ML20085M493

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LER 76/001:on 760105,mod Made to Certain Hydraulic Oil Sys Relief Valves W/O Proper Prior Approval.Caused by Misunderstanding by Personnel Performing Work.Review of Rules Held W/Working Foremen
ML20085M493
Person / Time
Site: Fort Saint Vrain Xcel Energy icon.png
Issue date: 01/15/1976
From: Hillyard H, Swart F
PUBLIC SERVICE CO. OF COLORADO
To: Howard E
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
References
LER-76-001-01, LER-76-1-1, NUDOCS 8311080604
Download: ML20085M493 (5)


Text

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!, , LICENSEE EVENT REPORT

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January 15, 1976 ABNORMAL OCCURRENCE 76/01

.. REPORT DATE: Page 1 of 3 January 5,1976 OCCURRENCE DATE:

' FORT ST. VRAIN NUCLEAR CENERATING STATION PUBLIC SERVICE COMPANY OF COLORADO P. O. BOX 361 3

PLATTEVILLE, COLORADO 80651 REPORT No. 50-267/76/01 Final IDENTIFICATION OF OCCURRENCE:

A modification was made to certain hydraulic oil system relief valves without Since the system is Class I, this is identified as proper prior approval. Vrain Technical Specification 2.1.g.

Abnormal Occurrence No. 76/01 per Fort St.

CONDITIONS PRIOR Routine Shutdown Steady State Power TO OCCURRENCE: __

Routine Load Change Hot Shutdown Other (specify)

X Cold Shutdown Refueling Shutdown Routine Startup The major plant parameters at the time of the event were as follows:

N/A Wth RTR Power

' ELECT N/A We

. 4 N/A psig

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Secondary Coolant Pressure _

N/A 'F Temperature Flow N/A f/hr.

N/A psig Primary Coolant Pressure N/A *F Core Inlet Temperature <

N/A *F Core Outlet Flow N/A #/hr.

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ABNORMAL 0CCURRENCE 76/01 Page 2 of 3 DESCRIPTION OF OCCURRENCE:

On January 5,1976, General Atomic Company stopped work on hydraulic oil system (91) relief valve vent line changes which had been requested by Public Service Company. The changes requested involved changing the relief valve discharge vent line from one location to another. This work which had been the subject of verbal discussions among Public Service Company management, General Atomic Company supervision, was part of a two week, around-the-clock effort to complete System 91 oil-side recirculation loop modifications.

This work was stopped because the documents authorizing the oil-side recircu-lation loop modifications only provided for disconnecting the common relief valve vent line as the first step of making the relief valve vent line changes, but did not include reconnection to the part of this system which had been in-dicated in modification discussions.

APPARENT CAUSE

- 0F OCCURRENCE: Design Unusual Service Cond.

Including Environment

. Manufacture Component Failure Installation /Const. Other (specify)

Operator X Procedure ANALYSIS OF -

OCCURRENCE:

The plant configuration in existence for doing the oil-side recirculation loop work was identical to that permitting the relief valve vent line changes. No conditions in plant configuration differing from those approved,: existed. -Comple-tion of the ' relief valve vent line changes was a change of convenience, and would in no way have comprimised the safe operation of System 91, or had any

  • adverse ef fect on the health or safety of the public.

CORRECT-IVE

' ACTION:

1. Written documentation authorizing the vent line change was completed prior to resumption of the work.
2. The work force has been instructed to have specific documents in hand covering the job to be done and to perform only those portions of the work described therein, even though the job to be done is separated into various steps.

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ABNORMAL OCCURRENCE 76/01 Page 3 of 3 FAILURE DATA /SiMILAR REPORTED OCCURRENCES:

None, PROGRAMMATIC IMPACT: ,

None CODE' IMPACT :

None Submitted by: / .

H. W. Hil$ard, Jr. [

Technical Services Supervisor Reviewed by:

H. Larry Brc\i \

Superintendent, Operatibns Approved by: m fu'fm 6. .,m Fr/deric E. Swart Sdperintendent, Nuclear Production e

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, iSFIG P. O. Box 361, Platteville, Colorado 80651 January 15, 1976 Fort St. Vrain Unit No.1 P-76007

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  • Mr. E. Morris Ilovard, Director ~1 %

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Nuc1 car Regulatory Co=nission 4 [;fy'<W., e %/d Region IV Office of Inspection and Enforeccent m

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Suite 1000 Arlington, Texas 76012 7 ,,'f7'2 s

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Ref: Facility Operating License No. DP2-34 Docket No. 50-267

Dear Mr. Ecr.rard:

Enclosed please find a copy of Abnormal Occurrence Report No. 50-267/

76/01, Final, submitted per the requirements of the Technical Specifi-n tions.

Also, please find enclosed one copy of the Licensee Event Report for Abnormal occurrence Report No. 50-267/76/01.

Very truly yours, Frederic E. Svart Superintendent, Nuclear Production

! Fort St. Vrain Nuclear I

Generating Station FES/alk cc: Mr. Roger S. Boyd

. 53y COPY SENT REGION 7 ,

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