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Category:Letter
MONTHYEARML24298A0552024-10-30030 October 2024 Response to Alternative RR-10, Auxiliary Feedwater Valve Testing IR 05000282/20244032024-10-25025 October 2024 – Security Baseline Inspection Report 05000282/2024403 and 05000306/2024403 05000282/LER-2024-001-01, Auxiliary Building Special Ventilation System Inoperable During Movement of Irradiated Fuel Assemblies2024-10-22022 October 2024 Auxiliary Building Special Ventilation System Inoperable During Movement of Irradiated Fuel Assemblies L-PI-24-044, Application to Revise Technical Specifications to Adopt TSTF-591, Revise Risk Informed Completion Time (RICT) Program2024-10-21021 October 2024 Application to Revise Technical Specifications to Adopt TSTF-591, Revise Risk Informed Completion Time (RICT) Program ML24277A1012024-10-0303 October 2024 Closure of Interim Report of a Potential Deviation or Failure to Comply Associated with Bentley Systems Incorporated Autopipe Software ML24221A3622024-09-27027 September 2024 Issuance of Amendment Nos. 245 and 233 Revise Technical Specification 3.8.1, AC Sources-Operating, Surveillance Requirement 3.8.1.2, Note 3 ML24241A1682024-09-23023 September 2024 Transmittal Letter Amendment No. 13 to Materials License No. Special Nuclear Material-2506 for the Prairie Island Independent Spent Fuel Storage Installation 05000282/LER-2024-001, Auxiliary Building Special Ventilation System Inoperable During Movement of Irradiated Fuel Assemblies2024-09-16016 September 2024 Auxiliary Building Special Ventilation System Inoperable During Movement of Irradiated Fuel Assemblies IR 05000282/20243012024-09-13013 September 2024 NRC Initial License Examination Report 05000282/2024301 and 05000306/2024301 IR 05000282/20240052024-08-28028 August 2024 Updated Inspection Plan and Assessment Follow-Up Letter for Prairie Island Nuclear Generating Plant, Units 1 and 2 (Report 05000282/2024005 and 05000306/2024005) L-PI-24-040, Post-Submittal Package Letter2024-08-23023 August 2024 Post-Submittal Package Letter IR 05000282/20245012024-08-0505 August 2024 Emergency Preparedness Inspection Report 05000282/2024501 and 05000306/2024501 ML24213A1592024-07-31031 July 2024 Operator Licensing Examination Approval - Prairie Island Nuclear Generating Plant IR 05000282/20240022024-07-30030 July 2024 Integrated Inspection Report 05000282/2024002 and 05000306/2024002 ML24208A1502024-07-26026 July 2024 Independent Spent Fuel Storage Installation - Submittal of Quality Assurance Topical Report (NSPM-1) ML24197A2012024-07-15015 July 2024 Notification of NRC Baseline Inspection and Request for Information; Inspection Report 05000282/2024004 IR 05000282/20240102024-06-28028 June 2024 Comprehensive Engineering Team Inspection Report 05000282/2024010 and 05000306/2024010 L-PI-24-036, – Preparation and Scheduling of Operator Licensing Examinations2024-06-28028 June 2024 – Preparation and Scheduling of Operator Licensing Examinations ML24158A5912024-06-0606 June 2024 CFR 50.46 LOCA Annual Report L-PI-24-031, Independent Spent Fuel Storage Installation, Supplement to License Amendment Request to Revise Independent Spent Fuel Storage Installation (ISFSI) License Conditions 23(a), 24(A)(2), and 24(B)(2)2024-06-0505 June 2024 Independent Spent Fuel Storage Installation, Supplement to License Amendment Request to Revise Independent Spent Fuel Storage Installation (ISFSI) License Conditions 23(a), 24(A)(2), and 24(B)(2) L-PI-24-014, License Amendment Request to Revise the Technical Specification Definition of Reactor Trip System (RTS) Response Time and Apply Response Time Testing to RTS Trip Functions with Time Delay Assumption2024-06-0303 June 2024 License Amendment Request to Revise the Technical