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Category:Letter
MONTHYEARML24351A0952024-12-17017 December 2024 Senior Reactor and Reactor Operator Initial License Examinations LR-N24-0071, Supplement to License Amendment Request - Revise Hope Creek Generating Station Technical Specification to Change Surveillance Intervals to Accommodate a 24-Month Fuel Cycle2024-12-0606 December 2024 Supplement to License Amendment Request - Revise Hope Creek Generating Station Technical Specification to Change Surveillance Intervals to Accommodate a 24-Month Fuel Cycle LR-N24-0069, Independent Spent Fuel Storage Installation - Report of 10 CFR 72.48 Changes, Tests and Experiments2024-12-0202 December 2024 Independent Spent Fuel Storage Installation - Report of 10 CFR 72.48 Changes, Tests and Experiments IR 05000354/20240032024-10-23023 October 2024 Integrated Inspection Report 05000354/2024003 ML24295A3742024-10-23023 October 2024 Project Manager Assignment ML24291A0572024-10-17017 October 2024 License Amendment Request (LAR) – Hope Creek Technical Specification Conversion to NUREG-1433, Revision 5, Supplement 1 LR-N24-0063, Emergency Plan Document Revision Implemented September 18, 2024. Includes NC.EP-EP.ZZ-0903, Rev. 7, Opening of Emergency Operations Facility (EOF)2024-10-0707 October 2024 Emergency Plan Document Revision Implemented September 18, 2024. Includes NC.EP-EP.ZZ-0903, Rev. 7, Opening of Emergency Operations Facility (EOF) LR-N24-0059, 2024 Annual 10 CFR 50.46 Report2024-09-30030 September 2024 2024 Annual 10 CFR 50.46 Report LR-N24-0056, Response to Request for Additional Information Associated with License Amendment Request - Revise Hope Creek Generating Station Technical Specification to Change Surveillance Intervals to Accommodate a 24-Month Fuel Cycle2024-09-26026 September 2024 Response to Request for Additional Information Associated with License Amendment Request - Revise Hope Creek Generating Station Technical Specification to Change Surveillance Intervals to Accommodate a 24-Month Fuel Cycle IR 05000272/20244032024-09-25025 September 2024 And Salem Nuclear Generating Station, Units 1 and 2, Cybersecurity Inspection Report 05000354/2024403, 05000272/2024403, and 05000311/2024403 (Cover Letter Only) IR 05000272/20244022024-09-23023 September 2024 And Salem Nuclear Generating Station, Units 1 and 2 - Security Baseline Inspection Report 05000354/2024402, 05000272/2024402, and 05000311/2024402 (Cover Letter Only) ML24255A8042024-09-11011 September 2024 Notification of Conduct of a Fire Protection Team Inspection LR-N24-0057, In-Service Inspection Activities2024-09-10010 September 2024 In-Service Inspection Activities 05000354/LER-2024-001-01, Invalid Primary Containment Integrated Leak Rate As-Found Test (ILRT) Supplement2024-09-0505 September 2024 Invalid Primary Containment Integrated Leak Rate As-Found Test (ILRT) Supplement ML24249A1362024-09-0404 September 2024 EN 57304 - Westinghouse Electric Company, LLC, Final Report - No Embedded Files. Notification of the Potential Existence of Defects Pursuant to 10 CFR Part 21 IR 05000354/20240052024-08-29029 August 2024 Updated Inspection Plan for Hope Creek Generating Station (Report 05000354/2024005) LR-N24-0044, Relief Request VR-042024-08-0606 August 2024 Relief Request VR-04 IR 05000354/20240022024-07-30030 July 2024 Integrated Inspection Report 05000354/2024002 ML24200A0572024-07-18018 July 2024 Request for Withholding Information from Public Disclosure for License Amendment Request to Revise Technical Specification Lift Settings for Reactor Coolant System Safety/Relief Valves ML24197A0552024-07-15015 July 2024 Requalification Program Inspection