on the Control Room Emergency Filtration System ( CREFS) to satisfy Technical Specification (TS) 3.7.9 surveillance requirements. W-14B, Control Room Charcoal Filter Fan, was declared inoperable at 1957 CST when the fan supply breaker tripped on thermal overload. Technical Specification Action Condition (TSAC) 3.7.9.A.1, with a completion time of 7 days, was entered. During follow-up extent of condition and troubleshooting activities on the W-14A fan on February 6, it was determined that the W-14A fan would not have operated under degraded grid voltage conditions with minimum design outside air temperature. The W-14A fan was declared inoperable at 1415 hours0.0164 days <br />0.393 hours <br />0.00234 weeks <br />5.384075e-4 months <br />. With both fans inoperable, an 8-hour non-emergency Event Notification ( EN 43149) was made in accordance with 10 CFR 50.72(bX3XvXD). The overload heater element size was increased for the W-14A and W-14B fans based on design basis requirements. Follow-up testing demonstrated the system to be operable and CREFS was returned to service. A root cause evaluation ( RCE) determined that some process procedures in the areas of design-control, maintenance and margin management need improvement. Process and procedure corrective actions will be tracked via the site's corrective action program. Plant-specific probabilistic risk analysis modeling and the defined system safety function determined the event to be of very low safety significance.
U.S. NUCLEAR REGULATORY COMMISSIONNRC FORM 366AA (1-2001) FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6 PAGE (3) |
Event Description:
On February 3, 2007, surveillance testing per TS-9 was conducted on the Control Room Emergency Filtration System (CREFS)U11 per Technical Specification (TS) 3.7.9 to satisfy Surveillance Requirements (SRs) 3.7.9.1, 3.7.9.3, and 3.7.9.4. Fan W-14B, "F-16 Control Room Charcoal Filter Fan," [FAN] was declared inoperable at 1957 CST when the fan motor power supply breaker tripped on thermal overload.
Investigations into fan inoperability determined a common cause associated with supply breaker thermal overload heater element device sizing existed. Accordingly, the W-14A fan was declared inoperable at 1415 CST on February 6, 2007. One or both fans inoperable causes Units 1 and 2 to enter Technical Specification 3.7.9, "Control Room Emergency Filtration System (CREFS)," Action Condition A, "CREFS Inoperable" with a Required Action of "Restore CREFS to OPERABLE status" in a completion time of seven (7) days. Both units were in Mode 1 at 100% rated thermal power at the time of the event.
The W-14B fan motor tripped on thermal overload during operation. The outside air temperature during testing was -6 deg F, as indicated by the primary meteorological tower, and during subsequent troubleshooting the temperature was consistently at or below 0 deg F. The investigation concluded that the increased air density at these temperatures was the cause for the elevated motor current draw.
Subsequently, the W-14A fan motor overload heater element sizing was considered, and it was determined that W-14A would trip under design basis conditions. Therefore, W-14A was declared inoperable.
Event Notification 43149 was made at 1908 hours0.0221 days <br />0.53 hours <br />0.00315 weeks <br />7.25994e-4 months <br /> EST on February 6, 2007.
Event Analysis:
A Root Cause Evaluation (RCE) team was chartered to investigate the cause(s) for the CREFS inoperability. RCE01075472-01 provided the following information:
In August 2004 a CREFS low air flow event occurred which resulted in RCE000270 being conducted. An action from RCE000270 was to increase system air flow margin which was subsequently satisfied by developing modifications.
In November 2004 it was proposed to replace the W-14A and B fan motors with higher efficiency 7.5 horsepower motors to achieve the desired flow margin. In March 2006 modification 05-016 R.1 was submitted for new fan motors. Support calculation 06-038 was submitted in April 2006. An assumption in the modification concluded that temperature had a negligible effect on motor performance so no compensation for low temperature was included in the calculation. Equipment changes to the system were subsequently made in accordance with the approved modification.
