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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000267/LER-1984-002, Final LER 84-002-01:on 840123,one of Three Bearing Water Pressure Differential Switches Found Inoperable.Caused by Dirt & Oil Accumulation on High Alarm Micro Switch.Switch Replaced1984-07-13013 July 1984 Final LER 84-002-01:on 840123,one of Three Bearing Water Pressure Differential Switches Found Inoperable.Caused by Dirt & Oil Accumulation on High Alarm Micro Switch.Switch Replaced 05000267/LER-1982-048, Final LER 82-048/03X-1:on 821207,primary Coolant to Purification Cooling Water Sys Leak Present in Purification Train B Helium Purification Cooler.Caused by Corrosion. Cooler Replaced1984-05-31031 May 1984 Final LER 82-048/03X-1:on 821207,primary Coolant to Purification Cooling Water Sys Leak Present in Purification Train B Helium Purification Cooler.Caused by Corrosion. Cooler Replaced 05000267/LER-1981-068, Revised LER 81-068/03X-2:on 811024,during Plant Temp Fluctuation Testing,Loop 2 Steam Generator Interspace Leakage Exceeded Tech Spec Limits.Caused by Inadequate Tech Specs.Tech Specs Revised1984-03-28028 March 1984 Revised LER 81-068/03X-2:on 811024,during Plant Temp Fluctuation Testing,Loop 2 Steam Generator Interspace Leakage Exceeded Tech Spec Limits.Caused by Inadequate Tech Specs.Tech Specs Revised 05000267/LER-1980-030, Revised LER 80-030/03X-3:on 800604,during Normal Operation, Loop 2 Steam Generator Penetration Leakage Greater than Tech Spec Limits.Caused by Inadequate Tech Specs.Tech Specs Modified1984-03-28028 March 1984 Revised LER 80-030/03X-3:on 800604,during Normal Operation, Loop 2 Steam Generator Penetration Leakage Greater than Tech Spec Limits.Caused by Inadequate Tech Specs.Tech Specs Modified 05000267/LER-1982-052, Revised LER 82-052/03L-1:during 821229-830111,eight Class I Hydraulic Shock Suppressors Found Inoperable.Caused by Improper Reservoir Orientation or Lack of Oil Due to Pipe Movement.Snubbers Rebuilt,Tested & Reinstalled or Repl1983-02-0707 February 1983 Revised LER 82-052/03L-1:during 821229-830111,eight Class I Hydraulic Shock Suppressors Found Inoperable.Caused by Improper Reservoir Orientation or Lack of Oil Due to Pipe Movement.Snubbers Rebuilt,Tested & Reinstalled or Replaced ML20064H8421978-12-20020 December 1978 /03X-1 on 781204:ITT Barton Model 289 Helium Circulation Seal Malfunction Pressure Differential Swithches Failed to Activate at Trippoint Due to Dirt Accumulation in Switches.Trip Settings Being Checked on Monthly Basis ML20064H4341978-12-14014 December 1978 /03L-0 on 781114:4 of 6 High Pwr Rod W/Drawal Prohibit Trip Points Were Set Too High.Accepted Test Procedure Voltage Range Permitted RWP to Be Set Higher than Tech Specs Allow ML20064G7311978-12-0707 December 1978 /03X-1 on 781107:malfunctions in 1A,1C & 1D Circulator Speed Measurement Caused Loss of High Speed Circulator Signals on Different Dates,Due to Elec Circuit Unbalance & Signal Cable Resistance Change in Modifiers ML20064G7451978-12-0606 December 1978 /03X-3 on 781009:primary Coolant Oxidant Concentration Exceeded 10vpm W/Core Average Outlet Temp Greater than 1200 Degrees F.Caused by Accumulation of Water in Pcrv Insulation ML20064G7091978-12-0606 December 1978 /03L-0 