On 10/07/07 at 1629 hours0.0189 days <br />0.453 hours <br />0.00269 weeks <br />6.198345e-4 months <br />, during the End-of-Cycle 15 Refueling Outage, calibration of Containment Valve Injection Water System (CVIWS) T surge chamber 2A level transmitter 2NWLT5020 was being performed. It was observed that the transmitter's loop output began to drop steadily after the transmitter was returned to service following its calibration.
Investigation revealed that CVIWS surge chamber 2A narrow range level high pressure root isolation valve 2NWIV5020 was closed.
TInvestigation concluded that the valve was most likely closed during the End-of-Cycle 14 Refueling Outage.T This rendered the associated CVIWS train inoperable for longer, than allowed by Technical Specifications. During the time period that valve 2NWIV5020 was closed, there were two instances during which the unit was unknowingly in Technical Specification Limiting Condition for Operation 3.0.3 for a time period longer than allowed.
TThis event was determined to be inconsequential from a'plant risk perspective based on the fact that the affected containment penetrations are not considered to be likely pathways for radiation release.
T Therefore, the health and safety of the public were not adversely affected by this event. |
LER-2007-002, Technical Specification Violation Associated with Containment Valve Injection Water SystemDocket Number |
Event date: |
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Report date: |
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Reporting criterion: |
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
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4142007002R00 - NRC Website |
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BACKGROUND
This event is being reported under the following criterion:
10 CFR 50.73(a)(2)(i)(B), any operation or condition which was prohibited by the plant's Technical Specifications.
Catawba Nuclear Station Unit 2 is a Westinghouse four-loop Pressurized Water Reactor (PWR) [EIIS: RCT].
The Containment Valve Injection Water System (CVIWS) [EIIS: none] ensures a water seal to a specific class of containment isolation valves [EIIS: ISV] during a Loss of Coolant Accident (LOCA), to prevent leakage of containment atmosphere through the gate valves.
The CVIWS is designed to inject water between the two seating surfaces of double disc gate valves.used for containment isolation. The injectionrpressure is higher than containment design peak pressure during a LOCA. 'This will prevent leakage of the containment atmosphere through the gate valves, thereby reducing potential offsite dose below regulatory limits following the postulated accident.
During normal power operation, the CVIWS is in a standby mode and does not perform any function. During accident situations, the CVIWS is activated to perform its safety related function. Containment isolation valves, for systems which are not used to mitigate the consequences of an accident, will be supplied with CVIWS seal water upon receipt of a Phase A isolation signal. Containment isolation valves, for accident mitigating systems which are supplied with seal water from the CVIWS, have their seal water supplies actuated by a Containment Pressure - High-High signal.
The CVIWS consists of two independent, redundant trains; one supplying gate valves powered by the A train diesel generator and the other supplying gate valves powered by the B train diesel generator. The separation of trains prevents the possibility of both containment isolation valves not sealing due to a single failure.
Each CVIWS train consists of.a surge chamber which is filled .with water and pressurized with nitrogen. One main header exits the chamber and .splits into several headers. A solenoid valve [EIIS: FSV] is located in the main header before any of the branch headers which will open after a 60 second delay on a Phase A isolation signal. Each of the headers supplies injection water to containment isolation valves located in the same general location, and close on the same engineered safety signal. A solenoid valve is located in each header which supplies seal water to valves closing on a Containment Pressure - High- High signal. These solenoid valves open after a 60 second delay on a Containment Pressure - High-High signal. Since a Phase A isolation signal occurs before a Containment Pressure - High-High signal, the solenoid valve located in the main header will already be injecting water to containment isolation valves closing on a Phase A isolation signal. This leaves an open path to the headers supplying injection water on a Containment Pressure - High-High signal. The delay for the solenoid valves opening is to allow adequate time for the slowest gate valve to close, before water is injected into the valve seat.