ML24145A1772024-07-15015 July 2024 And Salem Nuclear Generating Station, Unit Nos. 1 and 2 - Issuance of Amendment Nos. 236, 349, and 331 Modify Exclusion Area Boundary 05000354/LER-2024-001, Invalid Primary Containment Integrated Leak Rate As-Found Test (ILRT)2024-07-0202 July 2024 Invalid Primary Containment Integrated Leak Rate As-Found Test (ILRT) LR-N24-0030, License Amendment Request to Revise Technical Specification Lift Settings for Reactor Coolant System Safety/Relief Valves2024-06-28028 June 2024 License Amendment Request to Revise Technical Specification Lift Settings for Reactor Coolant System Safety/Relief Valves IR 05000272/20245012024-06-12012 June 2024 And Salem Nuclear Generating Station, Units 1 and 2 - Emergency Preparedness Biennial Exercise Inspection Report 05000354/2024501, 05000272/2024501 and 05000311/2024501 ML24150A1002024-05-28028 May 2024 Core Operating Limits Report, Reload 25, Cycle 26, Revision 23 ML24150A0032024-05-28028 May 2024 Request for Exemptions from 10 CFR 50.82(a)(8)(i)(A) and 10 CFR 50.75(h)(1)(iv) and Proposed Amendment to the Decommissioning Trust Agreement LR-N24-0041, Stations, Revisions to Emergency Plan Document Nc EP-EP-ZZ-01102, Rev. 28, Emergency Coordinator Response2024-05-22022 May 2024 Stations, Revisions to Emergency Plan Document Nc EP-EP-ZZ-01102, Rev. 28, Emergency Coordinator Response LR-N24-0004, License Amendment Request – Revise Technical Specification to Change Surveillance Intervals to Accommodate a 24-Month Fuel Cycle2024-05-20020 May 2024 License Amendment Request – Revise Technical Specification to Change Surveillance Intervals to Accommodate a 24-Month Fuel Cycle ML24142A4072024-05-20020 May 2024 License Amendment Request (LAR) - Hope Creek Technical Specification Conversion to NUREG-1433, Revision 5 IR 05000354/20240012024-05-0808 May 2024 Integrated Inspection Report 05000354/2024001 IR 05000354/20240102024-05-0707 May 2024 Information Request for Quadrennial Baseline Comprehensive Engineering Team Inspection; Notification to Perform Inspection 05000354/2024010 LR-N24-0034, 2023 Annual Radioactive Effluent Release Report (ARERR)2024-04-30030 April 2024 2023 Annual Radioactive Effluent Release Report (ARERR) LR-N24-0035, 2023 Annual Radiological Environmental Operating Report (AREOR)2024-04-30030 April 2024 2023 Annual Radiological Environmental Operating Report (AREOR) LR-N24-0024, Response to Request for Additional Information Associated with License Amendment Request (LAR) to Modify the Salem and Hope Creek Exclusion Area Boundary2024-04-26026 April 2024 Response to Request for Additional Information Associated with License Amendment Request (LAR) to Modify the Salem and Hope Creek Exclusion Area Boundary IR 05000354/20243012024-04-10010 April 2024 Initial Operator Licensing Examination Report 05000354/2024301 LR-N24-0011, Supplemental Information to License Amendment Request (LAR) to Modify the Salem and Hope Creek Exclusion Area Boundary2024-04-0505 April 2024 Supplemental Information to License Amendment Request (LAR) to Modify the Salem and Hope Creek Exclusion Area Boundary IR 05000272/20240112024-04-0101 April 2024 And Salem Nuclear Generating Station, Units 1 and 2 - Plant Modification and Annual Problem Identification and Resolution Inspection Report 05000354/2024011, 05000272/2024011, and 05000311/2024011 LR-N24-0028, And Salem Generating Station - Notice of Intent to Pursue Subsequent License Renewal2024-03-28028 March 2024 And Salem Generating Station - Notice of Intent to Pursue Subsequent License Renewal LR-N24-0021, And Salem Generating Station, Units 1 and 2 - Guarantees of Payment of Deferred Premiums2024-03-20020 March 