on 781107:during Normal Oper a Release of Reactor Bldg Sump Effluent Req Cooling Tower Blowdown Flow to Increase Above Normal Rate to 4.39 Million Gallons for the Day,Due to Need to Dilute Sump Effluent Discharge ML20064F1981978-11-22022 November 1978 /03L-0 on 781027:during Routing Surveillance of Steam Pipe Rupture Detection Sys,One of Three Bistables for High Temperature Under Pcrv Did Not Trip,Due to Corroded Cable Terminal Board at Junction Box ML20064F1411978-11-22022 November 1978 /03X-1 on 780510:while Oper at 40% Pwr,Moisture Concentrations in Pcrv Exceeded Limits of 4.2.11.Moisture Was Introduced During Previous Loop 1 Shutdown & Collected in Pcrv Insulation ML20069A0501978-10-24024 October 1978 /03L-0 on 780925:during Routine testing,1 of 5 Heating Ventilation & Air Conditioning Sys Isolation Dampers for 480 Volt Switchgear Room Would Not Shut,Due to Faulty O-ring in Damper Jamming Open Actuating Shaft ML20085M5791978-05-26026 May 1978 Updated LER 75/021A:on 751124,during Preventive Maint Check, Number of Reactor Bldg Pressure Relief Louvers Did Not Function as Required.Caused by Normal Outside Ambient Conditions.Preventive Maint Program Initiated 05000267/LER-1976-024, Update 1 to LER 76-024:on 760726,circulator 1C Tripped on Buffer Upset Following Discharge Valve Opening During Helium Recirculator Return to Svc.Caused by Buffer Differential Pressure Exceeding Trip Point1977-07-13013 July 1977 Update 1 to LER 76-024:on 760726,circulator 1C Tripped on Buffer Upset Following Discharge Valve Opening During Helium Recirculator Return to Svc.Caused by Buffer Differential Pressure Exceeding Trip Point 05000267/LER-1977-002, Updated LER 77-002A:on 761227,during Electrohydraulic Control Hydraulic Pump Test,Main Turbine Tripped.Trip Caused Loss of Power to Helium Circulator Bearing Water Pumps. Caused by Pump Control Malfunction1977-04-20020 April 1977 Updated LER 77-002A:on 761227,during Electrohydraulic Control Hydraulic Pump Test,Main Turbine Tripped.Trip Caused Loss of Power to Helium Circulator Bearing Water Pumps. Caused by Pump Control Malfunction ML20085L6091977-01-22022 January 1977 LER 76/010B:on 760917,during Power Ascension Tests,High Heat Load Revealed for Region 29.Caused by Hot Helium Entering Control Rod Drive to Liner Annulus.Control Rod Drive Changed Out ML20085M5251976-10-14014 October 1976 LER 75/016A:on 751009,failure of Control Sys for Circulator High Pressure Separator C Resulted in Flooding of High Pressure Separator.Caused by Main Drain Controller Lockup. Low Selector Disassembled & Cleaned ML20085M7361976-09-0303 September 1976 LER 75/014A:on 750530,while Setting Electrical Overspeed Trip,Engine B of a Diesel Generator Oversped to 1,900 Rpm. Caused by Procedural Error.Test Procedure Changed ML20085L6191976-08-0909 August 1976 LER 75/007A:on 750428,temporary Cables Not Separated from Permanent Cables & Color Coding Not Followed.Cause Not Stated 05000267/LER-1976-010, Handwritten LER 76-010A:on 760503,helium Circulators 1A & 1B Tripped.Caused by Bearing Water Pump Trip Due to Decreased Bearing Water Surge Tank Loop 1 Water Level. Appropriate Procedure Changes Implemented1976-06-26026 June 1976 Handwritten LER 76-010A:on 760503,helium Circulators 1A & 1B Tripped.Caused by Bearing