Makeup water is provided from the Makeup Demineralized Water System [EIIS: KC] for testing and for adding water to the surge chamber during normal plant operation. Assured water is provided from the essential header of the Nuclear Service Water System [EIIS: BI]. This supply is assured for at least 30 days following a postulated accident. If the water level in the surge chamber drops below the low-low level or if the surge chamber nitrogen pressure drops below the low-low pressure after a Phase A isolation signal, a solenoid valve in the supply line from the Nuclear Service Water System will automatically open and remain open, assuring makeup to the CVIWS at a pressure greater than 110% of peak containment accident pressure.
Technical Specification 3.6.17 governs the CVIWS. Limiting Condition for Operation 3.6.17 requires two CVIWS trains to be operable in Modes 1, 2, 3, and 4. Condition A states that with one CVIWS train inoperable, the train must be restored to operable status within 7 days. If this is not accomplished, Condition B requires the unit to be in Mode 3 within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in Mode 5 within 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />. There is no Condition for two CVIWS trains inoperable; therefore, Limiting Condition for Operation 3.0.3 is applicable in this case.
On November 5, 2007, when this event was determined to be reportable, Unit 2 was in Mode 5 during its End of Cycle 15 Refueling Outage.
EVENT DESCRIPTION
(Certain event times are approximate.) Date/Time�Event Description 10/07/07/1629 On 10/07/07, during the End-of-Cycle 15 Refueling Outage, calibration of CVIWS surge chamber 2A level transmitter 2NWLT5020 was being performed under Work Order 01775573-01.
It was observed that the transmitter's loop output began to drop steadily after the transmitter was returned to service following its calibration. Investigation revealed that CVIWS surge chamber 2A narrow range level high pressure root isolation valve 2NWIV5020 was closed.
CAUSAL FACTORS
The cause of root isolation valve 2NWIV5020 being closed could not be determined. The transmitter loop utilizes a filled reference leg design that requires the transmitter to be reverse acting in order to indicate surge chamber level. The root isolation valve isolates the filled reference leg from the surge chamber. Since the surge chamber normally operates with a fixed nitrogen overpressure, the effect on the transmitter loop due to the root isolation valve being closed depends on when it was closed. If it were closed while the surge chamber was pressurized, the surge chamber overpressure would be trapped on the high pressure side of the transmitter. This would result in a false high reading any time the surge chamber overpressure decreased below what it was when the valve was closed and in a false low reading any time the surge chamber overpressure increased above that value. If the root isolation valve were closed while there was no overpressure on the surge chamber, the high pressure side of the transmitter would not see the overpressure when the surge chamber was pressurized.
However, the low pressure side would, which would cause the transmitter to peg high and not respond to decreasing surge chamber level as long as the overpressure was present. Based on the observed transmitter behavior, it is believed that the root isolation valve was closed while there was no overpressure on the surge chamber.� The root isolation valve requires approximately one turn to move over its full travel.�it is not considered Therefore,� plausible that the valve could have been bumped into the fully closed position.
A review of Operator Aid Computer (OAC) trends indicated that the valve was most likely closed during the End-of-Cycle 14 Refueling Outage. On the trends prior to the End-of-Cycle 14 Refueling Outage, the indicated surge chamber level did not vary more than approximately 0.1 inch. After the End-of-Cycle 14 Refueling Outage, the trend varied approximately 0.3 inch. After the valve was opened following discovery of its closed position during the End-of-Cycle 15 Refueling Outage, the trend returned to normal (approximately 0.1 inch).
Plant personnel conducted a review of work orders and work requests. No maintenance work could be ascertained that would have manipulated valve 2NWIV5020 or any of the other root isolation valves on the CVIWS surge chambers. No procedures were found that would have manipulated this valve. The only potential evolution where Operations could have procedurally manipulated this valve was investigated. It was determined to be non-credible due to the fact that this evolution would have required multiple errors to have been made coupled with multiple incorrect independent verifications.