2024 And Salem Generating Station, Units 1 and 2 - Guarantees of Payment of Deferred Premiums ML24080A3962024-03-20020 March 2024 And Hope Creek Generating Station - Information Request for the Cybersecurity Baseline Inspection, Notification to Perform Inspection 05000272/2024403, 05000311/2024403, and 05000354/2024403 05000354/LER-2023-003-01, Inadvertent Main Turbine Control Valve Closure Caused Reactor Scram2024-03-19019 March 2024 Inadvertent Main Turbine Control Valve Closure Caused Reactor Scram LR-N24-0020, Generation Station and Salem Generating Station, Units 1 & 2 - Annual Property Insurance Status Report2024-03-0707 March 2024 Generation Station and Salem Generating Station, Units 1 & 2 - Annual Property Insurance Status Report IR 05000354/20230062024-02-28028 February 2024 Annual Assessment Letter for Hope Creek Generating Station (Report 05000354/2023006) IR 05000272/20244012024-02-26026 February 2024 And Salem Nuclear Generating Station, Units 1 and 2 - Security Baseline Inspection Report 05000354/2024401, 05000272/2024401 and 05000311/2024401 (Cover Letter Only) LR-N24-0010, Technical Specification 6.9.1.5.b: 2023 Annual Report of SRV Challenges2024-02-22022 February 2024 Technical Specification 6.9.1.5.b: 2023 Annual Report of SRV Challenges 05000354/LER-2023-003, Inadvertent Main Turbine Control Valve Closure Caused Reactor Scram2024-02-12012 February 2024 Inadvertent Main Turbine Control Valve Closure Caused Reactor Scram IR 05000354/20230042024-02-0101 February 2024 Integrated Inspection Report 05000354/2023004 ML24030A8752024-02-0101 February 2024 Operator Licensing Examination Approval ML24009A1022024-01-26026 January 2024 – Exemption from Select Requirements of 10 CF Part 73 (EPID L-2023-LLE-0045 (Security Notifications, Reports, and Recordkeeping and Suspicious Activity Reporting)) IR 05000354/20234012024-01-22022 January 2024 Material Control and Accounting Program Inspection Report 05000354/2023401 2024-09-05
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000354/LER-2024-001-01, Invalid Primary Containment Integrated Leak Rate As-Found Test (ILRT) Supplement2024-09-0505 September 2024 Invalid Primary Containment Integrated Leak Rate As-Found Test (ILRT) Supplement 05000354/LER-2024-001, Invalid Primary Containment Integrated Leak Rate As-Found Test (ILRT)2024-07-0202 July 2024 Invalid Primary Containment Integrated Leak Rate As-Found Test (ILRT) 05000354/LER-2023-003-01, Inadvertent Main Turbine Control Valve Closure Caused Reactor Scram2024-03-19019 March 2024 Inadvertent Main Turbine Control Valve Closure Caused Reactor Scram 05000354/LER-2023-003, Inadvertent Main Turbine Control Valve Closure Caused Reactor Scram2024-02-12012 February 2024 Inadvertent Main Turbine Control Valve Closure Caused Reactor Scram 05000354/LER-2023-001-02, Technical Specification Required Shutdown Due to Declaring the Suppression Chamber and Primary Containment Inoperable2023-09-25025 September 2023 Technical Specification Required Shutdown Due to Declaring the Suppression Chamber and Primary Containment Inoperable 05000354/LER-2023-001-01, Technical Specification Required Shutdown Due to Declaring the Suppression Chamber and Primary Containment Inoperable2023-09-11011 September 2023 Technical Specification Required Shutdown Due to Declaring the Suppression Chamber and Primary Containment Inoperable 05000354/LER-2023-001, Technical Specification Required Shutdown Due to Declaring the Suppression Chamber and Primary Containment Inoperable2023-06-20020 June 2023 Technical Specification Required Shutdown Due to Declaring the Suppression Chamber and Primary Containment Inoperable 05000354/LER-1922-002, Inoperable