Water Pump Trip Due to Decreased Bearing Water Surge Tank Loop 1 Water Level. Appropriate Procedure Changes Implemented ML20085L6911976-06-21021 June 1976 LER 75/005A:on 750323,returning Backup Bearing Water to Svc Caused buffer-mid-buffer Upset,Tripping Two Circulators. Caused by Response of Pressure & Level Controllers Associated W/Backup Bearing Water.Sys Revised 05000267/LER-1976-013, Handwritten LER 76-013:on 760607,circulators Tripped Due to Trouble Shooting.Caused by Pulled Module Interlock Circulator Isolation Relays.Modules inserted.W/760617 Ltr1976-06-17017 June 1976 Handwritten LER 76-013:on 760607,circulators Tripped Due to Trouble Shooting.Caused by Pulled Module Interlock Circulator Isolation Relays.Modules inserted.W/760617 Ltr ML20085M5011976-06-11011 June 1976 LER 75/022A:on 751223,restart of Primary Coolant Helium Circulator 1 Following Failure of Common Portion of Circulator Gas Buffer Sys Found to Be Jeopardized by Inability to Retract Circulator Static Seal 05000267/LER-1976-012, Handwritten LER 76-012:on 760527,circulator 1B Tripped. Caused by Buffer Seal Malfunction.Sys Operating Procedure for Reset Following Trip Will Be revised.W/760607 Ltr1976-06-0707 June 1976 Handwritten LER 76-012:on 760527,circulator 1B Tripped. Caused by Buffer Seal Malfunction.Sys Operating Procedure for Reset Following Trip Will Be revised.W/760607 Ltr 05000267/LER-1976-011, Handwritten LER 76-011:on 760520,helium Circulator 1C Tripped Due to Negative Buffer Differential Pressure.Caused by Concurrent Sys Complexity & Confusion Associated W/Shift Change1976-06-0101 June 1976 Handwritten LER 76-011:on 760520,helium Circulator 1C Tripped Due to Negative Buffer Differential Pressure.Caused by Concurrent Sys Complexity & Confusion Associated W/Shift Change ML20085L7461976-05-13013 May 1976 LER 75/003A:on 760209,while Opening Valve on Loop 2 Buffer Helium Recirculation,Loop 1,circulator 1B,tripped.Caused by Check Valve on Helium Supply.Spring Removed from Valve ML20085L7511976-05-13013 May 1976 LER 75/003B:on 760112,plant Instrument Bus 2 Tripped, Tripping One Circulator in Each Loop on Buffer Upset & Other Loop 2 Circulator on Loss of Bearing Water.Caused by Loss of Power.Buffer Sys Valve Failure Mode Changed ML20085M6561976-04-0505 April 1976 LER 75/017A:on 750808,instrument Air Compressor 1C Observed Running Continuously in Unloaded Condition.Caused by Component Failure.Failed Unloader Actuator Replaced W/New Identical Unloader Actuator & Tested 05000267/LER-1976-002, Suppl to LER 76-002A:on 760116,during Operation of Circulator W/Water Turbine Drives,Circulator Speed Reduced. Caused by Water Accumulation in Turbine Scroll Case. Investigation Continuing1976-04-0101 April 1976 Suppl to LER 76-002A:on 760116,during Operation of Circulator W/Water Turbine Drives,Circulator Speed Reduced. Caused by Water Accumulation in Turbine Scroll Case. Investigation Continuing ML20085M4231976-03-0101 March 1976 LER 76/002:on 760201,during Cable Dressing,Battery Charger Input Breaker Tripped.Power Cable Insulation Cut by Conduit Shorting Cable to Ground.Temporary Junction Box & Terminal Installed ML20085M4261976-02-23023 February 1976 LER 76/005:on 760207,during Cold Shutdown,Essential 480-volt Bus 2 Tripped,Causing Trip of