Specification Definition of Reactor Trip System (RTS) Response Time and Apply Response Time Testing to RTS Trip Functions with Time Delay Assumption 05000306/LER-2024-001-01, Reactor Trip and Auto-Start Actuation of Auxiliary Feedwater Due to Loss of Suction to the 22 Main Feedwater Pump2024-05-31031 May 2024 Reactor Trip and Auto-Start Actuation of Auxiliary Feedwater Due to Loss of Suction to the 22 Main Feedwater Pump ML24155A1922024-05-31031 May 2024 Refueling Outage Unit 2 R33 Owners Activity Report for Class 1, 2, 3 and Mc Inservice Inspections ML24262A1992024-05-29029 May 2024 L-PI-24-018 PINGP 75 Day Letter ML24149A3712024-05-29029 May 2024 (Ping) - Information Request for the Cyber-Security Baseline Inspection, Notification to Perform Inspection L-PI-24-030, Response to Request for Additional Information Regarding License Amendment Request to Revise Technical Specification 3.8.12024-05-22022 May 2024 Response to Request for Additional Information Regarding License Amendment Request to Revise Technical Specification 3.8.1 ML24141A1292024-05-22022 May 2024 Northern States Power Company - Use of Encryption Software for Electronic Transmission of Safeguards Information ML24141A0452024-05-20020 May 2024 Information Request to Support the NRC Annual Baseline Emergency Action Level and Emergency Plan Changes Inspection ML24128A2572024-05-16016 May 2024 ISFSI A13 Acceptance Letter IR 05000282/20240012024-05-15015 May 2024 Integrated Inspection Report 05000282/2024001 and 05000306/2024001 ML24130A2362024-05-0909 May 2024 Independent Spent Fuel Storage Installation - 2023 Annual Radiological Environmental Monitoring Program Report ML24130A2392024-05-0909 May 2024 2023 Annual Radioactive Effluent Report ML24071A1162024-05-0101 May 2024 Issuance of Amendment Nos. 244 and 232 Revise TS 3.7.8, Cooling Water (Cl) System ML24128A0882024-04-30030 April 2024 Submittal of Updated Safety Analysis Report (Usar), Revision 38 05000306/LER-2024-001, Reactor Trip and Auto-Start Actuation of Auxiliary Feedwater Due to Loss of Suction to the 22 Main Feedwater Pump2024-04-29029 April 2024 Reactor Trip and Auto-Start Actuation of Auxiliary Feedwater Due to Loss of Suction to the 22 Main Feedwater Pump ML24089A2382024-04-29029 April 2024 Summary of Nuclear Property Insurance IR 05000282/20244012024-04-25025 April 2024 – Security Baseline Inspection Report 05000282/2024401 and 05000306/2024401 ML24100A8042024-04-24024 April 2024 – Alternative Request RR-09 for Safety Injection and Volume Control System Category C Check Valve Inservice Testing ML24114A0882024-04-23023 April 2024 Annual Report of Individual Monitoring for the Prairie Island Nuclear Generating Plant (PINGP) ML24113A1182024-04-12012 April 2024 NRC Letter Re NRC Office of Investigations Report No. 3-2023-004 ML24100A1212024-04-0909 April 2024 Submittal of Revised Pressure and Temperature Limits Report ML24093A2832024-04-0202 April 2024 Nuclear Material Transaction Report L-PI-24-012, Independent Spent Fuel Storage Installation - License Amendment Request: Revise Independent Spent Fuel Storage Installation (ISFSI) License Conditions 23(a), 24(A)(2), and 24(B)(2)2024-04-0202 April 2024 Independent Spent Fuel Storage Installation - License Amendment Request: Revise Independent Spent Fuel Storage Installation (ISFSI) License Conditions 23(a), 24(A)(2), and 24(B)(2) ML24089A2402024-03-29029 March 2024 Guarantee of Payment of Deferred Premiums ML24060A1232024-03-27027 March 2024 To Request 1-RR-5-10 and 2-RR-5-10 Regarding Reactor Pressure Vessel Welds and Nozzle Welds 05000282/LER-2023-001-01, Reactor Trip, Auxiliary Feedwater and Emergency Service Water System Actuation Due to Electrical Transient in DC Control Power Cables2024-03-21021 March 2024 Reactor