Isolation Actuation Instrumentation Caused by Failure to Remove Electrical Jumper2023-01-18018 January 2023 Inoperable Isolation Actuation Instrumentation Caused by Failure to Remove Electrical Jumper 05000354/LER-2022-001, B EDG Inoperable Resulting in a Condition Prohibited by Technical Specifications2022-03-18018 March 2022 B EDG Inoperable Resulting in a Condition Prohibited by Technical Specifications 05000354/LER-2021-001, Safety Relief Valve (SRV) As-Found Setpoint Failures2021-08-13013 August 2021 Safety Relief Valve (SRV) As-Found Setpoint Failures 05000354/LER-2019-002, Safety Relief Valve (SRV) As-found Set-point Failures2020-01-0606 January 2020 Safety Relief Valve (SRV) As-found Set-point Failures 05000354/LER-2019-001, Manual Scram and Manual Actuation of Reactor Core Isolation Cooling2019-10-0202 October 2019 Manual Scram and Manual Actuation of Reactor Core Isolation Cooling 05000354/LER-2018-004, High Pressure Coolant Injection System Inoperable Due to Failed Fuse2018-11-20020 November 2018 High Pressure Coolant Injection System Inoperable Due to Failed Fuse 05000354/LER-2018-002-01, Safety Relief Valve L (SRV) As-Found Setpoint Failure2018-10-0303 October 2018 Safety Relief Valve L (SRV) As-Found Setpoint Failure 05000354/LER-2018-003-01, Feedwater Isolation Valve Leakage Exceeded Technical Specification Limit2018-09-12012 September 2018 Feedwater Isolation Valve Leakage Exceeded Technical Specification Limit LR-N18-0065, Safety Relief Valve (SRV) As-Found Setpoint Failure2018-06-18018 June 2018 Safety Relief Valve (SRV) As-Found Setpoint Failure 05000354/LER-2018-001, Operations with a Potential to Drain the Reactor Vessel Without Secondary Containment2018-06-18018 June 2018 Operations with a Potential to Drain the Reactor Vessel Without Secondary Containment 05000354/LER-2018-003, Feedwater Isolation Valve Leakage Exceeded Technical Specification Limit2018-06-18018 June 2018 Feedwater Isolation Valve Leakage Exceeded Technical Specification Limit 05000354/LER-1917-001, Regarding Secondary Containment Door Not Latched in Closed Position2017-07-0707 July 2017 Regarding Secondary Containment Door Not Latched in Closed Position 05000354/LER-2016-006, Regarding Mode Change Without B Channel Level Instrumentation Operable2017-01-0909 January 2017 Regarding Mode Change Without B Channel Level Instrumentation Operable 05000354/LER-2016-005, Regarding Reactor Protection System Actuation While the Reactor Was Shutdown2017-01-0404 January 2017 Regarding Reactor Protection System Actuation While the Reactor Was Shutdown 05000354/LER-2016-004, Regarding Operations with a Potential to Drain the Reactor Vessel (OPDRV) Without Secondary Containment2016-12-20020 December 2016 Regarding Operations with a Potential to Drain the Reactor Vessel (OPDRV) Without Secondary Containment 05000354/LER-2016-003, Regarding As-Found Values for Safety Relief Valve Lift Set Points Exceed Technical Specification Allowable Limit2016-12-20020 December 2016 Regarding As-Found Values for Safety Relief Valve Lift Set Points Exceed Technical Specification Allowable Limit 05000354/LER-2016-002, Regarding High Pressure Coolant Injection System Inoperable2016-10-0505 October 2016 Regarding High Pressure Coolant Injection System Inoperable 05000354/LER-2016-001, Regarding High Pressure Coolant Injection System Found to Be Inoperable During Testing2016-10-0404 October 2016 Regarding High Pressure Coolant Injection System Found to Be Inoperable During Testing 05000354/LER-2015-005, Regarding Reactor Scram Due to Invalid RRCS Actuation2015-11-24024 November 2015 Regarding Reactor Scram Due to Invalid RRCS Actuation 