2 was in Mode 1 at 100 percent power.
Event Description: On March 22, 1WL-65B CFAE sump discharge outside CIV failed the Isolation 2007, Valve Leak Rate Test Follow-up conducted during the Unit 1 end of cycle 18 refueling outage.
investigation and testing determined CIV 1WL-65B leakage exceeded acceptance criteria for total reactor building bypass leakage and was inoperable during Unit 1 Cycle 18 Operation.
(LRT) In addition, there was 88.15 hours1.736111e-4 days <br />0.00417 hours <br />2.480159e-5 weeks <br />5.7075e-6 months <br /> during the cycle when the redundant inside CIV 1WL-64A did not have an operable emergency power source; therefore, both containment isolation valves for penetration M-374 were simultaneously inoperable for that 88.15 hour1.736111e-4 days <br />0.00417 hours <br />2.480159e-5 weeks <br />5.7075e-6 months <br /> period. Since these conditions existed during a Technical Specification Mode of applicability, the event is reportable as a condition prohibited by Technical Specifications and a condition that could have prevented fulfillment of a safety function.
Safety Analysis has concluded that this condition was not significant with respect to the health and safety of the public.
Event Cause: 1WL-65B was over rotated during manual operation causing the overload clutch to slip past limit switch settings. the open and closed limit switch settings are shifted. When this occurs, Consequently, the open limit actuates later in the open direction and the closed limit switch actuates earlier in the closed direction which results in leakage past the seat. Human Error resulted in the condition going undetected when the requirement to LRT the valve following manual operation was waived.
Corrective Action: Corrective actions will place more stringent control on manual operation of Rotork operated diaphragm valves. |
BACKGROUND
Applicable Energy Industry Identification (EIIS) system and component codes are enclosed within brackets. McGuire unique system and component identifiers are contained within parentheses.
Containment Floor and Equipment (CFAE) sump discharge containment isolation valve [WD] (WL):
The Unit 1 CFAE sump discharge containment isolation valve, 1WL-65B, is part of the Liquid Waste System [WD] (WL). 1WL-65B is located on the discharge side of the CFAE sump pumps outside containment. 1WL-65B is normally closed and is remotely opened to allow pump out of the CFAE sump to the Liquid Waste system [WD] (WL) for processing. CFAE sump discharge inside Containment Isolation Valve (CIV), 1WL-64A, is normally open. Both valves are interlocked with the CFAE Sump pumps and Incore Instrumentation Sump pumps such that the pumps cannot be started unless the valves are opened, and the pumps will trip if any of these valves should close. The safety function performed by these valves is to close upon receipt of Phase "A" containment isolation signal (Engineered Safety Feature). Valves 1WL-65B and 1WL-64A are Grinnell Diaphragm valves (Duke Item # 05B-153) with Rotork electric actuators (model 11NA1-57).
Rotork actuators are vulnerable to slip the primary switch in the open direction when manually operated. For this slip to occur, the actuator is over rotated during manual operation until the over travel guide bar is against the stop on the actuator. A diaphragm valve stem backseat cannot reach the backseat of the valve bonnet therefore there is no hard stop for open travel. Because a diaphragm valve can continue past full open, once the over travel guide bar is against the actuator stop, the overload clutch will slip to prevent actuator damage. When this occurs, the open and closed limit switch settings are shifted. Consequently, the open limit actuates later in the open direction and the closed limit switch actuates earlier in the closed direction which results in leakage past the seat of the valve.
Essentially, the physical stroke length has not changed but the starting point from the open de-energized position has changed.
Containment Isolation Valve as-found Isolation Valve Leak Rate Test (LRT) are performed during end of cycle refueling outages. Individual leakage rates are not specifically part of the acceptance criteria of 10 CFR 50, Appendix J. Leakage rates exceeding individual limits only result in the containment being inoperable when leakage results in exceeding the overall acceptance criteria of 1.0 La (maximum allowable Type A leakage rate at pressure).
