to Loss of Feedwater Trains & Decreasing Steam Generator Levels.Caused by Condensate Pump High Temp Trip.Pressure & Steam Generator Levels Restored |
- on 870412,manual Plant Trip Initiated Due to Loss of Feedwater Trains & Decreasing Steam Generator Levels.Caused by Condensate Pump High Temp Trip.Pressure & Steam Generator Levels Restored
| 10 CFR 50.73(a)(2) |
| 05000400/LER-1987-020, :on 870413,reactor Trip Setpoints on All Three Overtemp Delta Temp (Odt) Bistables Incorrectly Set.Caused by Apparent Design Oversight in Odt Circuit Design & Vendor Testing Methodology.Test Procedures Revised |
- on 870413,reactor Trip Setpoints on All Three Overtemp Delta Temp (Odt) Bistables Incorrectly Set.Caused by Apparent Design Oversight in Odt Circuit Design & Vendor Testing Methodology.Test Procedures Revised
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
| 05000400/LER-1987-021, :on 870414,circulating Water Sys Flow to Main Condenser Restricted,Resulting in High Condensate Temps,Trip of Both Feedwater Trains & Manual Trip of Turbine & Reactor. Caused by Debris on Pump Suction Screens |
- on 870414,circulating Water Sys Flow to Main Condenser Restricted,Resulting in High Condensate Temps,Trip of Both Feedwater Trains & Manual Trip of Turbine & Reactor. Caused by Debris on Pump Suction Screens
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(e)(2) 10 CFR 50.73(s)(2) 10 CFR 50.73(e)(2)(v) |
| 05000400/LER-1987-022, :on 870402,Tech Spec 3.3.3.10 Discovered Violated Due to Flow Estimates Taken at Beginning & End of Radioactive Releases on 870327,28 & 0401 Instead of Every 4 H.Caused by Inoperable Flow Rate Instrument |
- on 870402,Tech Spec 3.3.3.10 Discovered Violated Due to Flow Estimates Taken at Beginning & End of Radioactive Releases on 870327,28 & 0401 Instead of Every 4 H.Caused by Inoperable Flow Rate Instrument
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(e)(2)(x) 10 CFR 50.73(e)(2) 10 CFR 50.73(e)(2)(v) |
| 05000400/LER-1987-023, :on 870420,alternate Miniflow Valves for Charging Safety Injection Pump Found Isolated.Verification of Correct Valve Lineup Unavailable.Caused by Personnel Error.Procedure OP-107 Being Revised |
- on 870420,alternate Miniflow Valves for Charging Safety Injection Pump Found Isolated.Verification of Correct Valve Lineup Unavailable.Caused by Personnel Error.Procedure OP-107 Being Revised
| 10 CFR 50.73(e)(2) 10 CFR 50.73(s)(2) 10 CFR 50.73(e)(2)(v) |
| 05000400/LER-1987-024, :on 870421,heater Drain Pumps a & B Tripped Due to Low Differential Pressure & Automatic Turbine Runback Initiated.Caused by Oscillating Feedwater Heater Levels.Pump Low Level Trip Setpoint Lowered |
- on 870421,heater Drain Pumps a & B Tripped Due to Low Differential Pressure & Automatic Turbine Runback Initiated.Caused by Oscillating Feedwater Heater Levels.Pump Low Level Trip Setpoint Lowered
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(s)(2)(i) 10 CFR 50.73(s)(2)(v) 10 CFR 50.73(s)(2) |
| 05000400/LER-1987-025, :on 870422,while Operating at 99% Power,Heater Drain Pump a Tripped from Low Flow Signal.Caused by Failure of Discharge Valve on Pump.Separated Air Connection on Pump Discharge Valve Repaired |
- on 870422,while Operating at 99% Power,Heater Drain Pump a Tripped from Low Flow Signal.Caused by Failure of Discharge Valve on Pump.Separated Air Connection on Pump Discharge Valve Repaired
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(s)(2) |
| 05000400/LER-1987-026, :on 870423 & 24,main Feedwater Pump Tripped & Actuated motor-driven Auxiliary Feedwater Pumps.Caused by Trip of Condensate Booster Pump.Main Feedwater Restored & Pumps Secured.Control Logic Under Evaluation |
- on 870423 & 24,main Feedwater Pump Tripped & Actuated motor-driven Auxiliary Feedwater Pumps.Caused by Trip of Condensate Booster Pump.Main Feedwater Restored & Pumps Secured.Control Logic Under Evaluation
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(c)(2) 10 CFR 50.73(c)(2)(xiii)(A) |