Considerable work occurred near this valve during the End-of-Cycle 15 Refueling Outage; however, no explanation was evident as to how the valve could have been closed. Based on theavailable information, it appears likely that the valve was actually closed during the End-of-Cycle 14 Refueling Outage based on the OAC trends for the affected loop.
CORRECTIVE ACTIONS
Immediate:
1: Root isolation valve 2NWIV5020 was re-opened following its discovered closed position.
Subsequent:
1. Plant personnel conducted a review of this event to determine the cause of the valve being mispositioned. No conclusive cause of this event could be determined.
Planned:
None.
There are no NRC commitments contained in this LER.
SAFETY ANALYSIS
Had an event occurred requiring the operation of the CVIWS, given the as-found position of root isolation valve 2NWIV5020, the A train of the CVIWS could have been rendered ineffective in maintaining the required water seal to its supported containment isolation valves. As a result of the mispositioned root isolation valve, nitrogen would have been eventually injected into the supported A train containment isolation valves. During the time period for which the train was inoperable, no events occurred that would have required the operation of the CVIWS.
Except for the brief periods noted below, the B train of the CVIWS was operable and capable of supporting its respective B train containment isolation valves.
It is believed that CVIWS root isolation valve 2NWIV5020 was closed sometime during the End-of-Cycle 14 Refueling Outage. Unit 2 entered Mode 4 following the completion of the End-of-Cycle 14 Refueling Outage on 4/16/06. Unit 2 entered Mode 5 to begin the End-of-Cycle 15 Refueling Outage on 9/15/07. During the time period that Unit 2 was operating in modes where the CVIWS was required to be operable (from 4/16/06 to 9/15/07), there were fifteen documented instances where the B train of the CVIWS was also inoperable. Therefore, Unit 2 was unknowingly in TS Limiting Condition for Operation 3.0.3 during these instances. Four of the fifteen instances were "tracking only" entries for the B train of the CVIWS (i.e., the train was not functionally inoperable and still would have performed its function), but for the other eleven instances, the train was functionally inoperable. For nine of these eleven instances, the duration of time that both CVIWS trains were unknowingly inoperable ranged from approximately 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> to approximately 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> in length (i.e., the durations were within the time period allowed by TS Limiting Condition for Operation 3.0.3). The remaining two instances were as follows:
Technical Specification Action Item Log Entry C2-06-01383:
B train CVIWS inoperable for 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> and 33 minutes beginning on 5/27/06 to investigate and repair an indication problem on valve 2NW 222B Technical Specification Action Item Log Entry C2-07-00176:
B train CVIWS inoperable for 40 hours4.62963e-4 days <br />0.0111 hours <br />6.613757e-5 weeks <br />1.522e-5 months <br /> and 11 minutes beginning on 1/23/07 to replace a switch and solenoid housing 0-rings on valve 2NW 237B This event was determined to be inconsequential from a plant risk perspective. The containment isolation valves serviced by the A train of the CVIWS are located in the Component Cooling Water System, the Intermediate Head Safety Injection System, the Containment Spray System, the High Head Safety Injection System, the Nuclear Service Water System, and the Liquid Waste Recycle System. Catawba's Probabilistic Risk Analysis (PRA) screens out these system containment penetrations as potential containment isolation failures because they are not air-to-air pathways and would not constitute a probabilistically significant pathway for the release of airborne fission products. The only pathway with statistically significant relevance is the pathway from the Liquid Waste Recycle System to the Containment Ventilation Unit Condensate Drain Tank. However, at Catawba, this pathway is a small isolation failure and it is screened out from the calculation of Large Early Release Frequency (LERF) due to the small diameter piping involved. The PRA does not consider this to be a LERF pathway even if its associated containment isolation valves are open. A closed valve in this pathway that leaks because the CVIWS is inoperable still would not result in a change in LERF.
The health and safety of the public were not adversely affected by this event.
ADDITIONAL INFORMATION
Within the previous three years, there were no LER events involving the CVIWS. Therefore, this event is considered to be non-recurring.
