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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000267/LER-1984-002, Final LER 84-002-01:on 840123,one of Three Bearing Water Pressure Differential Switches Found Inoperable.Caused by Dirt & Oil Accumulation on High Alarm Micro Switch.Switch Replaced1984-07-13013 July 1984 Final LER 84-002-01:on 840123,one of Three Bearing Water Pressure Differential Switches Found Inoperable.Caused by Dirt & Oil Accumulation on High Alarm Micro Switch.Switch Replaced 05000267/LER-1982-048, Final LER 82-048/03X-1:on 821207,primary Coolant to Purification Cooling Water Sys Leak Present in Purification Train B Helium Purification Cooler.Caused by Corrosion. Cooler Replaced1984-05-31031 May 1984 Final LER 82-048/03X-1:on 821207,primary Coolant to Purification Cooling Water Sys Leak Present in Purification Train B Helium Purification Cooler.Caused by Corrosion. Cooler Replaced 05000267/LER-1981-068, Revised LER 81-068/03X-2:on 811024,during Plant Temp Fluctuation Testing,Loop 2 Steam Generator Interspace Leakage Exceeded Tech Spec Limits.Caused by Inadequate Tech Specs.Tech Specs Revised1984-03-28028 March 1984 Revised LER 81-068/03X-2:on 811024,during Plant Temp Fluctuation Testing,Loop 2 Steam Generator Interspace Leakage Exceeded Tech Spec Limits.Caused by Inadequate Tech Specs.Tech Specs Revised 05000267/LER-1980-030, Revised LER 80-030/03X-3:on 800604,during Normal Operation, Loop 2 Steam Generator Penetration Leakage Greater than Tech Spec Limits.Caused by Inadequate Tech Specs.Tech Specs Modified1984-03-28028 March 1984 Revised LER 80-030/03X-3:on 800604,during Normal Operation, Loop 2 Steam Generator Penetration Leakage Greater than Tech Spec Limits.Caused by Inadequate Tech Specs.Tech Specs Modified 05000267/LER-1982-052, Revised LER 82-052/03L-1:during 821229-830111,eight Class I Hydraulic Shock Suppressors Found Inoperable.Caused by Improper Reservoir Orientation or Lack of Oil Due to Pipe Movement.Snubbers Rebuilt,Tested & Reinstalled or Repl1983-02-0707 February 1983 Revised LER 82-052/03L-1:during 821229-830111,eight Class I Hydraulic Shock Suppressors Found Inoperable.Caused by Improper Reservoir Orientation or Lack of Oil Due to Pipe Movement.Snubbers Rebuilt,Tested & Reinstalled or Replaced ML20064H8421978-12-20020 December 1978 /03X-1 on 781204:ITT Barton Model 289 Helium Circulation Seal Malfunction Pressure Differential Swithches Failed to Activate at Trippoint Due to Dirt Accumulation in Switches.Trip Settings Being Checked on Monthly Basis ML20064H4341978-12-14014 December 1978 /03L-0 on 781114:4 of 6 High Pwr Rod W/Drawal Prohibit Trip Points Were Set Too High.Accepted Test Procedure Voltage Range Permitted RWP to Be Set Higher than Tech Specs Allow ML20064G7311978-12-0707 December 1978 /03X-1 on 781107:malfunctions in 1A,1C & 1D Circulator Speed Measurement Caused Loss of High Speed Circulator Signals on Different Dates,Due to Elec Circuit Unbalance & Signal Cable Resistance Change in Modifiers ML20064G7451978-12-0606 December 1978 /03X-3 on 781009:primary Coolant Oxidant Concentration Exceeded 10vpm W/Core Average Outlet Temp Greater than 1200 Degrees F.Caused by Accumulation of Water in Pcrv Insulation ML20064G7091978-12-0606 December 