05000354/LER-2015-004, Regarding As-Found Values for Safety Relief Valve Lift Set Points Exceed Technical Specification Allowable Limit2015-07-30030 July 2015 Regarding As-Found Values for Safety Relief Valve Lift Set Points Exceed Technical Specification Allowable Limit 05000354/LER-2015-003, Regarding Conditions Prohibited by Technical Specifications Due to Low Pressure ECCS2015-07-0606 July 2015 Regarding Conditions Prohibited by Technical Specifications Due to Low Pressure ECCS 05000354/LER-2015-002, Regarding Operations with a Potential to Drain the Reactor Vessel (OPDRV) Without Secondary Containment2015-06-10010 June 2015 Regarding Operations with a Potential to Drain the Reactor Vessel (OPDRV) Without Secondary Containment 05000354/LER-2015-001, Regarding Conditions Prohibited by Technical Specifications Due to Core Spray Lnoperabilities2015-05-29029 May 2015 Regarding Conditions Prohibited by Technical Specifications Due to Core Spray Lnoperabilities 05000354/LER-2013-011, Regarding Filtration, Recirculation, and Ventilation System Exceeded Technical Specification Allowed Outage Time2015-03-25025 March 2015 Regarding Filtration, Recirculation, and Ventilation System Exceeded Technical Specification Allowed Outage Time 05000354/LER-2013-010, Regarding Loss of Both Control Room Chillers2014-02-18018 February 2014 Regarding Loss of Both Control Room Chillers 05000354/LER-2013-009, Regarding Automatic Actuation of the Reactor Protection System Due to a Main Turbine Trip2014-01-28028 January 2014 Regarding Automatic Actuation of the Reactor Protection System Due to a Main Turbine Trip 05000354/LER-2013-008, Regarding Automatic Actuation of the Reactor Protection System Due to a Main Turbine Trip2014-01-28028 January 2014 Regarding Automatic Actuation of the Reactor Protection System Due to a Main Turbine Trip 05000354/LER-2013-007, Regarding As-Found Values for Safety Relief Valve Lift Set Points Exceed Technical Specification Allowable Limit2014-01-16016 January 2014 Regarding As-Found Values for Safety Relief Valve Lift Set Points Exceed Technical Specification Allowable Limit 05000354/LER-2013-006, Regarding Operations with a Potential to Drain the Reactor Vessel (OPDRV) Without Secondary Containment Operable2013-12-24024 December 2013 Regarding Operations with a Potential to Drain the Reactor Vessel (OPDRV) Without Secondary Containment Operable 05000354/LER-2013-005, Regarding Low-Low Set Safety/Relief Valve Pilot Solenoid Operated Valve Failed As-Found Testing2013-12-17017 December 2013 Regarding Low-Low Set Safety/Relief Valve Pilot Solenoid Operated Valve Failed As-Found Testing 05000354/LER-2013-004, Regarding Operations with a Potential to Drain the Reactor Vessel (OPDRV) Without Secondary Containment2013-12-10010 December 2013 Regarding Operations with a Potential to Drain the Reactor Vessel (OPDRV) Without Secondary Containment 05000354/LER-2013-003, Through-wall Flaw Discovered on RHR Shutdown Cooling Return Vent Line2013-08-0808 August 2013 Through-wall Flaw Discovered on RHR Shutdown Cooling Return Vent Line 05000354/LER-2013-002, Regarding Reactor Scram Due to Degrading Condenser Vacuum2013-08-0808 August 2013 Regarding Reactor Scram Due to Degrading Condenser Vacuum 05000354/LER-2013-001, Regarding High Pressure Coolant Injection System Inoperable Due to Control Relay Failure2013-06-0505 June 2013 Regarding High Pressure Coolant Injection System Inoperable Due to Control Relay Failure 05000354/LER-2012-004-01, Regarding As-found Values for Safety Relief Valve Lift Setpoints Exceed Technical Specification Allowable2012-12-10010 December 2012 Regarding As-found Values for Safety Relief Valve