Three Circulators.Caused by Electrician Carelessness.Electricians Reminded to Be More Careful ML20085M4451976-02-13013 February 1976 LER 76/004:on760206,during Weekly Surveillance on 1A Standby generator,1B Engine Partially Declutched Under Load.Caused by Clutch Engaging Pressure Not within Acceptable Tolerance ML20085M4571976-02-13013 February 1976 LER 76/003:on 760206,during Weekly Surveillance Test on 1B Standby Generator Set,Output Breaker Would Not Close.Caused by Store Energy Arm Shaft Keeper & Arm Falling Off,Reducing Spring Force to Below Requirements ML20085M4861976-02-13013 February 1976 LER 76/001:on 760113,during Shutdown,Inverter Supplying Noninterruptible Bus Failed.Backup Transformers Put Into Svc.Caused by Blown 150-amp Fuse.No Cause Could Be Found. Inverter Returned to Svc ML20085M5041976-01-22022 January 1976 LER 75/022:on 751223,restart of Primary Coolant Helium Circulator 1 Following Failure of Common Portion of Circulator Gas Buffer Sys Found to Be Jeopardized by Inability to Retract Circulator Static Seal ML20085M4931976-01-15015 January 1976 LER 76/001:on 760105,mod Made to Certain Hydraulic Oil Sys Relief Valves W/O Proper Prior Approval.Caused by Misunderstanding by Personnel Performing Work.Review of Rules Held W/Working Foremen ML20085M5601975-12-31031 December 1975 LER 75/025:on 751114,during Cold Shutdown,Helium Circulator C-2103 Tripped.Caused by Loop 2 Bearing Water Sys Perturbation.No Explanation Found.Circulator Restarted & Continued to Self Turbine ML20085M4911975-12-23023 December 1975 LER 75/021:on 751124,during Shutdown & Monthly Surveillance on Reactor Bldg louvers,66 of 94 Louvers Were Sluggish or Did Not Fully Open.Due to Slightly Negative Pressure on One Side of Louvers & Hinges Collecting Dust/Water 1984-07-13
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20196G6731997-07-0101 July 1997 Informs Commission That Decommissioning Process Has Been Completed at PSC of Colorado Fsvngs,Unit 1 Located in Town of Platteville in Weld County,Co ML20141K9961997-05-0505 May 1997 Safety Evaluation Supporting Amend 89 to License DPR-34 ML20140E1121997-04-10010 April 1997 Confirmatory Survey of Group Effluent Discharge Pathway Areas for Fsv Nuclear Station,Platteville,Co ML20134D1661997-01-30030 January 1997 Rev 1,Vol 6 to Final Survey Rept,Final Survey of Group E (Book 2A of 2) ML20137S6111996-12-31031 December 1996 Annual Rept Pursuant to Section 13 or 15(d) of Securities Exchange Act 1934, for Fy Ended Dec 1996 ML20134G6401996-10-29029 October 1996 Rev 0,Volume 6,Books 1 & 2 of 2 to Final Survey of Group E ML20134G6171996-10-29029 October 1996 Rev 2,Volume 1,Books 1 & 2 of 2 to Final Survey Description & Results ML20134G7271996-10-29029 October 1996 Rev 0,Volume 11,Book 1 of 1 to Final Survey of Group J ML20134G6861996-10-29029 October 1996 Rev 0,Volume 8,Books 1 & 2 of 2 to, Final Survey of Group G ML20134G6321996-10-26026 October 1996 Rev 1,Volume 5,Books 2 & 3 of 3 to Final Survey of Group D ML20133D7831996-10-22022 October 1996 Preliminary Rept - Orise Support of NRC License Insp at Fsv on 960930-1003 ML20116A4661996-07-19019 July 1996 Fsv Final Survey Exposure Rate Measurements ML20112J6861996-05-31031 May 1996 June 1996 Quarterly 10CFR50.59 Rept of Changes,Tests & Experiments for Fsv Decommissioning.Rept Covers Period of 960216-0531 ML20112C1531996-05-17017 May 1996 Fsv Final Survey Exposure Rate Measurements ML20101G5521996-03-21021 March 1996 Confirmatory Survey Activities for Fsv Nuclear Station PSC Platteville,Co, Final Rept ML20097E3201996-01-31031 January 1996 Nonproprietary Fort St Vrain Technical Basis Documents for Piping Survey Instrumentation ML20095K4131995-12-26026 December 1995 Rev 3 to Decommissioning Plan ML20095H7211995-12-20020 December 1995 Revs to Fort St Vrain Decommissioning Fire Protection Plan Update ML20095K9751995-12-15015 December 1995 Fort St Vrain Project Update Presentation to NRC, on 951207 & 15 ML20096C1671995-12-13013 December 1995 Rev 4 to Decommissioning Fire Protection Plan ML20094M1651995-11-30030 November 1995 Nonproprietary Fsv Technical Basis Documents for Piping Survey Implementation ML20092F3461995-09-14014 September 1995 Quarterly 10CFR50.59 Rept of Changes,Tests & Experiments for Fsv Decommissioning, Covering Period of 950516-0815.W/ ML20137H3531994-12-31031 December 1994 Partially Withheld, Rept of Independent Counsel Investigation Concerning Issues at Fort St Vrain Nuclear Generating Station Decommissioning Project, App D,Comments by Mkf & Westinghouse Team & Responses ML20137S2331994-12-31031 December 1994 Rept of Independent Counsel Investigation Concerning Issues at Fort St Vrain Nuclear Generating Station Decommissioning Project, Dec 1994 ML20029C6031993-12-31031 December 1993 1993 Annual Rept Public Svc Co of Colorado. W/940405 Ltr ML20058Q3791993-12-21021 December 1993 Rev 1 to Decommissioning Plan for Fort St Vrain Nuclear Generating Station ML20045B3641993-06-30030 June 1993 June 1993 Quarterly 10CFR50.59 Rept of Changes,Tests & Experiments for Fsv Decommissioning. ML20045A4291993-06-0303 June 1993 LER 93-003-00:on 930505,new Source of Natural Gas Introduced within 0.5 Miles of ISFSI & Reactor Bldg W/O Prior NRC Approval.Caused by Field Routing of Natural Gas Pipe.Well Isolated by Well operator.W/930603 Ltr ML20077D1631993-05-10010 May 1993 Enforcement Conference, in Arlington,Tx ML20125C7161992-12-0707 December 1992 Part 21 Rept Re Possibility for Malfunction of Declutching Mechanisms in SMB/SB-000 & SMB/SB/SBD-00 Actuators. Malfunction Only Occurs During Seismic Event.Balanced Levers May Be Purchased from Vendor.List of Affected Utils Encl ML20128D7191992-12-0101 December 1992 Safety Evaluation Approving Exemption from Requirement of 10CFR50.54(q) to Change to Biennial Emergency Plan Exercise Rather than Annual Following Completion of Next Scheduled Exercise at Plant ML20127P5861992-11-23023 November 1992 Followup to 921005 Part 21 Rept Re Potential Defect in SB/SBD-1 Housing Cover Screws.Procedure Re Replacement of SBD-1 Spring Cover Bolts Encl.All Fasteners Should Be Loosened & Removed.List of Affected Utils Encl ML20127F5691992-11-0303 November 1992 Informs Commission of Intent to Issue Order Approving Plant Decommissioning Plan & Corresponding Amend to License DPR-34 ML20101E5761992-05-31031 May 1992 Monthly Defueling Operations Rept for May 1992 for Fort St Vrain ML20096E8221992-04-30030 April 1992 Monthly Operating Rept for Apr 1992 for Fort St Vrain.W/ ML20095E9601992-04-17017 April 1992 Rev to Fort St Vrain