1978 /03L-0 on 781107:during Normal Oper a Release of Reactor Bldg Sump Effluent Req Cooling Tower Blowdown Flow to Increase Above Normal Rate to 4.39 Million Gallons for the Day,Due to Need to Dilute Sump Effluent Discharge ML20064F1981978-11-22022 November 1978 /03L-0 on 781027:during Routing Surveillance of Steam Pipe Rupture Detection Sys,One of Three Bistables for High Temperature Under Pcrv Did Not Trip,Due to Corroded Cable Terminal Board at Junction Box ML20064F1411978-11-22022 November 1978 /03X-1 on 780510:while Oper at 40% Pwr,Moisture Concentrations in Pcrv Exceeded Limits of 4.2.11.Moisture Was Introduced During Previous Loop 1 Shutdown & Collected in Pcrv Insulation ML20069A0501978-10-24024 October 1978 /03L-0 on 780925:during Routine testing,1 of 5 Heating Ventilation & Air Conditioning Sys Isolation Dampers for 480 Volt Switchgear Room Would Not Shut,Due to Faulty O-ring in Damper Jamming Open Actuating Shaft ML20085M5791978-05-26026 May 1978 Updated LER 75/021A:on 751124,during Preventive Maint Check, Number of Reactor Bldg Pressure Relief Louvers Did Not Function as Required.Caused by Normal Outside Ambient Conditions.Preventive Maint Program Initiated 05000267/LER-1976-024, Update 1 to LER 76-024:on 760726,circulator 1C Tripped on Buffer Upset Following Discharge Valve Opening During Helium Recirculator Return to Svc.Caused by Buffer Differential Pressure Exceeding Trip Point1977-07-13013 July 1977 Update 1 to LER 76-024:on 760726,circulator 1C Tripped on Buffer Upset Following Discharge Valve Opening During Helium Recirculator Return to Svc.Caused by Buffer Differential Pressure Exceeding Trip Point 05000267/LER-1977-002, Updated LER 77-002A:on 761227,during Electrohydraulic Control Hydraulic Pump Test,Main Turbine Tripped.Trip Caused Loss of Power to Helium Circulator Bearing Water Pumps. Caused by Pump Control Malfunction1977-04-20020 April 1977 Updated LER 77-002A:on 761227,during Electrohydraulic Control Hydraulic Pump Test,Main Turbine Tripped.Trip Caused Loss of Power to Helium Circulator Bearing Water Pumps. Caused by Pump Control Malfunction ML20085L6091977-01-22022 January 1977 LER 76/010B:on 760917,during Power Ascension Tests,High Heat Load Revealed for Region 29.Caused by Hot Helium Entering Control Rod Drive to Liner Annulus.Control Rod Drive Changed Out ML20085M5251976-10-14014 October 1976 LER 75/016A:on 751009,failure of Control Sys for Circulator High Pressure Separator C Resulted in Flooding of High Pressure Separator.Caused by Main Drain Controller Lockup. Low Selector Disassembled & Cleaned ML20085M7361976-09-0303 September 1976 LER 75/014A:on 750530,while Setting Electrical Overspeed Trip,Engine B of a Diesel Generator Oversped to 1,900 Rpm. Caused by Procedural Error.Test Procedure Changed ML20085L6191976-08-0909 August 1976 LER 75/007A:on 750428,temporary Cables Not Separated from Permanent Cables & Color Coding Not Followed.Cause Not Stated 05000267/LER-1976-010, Handwritten LER 76-010A:on 760503,helium Circulators 1A & 1B Tripped.Caused by Bearing Water Pump Trip Due to Decreased Bearing Water Surge Tank Loop 1 Water Level. Appropriate Procedure Changes Implemented1976-06-26026 June 1976 Handwritten LER 76-010A:on 760503,helium Circulators 1A & 1B Tripped.Caused