McGuire Technical Specification (TS) 3.6.1 - Containment:
TS specify that the containment shall be OPERABLE in MODES 1, 2, 3 and 4.
Maintaining the containment operable requires compliance with the visual examinations and leakage rate requirements of the Containment Leakage Rate Testing Program in accordance with TS Surveillance Requirement (SR) 3.6.1.1.
The TS 3.6.1.1 Bases states, "Failure to meet specific leakage limits for the air lock, secondary containment bypass leakage path, and purge valve with resilient seals (as specified in LCO 3.6.2 and LCO 3.6.3) does not invalidate the acceptability of the overall containment leakage determinations unless the specific leakage contribution to overall Type A, B, and C leakage causes one of these overall leakage limits to be exceeded.
As-left leakage prior to the first startup after performing a required Containment Leakage Rate Testing Program leakage test is required to be� 0.6 La for combined Type B and C leakage, and Type A leakage." At� 1.0 La the offsite dose consequences are bounded by the assumptions of the safety analysis.
TS 3.6.1, Condition A, require an inoperable containment to be returned to an operable status within one hour.
TS 3.6.1, Condition B, require the unit to be placed in Mode 3 within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and Mode 5 in 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br /> whenever the required action and associated completion time is not met.
McGuire Technical Specification (TS) 3.6.3 - Containment Isolation Valves:
TS 3.6.3 specify that each containment isolation valve shall be operable in Modes 1, 2, 3, and 4.
Per 3.6.3 Note 4: Enter applicable Conditions and Required Actions of LCO 3.6.1, "Containment," when isolation valve leakage results in exceeding the overall containment leakage rate acceptance criteria.
As per Condition A, if ONE containment isolation valve in a flow path that contains two isolation valves is inoperable, the affected penetration flow path shall be appropriately isolated within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />.
As per Condition B, if TWO containment isolation valves in a flow path that contains two isolation valves are inoperable, the affected penetration flow path shall be appropriately isolated within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />.
If the required action and associated completion time of Condition A or B are not met, then TS 3.6.3, Condition F, states that the respective Unit must be in Mode 3 within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> AND in Mode 5 within 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />.
TS Surveillance Requirement 3.6.3.8 requires the combined leakage rate for all reactor building bypass leakage paths is .07 La when pressurized to Pa, 14.8 psig. If reactor building bypass leakage not within limit, TS 3.6.3.D requires leakage to be restored within limit in 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />. If the required action and associated completion time are not met, then TS 3.6.3, Condition F, states that the respective Unit must be in Mode 3 within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in Mode 5 within 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />.
McGuire TS 3.8.1 AC Source-Operating TS 3.8.1 specifies that two diesel generators (DGs), capable of supplying the onsite Essential Auxiliary Power Systems, shall be operable in Modes 1, 2, 3, and 4. With one DG inoperable, required action B.2 specifies that the required feature(s) supported by the inoperable DG shall be declared inoperable when its required redundant feature(s) is inoperable. The completion time for required action, B.2 is within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> from discovering that one DG is inoperable concurrent with inoperability of redundant required feature(s).
EVENT DESCRIPTION
Note: The following timeline shows the sequence of pertinent activities that occurred between the last acceptable LRT of CIV 1WL-65B and the as-found LRT failure on March 22, 2007.
9/27/05 Local Leak Rate Testing performed and 1WL-65B meets acceptance criteria during 1EOC17 refuel outage.
10/03/05 Work order 562987 (PT 1WL-65B/Elec/Mech Inspection of Rotork Actuator) was performed on 1WL-65B. IP/0/A/3066/002D (Rotork Actuator Preventative Maintenance) directs the manual operation of 1WL-65B and it was cycled at least twice manually during the PM.
The requirement to LRT the valve following manual operation was waived.