Proposed Decommissioning Plan ML20100R7431992-03-31031 March 1992 Monthly Operating Rept for Mar 1992 for Fort St Vrain.W/ ML20090L0621992-02-29029 February 1992 Monthly Operating Rept for Feb 1992 for Fort St Vrain Unit 1 ML20092D0081992-01-31031 January 1992 Monthly Operating Rept for Jan 1992 for Fort St Vrain Nuclear Generating Station ML20102B2241992-01-22022 January 1992 Fort St Vrain Station Annual Rept of Changes,Tests & Experiments Not Requiring Prior Commission Approval Per 10CFR50.59, for Period 910123-920122 ML20094N6701991-12-31031 December 1991 Public Svc Co Annual Financial Rept for 1991 ML20091J6251991-12-31031 December 1991 Monthly Operating Rept for Dec 1991 for Fort St Vrain.W/ ML20094D6711991-11-30030 November 1991 Monthly Operating Rept for Nov 1991 for Fort St Vrain Unit 1 ML20090M1871991-11-20020 November 1991 FOSAVEX-91 Scenario for 1991 Plant Exercise of Defueling Emergency Response Plan ML20086D6891991-11-15015 November 1991 Proposed Decommissioning Plan for Fort St Vrain Nuclear Generating Station ML20085N1451991-11-0505 November 1991 Revised Ro:Operability Date of 910830 for Electric Motor Driven Fire Water Pump P-4501 Not Met.Pump Not Actually Declared Operable Until 911025.Caused by Unforseen Matl & Testing Problems.Equivalent Pump Available ML20086C5451991-10-31031 October 1991 Monthly Operating Rept for Oct 1991 for Fort St Vrain.W/ ML20085H6611991-10-10010 October 1991 Assessment of Mgt Modes for Graphite from Reactor Decommissioning ML20091D7671991-10-0101 October 1991 Rev B to Engineering Evaluation of Prestressed Concrete Reactor Vessel & Core Support Floor Structures for Proposed Sys 46 Temp Change ML20085D9861991-09-30030 September 1991 Monthly Operating Rept for Sept 1991 for Fort St Vrain.W/ 1997-07-01
[Table view] |
LER-2080-030, Revised LER 80-030/03X-3:on 800604,during Normal Operation, Loop 2 Steam Generator Penetration Leakage Greater than Tech Spec Limits.Caused by Inadequate Tech Specs.Tech Specs Modified |
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U.S. NUCLEAH HEGULA10HY COMMISSION NRC FORM 366 n.rn -
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10121 I On June 4.1980. durina nonnal oower operation while nerforming SR 5.2.16a-m. Loop 2 I steam generator penetration leakage appeared to be greater than 400 pounds per day. l o 3
. o A i Further testing revealed' the leakage was internal to thb steam generator and not I o s I through the seals. Leakage was greater than 700 pounds per day on several occasions I oe I during February and March,1981, and resulted in a plant shutdown on March 22, 1981, I
) o 7 l for further investigation. These events were reported as operation in a degraded I 1o#a 1 mode of LCO 4.2.9 per Fort St. Vrain Technical Specification AC 7.5.2(b)2. No affectc0I 7 seonpuDl1Cggthorspety. g similar reportable oCCurrenceg. sueCODE sueCODE CODE CODE sV8 CODE COMPONENT CODE o e I HI RI@ [2,j@ [,Z j @ l HI Tl El XI Cl H 18l@ L Fj@ [Z,,J 19 20 9 10 ft 12 13
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- CAUSE DESCRIPTION AND CORRECTIVE ACTIONS 27 l 'jE I The ourified helium leakaoe is internal to the nei. ation intersnace and -occurred I Public Service l l N I between the interspace and associated cold reheat steam pipina.