| 05000400/LER-1987-027, :on 870426,during Test,Redundant Transmitter Pressurizer Pressure Channels Declared Inoperable.Caused by Two Out of Three Channels Out of Calibr & Reading Low. Channels Recalibr & Test Completed |
- on 870426,during Test,Redundant Transmitter Pressurizer Pressure Channels Declared Inoperable.Caused by Two Out of Three Channels Out of Calibr & Reading Low. Channels Recalibr & Test Completed
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(c)(2) 10 CFR 50.73(e)(2) 10 CFR 50.73(e)(2)(v) 10 CFR 50.73(c)(2)(vii) 10 CFR 50.73(e)(2)(9) |
| 05000400/LER-1987-028, :on 870502,manual Turbine Trip Initiated During Performance of Power Ascension Test Procedure 9108-S-14. Caused by Tandem Trip of Both Heater Drain Pumps.Evaluation of Feedwater Response to Transients Continues |
- on 870502,manual Turbine Trip Initiated During Performance of Power Ascension Test Procedure 9108-S-14. Caused by Tandem Trip of Both Heater Drain Pumps.Evaluation of Feedwater Response to Transients Continues
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(s)(2) 10 CFR 50.73(s)(2)(viii)(A) |
| 05000400/LER-1987-029, :on 870428,engineer Determined That Snubber Found Damaged on 870422 Per Required Action of Tech Spec. Snubber Damaged Due to Water Hammer Occurring When Valve Isolated.Snubber Replaced |
- on 870428,engineer Determined That Snubber Found Damaged on 870422 Per Required Action of Tech Spec. Snubber Damaged Due to Water Hammer Occurring When Valve Isolated.Snubber Replaced
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(s)(2) |
| 05000400/LER-1987-030, :on 870512,Maint Surveillance Tests I0140, I0141 & I0142 for P-12 Interlock Missed Thus Violating Tech Specs Requirements.Caused by Personnel Error.Procedures Revised |
- on 870512,Maint Surveillance Tests I0140, I0141 & I0142 for P-12 Interlock Missed Thus Violating Tech Specs Requirements.Caused by Personnel Error.Procedures Revised
| |
| 05000400/LER-1987-031, :on 870524,while Operating at 100% Power,Heater Drain Pump a Tripped.Caused by Failure of Discharge Valve on Heater Drain Pump a Due to Faulty Valve Positioner.Control Valve Positioner Repaired |
- on 870524,while Operating at 100% Power,Heater Drain Pump a Tripped.Caused by Failure of Discharge Valve on Heater Drain Pump a Due to Faulty Valve Positioner.Control Valve Positioner Repaired
| 10 CFR 50.73(a)(2) 10 CFR 50.73(e)(2) |
| 05000400/LER-1987-032, :on 870602,radiation Monitor REM-21WL-3541 Sample Chamber Instead of REM-21WS-354 Drained for Disconnection Leaving Monitor Inoperable.Caused by Personnel Error.Procedure HPP-495 Prepared |
- on 870602,radiation Monitor REM-21WL-3541 Sample Chamber Instead of REM-21WS-354 Drained for Disconnection Leaving Monitor Inoperable.Caused by Personnel Error.Procedure HPP-495 Prepared
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(o)(2) 10 CFR 50.73(o)(2)(8) |
| 05000400/LER-1987-033, :on 870607,experienced Trouble W/Engine Barring Device Not Rotating Engine as Required Using Plant Svc Air. Caused by Low Plant Svc Air Pressure.Mod Installed Attaching Engine Barring Device to Starting Air Tank Air |
- on 870607,experienced Trouble W/Engine Barring Device Not Rotating Engine as Required Using Plant Svc Air. Caused by Low Plant Svc Air Pressure.Mod Installed Attaching Engine Barring Device to Starting Air Tank Air
| 10 CFR 50.73(e)(2) 10 CFR 50.73(s)(2) 10 CFR 50.73(e)(2)(9) |
| 05000400/LER-1987-034, :on 870611,air Leakage by Inner & Outer Doors of Personnel Air Lock Excessive.Caused by Flat Spots on O-ring Seal.Seals on Inner & Outer Doors Replaced & Procedure OMM-001 Revised |
- on 870611,air Leakage by Inner & Outer Doors of Personnel Air Lock Excessive.Caused by Flat Spots on O-ring Seal.Seals on Inner & Outer Doors Replaced & Procedure OMM-001 Revised
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(5) |
| 05000400/LER-1987-035, :on 870617,reactor Coolant Pump C Tripped, Resulting in Reactor Trip Due to Low Flow in Reactor Coolant Loop C.Caused by Physical Contact W/Bus Encl.Program to Check & Drain Steam Supply Lines Initiated |