Trip, Auxiliary Feedwater and Emergency Service Water System Actuation Due to Electrical Transient in DC Control Power Cables ML24262A1512024-03-15015 March 2024 L-PI-24-011 150 Day Letter 2024 PINGP ILT NRC Exam ML24010A0582024-03-0505 March 2024 Amendment No. 12 to Materials License No. Special Nuclear Material-2506 for the Prairie Island Independent Spent Fuel Storage Installation L-PI-24-004, Independent Spent Fuel Storage Installation - Annual Effluent Report, January Through December 20232024-02-29029 February 2024 Independent Spent Fuel Storage Installation - Annual Effluent Report, January Through December 2023 IR 05000282/20230062024-02-28028 February 2024 Annual Assessment Letter for Prairie Island Nuclear Generating Plant, Units 1 and 2 (Report 05000282/2023006 and 05000306/2023006) 2024-09-27
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000282/LER-2024-001-01, Auxiliary Building Special Ventilation System Inoperable During Movement of Irradiated Fuel Assemblies2024-10-22022 October 2024 Auxiliary Building Special Ventilation System Inoperable During Movement of Irradiated Fuel Assemblies 05000282/LER-2024-001, Auxiliary Building Special Ventilation System Inoperable During Movement of Irradiated Fuel Assemblies2024-09-16016 September 2024 Auxiliary Building Special Ventilation System Inoperable During Movement of Irradiated Fuel Assemblies 05000306/LER-2024-001-01, Reactor Trip and Auto-Start Actuation of Auxiliary Feedwater Due to Loss of Suction to the 22 Main Feedwater Pump2024-05-31031 May 2024 Reactor Trip and Auto-Start Actuation of Auxiliary Feedwater Due to Loss of Suction to the 22 Main Feedwater Pump 05000306/LER-2024-001, Reactor Trip and Auto-Start Actuation of Auxiliary Feedwater Due to Loss of Suction to the 22 Main Feedwater Pump2024-04-29029 April 2024 Reactor Trip and Auto-Start Actuation of Auxiliary Feedwater Due to Loss of Suction to the 22 Main Feedwater Pump 05000282/LER-2023-001-01, Reactor Trip, Auxiliary Feedwater and Emergency Service Water System Actuation Due to Electrical Transient in DC Control Power Cables2024-03-21021 March 2024 Reactor Trip, Auxiliary Feedwater and Emergency Service Water System Actuation Due to Electrical Transient in DC Control Power Cables 05000282/LER-2023-001, Reactor Trip, Auxiliary Feedwater and Emergency Service Water System Actuation Due to Electrical Transient in DC Control Power Cables2023-12-0404 December 2023 Reactor Trip, Auxiliary Feedwater and Emergency Service Water System Actuation Due to Electrical Transient in DC Control Power Cables 05000306/LER-2023-001, Gt/Xfmr Lockout Due to Failure of Lightning Arrester Caused Unit 2 Reactor Trip2023-07-18018 July 2023 Gt/Xfmr Lockout Due to Failure of Lightning Arrester Caused Unit 2 Reactor Trip 05000282/LER-2022-001, Fuel Assemblies Incorrectly Placed in Spent Fuel Pool2022-10-17017 October 2022 Fuel Assemblies Incorrectly Placed in Spent Fuel Pool 05000282/LER-2021-002, Loss of Electrical Bus Results in 121 Motor Driven Cooling Water Pump Auto Start2021-12-13013 December 2021 Loss of Electrical Bus Results in 121 Motor Driven Cooling Water Pump Auto Start 05000306/LER-2021-001, Turbine Driven Auxiliary Feedwater Pump Actuation Signal Due to Procedure Error2021-11-18018 November 2021 Turbine Driven Auxiliary Feedwater Pump Actuation Signal Due to Procedure Error ML19353A4092019-12-19019 December 2019 Technical Specification 5.6.8 Special Report: Inoperable Containment Isolation Valve Indication Supplemental Report 05000306/LER-2017-0032018-01-11011 January 2018 Both Containment SEa) Pump Control Switches in Pull-out in Mode 4, LER 17-003-00 for Prairie Island Nuclear Generating Plant, Unit 2 Regarding Both Containment Spray Pump Control Switches in Pull-Out in Mode 4 