by Bearing Water Pump Trip Due to Decreased Bearing Water Surge Tank Loop 1 Water Level. Appropriate Procedure Changes Implemented ML20085L6911976-06-21021 June 1976 LER 75/005A:on 750323,returning Backup Bearing Water to Svc Caused buffer-mid-buffer Upset,Tripping Two Circulators. Caused by Response of Pressure & Level Controllers Associated W/Backup Bearing Water.Sys Revised 05000267/LER-1976-013, Handwritten LER 76-013:on 760607,circulators Tripped Due to Trouble Shooting.Caused by Pulled Module Interlock Circulator Isolation Relays.Modules inserted.W/760617 Ltr1976-06-17017 June 1976 Handwritten LER 76-013:on 760607,circulators Tripped Due to Trouble Shooting.Caused by Pulled Module Interlock Circulator Isolation Relays.Modules inserted.W/760617 Ltr ML20085M5011976-06-11011 June 1976 LER 75/022A:on 751223,restart of Primary Coolant Helium Circulator 1 Following Failure of Common Portion of Circulator Gas Buffer Sys Found to Be Jeopardized by Inability to Retract Circulator Static Seal 05000267/LER-1976-012, Handwritten LER 76-012:on 760527,circulator 1B Tripped. Caused by Buffer Seal Malfunction.Sys Operating Procedure for Reset Following Trip Will Be revised.W/760607 Ltr1976-06-0707 June 1976 Handwritten LER 76-012:on 760527,circulator 1B Tripped. Caused by Buffer Seal Malfunction.Sys Operating Procedure for Reset Following Trip Will Be revised.W/760607 Ltr 05000267/LER-1976-011, Handwritten LER 76-011:on 760520,helium Circulator 1C Tripped Due to Negative Buffer Differential Pressure.Caused by Concurrent Sys Complexity & Confusion Associated W/Shift Change1976-06-0101 June 1976 Handwritten LER 76-011:on 760520,helium Circulator 1C Tripped Due to Negative Buffer Differential Pressure.Caused by Concurrent Sys Complexity & Confusion Associated W/Shift Change ML20085L7461976-05-13013 May 1976 LER 75/003A:on 760209,while Opening Valve on Loop 2 Buffer Helium Recirculation,Loop 1,circulator 1B,tripped.Caused by Check Valve on Helium Supply.Spring Removed from Valve ML20085L7511976-05-13013 May 1976 LER 75/003B:on 760112,plant Instrument Bus 2 Tripped, Tripping One Circulator in Each Loop on Buffer Upset & Other Loop 2 Circulator on Loss of Bearing Water.Caused by Loss of Power.Buffer Sys Valve Failure Mode Changed ML20085M6561976-04-0505 April 1976 LER 75/017A:on 750808,instrument Air Compressor 1C Observed Running Continuously in Unloaded Condition.Caused by Component Failure.Failed Unloader Actuator Replaced W/New Identical Unloader Actuator & Tested 05000267/LER-1976-002, Suppl to LER 76-002A:on 760116,during Operation of Circulator W/Water Turbine Drives,Circulator Speed Reduced. Caused by Water Accumulation in Turbine Scroll Case. Investigation Continuing1976-04-0101 April 1976 Suppl to LER 76-002A:on 760116,during Operation of Circulator W/Water Turbine Drives,Circulator Speed Reduced. Caused by Water Accumulation in Turbine Scroll Case. Investigation Continuing ML20085M4231976-03-0101 March 1976 LER 76/002:on 760201,during Cable Dressing,Battery Charger Input Breaker Tripped.Power Cable Insulation Cut by Conduit Shorting Cable to Ground.Temporary Junction Box & Terminal Installed ML20085M4261976-02-23023 February 1976 LER 76/005:on 760207,during Cold Shutdown,Essential 480-volt Bus 2 