10/14/05 Unit 1 entered startup Mode 4 at 1558 hours0.018 days <br />0.433 hours <br />0.00258 weeks <br />5.92819e-4 months <br /> 10/16/05 (WL Train B Valve Stroke Timing - Quarterly) was PT/1/A/4502/002 B performed on 1WL-65B.0 (.6)0 The stroke time was six tenths of a second different than previous recorded stroke times but within the acceptance criteria specified in the test procedure.
Unit 1 entered shutdown Mode 5 at 1904 hours0.022 days <br />0.529 hours <br />0.00315 weeks <br />7.24472e-4 months <br /> 3/10/07 3/22/07 Valve 1WL-65B failed Isolation Valve Leak Rate Test PT/1/A/4200/001 C Enclosure 13.40 (Test Sheet for Penetration M- 374) 4/20/07 It was determined that the failed LLRT on penetration M-374 resulted in exceeding the combined leakage rate for reactor building bypass leakage.
On March 22,0Containment Isolation Valve 1WL65B failed Isolation Valve 2007, Leak Rate Test PT/1/A/4200/001 C Enclosure 13.40 (Test Sheet for Penetration M-374).
Investigation revealed that the most probable cause of 1WL-65B failing its leak test was an open limit switch slip due to manual operation past the open limit. Although the exact slippage event could not be determined, a periodic valve stroke timing test performed on 10/16/05 indicated a change in the stroke time of 0.6 sec had occurred. The condition is assumed to have existed since the last successful leak rate test completed September 27, 2005. Subsequent calculations indicated the amount of slippage to be about 0.114 inches of stem travel in the closed direction which would have resulted in additional seat leakage.
The estimated leakage exceeded the combined leakage rate for reactor building bypass leakage paths (5.07 La; 9820 sccm) and the specific conditions of TS 3.6.3 D were applicable during Modes 1 through 4. The leakage rate also exceeded the combined leakage rate for penetrations and valves subject to type B and C test (5.60 La; 84,200 sccm) and Integrated Leak Rate Testing (ILRT) acceptance criteria (5.75 La; 105,000 sccm). TS 5.5.2 (Containment Leakage Rate Testing Program) specifies the acceptance criteria for leakage rates and TS 3.6.1 condition A applies whenever leakage exceeds the acceptance criteria for type'B and C test or Integrated Leak Rate Testing.
On October 14, 2005, Unit 1 entered Mode 4, which requires an operable containment system in accordance with TS Section 3.6.1 (Containment) and 3.6.3 (Containment Isolation Valves). Since the inoperability of 1WL-65B is being considered to have existed since the last successful leak test completed September 27, 2007, several TSs applied when Unit 1 entered Mode 4 and until the unit was placed in Mode 5 on March 10, 2007. The condition of the valve was not recognized and no TS required actions were taken to ensure remained in operation for a period longer than allowed by TS sections 3.6.1, 3.6.3, and 3.8.1. In addition to not meeting these required completion times, surveillance requirements 3.6.3.8 and 3.6.1.1 were not met. This condition represents an operation prohibited by Technical Specifications and is reportable per the requirements of 10 CFR 50.73 (a) (2) (i) (B).
Although individual leakage rates are not specifically part of the acceptance criteria of 10 CRF 50, Appendix J, combined leakage rates exceeding the acceptance criteria of 0.75 La result in the containment being inoperable. Therefore, Unit 1 was operated with an inoperable containment during cycle 18 and the condition is reportable per 10 CFR 50.73 (a) (2) (i) (B), "Any operation or condition which was prohibited by the plant's Technical Specifications.