l l3 1 Company Charige Notice (CN) 1436 modified the steam generator interspace to operate at I Revisions to LCO 4.2.7 and 4.2.9 i
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/( - o REPORT DATE: March 28, 1984 REPORTABLE OCCURRENCE 80-30 ISSUE 3 OCCURRENCE DATE: June 4, 1980 Page 1 of 6 FORT ST. VRAIN NUCLEAR GENERATING STATION PUBLIC SERVICE COMPANY OF COLORADO 16805 WELD COUNTY ROAD 19 1/2 PLATTEVILLE, COLORADO 80651-9298 l REPORT NO. 50-267/80-30/03-X-3 l Revised Final i
- IDENTIFICATION OF OCCURRENCE:
During performance of plant test T-147, the steam generator penetration interspace leakage appeared to be in excess of the limit allowed by LCO 4.2.9 and the variance granted by the Nuclear Regulatory Commission on June 5,1980.
This was reported as operation in a degraded mode of LCO 4.2.9 per Fort St. Vrain Technical Specification AC 7.5.2(b)2.
EVENT DESCRIPTION:
On May 28, 1980, during performance of the scheduled surveillance on PCRV leakage, Loop 2 steam generator penetration was found to have a 1eak rate of 8.23 pounds per hour or 198 pounds per day. This was well within the 400 pounds per day limit of LCO 4.2.9.
On June 4, 1980, the surveillance was again performed and indicated steam generator penetration leakage to be 17.83 pounds per hour.
This was 428 pounds per day and in excess of the LCO 4.2.9 limit of 400 pounds per day. A special. test, T-145, using a pressure decay method, was written, approved, and performed later that day and l . showed the leakage rate to be 10.74 pounds per hour or 258 pounds per
- day, within the limits of LCO 4.2.9. T-145 was a more accurate test and was used at this time to insure Technical Specification compliance. .
During performance ~of T-145, it was noted that the pressure decay j, rate did not decrease as reactor pressure was approached. This E indicated that a primary closure seal was not leaking. Further
, investigation revealed a noncondensible gas was in the hot reheat sample line. A sample was taken, analyzed, and determined to be
[. clean helium. The leakage flow path was believed to be from the
- - penetration interspace to the cold reheat piping and out of the steam l generator via the hot reheat piping (see Figure 1).
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REPORTABLE OCCURRENCE 80-30 ISSUE 3 Page 2 of 6 On June 5, 1980, T-145 was again performed and revealed a leakage rate of 10.37 pounds per hour or 249 pounds per day. A letter was sent to the Nuclear Regulatory Commission explaining the situation and requesting temporary relief from LCO 4.2.9, permitting up to 700 pounds per day instead of 400 pounds per day for the suspected internal leakage path.
The Nuclear Regulatory Commission granted the requested temporary relief, agreed to the four administrative controls proposed by Public Service Company, and added one additional administrative control.
The five administrative controls agreed to are as follows:
- 1. SR 5.3.7, Secondary Coolant Activity, be conducted once each 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> in lieu of once per week.
- 2. A pressure decay test be conducted for the Loop 2 steam generator penetration closures on a weekly basis. This pressure decay test was utiTized to determine the leakage rate. Leakage rate increases of 25% over previous values required conducting pressure decay tests daily until it was established that the leak i rate had reached an equilibrium value within the 700 pounds per day.
- 3. SR 5.2.16, PCRV Closure Leakage, be conducted once every two weeks for Loop 2 steam generator penetration closure rather than monthly as a comparison to the pressure decay tests.
' 4. Radiation process monitors for the reheat steam system will be monitored once per shift for indication of primary coolant leakage into the secondary system.
! 5. Check and record the interspace differential pressure once per
, shift to comply with LCO 4.2.7.
To collect all the required data, T-145 was expanded and renumbered
- . T-147. Both T-147 and SR 5.2.16 were performed during each power i increase, as required, and also as the leakage appeared to be somewhat dependent on power level.