Tripped,Causing Trip of Three Circulators.Caused by Electrician Carelessness.Electricians Reminded to Be More Careful ML20085M4451976-02-13013 February 1976 LER 76/004:on760206,during Weekly Surveillance on 1A Standby generator,1B Engine Partially Declutched Under Load.Caused by Clutch Engaging Pressure Not within Acceptable Tolerance ML20085M4571976-02-13013 February 1976 LER 76/003:on 760206,during Weekly Surveillance Test on 1B Standby Generator Set,Output Breaker Would Not Close.Caused by Store Energy Arm Shaft Keeper & Arm Falling Off,Reducing Spring Force to Below Requirements ML20085M4861976-02-13013 February 1976 LER 76/001:on 760113,during Shutdown,Inverter Supplying Noninterruptible Bus Failed.Backup Transformers Put Into Svc.Caused by Blown 150-amp Fuse.No Cause Could Be Found. Inverter Returned to Svc ML20085M5041976-01-22022 January 1976 LER 75/022:on 751223,restart of Primary Coolant Helium Circulator 1 Following Failure of Common Portion of Circulator Gas Buffer Sys Found to Be Jeopardized by Inability to Retract Circulator Static Seal ML20085M4931976-01-15015 January 1976 LER 76/001:on 760105,mod Made to Certain Hydraulic Oil Sys Relief Valves W/O Proper Prior Approval.Caused by Misunderstanding by Personnel Performing Work.Review of Rules Held W/Working Foremen ML20085M5601975-12-31031 December 1975 LER 75/025:on 751114,during Cold Shutdown,Helium Circulator C-2103 Tripped.Caused by Loop 2 Bearing Water Sys Perturbation.No Explanation Found.Circulator Restarted & Continued to Self Turbine ML20085M4911975-12-23023 December 1975 LER 75/021:on 751124,during Shutdown & Monthly Surveillance on Reactor Bldg louvers,66 of 94 Louvers Were Sluggish or Did Not Fully Open.Due to Slightly Negative Pressure on One Side of Louvers & Hinges Collecting Dust/Water 1984-07-13
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20196G6731997-07-0101 July 1997 Informs Commission That Decommissioning Process Has Been Completed at PSC of Colorado Fsvngs,Unit 1 Located in Town of Platteville in Weld County,Co ML20141K9961997-05-0505 May 1997 Safety Evaluation Supporting Amend 89 to License DPR-34 ML20140E1121997-04-10010 April 1997 Confirmatory Survey of Group Effluent Discharge Pathway Areas for Fsv Nuclear Station,Platteville,Co ML20134D1661997-01-30030 January 1997 Rev 1,Vol 6 to Final Survey Rept,Final Survey of Group E (Book 2A of 2) ML20137S6111996-12-31031 December 1996 Annual Rept Pursuant to Section 13 or 15(d) of Securities Exchange Act 1934, for Fy Ended Dec 1996 ML20134G6401996-10-29029 October 1996 Rev 0,Volume 6,Books 1 & 2 of 2 to Final Survey of Group E ML20134G6171996-10-29029 October 1996 Rev 2,Volume 1,Books 1 & 2 of 2 to Final Survey Description & Results ML20134G7271996-10-29029 October 1996 Rev 0,Volume 11,Book 1 of 1 to Final Survey of Group J ML20134G6861996-10-29029 October 1996 Rev 0,Volume 8,Books 1 & 2 of 2 to, Final Survey of Group G ML20134G6321996-10-26026 October 1996 Rev 1,Volume 5,Books 2 & 3 of 3 to Final Survey of Group D ML20133D7831996-10-22022 October 1996 Preliminary Rept - Orise Support of NRC License Insp at Fsv on 960930-1003 ML20116A4661996-07-19019 July 1996 Fsv Final Survey Exposure Rate Measurements ML20112J6861996-05-31031 May 1996 June 1996 Quarterly 