On December 8, 2006, at 1812 hours0.021 days <br />0.503 hours <br />0.003 weeks <br />6.89466e-4 months <br /> during TS-9 testing, the W-14A fan overload relay tripped. Outside air temperature at the time of the event was 23 deg F. The relay was investigated and the cause of the actuation determined to be premature failure of the relay.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3) 2007� 001� 00J On January 3, 2007, TS-9 was conducted successfully. During the next scheduled TS-9 in February 2007, the W-14B fan overload relay tripped. Results of troubleshooting showed motor current averaging 9.3 amps. The overload relay should have tripped at approximately 10.3 amps given vendor instructions for ultimate trip current. The cause of the above expected current draw was determined to be increased air density at low outside air temperatures. Upon understanding the cause for the W-14B fan relay actuation, the W-14A fan was evaluated. The determination was made that W-14A was not operable.
Cause:
The root cause of the February 2007 event was that PBNP processes contain no requirement or method for ensuring overload relays trip at a value that both protects the motor and provides Technical Specification functionality under design basis conditions. A contributing cause was that there was no formal process or decision-making model in place that provided a strategy for managing identified margin (margin in this case is the difference between Technical Specification requirements and actual equipment capabilities) related issues. Another contributing factor, although not causal, was the assumption that air temperature had negligible effects on motor performance.
Corrective Action:
The overload heater elements were replaced with elements having trip current setpoints adjusted to values that considered design requirements. The previously installed FH38 overload heater elements were sized for a motor nameplate current of 8.8 amps. The overload relay with FH38 heater elements should have tripped at approximately 10.3 amps given vendor instructions for ultimate trip current. The overload relays with FH38 heater elements were replaced with FH40 elements with tripping current setpoints adjusted to between 11.5 to 12.3 amps. In accordance with the 2002 National Electric Code, Section 430.32(c), motors with a marked service factor of 1.15 or greater may have overload protection up to 140% of nameplate current. In this case, 140% of the nameplate current is 12.32 amps. Thus, the replacement elements provide adequate electrical protection while at the same time allowing operation with degraded voltage and at the -15 deg F design temperature required by the FSAR. Following the overload heater element replacements, W-14A and W-14B were tested on February 8, 2007, in accordance with TS-9. Outside air temperature was at 10 to 15 deg F as indicated by the primary meteorological tower.
Other corrective actions being tracked to completion via the site's corrective action program are:
- Creation and implementation of a design guide addressing motor overload selection and sizing.
- Revision of maintenance procedures to provide methods of setting and testing motor overload relays.
- Implement and/or revise process procedures on margin management, operational decision-making results revision and other associated decision-making processes.
Safety Significance:
The W-14A and B, "F-16 Control Room Charcoal Filter Fans," are part of the control room ventilation system used for emergency operation to maintain control room personnel radiation dose within regulatory requirements.
FACILITY NAME DOCKET NUMBER 2 LER NUMBER 6 PAGE 3 2007 001 00 I This event was of low safety significance because the system affected, CREFS, has no direct accident mitigation effect as would, for example, safety injection, containment spray or auxiliary feedwater. The accident mitigation feature the system provides is the reduction in the control room operating staffs whole-body radiation exposure, which is a long-term health effect.
Probabilistic risk assessment (PRA) engineers evaluated the event and determined that because the tripping of the control room ventilation fans cannot impact either the Core Damage Frequency (CDF) or the Large Early Release Frequency (LERF), this event had no significance with respect to the health and safety of the public. However, because the tripping of these ventilation fans could affect the radiological dose to the control room operators following a core damage accident, the likelihood of this happening was examined.
The probability of this event having a radiological impact on the control room operators was evaluated for Unit 1 operating at 100% power. The results are also applicable to Unit 2 operating at 100% power. The conclusion is that this event had a very low probability of impacting the control room operators, primarily because of the small fraction of the year when both Engineering Change (EC) 1601 (formerly modification MR 05-016) was installed and the outside air temperature was low enough to have an increased air density sufficient to cause the control room fan motor to trip on thermal overload.