For short periods of time during the cycle, the associated emergency power source was not available to the redundant CIV (1WL-64A). Unit 1 train "A" Diesel Generator (1A D/G) was removed from service 10 times for a total of 88.15 hours1.736111e-4 days <br />0.00417 hours <br />2.480159e-5 weeks <br />5.7075e-6 months <br /> during cycle 18, Mode 1 through 4. In addition to being reported as a condition prohibited by TS, this condition is also reportable per 10 CFR 50.73 (a) (2) (v) (C) as a condition that could have prevented the fulfillment of the safety function. This is because CIV 1WL-65B's normally open redundant feature, CIV 1WL-64A, would not have automatically closed assuming a loss of offsite power. Loss of offsite power is assumed concurrent with 1WL-65B's inoperability and inoperability of the 1A D/G due to planned maintenance.
CAUSAL FACTORS:
The most probable cause for LRT failure was manual operation of CIV 1WL-65B past the open limit causing the open limit switch to slip. The actuator was over rotated until the over travel guide bar was against the stop on the actuator. Once the over travel guide bar was against the actuator stop, the overload clutch slipped to prevent actuator damage. When this occurs, the open and closed limit switch settings are shifted. Consequently, the open limit actuates later in the open direction and the closed limit switch actuates earlier in the closed direction which results in leakage past the seat. Corrective actions following a previous occurrence (LER 370/2005-006) included a requirement to perform leak rate test following manual operation of containment isolation valves with Rotork operated diaphragm valves. The LRT was not performed due to human error.
The shift in valve stroke time was used to justify the extent of condition operability of similar Rotork operated diaphragm valves; however, corrective actions were not developed to identify future step changes in valve stroke time as indicators of potential failures of these valves.
The root cause was determined to be barriers that were put in place following a previous LRT failure of CIV 2WL-65B (LER 370/2005-006) were not robust enough to prevent human error from waiving a LRT requirement which resulted in the repeat condition on CIV 1WL-65B.
CORRECTIVE ACTIONS
Immediate:
1. 1WL-65B limit switches internal to the rotork actuator were adjusted followed by a successful Leak Rate Test.
Subsequent:
1. Actions were taken to evaluate the Unit 1 and 2 rotork operated diaphragm valves for extent of condition and no additional discrepancies were identified.
Planned:
1 Revise Appendix J program to perform Local Leak Rate Test (LRT) on all unit specific Rotork motor operated diaphragm valves prior to Mode 4 during refueling outages.
2 Perform Valve Stroke Timing on all unit specific Rotork motor operated diaphragm valves prior to Mode 4 during refueling outages.
3 Install positive controls (such as locks or tamper seals) to the hand/auto levers of all Rotork Actuated Diaphragm Valves after successful LRT and revise the appropriate administrative and technical procedures to control the locks and/or tamper seals.
SAFETY ANALYSIS
Based on a review of the potential consequences of excessive leakage through valve 1WL-65B, it is concluded that there is no change in the estimated Core Damage Frequency (CDF) or Large Early Release frequency (LERF) for McGuire.
The McGuire PRA categorizes containment isolation failures of less than 6 inches in diameter as small. Small containment isolation failures are not included in the LERF estimation because they have been shown to make a negligible contribution to early offsite health consequences. The WL line that 1WL-65B is in is a 4 inch line and would therefore be classified as a small containment isolation failure. The event of interest is not a complete failure of the valve but leakage beyond the allowable.
Consequently, there are no LERF implications for the excessive leakage experienced by the valve.
This pathway does not support any accident mitigation function and does not impact the core damage frequency calculation directly. Any potential contribution for diversion of containment sump inventory is judged to be negligible given that the redundant valve must fail, the sump pumps should not be running, and the small effective area of the failure would allow a very long time before the sump inventory could deplete. Based on this qualitative evaluation, there is a negligible impact on the CDF evaluation.
ADDITIONAL INFORMATION
Since 2WL-65B had a similar failure during 2E0017 (PIP M-05-1794), this failure is classified as a Recurring Event (LER 370/2005-06).
Additional actions have been identified during the root cause investigation that strengthens station programs, procedures and processes to ensure corrective actions minimize the potential of recurring events.