10CFR50.59 Rept of Changes,Tests & Experiments for Fsv Decommissioning.Rept Covers Period of 960216-0531 ML20112C1531996-05-17017 May 1996 Fsv Final Survey Exposure Rate Measurements ML20101G5521996-03-21021 March 1996 Confirmatory Survey Activities for Fsv Nuclear Station PSC Platteville,Co, Final Rept ML20097E3201996-01-31031 January 1996 Nonproprietary Fort St Vrain Technical Basis Documents for Piping Survey Instrumentation ML20095K4131995-12-26026 December 1995 Rev 3 to Decommissioning Plan ML20095H7211995-12-20020 December 1995 Revs to Fort St Vrain Decommissioning Fire Protection Plan Update ML20095K9751995-12-15015 December 1995 Fort St Vrain Project Update Presentation to NRC, on 951207 & 15 ML20096C1671995-12-13013 December 1995 Rev 4 to Decommissioning Fire Protection Plan ML20094M1651995-11-30030 November 1995 Nonproprietary Fsv Technical Basis Documents for Piping Survey Implementation ML20092F3461995-09-14014 September 1995 Quarterly 10CFR50.59 Rept of Changes,Tests & Experiments for Fsv Decommissioning, Covering Period of 950516-0815.W/ ML20137H3531994-12-31031 December 1994 Partially Withheld, Rept of Independent Counsel Investigation Concerning Issues at Fort St Vrain Nuclear Generating Station Decommissioning Project, App D,Comments by Mkf & Westinghouse Team & Responses ML20137S2331994-12-31031 December 1994 Rept of Independent Counsel Investigation Concerning Issues at Fort St Vrain Nuclear Generating Station Decommissioning Project, Dec 1994 ML20029C6031993-12-31031 December 1993 1993 Annual Rept Public Svc Co of Colorado. W/940405 Ltr ML20058Q3791993-12-21021 December 1993 Rev 1 to Decommissioning Plan for Fort St Vrain Nuclear Generating Station ML20045B3641993-06-30030 June 1993 June 1993 Quarterly 10CFR50.59 Rept of Changes,Tests & Experiments for Fsv Decommissioning. ML20045A4291993-06-0303 June 1993 LER 93-003-00:on 930505,new Source of Natural Gas Introduced within 0.5 Miles of ISFSI & Reactor Bldg W/O Prior NRC Approval.Caused by Field Routing of Natural Gas Pipe.Well Isolated by Well operator.W/930603 Ltr ML20077D1631993-05-10010 May 1993 Enforcement Conference, in Arlington,Tx ML20125C7161992-12-0707 December 1992 Part 21 Rept Re Possibility for Malfunction of Declutching Mechanisms in SMB/SB-000 & SMB/SB/SBD-00 Actuators. Malfunction Only Occurs During Seismic Event.Balanced Levers May Be Purchased from Vendor.List of Affected Utils Encl ML20128D7191992-12-0101 December 1992 Safety Evaluation Approving Exemption from Requirement of 10CFR50.54(q) to Change to Biennial Emergency Plan Exercise Rather than Annual Following Completion of Next Scheduled Exercise at Plant ML20127P5861992-11-23023 November 1992 Followup to 921005 Part 21 Rept Re Potential Defect in SB/SBD-1 Housing Cover Screws.Procedure Re Replacement of SBD-1 Spring Cover Bolts Encl.All Fasteners Should Be Loosened & Removed.List of Affected Utils Encl ML20127F5691992-11-0303 November 1992 Informs Commission of Intent to Issue Order Approving Plant Decommissioning Plan & Corresponding Amend to License DPR-34 ML20101E5761992-05-31031 May 1992 Monthly Defueling Operations Rept for May 1992 for Fort St Vrain ML20096E8221992-04-30030 April 1992 Monthly Operating Rept for Apr 1992 for Fort St Vrain.W/ ML20095E9601992-04-17017 