The outside air temperature from PPCS for the primary meteorological tower (PPCS Point MT1TLO) was evaluated from October 6, 2006, (date of completion of EC 1601) to February 3, 2007, (date of W-14B tripping on thermal overload). For these 120 days, the outside air temperature fell below +10 deg F twelve (12) times. For each instance of these 12 occurrences, the duration of being below +10 deg F was added to 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> to obtain a conservative estimate of the time when the plant may have been susceptible to potential thermal overload of the fans at a time when the fans may have been needed in the event of an accident. The 24-hour duration is the mission time used in the PRA. From October 6, 2006, to February 3, 2007, the combination of the 24-hour mission time and the time that the outside air temperature was below +10 deg F totals approximately 18 days, which is referred to below as the "vulnerable time.
Each initiating event postulated to cause core damage for PBNP was evaluated to determine the probability of having core damage during the 18 days of vulnerable time. The sum of these probabilities totals 4.0E-6.
This value represents the probability of having an event that causes core damage during the vulnerable time.
At this point, if containment remained intact and there was not sufficient leakage, there would not be a radiological consequence of the event.
Each initiating event postulated to cause a large early release from containment for PBNP was evaluated to determine the probability of having core damage and a large early release during the 18 days of vulnerable time. The sum of these probabilities totals 1.5E-7. This value represents the probability of having an event that causes core damage and a large early release during the vulnerable time. At this point, if the release from containment were completely directed to the control room outside air intake and the control room fans tripped on thermal overload, there could be radiological consequences for the control room operators.
These probabilities are conservatively high for the following reasons:
1) For conservatism in this evaluation, the potential to trip on thermal overload was assumed to occur below +10 deg F (i.e., colder than 10 deg F above zero). The outside air temperature at the time that the W-14B fan motor tripped on thermal overload was actually below -5 deg F (i.e., colder than 5 deg F below zero). In FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3) Point Beach Nuclear Plant 05000266 YEAR reality, the trip on thermal overload would not always happen when the outside temperature was below +10 deg F.
2) Both fans were assumed to trip. No credit was taken for the operators attempting to restart the tripped fans once the temperature rose above +10 deg F.
3) For conservatism in this evaluation, the leak or release from containment was assumed to be entirely directed to the control room outside air intake. In reality, the control room operators would only be vulnerable to a release from containment a small fraction of this time because the wind would disperse the release and could even direct the entire release away from the control room due to the wind direction at the time.
The impact of having a fan trip due to a degraded grid voltage condition was also examined. There has not been a degraded voltage condition at the PBNP during its operating life. The probability of having a degraded grid condition during the four months between installation of the engineering change and when the issue was discovered was, therefore, determined to be significantly less than the fraction of that same time where a temperature less than 10 deg F occurred. The estimated likelihood of a fan trip due to low temperature impacting dose to the control room operators, therefore, bounds any impact that a degraded grid voltage condition would have had.
The very low probabilities of having a core damage accident or release from containment while the temperature was such that the control room ventilation fans were susceptible to tripping (4E-06 and 1.5E-07, respectively) concluded that the increase in risk to the health and safety of the control room operators due to this condition was insignificant. This conclusion also bounds the impact of a potential degraded grid voltage condition during the four months between installation of the mod and discovery of the issue.
This event had no personnel industrial safety implications.
However, because CREFS was unable to perform its function, it is concluded the event is a Safety System Functional Failure.
Component and System Description:
The CREFS provides a protected environment from which operators can control the unit following an uncontrolled release of radioactivity.
The CREFS consists of one emergency makeup air filtration unit, two emergency makeup fans, two recirculation fans, and the required ducts and dampers necessary to establish the required flow paths and isolation boundaries. The CREFS is an emergency system, parts of which operate during normal operations.
The air entering the control room is continuously monitored by a noble gas radiation monitor and the control room itself is continuously monitored by an area radiation monitor. One detector output above its setpoint will actuate the emergency makeup mode of operation for the CREFS.
The limiting design bases accident for the control room dose analysis is the large break Loss of Coolant Accident (LOCA).
FACILITY NAME (1)� I DOCKET NUMBER (2) LER NUMBER (6 PAGE (3) The CREFS will pressurize the control and computer rooms to at least 0.125 inches water gauge in the emergency makeup mode of operation. The CREFS role in maintaining control room habitability is discussed in the Final Safety Analysis Report (FSAR), Section 9.8.