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05000498/LER-2007-001 | Turbine-Driven Auxiliary Feedwater Pump Failed to Start During Surveillance Testing (Supplement 1) | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000315/LER-2007-001 | -f Unit 1 Automatic Reactor Trip | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000263/LER-2007-001 | | | 05000266/LER-2007-001 | | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000269/LER-2007-001 | Dual Unit Trip from Jocassee Breaker Failure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000272/LER-2007-001 | ESF Actuation of Auxiliary Feedwater Pumps in Mode 3. | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000265/LER-2007-001 | Manual Reactor Scram on Increasing Condenser Backpressure Due to a Decrease in 2A Offgas Train Efficiency | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000278/LER-2007-001 | Laboratory Analysis Identifies Safety Relief Valves and Safety Valve Set Point Deficiencies | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000249/LER-2007-001 | Unit 3 High Pressure Coolant Injection System Declared Inoperable | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000282/LER-2007-001 | | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000247/LER-2007-001 | 450 Broadway, GSB P.O. Box 249 Buchanan, N.Y. 10511-0249Entergy Tel (914) 734-6700 Fred Dacimo Site Vice President Administration February 28, 2007 Indian Point Unit No. 2 Docket No. 50-247 NL-07-013 Document Control Desk U.S. Nuclear Regulatory Commission Mail Stop O-P1-17 Washington, DC 20555-0001 Subject:L Licensee Event Report # 2007-001-00, "Technical Specification Prohibited Condition Due to Exceeding the Allowed Completion Time for an Inoperable Residual Heat Removal Pump Due to an Electrical Supply Breaker Failure" Dear Sir: Pursuant to 10 CFR 50.73(a)(1), Entergy Nuclear Operations Inc. (ENO) hereby provides Licensee Event Report (LER) 2007-001-00. The enclosed LER identifies an event where the plant was operated in a condition prohibited by Technical Specifications, which is reportable under 10 CFR 50.73(a)(2)(i)(B). This condition has been recorded in the Entergy Corrective Action Program as Condition Report CR-IP2-2007-00013. There are no commitments contained in this letter. Should you or your staff have any questions regarding this matter, please contact Mr. Patric W. Conroy, Manager, Licensing, Indian Point Energy Center at (914) 734-6668. Sincerely, -Thr red R. Dacimo ite Vice President Indian Point Energy Center E Docket No. 50-247 NL-07-013 Page 2 of 2 Attachment: LER-2007-001-00 CC: Mr. Samuel J. Collins Regional Administrator — Region I U.S. Nuclear Regulatory Commission U.S. Nuclear Regulatory Commission Resident Inspector's Office Resident Inspector Indian Point Unit 2 Mr. Paul Eddy State of New York Public Service Commission INPO Record Center NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104DEXPIRES: 06/30/2007 (6-2004) Estimated burden per response to comply with this mandatory collection request: 50 hours.DReported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F52), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internetLICENSEE EVENT REPORT (LER) e-mail to infocollects@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-l0202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection. 2. DOCKET NUMBER 1 3. PAGE1. FACILITY NAME: INDIAN POINT 2 05000-247 1 OF 4 4. TITLE: Technical Specification Prohibited Condition Due to Exceeding the Allowed Completion Time for an Inoperable Residual Heat Removal Pump Due to an Electrical Supply Breaker Failure | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ix) | 05000483/LER-2007-001 | . Single Train Inoperability in the Essential Service Water System due to Inadequate Valve Closure Setup | | 05000286/LER-2007-001 | 450 Broadway, GSB P.O. Box 249 Buchanan, N.Y. 10511-0249Entergy Tel (914) 734-6700 Fred Dacimo Site Vice President June 4, 2007 Indian Point 3 Docket No. 50-286 N L-07-052 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Mail Stop O-P1-17 Washington, D.C. 20555-0001 Subject:LLicensee Event Report # 2007-001-00, "Manual Reactor Trip Due to Decreasing Steam Generator Levels as a Result of the Loss of Feedwater Flow Caused by the Failure of 32 Main Feedwater Pump Train A Control Logic Power