April 1992 Rev to Fort St Vrain Proposed Decommissioning Plan ML20100R7431992-03-31031 March 1992 Monthly Operating Rept for Mar 1992 for Fort St Vrain.W/ ML20090L0621992-02-29029 February 1992 Monthly Operating Rept for Feb 1992 for Fort St Vrain Unit 1 ML20092D0081992-01-31031 January 1992 Monthly Operating Rept for Jan 1992 for Fort St Vrain Nuclear Generating Station ML20102B2241992-01-22022 January 1992 Fort St Vrain Station Annual Rept of Changes,Tests & Experiments Not Requiring Prior Commission Approval Per 10CFR50.59, for Period 910123-920122 ML20094N6701991-12-31031 December 1991 Public Svc Co Annual Financial Rept for 1991 ML20091J6251991-12-31031 December 1991 Monthly Operating Rept for Dec 1991 for Fort St Vrain.W/ ML20094D6711991-11-30030 November 1991 Monthly Operating Rept for Nov 1991 for Fort St Vrain Unit 1 ML20090M1871991-11-20020 November 1991 FOSAVEX-91 Scenario for 1991 Plant Exercise of Defueling Emergency Response Plan ML20086D6891991-11-15015 November 1991 Proposed Decommissioning Plan for Fort St Vrain Nuclear Generating Station ML20085N1451991-11-0505 November 1991 Revised Ro:Operability Date of 910830 for Electric Motor Driven Fire Water Pump P-4501 Not Met.Pump Not Actually Declared Operable Until 911025.Caused by Unforseen Matl & Testing Problems.Equivalent Pump Available ML20086C5451991-10-31031 October 1991 Monthly Operating Rept for Oct 1991 for Fort St Vrain.W/ ML20085H6611991-10-10010 October 1991 Assessment of Mgt Modes for Graphite from Reactor Decommissioning ML20091D7671991-10-0101 October 1991 Rev B to Engineering Evaluation of Prestressed Concrete Reactor Vessel & Core Support Floor Structures for Proposed Sys 46 Temp Change ML20085D9861991-09-30030 September 1991 Monthly Operating Rept for Sept 1991 for Fort St Vrain.W/ 1997-07-01
[Table view] |
Text
/ ~
O UCENSEE EVENT REPCT
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, 1 6 NAME LCENSE NUMBER PE TV O1 16101 FMI vl / l l C1 Cl-I d Cl Cl CICl-lOlOl 14l/l/121Cl 10151 7 89 14 15 25 26 30 31 32 CATEGORY TV $ RC DOCKET NUMOER EVENT DATE REPORT DATE
@ CONT l FI Ol y it I 16lS cl-l(;lf_id-lM 16l312lSl7lSI l l l l l l l 7 8 57 58 59 60 61 68 69 74 75 80 EVENT DESCRIPTION 35 l Ce h r u m Fwkon '
b e i-;,,o witb r 4 s c r.., e e. nntud ,1 1 7 89 d J 80 h I hr $+' f ~ VM i b ~ h e S V~ rtnt?k 1U$1i0h +finh?d ftGO
- f f HOD & f e' e l 7 89 80 S$ ItMMek hnOYn hv &f nn4N htGOg.jmgg,1 e pgg 't r$ f t \f1&fC02_n s he b S I) r O f M bC . l 7 89 * '\ J 80 Bs lres k t+ect h vo eJr?refn~Lert. I 7 89 80
@l 7 89 (m ~76 /o6 A 80 I
m C CE COMPONENT CCCE MANuFacTumR viOLAt1ON 83 IcIBl lei 7 89 10 11 IV Iv lx IV I xl Yi 12 '
17 LEl 43 12 ir if If I 44 47
[fjj 48 CAUSE DESCRIPTION SE l 0.USd c.ut$ res port Ce of DrtCSM ct), W /t Wd/ CD/t)f"0 //c/~S I 7 89 80 05 10 C'***FUrt-le$ d)/k b7/t t k C/1) b ettf*//'a f LY7 ld /~ $ 1/ $ f ? M b d <~ l 7 89 '
/ / 80 li@ l Ae v, ,-e wwc/ a>1) fesA el I
% PCwtR CTHER STATUS DESCOVE DISCOVERY CESCRipTON 8
7 8 9 LGJ l ol ol ci i 10 12 13 I
44 Laj 45 lv4 48 80 1
ACTIVITY CCMTENT ED CF RELEASE LOCATON OF RELEASE 8
7 8 REL[E[j 9
[f.1 10 1 M [~ CUNT CF ACTMTV 11 l
44 I /VA 45 80 I
PERSONNEL EXFOSURES NUM8ER TYPE IH Idl olo i IEl I CESCNTCN# 4 1 7 89 11 12 13 80 PERSONNEL INJURIES .