Lift Setpoints Exceed Technical Specification Allowable 05000354/LER-2012-006, High Pressure Coolant Injection System Inoperable2012-10-31031 October 2012 High Pressure Coolant Injection System Inoperable 05000354/LER-2012-005, Regarding RCIC Bearing Low Oil Pressure Indication on Remote Shutdown Panel Inoperable2012-08-23023 August 2012 Regarding RCIC Bearing Low Oil Pressure Indication on Remote Shutdown Panel Inoperable 05000354/LER-2012-004, As Found Values for Safety Relief Valve Lift Setpoints Exceed Technical Specification Allowable2012-07-0303 July 2012 As Found Values for Safety Relief Valve Lift Setpoints Exceed Technical Specification Allowable 05000354/LER-2012-003, Regarding Operation with the Potential to Drain the Reactor Vessel2012-05-14014 May 2012 Regarding Operation with the Potential to Drain the Reactor Vessel 05000354/LER-2012-002, Regarding High Pressure Coolant Injection System Inoperable2012-05-14014 May 2012 Regarding High Pressure Coolant Injection System Inoperable 05000354/LER-2012-001, Regarding Average Power Range Monitor Flow Unit Summers Out of Tech Spec Tolerance2012-05-0303 May 2012 Regarding Average Power Range Monitor Flow Unit Summers Out of Tech Spec Tolerance LR-N12-0114, Retraction of Licensee Event Report 2011-0012012-04-13013 April 2012 Retraction of Licensee Event Report 2011-001 LR-N05-0143, Special Report 05-001-01 Regarding the Cause of Failure and Channel Restoration2005-03-31031 March 2005 Special Report 05-001-01 Regarding the Cause of Failure and Channel Restoration 2024-09-05
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LER-2018-003, Feedwater Isolation Valve Leakage Exceeded Technical Specification Limit |
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PSEG Nuclear LLC P.O. Box 236, Hancocks Bridge, New Jersey 08038-0236 0PSEG Nuclear LLC LR-N 18-0093 SEP 12 2018 United States Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC. 20555-001 Hope Creek Generating Station Renewed Facility Operating License No. NPF-57 Docket No. 50-354 10CFR50.73
Subject:
Supplemental Licensee Event Report 2018-003-01, Feedwater Isolation Valve Leakage Exceeded Technical Specification Limit
Reference:
PSEG Letter LR-N18-0068, dated June 18, 2018 Licensee Event Report 2018-003-00 In accordance with 10 CFR 50.73(a)(2)(i)(B), PSEG Nuclear LLC is submitting Supplemental Licensee Event Report (LER) Number 2018-003-01, "Feedwater Isolation Valve Leakage Exceeded Technical Specification Limit." The Reference LER stated that Hope Creek Generating Station would supply a supplement to the LER with the results of an evaluation to determine if the leakage would have prevented the fulfillment of a safety function. The results of the evaluation are communicated in the LER supplement attached to this letter.
If you have any questions or require additional information, please contact Mr. Thomas MacEwen at (856) 339-1097.
There are no regulatory commitments contained in this letter.
Sincerely,
~TUI Edward T. Casulli Plant Manager Hope Creek Generating Station Attachment: Supplemental Licensee Event Report 2018-003-01
LR-N18-0093 Page 2 cc:
Mr. David Lew, Regional Administrator-Region I, NRC Mr. James Kim, Project Manager-US NRC 10CFR50.73 Mr. Justin Hawkins, NRC Senior Resident Inspector-Hope Creek (X24)
Mr. Patrick Mulligan, Manager IV, NJBNE Mr. Thomas MacEwen, Hope Creek Commitment Tracking Coordinator (H02)
Mr. Lee Marabella, Corporate Commitment Tracking Coordinator (N21)
NRCFORM366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104 EXPIRES: 0313112020 (04-2018)
, the NRC may not conduct or sponsor, and a oerson is not reauired to resoond to the information collection.