Energy Industry Identification System (EIIS) codes are identified in the text as [EIIS: XX]. This event is not considered reportable to the Equipment Performance and Information Exchange (EPIX) program.
This event is not considered to constitute a Safety System Functional Failure. There was no release of radioactive material, radiation overexposure, or personnel injury associated with the event described in this LER.
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05000498/LER-2007-001 | Turbine-Driven Auxiliary Feedwater Pump Failed to Start During Surveillance Testing (Supplement 1) | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000315/LER-2007-001 | -f Unit 1 Automatic Reactor Trip | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000263/LER-2007-001 | | | 05000266/LER-2007-001 | | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000269/LER-2007-001 | Dual Unit Trip from Jocassee Breaker Failure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000272/LER-2007-001 | ESF Actuation of Auxiliary Feedwater Pumps in Mode 3. | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000265/LER-2007-001 | Manual Reactor Scram on Increasing Condenser Backpressure Due to a Decrease in 2A Offgas Train Efficiency | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000278/LER-2007-001 | Laboratory Analysis Identifies Safety Relief Valves and Safety Valve Set Point Deficiencies | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000249/LER-2007-001 | Unit 3 High Pressure Coolant Injection System Declared Inoperable | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000282/LER-2007-001 | | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000247/LER-2007-001 | 450 Broadway, GSB P.O. Box 249 Buchanan, N.Y. 10511-0249Entergy Tel (914) 734-6700 Fred Dacimo Site Vice President Administration February 28, 2007 Indian Point Unit No. 2 Docket No. 50-247 NL-07-013 Document Control Desk U.S. Nuclear Regulatory Commission Mail Stop O-P1-17 Washington, DC 20555-0001 Subject:L Licensee Event Report # 2007-001-00, "Technical Specification Prohibited Condition Due to Exceeding the Allowed Completion Time for an Inoperable Residual Heat Removal Pump Due to an Electrical Supply Breaker Failure" Dear Sir: Pursuant to 10 CFR 50.73(a)(1), Entergy Nuclear Operations Inc. (ENO) hereby provides Licensee Event Report (LER) 2007-001-00. The enclosed LER identifies an event where the plant was operated in a condition prohibited by Technical Specifications, which is reportable under 10 CFR 50.73(a)(2)(i)(B). This condition has been recorded in the Entergy Corrective Action Program as Condition Report CR-IP2-2007-00013. There are no commitments contained in this letter. Should you or your staff have any questions regarding this matter, please contact Mr. Patric W. Conroy, Manager, Licensing, Indian Point Energy Center at (914) 734-6668. Sincerely, -Thr red R. Dacimo ite Vice President Indian Point Energy Center E Docket No. 50-247 NL-07-013 Page 2 of 2 Attachment: LER-2007-001-00 CC: Mr. Samuel J. Collins Regional Administrator — Region I U.S. Nuclear Regulatory Commission U.S. Nuclear Regulatory Commission Resident Inspector's Office Resident Inspector Indian Point Unit 2 Mr. Paul Eddy State of New York Public Service Commission INPO Record Center NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104DEXPIRES: 06/30/2007 (6-2004) Estimated burden per response to comply with this mandatory collection request: 50 hours.DReported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F52), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internetLICENSEE EVENT REPORT (LER) e-mail to infocollects@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-l0202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection. 