NUMBER DESC M' 3 1010101 1 N hN I 7 89 11 12 80 OFFSITE CONSEQUENCES asI//4 7 89
~j go LOSS OR DAMAGE TO FACILITY TYPE DESCRIPTON 8L?Jlu4 7 89 10 8311020344 760621 I 80 PUSUCITY PDR ADOCK 05000267 s PDR DE I /V M i 7 89 80 l ADDITIONAL FACTORS MIN 4 7 89 1
80 32 I n I-NAME: W ' 30 M 7 7 7- 2*L.C2, y
PH ,ON .. ......,
O O
. 'Ci- ,-j l
pubne service company ce cdlada P. O. Box 361, Platteville. Colorado 80651
- e. .. J 2 3 SECE 7 h y,1,I'g?ygg'7g June 21, 1976 Fort St. Vrain
- D' P-76140 Of b G 8 Mr. E. Morris Howard, Director Nuclear Regulatory Commission Region IV Office of Inspection and Enforcement Suite 1000 Arlington, Texas 76012 REF: Facility Operating License No. DPR-34 4
Docket No. 50-267 Dear Mr. Howard.
Enclosed please find a copy of Unusual Event Report No. 50-267/75/05A, Final, submitted per the requirements of the Technical Specifications.
Also, please find enclosed one copy of the Licensee Event Report for Unusual Event Report No. 50-267/75/05A.
Very truly yours,
& L ad[
Frederic E. Swart Superintendent, Nuclear Production Fort St. Vrain Nuclear Generating Station
- FES/alk cc: Mr. Roger S. Boyd gg ggEIOR d384
e .* p V
' REPORT DATE: June 21, 1976 UNUSUAL EVENT 75/05A Page 1 of 4 OCCURRENCE DATE: March 23,1975 FORT ST. VRAIN NUCLEAR CENERATING STATION PUBLIC SERVICE COMPANY OF COLORADO P. O. BOX 361 -
PLATTEVILLE, COLORADO 80651 REPORT No. 50-267/75/05A Final IDENTIFICATION OF OCCURRENCE:
A situation occurred while testing the helium circulator backup bearing water system which resulted in "A" and "B" circulators automatically tripping off and the buffer indication on "C" and "D" circulators to drop resulting in operator action to set the brake and seal.
This is identified as an Unusual Event, per Technical Specification definition AC 7.6c, paragraph 3.
7 CONDITIONS PRIOR TO OCCURRENCE: Steady State Power Routine Shutdown Hot Shutdown Routine Load Change X Cold Shutdown Other (speckfy)
Refueling Shutdown Routine Startup The major plant parameters at the time of the event were as follows:
i Power RTR 0 MWth ELECT 0 MWe Secondary Coolant Pressurb N/A psig Temperature N/A 'F Flow N/A f/hr.
Primary Coolant Pressure 85 psig Temperature N200 *F Core Inlet
%200 *F Core Outlet
- . Flow Helium circulator self- f/hr.
turbining
- s-
i : O O
^
UNUSUAL EVENT 75/05A Page 2 of 4 DESCRIPTION OF
~
OCCURRENCE:
The emergency feedwater header had been isolated via V-21453 in order to repair the pressure control for valve' PV-21105. Upon completion of this repair, pressurization of the emergency feedwater header was initiated by slowly opening the isolation valve V-21453. The following events then occurred:
- 1. Helium circulators lA and IB tripped on negative buf fer-mid-buffer differential pressure.
- 2. HV-2366-1 and HV-2366-2 changed from supplying makeup buffer gas to the helium circulators via the purified helium header, to the helium storage system. At a PCRV pressure of 85 psig helium density is barely suf ficient to place the purified helium com-pressors in service. Loss of a major helium user such as circu-lator lA and IB buffer caused the purified helium compressor to trip and the automatic controls to switch to the high pressure helium storage system.
y 3. The bearing water surge tank pressure in both loops increased to 140 psi, causing the buffer return flows to drop to 0 on the
~ remaining circulators. Circulator 1C buffer dif ferential pressure decreased to 10" negative but did not trip. Circulator ID buffer differential pressure dropped but did not go negative. The operator set the brake and seal on both of these circulators be-cause the return flow was so low. The Rix recovery compressors were then set up to vent to atmosphere in order to get the bearing water surge tank pressure down. When surge tank pressure equalled reactor vessel pressure, 1C and ID helium circulators were restarted.