05000306/LER-2017-0022017-12-11011 December 2017 Reactor Coolant System Shutdown Communication Live Vent Through Wall Defect, LER 17-002-00 for Prairie Island, Unit 2, Regarding Reactor Coolant System Shutdown Communication Live Vent Through Wall Defect 05000306/LER-2017-0012017-11-29029 November 2017 23 Containment Fan Coil Unit Operability, LER 17-001-00 for Prairie Island, Unit 2, Regarding 23 Containment Fan Coil Unit Operability 05000282/LER-2016-0062017-02-15015 February 2017 121 Motor Driven Cooling Water Pump Auto Start, LER 16-006-00 for Prairie Island Nuclear Generating Plant, Units 1 and 2 Regarding 121 Motor Driven Cooling Water Pump Auto Start 05000306/LER-2015-0022016-06-22022 June 2016 21 Feedwater Pump Lockout, Unit 2 Reactor Trip Due to Pressure Switch Failure, LER 15-002-01 for Prairie Island, Unit, Regarding 21 Feedwater Pump Lockout, Reactor Trip Due to Pressure Switch Failure 05000282/LER-2016-0042016-06-21021 June 2016 1 OF 4, LER 16-004-00 for Prairie Island, Unit 1, Regarding Missing Fire Barrier Between Fire Area (FA) 59 and 85 / Fire Hazard Analysis Drawings Do Not Match Boundary Description 05000282/LER-2016-0022016-03-25025 March 2016 Listed System Actuation - Motor-Driven Cooling Water Pump Auto-Start, LER 16-002-00 for Prairie Island, Unit 1, Regarding Listed System Actuation - Motor-Driven Cooling Water Pump Auto-Start 05000306/LER-2016-0012016-02-12012 February 2016 Unit 2 Reactor Trip due to a Ground Fault resulting in a Generator Trip, LER 16-001-00 for Prairie Island, Unit 2, Regarding Reactor Trip Due to a Ground Fault Resulting in a Generator Trip L-PI-15-071, Cancellation of License Event Report (LER)50-282/2015-001-00, 14 Fan Coil Unit Leak2015-09-0303 September 2015 Cancellation of License Event Report (LER)50-282/2015-001-00, 14 Fan Coil Unit Leak L-PI-11-023, Reinstatement of Licensee Event Reports Associated with Flooding Scenarios2011-03-31031 March 2011 Reinstatement of Licensee Event Reports Associated with Flooding Scenarios L-PI-07-101, LER 07-03-001 for Prairie Island, Unit 1 Regarding Unanalyzed Condition Due to Breached Fire Barrier2008-01-25025 January 2008 LER 07-03-001 for Prairie Island, Unit 1 Regarding Unanalyzed Condition Due to Breached Fire Barrier L-PI-06-046, Cancellation of Licensee Event Report (LER) 1-05-01, Discovery of Single Failure Vulnerability of Unit 1 Safeguards Buses2006-06-0909 June 2006 Cancellation of Licensee Event Report (LER) 1-05-01, Discovery of Single Failure Vulnerability of Unit 1 Safeguards Buses 2024-09-16
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LER-2021-001, Turbine Driven Auxiliary Feedwater Pump Actuation Signal Due to Procedure Error |
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10 CFR 50.73(a)(2)(iv)(A), System Actuation |
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3062021001R00 - NRC Website |
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PRAIRIE ISLAND NUCLEAR GENERATING PLANT LICENSEE EVENT REPORT 50-306/2021-001-00
2 pages follow
Abstract
On October 3, 2021, with Prairie Island Nuclear Generating Plant (PINGP) Unit 2 in Cold Shutdown, the 22 Turbine Driven Auxiliary Feedwater (AFW) Pump received a valid actuation signal. While performing the prerequisite checklists for Surveillance Procedure (SP) 2083A Unit 2 Integrated SI Test with a Simulated Loss of Offsite Power Train A, the Train B 22 Turbine Driven Auxiliary Feedwater (AFW) Pump selector switch in the Main Control Room was placed in Shutdown Auto from Manual. This, combined with having the Non-Safety Related 4160 Volt buses 21 and 22 isolated for maintenance, completed the automatic start signal. The turbine and pump did not turn because the equipment was out of service with the steam supply valves closed.