3.Page Hope Creek Generating Station 05000-354 1 OF3
- 4. Title Feedwater Isolation Valve Leakaqe Exceeded Technical Specification Limit
- 5. Event Date
- 6. LER Number
- 7. Report Date
- 8. other Facilities Involved Sequential Rev Facility Name Docket Number Month Day Year Year Month Day Year Number No.
05000 04 18 2018 2018
- - 003
- - 01 09 12 2018 Facility Name Docket Number 05000
- 9. Operating Mode
~bstract (Limit to 1400 spaces, i.e., approximately 14 single-spaced typewritten lines)
On April 18, 2018, with Hope Creek Generating Station (HCGS) in a planned refueling outage, HCGS performed a required surveillance test of the long term seal of the feedwater lines. The test criteria could not be met due to leakage past feedwater isolation valve H1AE -AE-HVF032B. The valve is sealed with a water seal from the High Pressure Reactor Coolant (HPCI) system, or Reactor Core Isolation Cooling (RCIC) system, to form a long-term seal boundary of the feedwater lines. The valve is tested per Technical Specification Surveillance Requirement 4.6.1.2.g to verify a maximum leak rate of 10 gpm at a test pressure of 55.7 psig. During the test, a test pressure of 44 psig was the highest pressure that could be obtained, which does not meet the acceptance criterion.
This condition is being reported in accordance with 10 CFR 50. 73(a)(2)(i)(B) as a condition prohibited by plant Technical Specifications.
NRC FORM 366 {04-2018)
PLANT AND SYSTEM IDENTIFICATION
General Electric-Boiling Water Reactor (BWR/4)*
Feedwater System (SJ)- EllS Identifier {SJ/ISV}
High Pressure Coolant Injection (BJ ) - EllS Identifier {BJ}
Reactor Core Isolation Cooling (BN)- EllS Identifier {BN}
Secondary Containment (NG)- EllS Identifier {NG}
YEAR 2018 SEQUENTIAL NUMBER
- - 003
- Energy Industry Identification System {EllS} codes and component function identifier codes appear as {SS/CCC}
IDENTIFICATION OF OCCURRENCE Event Dates: April18, 2018 Discovery Dates: April 18, 2018 CONDITIONS PRIOR TO OCCURRENCE Hope Creek was shut down for Refueling Outage H1 R21 in Operational Condition (OPCON) 5-Refueling Operations.
DESCRIPTION OF OCCURRENCE REV NO.
- - 01 On April 18, 2018, with Hope Creek Generating Station (HCGS) in a planned refueling outage, HCGS performed a required surveillance test of the long term seal of the feedwater lines. The test criteria could not be met due to leakage past feedwater system {SJ} isolation valve H1AE -AE-HVF032B. The valve is sealed with a water seal from the High Pressure Coolant Injection (HPCI) {BJ} system, or Reactor Core Isolation Cooling (RCIC) {BN} system, to form a long-term seal boundary of the feedwater lines. The valve is tested with water at a test pressure of 55.7 psig to ensure the seal boundary will prevent bypass leakage. At the maximum water test rig pressure, the test rig's downstream pressure was only able to achieve approximately 44 psig, 11.7 psig less than the required 55.7 psig to perform the test.
Although no flow rate was achieved or directly measured, the test was considered failed due to not being able to meet procedural test acceptance criterion.
The H1AE -AE-HV-F032B is 24 inch anchor darling "Y" type swing check valve with a Limitorque SMB-4 motor operator to assist in maintaining the valve closed.
Technical Specification 3.6.1.2.d limits the total combined leakage rate to 10 gpm, or less, for all the containment isolation valves which form the boundary for the long term seal of the feedwater lines, when tested at 55.7 psig. Based on the cause of the failure, and the maintenance history of the valve, it was concluded that the condition is reportable as a condition prohibited by Technical Specifications under 10 CFR 50. 73{a)(2)(i)(B).