Supply" Dear Sir or Madam: Pursuant to 10 CFR 50.73(a)(1), Entergy Nuclear Operations Inc. (ENO) hereby provides Licensee Event Report (LER) 2007-001-00. The attached LER identifies an event where the reactor was manually tripped while critical, which is reportable under 10 CFR 50.73(a)(2)(iv)(A) . This condition has been recorded in the Entergy Corrective Action Program as Condition Report CR-IP3-2007-01775. There are no new commitments identified in this letter. Should you have any questions regarding this submittal, please contact Mr. T. R. Jones, Manager, Licensing at (914) 734-6670. Sincerely, Fred R. Dacimo Site Vice President Indian Point Energy Center cc:LMr. Samuel J Collins, Regional Administrator, NRC Region I NRC Resident Inspector's Office, Indian Point 3 Mr. Paul Eddy, New York State Public Service Commission INPO Record Center pP,c.1)-1
NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 EXPIRES: 6/30/2007 (6-2004) Estimated burden per response to comply with this mandatory collection request:D50 hours.DReportedDlessons learned areDincorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F52), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internetLICENSEE EVENT REPORT (LER) e-mail to infocollects@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection. 1. FACILITY NAME INDIAN POINT 3 2. DOCKET NUMBER 13. PAGE 05000-286 1 OFTD5 4. TITLE Manual Reactor Trip Due to Decreasing Steam Generator Levels as a Result of the Loss of Feedwater Flow Caused by the Failure of 32 Main Feedwater Pump Train A Control Logic Power Supply | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000293/LER-2007-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000306/LER-2007-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000309/LER-2007-001 | Uncompensated Degradation in a Security System | | 05000414/LER-2007-001 | Failure to Comply with Action Statement in Technical Specification (TS) 3.3.1 for Loss of a Channel of the Solid State Protection System | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000311/LER-2007-001 | Inoperability of the Chilled Water System - (21 and 22 Chillers Inoperable) | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000331/LER-2007-011 | . Undervoltage ConditiOn Resulted in the Actuation of the Emergency Diesel Generators | | 05000346/LER-2007-001 | Station Vent Radiation Monitor in Bypass due to Faulty Optical Isolation Board | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000348/LER-2007-001 | Vire President - Farley Operating Company, Inc. Po51 Office Drawer 470 Ashford, Alabarid 36312-0470 Tel 334 814 4511 Fax 334 814 4728 SOUTHERN June 22, 2007 COMPANY Energy to Serve Your World Docket Nos.: 50-348 NL-07-1231 50-364 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D. C. 20555-0001 Joseph M. Farley Nuclear Plant — Units 1 and 2
Licensee Event Report 2007-001-00
Technical Specification 3.8.1 Violation Due to
Failure of Breaker / Mechanism-Operated Cell Switch
Ladies and Gentlemen: Joseph M. Farley Nuclear Plant - Licensee Event Report (LER) No. 2007-001-00 is being submitted in accordance with 10 CFR 50.73(a)(2)(i)(B) and 10 CFR 50.73(a)(2)(v)(B). This letter contains no NRC commitments. If you have any questions, please advise. Sincerely, 7e. R. Johnson Vice President — Farley Joseph M. Farley Nuclear Plant 7388 North State Highway 95 Columbia AL 36319 JRJ/CHM Enclosure: Licensee Event Report 2007-001-00 - Unit 1 U. S. Nuclear regulatory Commission NL-07-1231 Page 2 cc:� Southern Nuclear Operating Company Mr. J. T. Gasser, Executive Vice President Mr. J. R. Johnson, Vice President — Farley Mr. D. H. Jones, Vice President — Engineering RTYPE: CFA04.054; LC # 14596 U. S. Nuclear Regulatory Commission Dr. W. D. Travers, Regional Administrator Ms. K. R. Cotton, NRR Project Manager — Farley Mr. E. L. Crowe, Senior Resident Inspector— Farley NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104 EXPIRES: 06/30/2007 (6-2004) Estimated burden per response to comply with this mandatory collection request: 50 hours. Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F52), U.S. Nudear Regulatory Commission, Washington, DC 2055570001, or by InternetLICENSEE EVENT REPORT (LER) e-mail to infocolledsanrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information(See reverse for required number of collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, thedigits/characters for each block) information collection. 