. APPARENT CAUSE
,' 0F OCCURRENCE: X Design Unusual Service Cond.
Including Environment Manufacture
~
. - - Component Failure '
, Installation /Censt. Other (specify)
~
Operator ~ "
~
Procedure. ,
The increased. pressure in the surge tanks due to the water inflow displaced j- -
helium from these tanks thereby increasing the buffer helium recirculstion suction pressure. This reduced the buffer return flow from the helium circu-l~ 1ators causing them to trip on buffer-mid-buffer. ,
e Y e 9
m { '
g g/
U C UNUSUAI. EVENT 75/05A Page 3 of 4 ANALYSIS OF ~ ~' ~ '~~~ ~ ~ '
OCCURRENCE: ~ "~
It appears that PC-21105 failed to control as did PCV-2191 and PCV-2192. With these valves not operating while V-21453 was being opened, there was no con-trol of the backup bearing water flow. The large amount of flow into the bearing water surge tanks caused a displacement of the helium from the surge tanks (due to a level increase). This helium flowed backward through the eq'u alization line 'to the sucEion' of the buffer helium recirculators, which
~
caused reverse flow of the buffer return from the helium circulators. The reverse flow of buffer return caused a buffer-mid-buffer dif ferential suffici-ently nega:ive to initiate the automatic circulator trips.
The level increase would not have occurred under normal circumstances because with the normal bearing water pumps tripped and bearing water supplied from the backup bearing water system, a feedforward signal from the control system would have opened the surge tank drain valves. Under these conditions, the possibility of high rate of change in the surge tank level and the reversal of return flow from the circulators, is eliminated.
CORRECTIVE -
ACTION:
A test of the backup bearing water system was completed. This test, RT-356, was.
performed to verify that backup bearing water will function correctly and re-laced transients are repeatable. This test was performed at (1) pressures simulating the most adverse requirements for backup bearing water, and (2) at the pressure which also causes the most adverse helium buffer-mid-buffer inter-
'~~ ~
actions.
The test of (1) was performed five (5) times, by simultaneously transferring all four circulators to backup bearing water. The results of the test results show that on the most severe' transient there was a margin of 25 psid between the
~
transient and the circulator trip point. All other test results show a larger margin.
The test of (2) was performed and the results show that the cost sev'ere differ- __.
ential pressure transient on the buffer-mid-buffer decreased but remained
, positive. The trip point is -9" water dif ferential pressure. The results of 2 test RT-356 verify the operability of the backup bearing water system and con-cludes_this report.
l No further corrective action is planned or required.
\ ... --
. .... . . _ _ . - .. ._ a - .. - . ,,. -- ,
j FAILURE DATA /
SIMILAR REPORTED OCCURRENCES: - - - - - - -
Unusual Occurrence No. 50-267/75/02 reports a failure of PV-21105-1 in the backup bearing water system which occurred on April 10, 1975.
w- 9
f e .
UNUSUAL EVENT 75/05A Page 4 of 4 PROGRAMMATIC UfPACT:
None CODE D! PACT:
None Submitted by: N c t u (L % U I. M .. .
H. W.' Hillyard , Jr.
- Technical Services Supervisor -
Reviewed by: ) M ..
K.LarryBQy
- z. ... . .
.-. . .. __. ....S.
u.pe. rint.ende. n.t t ..Oper tions Approved by: as m,, .M a a,_
..FrpericE.. Swart. . .
. .m. . ._.... . _ . . . ..
. . ...S.upe r.. int _e.ndent . Nuc. l..e. ar. .P.r.o.d.u. c ti.o. n. . . ... _. ... . .
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