The leakage was within the 700 pounds per day limit, except for three occasions during power level increases:
l:
- 1. On February 23, 1981, SR 5.2.16a-M was performed and indicated
!~ S02.4 pounds per day leakage. Test T-147 was performed as part of this surveillance and indicated the leakage to be 680.4 pounds per day. Later the same day, T-147 was again performed and indicated the leakage to be 777.6 pounds per day.
l l 2. ' On' February 25, 1981, T-147 was performed and indicated leakage of 709.7 pounds per day.
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" * - t REPORTABLEOCCURRENCE80-35 ISSUE 3 Page 3 of 6
- 3. On March 4, 1981, T-147 was performed and indicated leakage of 709.7 pounds per day.
Plant operation was changed in each of these three situations and the leakage rate was reduced to less than the 700 pound per day limit.
On March 21, 1981, at 0227 hours0.00263 days <br />0.0631 hours <br />3.753307e-4 weeks <br />8.63735e-5 months <br />, during plant testing, a turbine trip occurred. Prior to this trip, reactor power had been 69%, and the Loop 2 steam generator interspace leakage rate had been 568 pounds per day. The plant was restored to a stable condition, power increased, and the generator placed back on line at 0702 hours0.00813 days <br />0.195 hours <br />0.00116 weeks <br />2.67111e-4 months <br /> the same day. Reactor power was increased, and normal plant operation resumed during the remainder of the day shift. At 1600 hours0.0185 days <br />0.444 hours <br />0.00265 weeks <br />6.088e-4 months <br />, T-147 was performed and indicated the steam generator interspace leakage to be 1312 pounds per day at 57% reactor power.
Various changes were made to plant operations, but the steam generator interspace leakage rate remained above the 700 pounds per day limit. An orderly plant shutdown was initiated at 1832 hours0.0212 days <br />0.509 hours <br />0.00303 weeks <br />6.97076e-4 months <br /> with the turbine generator off line at 0358 hours0.00414 days <br />0.0994 hours <br />5.919312e-4 weeks <br />1.36219e-4 months <br /> on March 22, 1981, and the reactor manually scrammed from approximately 2% power at 1145 hours0.0133 days <br />0.318 hours <br />0.00189 weeks <br />4.356725e-4 months <br />. The reactor was depressurized and investigation began on the cause of the excessive steam generator Loop 2 interspace leakage.
CAUSE DESCRIPTION:
Other. ,
The purified helium leakage was internal to the Loop 2 steam generator penetration and occurred between the penetration interspace and the cold reheat steam piping internal to the penetration (see Figure 1).
l CORRECTIVE l ACTION:
l Public Service Company Change Notice (CN) 1436'was initiated in l November, 1981, and has installed instrumentation, piping, valves, and control equipment to allow operation of the steam generator
! . penetration interspaces at a pressure slightly greater than cold reheat but less than reactor pressure. Additional capability to r- monitor the interspace helium was also provided. These modifications maintain steam generator interspace helium leakage to within the limits of LCO 4.2.9.
Revisions to the Fort St. Vrain Technical Specifications, LCO 4.2.7
_and LCO 4.2.9, were proposed by Public Service Company in
! January, 1982, and approved by the Nuclear Regulatory Commission in March, 1982, as Amendment No. 26 to the Fort St. Vrain Facility
- _ Operating License DPR-34.
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REPORTABLE OCCURRENCE 80-30'~
ISSUE 3 Page 4 of 6 Amendment No. 26 revised the Technical Specifications to:
(1) permit the interspace between primary and secondary closures of the steam generator modules to be maintained at a pressure slightly above cold reheat steam pressure; and (2) set a limit on the possible release of primary coolant activity through the primary closure seals of no greater than 1.4 curies
.per day.
No further corrective action is anticipated or required.
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REPORTABLE OCCURRENCE 80-30 ISSUE 3 Page 6 of 6 Prepared By: aarA Duane L. Frye
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Frank Jif ovachek Technic (1 Services Engineering Supervisor Reviewed By: DM Weed L. M. McBride Station Manager Approved By: dW Don Warembourg Manager, Nuclear ProductTon
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