1. FACILITY NAME 2. DOCKET NUMBER 3. PAGE Joseph M. Farley Nuclear Plant - Unit 1 05000 348 1 OF 4 4. TITLE Technical Specification 3.8.1 Violation Due to Failure of Breaker / Mechanism-Operated Cell (MOC) Switch | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000316/LER-2007-001 | As-Found Local Leak Rate Tests Not Performed | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000456/LER-2007-001 | Unit 1 Reactor Trip Following a 345 Kv Transmission Line Lightning Strike | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000333/LER-2007-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000254/LER-2007-001 | Quad Cities Nuclear Power Station Unit 1 05000254 1 of 3 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000389/LER-2007-001 | S, Reactor Shutdown Due to Unidentified RCS Leakage | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000255/LER-2007-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000369/LER-2007-001 | 369 5McGuire Nuclear Station Unit 1 05000 1 OF5 | | 05000335/LER-2007-001 | Mispositioned Service Air Containment Isolation Valves | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000362/LER-2007-001 | Failure to declare Emergency Diesel Generator Inoperable and enter TS Action | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000353/LER-2007-001 | Scram Discharge Volume Vent and Drain Valves Opened Due To Fuse Removal | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | 05000400/LER-2007-001 | Control Rod Shutdown Bank Anomaly Causes Entry into Technical Specification 3.0.3 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000261/LER-2007-001 | Reactor Trip Due to a Loose Wire in the Main Transformer Monitoring Circuitry | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000389/LER-2007-002 | 2B2 Reactor Coolant Pump (RCP) Seal Housing Leakage | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000255/LER-2007-002 | | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material | 05000395/LER-2007-002 | Failure to Follow Administrative Controls Results in LCO 3.6.4 Violation | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000306/LER-2007-002 | | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000440/LER-2007-002 | Shutdown Cooling Pump Trip Results in Operation Prohibited by Technical Specifications | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) | 05000414/LER-2007-002 | Technical Specification Violation Associated with Containment Valve Injection Water System | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000416/LER-2007-002 | Reactor SCRAM due to Turbine Trip caused by Loss of Condenser Vacuum | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(iv), System Actuation | 05000423/LER-2007-002 | Loss of Offsite Power Caused by Transmission System Operator While Defueled | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(iv), System Actuation | 05000311/LER-2007-002 | RReactor Trip Due to a Breach in the Condensate System | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000369/LER-2007-002 | | | 05000454/LER-2007-002 | Technical Specification Required Shutdown of Unit 1 and Unit 2 Due to an Ultimate Heat Sink Pipe Leak Common to Both Units | | 05000282/LER-2007-002 | | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | 05000315/LER-2007-002 | Failure to Declare Essential Service Water Inoperable | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000247/LER-2007-002 | Technical Specification Prohibited Condition Due to Exceeding Containment Air Temperature Limit Allowed Outage Time as a Result of Changes in Instrument Uncertainty | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000250/LER-2007-002 | Completion of Shutdown Required by Technical Specifications due to Inoperable Rod Position Indication for Two Control Rods in the Same Control Bank | 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000353/LER-2007-002 | Automatic Actuation of Main Condenser Low Vacuum Isolation Logic During Refueling Outage | 10 CFR 50.73(a)(2)(iv), System Actuation | 05000272/LER-2007-002 | MManual Reactor Trips Due to Degraded Condenser Heat Removal | 10 CFR 50.73(a)(2)(iv)(A), System Actuation |
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