CAUSE OF EVENT
An internal inspection was performed on the H1 AE -AE-HV-F032B under work order 60138581 in H1 R21. The following was identified during this inspection:
- - One bore on the hinge arm was larger than the acceptance criteria by an average of 0.004 inches. (2.039 inches vs 2.029-2.035 inches)
- - The hinge pin was worn and undersized by 0.002 inches. (1.997 inches vs 2.000 +/- 0.001 inches)
- - The gap between the hinge arm and disc was smaller by 0.0325 inches {0.030 inches vs 0.0625 inches)
The combination of the wear on the hinge arm bores, the wear on the hinge pin, and the smaller gap between the hinge arm and disc prevented the valve disc from properly seating, which resulted in the high leak rate.
NRC FORM 3668 (04-2018)
Page 2 of 3 (04-2018)
U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)
CONTINUATION SHEET (See NUREG-1022, R.3 for instruction and guidance for completing this form htto://www.nrc.gov/readinq-rm/doc-collections/nureos/staff/sr1022/r3/)
APPROVED BY OMB: NO. 3150-0104 EXPIRES: 3/31/2020
, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
- 1. FACILITYNAME
- 2. DOCKET NUMBER
- 3. L.ER NUMBER Hope Creek Generating Station 05000-354
SAFETY CONSEQUENCES AND IMPLICATIONS
YEAR 2018 SEQUENTIAL NUMBER
- - 003 The long term feedwater seal is established following a Loss of Coolant Accident (LOCA) by manually aligning the RCIC and/or HPCI jockey pumps to the feedwater lines between the inboard and outboard containment isolation REV NO.
- - 01 valves. H1AE -AE-HV-F032B is the outboard containment isolation valve on one of two feedwater supply lines. The purpose of the feedwater seal, as described in the UFSAR, is to establish a water seal of the feedwater penetrations to eliminate bypass leakage. The seal is established following a LOCA, and is to be maintained for a minimum of 30 days.
The purpose of the leak rate testing is to verify that the leakage is within the capability of the system to maintain the seal for the 30 day minimum.
A Technical Evaluation was performed to determine the impact on the ability to maintain a leak seal for the 30 day minimum. The evaluation of test data indicates leakage through the F032B would not have posed a challenge to the ability to establish and maintain the required feedwater seal for 30 days post-LOCA.
SAFETY SYSTEM FUNCTIONAL FAILURE A review of this condition, and the associated technical evaluation, determined that a Safety System Functional Failure (SSFF) as defined in Nuclear Energy Institute (NEI) 99-02, "Regulatory Assessment Performance Indicator Guideline,"
did not occur. This event did not prevent the ability of a system to fulfill its safety function to either shutdown the reactor, remove residual heat, control the release of radioactive material, or mitigate the consequences of an accident.
PREVIOUS EVENTS A review of Licensee Event Reports and the corrective action program for the past three years identified no LERs issued for similar conditions.
CORRECTIVE ACTIONS
The F032B check valve was opened and inspected. Corrective maintenance was performed to address the dimensional clearances and deficiencies identified in the Cause of Event section above. A satisfactory leak rate test was performed following the corrective maintenance.
COMMITMENTS
This LER contains no regulatory commitments. Page 3 of 3
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05000354/LER-2018-001, Operations with a Potential to Drain the Reactor Vessel Without Secondary Containment | Operations with a Potential to Drain the Reactor Vessel Without Secondary Containment | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | 05000354/LER-2018-002-01, Safety Relief Valve L (SRV) As-Found Setpoint Failure | Safety Relief Valve L (SRV) As-Found Setpoint Failure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | 05000354/LER-2018-003-01, Feedwater Isolation Valve Leakage Exceeded Technical Specification Limit | Feedwater Isolation Valve Leakage Exceeded Technical Specification Limit | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000354/LER-2018-003, Feedwater Isolation Valve Leakage Exceeded Technical Specification Limit | Feedwater Isolation Valve Leakage Exceeded Technical Specification Limit | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000354/LER-2018-004, High Pressure Coolant Injection System Inoperable Due to Failed Fuse | High Pressure Coolant Injection System Inoperable Due to Failed Fuse | 10 CFR 50.73(a)(2)(v), Loss of Safety Function |
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