The CREFS provides airborne radiological protection for control room personnel, as demonstrated by the limiting control room dose analysis for the design basis LOCA. Control room dose analysis assumptions are presented in the FSAR, Section 14.3.5.
Previous Occurrences:
A review of recent LERs (past three years) identified one other event reported as a condition that could have prevented fulfillment of a safety function needed to mitigate the consequences of an accident for the same system. This previous similar event contained no causal connections with the current event o LER 266/2006-001-00, Control Room Emergency Filtration System Inoperable Failed Components Identified: None.
Additional Information:
Past operability evaluations are continuing. A supplement to this report will be submitted, if appropriate, based upon the results of those evaluations.
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05000498/LER-2007-001 | Turbine-Driven Auxiliary Feedwater Pump Failed to Start During Surveillance Testing (Supplement 1) | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000315/LER-2007-001 | -f Unit 1 Automatic Reactor Trip | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000263/LER-2007-001 | | | 05000266/LER-2007-001 | | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000269/LER-2007-001 | Dual Unit Trip from Jocassee Breaker Failure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000272/LER-2007-001 | ESF Actuation of Auxiliary Feedwater Pumps in Mode 3. | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000265/LER-2007-001 | Manual Reactor Scram on Increasing Condenser Backpressure Due to a Decrease in 2A Offgas Train Efficiency | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000278/LER-2007-001 | Laboratory Analysis Identifies Safety Relief Valves and Safety Valve Set Point Deficiencies | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000249/LER-2007-001 | Unit 3 High Pressure Coolant Injection System Declared Inoperable | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000282/LER-2007-001 | | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000247/LER-2007-001 | 450 Broadway, GSB P.O. Box 249 Buchanan, N.Y. 10511-0249Entergy Tel (914) 734-6700 Fred Dacimo Site Vice President Administration February 28, 2007 Indian Point Unit No. 2 Docket No. 50-247 NL-07-013 Document Control Desk U.S. Nuclear Regulatory Commission Mail Stop O-P1-17 Washington, DC 20555-0001 Subject:L Licensee Event Report # 2007-001-00, "Technical Specification Prohibited Condition Due to Exceeding the Allowed Completion Time for an Inoperable Residual Heat Removal Pump Due to an Electrical Supply Breaker Failure" Dear Sir: Pursuant to 10 CFR 50.73(a)(1), Entergy Nuclear Operations Inc. (ENO) hereby provides Licensee Event Report (LER) 2007-001-00. The enclosed LER identifies an event where the plant was operated in a condition prohibited by Technical Specifications, which is reportable under 10 CFR 50.73(a)(2)(i)(B). This condition has been recorded in the Entergy Corrective Action Program as Condition Report CR-IP2-2007-00013. There are no commitments contained in this letter. Should you or your staff have any questions regarding this matter, please contact Mr. Patric W. Conroy, Manager, Licensing, Indian Point Energy Center at (914) 734-6668. Sincerely, -Thr red R. Dacimo ite Vice President Indian Point Energy Center E Docket No. 50-247 NL-07-013 Page 2 of 2 Attachment: LER-2007-001-00 CC: Mr. Samuel J. Collins Regional Administrator — Region I U.S. Nuclear Regulatory Commission U.S. Nuclear Regulatory Commission Resident Inspector's Office Resident Inspector Indian Point Unit 2 Mr. Paul Eddy State of New York Public Service Commission INPO Record Center NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104DEXPIRES: 06/30/2007 (6-2004) Estimated burden per response to comply with this mandatory collection request: 50 hours.DReported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F52), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internetLICENSEE EVENT REPORT (LER) e-mail to infocollects@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-l0202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection. 