This event is reportable under 10CFR 50.73(a)(2)(iv)(A) due to a valid Pressurized Water Reactor Auxiliary Feedwater actuation signal.
T h e r e w a s n o i m p a c t on the ability to maintain safe shutdown conditions. The system operated as designed.
The cause of this event was a latent procedure error in SP 2083A.
The corrective action was an update to the SP 2083A prerequisite checklist to place the 22 Turbine Driven AFW Pump selector switch to Manual.
EVENT DESCRIPTION
On October 3, 2021, the Prairie Island Nuclear Generating Plant (PINGP) Unit 2 was in Mode 5, Cold Shutdown, at 0 percent power with Non-Safety Related 4160 Volt buses 21 and 22 isolated for maintenance. At 1525 CDT, the 22 Turbine Driven Auxiliary Feedwater (AFW) Pump received an unplanned actuation signal while performing the prerequisite checklists of Surveillance Procedure (SP) 2083A Unit 2 Integrated SI Test with a Simulated Loss of Offsite Power Train A when the 22 Turbine Driven AFW Pump selector switch in the Main Control Room was placed in Shutdown Auto from Manual.
This event is reportable under 10CFR 50.73(a)(2)(iv)(A) due to a valid Pressurized Water Reactor Auxiliary Feedwater actuation signal, per NUREG 1022, Revision 3.
EVENT ANALYSIS
The 22 Turbine Driven AFW Pump is a part of the PINGP AFW System (EIIS CODE: BA). The AFW System automatically supplies feedwater to the steam generators (SG) to remove decay heat from the Reactor Coolant System upon the loss of normal feedwater supply. The AFW system is configured into two redundant trains. One train has a turbine driven AFW pump; the other has a motor driven AFW pump. One automatic start signal for the turbine driven AFW Pump is the loss of both non-safety related 4160 Volt buses that provide power to the Main Feedwater (MFW) pumps. A loss of power for both MFW pumps will start the turbine driven AFW pump to ensure that at least one SG contains enough water to serve as the heat sink for reactor decay heat and sensible heat removal following the reactor trip.
With Non-Safety Related 4160 Volt buses 21 and 22 isolated for maintenance, placing the 22 Turbine Driven AFW Pump selector switch in Shutdown Auto completed the automatic start signal causing the associated 22 Turbine Driven AFW Pump Steam Block Valve to open. The turbine and pump did not turn because the equipment was out of service with the steam supply valves closed. The 22 Turbine Driven AFW Pump Steam Block Valve then returned to the closed position on a Low Pump discharge pressure signal.
ASSESSMENT OF SAFETY CONSEQUENCES
The actuation signal for the 22 Turbine Driven AFW Pump did not challenge the ability to maintain safe shutdown conditions. There were no radiological, environmental, or industrial impacts associated with this event. The health and safety of the public and site personnel were not impacted during this event.
CAUSE OF THE EVENT
The cause of this event was a latent procedure error in SP 2083A from when the procedure was changed from testing both trains of the system to testing each of the trains separately.
CORRECTIVE ACTIONS
Operations updated the SP 2083A prerequisite checklist to place the 22 Turbine Driven AFW Pump selector switch to Manual.
PREVIOUS SIMILAR EVENTS
No previous similar events have occurred at PINGP in the prior 3 years.