- on 870617,reactor Coolant Pump C Tripped, Resulting in Reactor Trip Due to Low Flow in Reactor Coolant Loop C.Caused by Physical Contact W/Bus Encl.Program to Check & Drain Steam Supply Lines Initiated
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(e)(2)(i) 10 CFR 50.73(e)(2) 10 CFR 50.73(e)(2)(ii) 10 CFR 50.73(e)(2)(v) 10 CFR 50.73(e)(2)(viii)(8) |
| 05000400/LER-1987-036, :on 870621,air Roll of 1A-SA Diesel Engine Not Performed within 4 to 8 H After Engine Shutdown.Caused by Marking in Test Procedure Step as Not Applicable.Engine Air Rolled.No Accumulation of Water Detected |
- on 870621,air Roll of 1A-SA Diesel Engine Not Performed within 4 to 8 H After Engine Shutdown.Caused by Marking in Test Procedure Step as Not Applicable.Engine Air Rolled.No Accumulation of Water Detected
| 10 CFR 50.73(e)(2) 10 CFR 50.73(s)(2) |
| 05000400/LER-1987-037, :on 870621,manual Reactor Trip Initiated from 30% Power After Operating Main Feedwater Train Tripped. Caused by Failed Open Feedwater Pump Recirculation Valve. Circuit Repaired & Plant Returned to Svc |
- on 870621,manual Reactor Trip Initiated from 30% Power After Operating Main Feedwater Train Tripped. Caused by Failed Open Feedwater Pump Recirculation Valve. Circuit Repaired & Plant Returned to Svc
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(s)(2) |
| 05000400/LER-1987-038, :on 870622,high Steam Generator Water Level Turbine Trip & Main Feedwater Isolation Actuated Automatic Reactor Trip on Interlock.Caused by Sudden Increase in Electrical Load.Precautionary Measures Taken |
- on 870622,high Steam Generator Water Level Turbine Trip & Main Feedwater Isolation Actuated Automatic Reactor Trip on Interlock.Caused by Sudden Increase in Electrical Load.Precautionary Measures Taken
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000400/LER-1987-039, :on 870619,intermediate Range (IR) High Neutron Flux Trip Setpoint Found Out of Calibr.Caused by Previous Adjustment to IR Setpoints.New Scaling Currents for 25% Trip Incorporated Into Applicable Procedures |
- on 870619,intermediate Range (IR) High Neutron Flux Trip Setpoint Found Out of Calibr.Caused by Previous Adjustment to IR Setpoints.New Scaling Currents for 25% Trip Incorporated Into Applicable Procedures
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(s)(2)(x) 10 CFR 50.73(s)(2) |
| 05000400/LER-1987-040, :on 870630,discovered That Surveillance Interval for Calorimetric Exceeded.Caused by Personnel Error.Night Order Issued Instructing Personnel on Importance of Performing Surveillances |
- on 870630,discovered That Surveillance Interval for Calorimetric Exceeded.Caused by Personnel Error.Night Order Issued Instructing Personnel on Importance of Performing Surveillances
| 10 CFR 50.73(a)(2)(B) |
| 05000400/LER-1987-041, :on 870804,restoration Alignment on Clearance for Placing Dryer 1B Back Into Svc Incorrect.Caused by Personnel Error.Valve Lineup for Instrument Air Dryer 1B Put Into Correct Configuration |
- on 870804,restoration Alignment on Clearance for Placing Dryer 1B Back Into Svc Incorrect.Caused by Personnel Error.Valve Lineup for Instrument Air Dryer 1B Put Into Correct Configuration
| 10 CFR 50.73(a)(2) 10 CFR 50.73(e)(2) |
| 05000400/LER-1987-042, :on 870709,wrong Fuses Pulled During Process of Placing Clearance OP-87-1290 Resulting in Automatic Reactor/ Turbine Trip.Caused by Personnel Error.Operator Training Conducted Re Fuse Labeling Conventions |
- on 870709,wrong Fuses Pulled During Process of Placing Clearance OP-87-1290 Resulting in Automatic Reactor/ Turbine Trip.Caused by Personnel Error.Operator Training Conducted Re Fuse Labeling Conventions
| 10 CFR 50.73(e)(2)(v) 10 CFR 50.73(e)(2)(viii)(A) |
| 05000400/LER-1987-043, :on 870820,discovered That Six Manual Isolation Valves Not Included in Operations Surveillance Test OST-1029.Caused by Personnel Error.Test Revised to Include Valves in Monthly Verification of Position |
- on 870820,discovered That Six Manual Isolation Valves Not Included in Operations Surveillance Test OST-1029.Caused by Personnel Error.Test Revised to Include Valves in Monthly Verification of Position