2. DOCKET NUMBER 1 3. PAGE1. FACILITY NAME: INDIAN POINT 2 05000-247 1 OF 4 4. TITLE: Technical Specification Prohibited Condition Due to Exceeding the Allowed Completion Time for an Inoperable Residual Heat Removal Pump Due to an Electrical Supply Breaker Failure | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ix) | 05000483/LER-2007-001 | . Single Train Inoperability in the Essential Service Water System due to Inadequate Valve Closure Setup | | 05000286/LER-2007-001 | 450 Broadway, GSB P.O. Box 249 Buchanan, N.Y. 10511-0249Entergy Tel (914) 734-6700 Fred Dacimo Site Vice President June 4, 2007 Indian Point 3 Docket No. 50-286 N L-07-052 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Mail Stop O-P1-17 Washington, D.C. 20555-0001 Subject:LLicensee Event Report # 2007-001-00, "Manual Reactor Trip Due to Decreasing Steam Generator Levels as a Result of the Loss of Feedwater Flow Caused by the Failure of 32 Main Feedwater Pump Train A Control Logic Power Supply" Dear Sir or Madam: Pursuant to 10 CFR 50.73(a)(1), Entergy Nuclear Operations Inc. (ENO) hereby provides Licensee Event Report (LER) 2007-001-00. The attached LER identifies an event where the reactor was manually tripped while critical, which is reportable under 10 CFR 50.73(a)(2)(iv)(A) . This condition has been recorded in the Entergy Corrective Action Program as Condition Report CR-IP3-2007-01775. There are no new commitments identified in this letter. Should you have any questions regarding this submittal, please contact Mr. T. R. Jones, Manager, Licensing at (914) 734-6670. Sincerely, Fred R. Dacimo Site Vice President Indian Point Energy Center cc:LMr. Samuel J Collins, Regional Administrator, NRC Region I NRC Resident Inspector's Office, Indian Point 3 Mr. Paul Eddy, New York State Public Service Commission INPO Record Center pP,c.1)-1
NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 EXPIRES: 6/30/2007 (6-2004) Estimated burden per response to comply with this mandatory collection request:D50 hours.DReportedDlessons learned areDincorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F52), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internetLICENSEE EVENT REPORT (LER) e-mail to infocollects@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection. 1. FACILITY NAME INDIAN POINT 3 2. DOCKET NUMBER 13. PAGE 05000-286 1 OFTD5 4. TITLE Manual Reactor Trip Due to Decreasing Steam Generator Levels as a Result of the Loss of Feedwater Flow Caused by the Failure of 32 Main Feedwater Pump Train A Control Logic Power Supply | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000293/LER-2007-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000306/LER-2007-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000309/LER-2007-001 | Uncompensated Degradation in a Security System | | 05000414/LER-2007-001 | Failure to Comply with Action Statement in Technical Specification (TS) 3.3.1 for Loss of a Channel of the Solid State Protection System | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000311/LER-2007-001 | Inoperability of the Chilled Water System - (21 and 22 Chillers Inoperable) | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000331/LER-2007-011 | . Undervoltage ConditiOn Resulted in the Actuation of the Emergency Diesel Generators | | 05000346/LER-2007-001 | Station Vent Radiation Monitor in Bypass due to Faulty Optical Isolation Board | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000348/LER-2007-001 | Vire President - Farley Operating Company, Inc. Po51 Office Drawer 470 Ashford, Alabarid 36312-0470 Tel 334 814 4511 Fax 334 814 4728 SOUTHERN June 22, 2007 COMPANY Energy to Serve Your World Docket Nos.: 50-348 NL-07-1231 50-364 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D. C. 20555-0001 Joseph M. Farley Nuclear Plant — Units 1 and 2
Licensee Event Report 2007-001-00
Technical Specification 3.8.1 Violation Due to
Failure of Breaker / Mechanism-Operated Cell Switch
Ladies and Gentlemen: Joseph M. Farley Nuclear Plant - Licensee Event Report (LER) No. 2007-001-00 is being submitted in accordance with 10 CFR 50.73(a)(2)(i)(B) and 10 CFR 50.73(a)(2)(v)(B). This letter contains no NRC commitments. If you have any questions, please advise. Sincerely, 7e. R. Johnson Vice President — Farley Joseph M. Farley Nuclear Plant 7388 North State Highway 95 Columbia AL 36319 JRJ/CHM Enclosure: Licensee Event Report 2007-001-00 - Unit 1 U. S. Nuclear regulatory Commission NL-07-1231 Page 2 cc:� Southern Nuclear Operating Company Mr. J. T. Gasser, Executive Vice President Mr. J. R. Johnson, Vice President — Farley Mr. D. H. Jones, Vice President — Engineering RTYPE: CFA04.054; LC # 14596 U. S. Nuclear Regulatory Commission Dr. W. D. Travers, Regional Administrator Ms. K. R. Cotton, NRR Project Manager — Farley Mr. E. L. Crowe, Senior Resident Inspector— Farley NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104 EXPIRES: 06/30/2007 (6-2004) Estimated burden per response to comply with this mandatory collection request: 50 hours. Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F52), U.S. Nudear Regulatory Commission, Washington, DC 2055570001, or by InternetLICENSEE EVENT REPORT (LER) e-mail to infocolledsanrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information(See reverse for required number of collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, thedigits/characters for each block) information collection. 1. FACILITY NAME 2. DOCKET NUMBER 3. PAGE Joseph M. Farley Nuclear Plant - Unit 1 05000 348 1 OF 4 4. TITLE Technical Specification 3.8.1 Violation Due to Failure of Breaker / Mechanism-Operated Cell (MOC) Switch | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000316/LER-2007-001 | As-Found Local Leak Rate Tests Not Performed | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000456/LER-2007-001 | Unit 1 Reactor Trip Following a 345 Kv Transmission Line Lightning Strike | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000333/LER-2007-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000254/LER-2007-001 | Quad Cities Nuclear Power Station Unit 1 05000254 1 of 3 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000389/LER-2007-001 | S, Reactor Shutdown Due to Unidentified RCS Leakage | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000255/LER-2007-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000369/LER-2007-001 | 369 5McGuire Nuclear Station Unit 1 05000 1 OF5 | | 05000335/LER-2007-001 | Mispositioned Service Air Containment Isolation Valves | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000362/LER-2007-001 | Failure to declare Emergency Diesel Generator Inoperable and enter TS Action | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000353/LER-2007-001 | Scram Discharge Volume Vent and Drain Valves Opened Due To Fuse Removal | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | 05000400/LER-2007-001 | Control Rod Shutdown Bank Anomaly Causes Entry into Technical Specification 3.0.3 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000261/LER-2007-001 | Reactor Trip Due to a Loose Wire in the Main Transformer Monitoring Circuitry | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000389/LER-2007-002 | 2B2 Reactor Coolant Pump (RCP) Seal Housing Leakage | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000255/LER-2007-002 | | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material | 05000395/LER-2007-002 | Failure to Follow Administrative Controls Results in LCO 3.6.4 Violation | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000306/LER-2007-002 | | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000440/LER-2007-002 | Shutdown Cooling Pump Trip Results in Operation Prohibited by Technical Specifications | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) | 05000414/LER-2007-002 | Technical Specification Violation Associated with Containment Valve Injection Water System | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000416/LER-2007-002 | Reactor SCRAM due to Turbine Trip caused by Loss of Condenser Vacuum | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(iv), System Actuation | 05000423/LER-2007-002 | Loss of Offsite Power Caused by Transmission System Operator While Defueled | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(iv), System Actuation | 05000311/LER-2007-002 | RReactor Trip Due to a Breach in the Condensate System | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000369/LER-2007-002 | | | 05000454/LER-2007-002 | Technical Specification Required Shutdown of Unit 1 and Unit 2 Due to an Ultimate Heat Sink Pipe Leak Common to Both Units | | 05000282/LER-2007-002 | | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | 05000315/LER-2007-002 | Failure to Declare Essential Service Water Inoperable | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000247/LER-2007-002 | Technical Specification Prohibited Condition Due to Exceeding Containment Air Temperature Limit Allowed Outage Time as a Result of Changes in Instrument Uncertainty | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000250/LER-2007-002 | Completion of Shutdown Required by Technical Specifications due to Inoperable Rod Position Indication for Two Control Rods in the Same Control Bank | 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000353/LER-2007-002 | Automatic Actuation of Main Condenser Low Vacuum Isolation Logic During Refueling Outage | 10 CFR 50.73(a)(2)(iv), System Actuation | 05000272/LER-2007-002 | MManual Reactor Trips Due to Degraded Condenser Heat Removal | 10 CFR 50.73(a)(2)(iv)(A), System Actuation |
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