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(e)(2) 10 CFR 50.73(e)(2)(xiii)(A) |
| 05000400/LER-1987-044, :on 870713,Tech Spec Surveillance for Axial Flux Difference Missed.Caused by Personnel Error.Operator Counseled.Repairs in Progress to Repair Automatic Axial Flux Difference Monitor |
- on 870713,Tech Spec Surveillance for Axial Flux Difference Missed.Caused by Personnel Error.Operator Counseled.Repairs in Progress to Repair Automatic Axial Flux Difference Monitor
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(e)(2) |
| 05000400/LER-1987-045, :on 870716,RCS Pressure Fell Below Accumulator Pressure,Initiating Partial Injection of All Three Accumulators.Caused by Reactor Operator Error.Operating Shift Disciplined & Procedure Revised |
- on 870716,RCS Pressure Fell Below Accumulator Pressure,Initiating Partial Injection of All Three Accumulators.Caused by Reactor Operator Error.Operating Shift Disciplined & Procedure Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(e)(2) 10 CFR 50.73(e)(2)(v) 10 CFR 50.73(e)(2)(5) |
| 05000400/LER-1987-046, :on 870722,main Feedwater Pump B Tripped Due to Low Flow Resulting in Automatic Start of Auxiliary Feedwater Pumps.Caused by Loose Linkage on Recirculation Valve Due to Vibration.Valve Repaired.Procedures Changed |
- on 870722,main Feedwater Pump B Tripped Due to Low Flow Resulting in Automatic Start of Auxiliary Feedwater Pumps.Caused by Loose Linkage on Recirculation Valve Due to Vibration.Valve Repaired.Procedures Changed
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(e)(2) |
| 05000400/LER-1987-047, :on 870804-05,auxiliary Feedwater Actuations Occurred Due to Trips of Main Feedwater Pump 1A.Caused by Discharge Pressure Switches Out of Calibr.Discharge Pressure Switches Recalibr |
- on 870804-05,auxiliary Feedwater Actuations Occurred Due to Trips of Main Feedwater Pump 1A.Caused by Discharge Pressure Switches Out of Calibr.Discharge Pressure Switches Recalibr
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(e)(2)(x) 10 CFR 50.73(e)(2) |
| 05000400/LER-1987-048, :on 870811,failure to Take 9:30 Am Reading of Axial Flux Difference (Afd) as Required by Tech Specs Discovered.Caused by Personnel Error.Operator Disciplined. Addl Guidance Being Provided to Operators |
- on 870811,failure to Take 9:30 Am Reading of Axial Flux Difference (Afd) as Required by Tech Specs Discovered.Caused by Personnel Error.Operator Disciplined. Addl Guidance Being Provided to Operators
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(8) |
| 05000400/LER-1987-049, :on 870925,operating Main Feedwater Pump Tripped on Low Flow.Caused by High Vibration in Recirculation Piping.Valve Stem Replaced & Recirculation Valve Returned to Svc on 870925 |
- on 870925,operating Main Feedwater Pump Tripped on Low Flow.Caused by High Vibration in Recirculation Piping.Valve Stem Replaced & Recirculation Valve Returned to Svc on 870925
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(e)(2) |
| 05000400/LER-1987-050, :on 870830,RCS Unidentified Leakage Exceeded 1 Gallon Per Minute & on 870831 Insp Showed Evidence of Minor Leaks Due to Normal Wear.Caused by Equipment Failure. Valve Packing Repairs Initiated |
- on 870830,RCS Unidentified Leakage Exceeded 1 Gallon Per Minute & on 870831 Insp Showed Evidence of Minor Leaks Due to Normal Wear.Caused by Equipment Failure. Valve Packing Repairs Initiated
| 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(e)(2)(i) 10 CFR 50.73(e)(2) 10 CFR 50.73(e)(2)(ii) 10 CFR 50.73(e)(2)(v) |
| 05000400/LER-1987-051, :on 870831,main Feedwater Pump a Tripped Due to Feedwater Oscillation.Caused by Feedwater Sys Design Problems.Valve Stem Repaired & Feedwater Sys Changes to Improve Reliability Under Evaluation |
- on 870831,main Feedwater Pump a Tripped Due to Feedwater Oscillation.Caused by Feedwater Sys Design Problems.Valve Stem Repaired & Feedwater Sys Changes to Improve Reliability Under Evaluation
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(e)(2) 10 CFR 50.73(e)(2)(viii) |