2. DOCKET NUMBER 1 3. PAGE1. FACILITY NAME: INDIAN POINT 2 05000-247 1 OF 4 4. TITLE: Technical Specification Prohibited Condition Due to Exceeding the Allowed Completion Time for an Inoperable Residual Heat Removal Pump Due to an Electrical Supply Breaker Failure | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ix) | 05000483/LER-2007-001 | . Single Train Inoperability in the Essential Service Water System due to Inadequate Valve Closure Setup | | 05000286/LER-2007-001 | 450 Broadway, GSB P.O. Box 249 Buchanan, N.Y. 10511-0249Entergy Tel (914) 734-6700 Fred Dacimo Site Vice President June 4, 2007 Indian Point 3 Docket No. 50-286 N L-07-052 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Mail Stop O-P1-17 Washington, D.C. 20555-0001 Subject:LLicensee Event Report # 2007-001-00, "Manual Reactor Trip Due to Decreasing Steam Generator Levels as a Result of the Loss of Feedwater Flow Caused by the Failure of 32 Main Feedwater Pump Train A Control Logic Power Supply" Dear Sir or Madam: Pursuant to 10 CFR 50.73(a)(1), Entergy Nuclear Operations Inc. (ENO) hereby provides Licensee Event Report (LER) 2007-001-00. The attached LER identifies an event where the reactor was manually tripped while critical, which is reportable under 10 CFR 50.73(a)(2)(iv)(A) . This condition has been recorded in the Entergy Corrective Action Program as Condition Report CR-IP3-2007-01775. There are no new commitments identified in this letter. Should you have any questions regarding this submittal, please contact Mr. T. R. Jones, Manager, Licensing at (914) 734-6670. Sincerely, Fred R. Dacimo Site Vice President Indian Point Energy Center cc:LMr. Samuel J Collins, Regional Administrator, NRC Region I NRC Resident Inspector's Office, Indian Point 3 Mr. Paul Eddy, New York State Public Service Commission INPO Record Center pP,c.1)-1
NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 EXPIRES: 6/30/2007 (6-2004) Estimated burden per response to comply with this mandatory collection request:D50 hours.DReportedDlessons learned areDincorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F52), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internetLICENSEE EVENT REPORT (LER) e-mail to infocollects@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection. 1. FACILITY NAME INDIAN POINT 3 2. DOCKET NUMBER 13. PAGE 05000-286 1 OFTD5 4. TITLE Manual Reactor Trip Due to Decreasing Steam Generator Levels as a Result of the Loss of Feedwater Flow Caused by the Failure of 32 Main Feedwater Pump Train A Control Logic Power Supply | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000293/LER-2007-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000306/LER-2007-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000309/LER-2007-001 | Uncompensated Degradation in a Security System | | 05000414/LER-2007-001 | Failure to Comply with Action Statement in Technical Specification (TS) 3.3.1 for Loss of a Channel of the Solid State Protection System | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000311/LER-2007-001 | Inoperability of the Chilled Water System - (21 and 22 Chillers Inoperable) | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000331/LER-2007-011 | . Undervoltage ConditiOn Resulted in the Actuation of the Emergency Diesel Generators | | 05000346/LER-2007-001 | Station Vent Radiation Monitor in Bypass due to Faulty Optical Isolation Board | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000348/LER-2007-001 | Vire President - Farley Operating Company, Inc. Po51 Office Drawer 470 Ashford, Alabarid 36312-0470 Tel 334 814 4511 Fax 334 814 4728 SOUTHERN June 22, 2007 COMPANY Energy to Serve Your World Docket Nos.: 50-348 NL-07-1231 50-364 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D. C. 20555-0001 Joseph M. Farley Nuclear Plant — Units 1 and 2
Licensee Event Report 2007-001-00
Technical Specification 3.8.1 Violation Due to
Failure of Breaker / Mechanism-Operated Cell Switch
Ladies and Gentlemen: Joseph M. Farley Nuclear Plant - Licensee Event Report (LER) No. 2007-001-00 is being submitted in accordance with 10 CFR 50.73(a)(2)(i)(B) and 10 CFR 50.73(a)(2)(v)(B). This letter contains no NRC commitments. If you have any questions, please advise. Sincerely, 7e. R. Johnson Vice President — Farley Joseph M. Farley Nuclear Plant 7388 North State Highway 95 Columbia AL 36319 JRJ/CHM Enclosure: Licensee Event Report 2007-001-00 - Unit 1 U. S. Nuclear regulatory Commission NL-07-1231 Page 2 cc:� Southern Nuclear Operating Company Mr. J. T. Gasser, Executive Vice President Mr. J. R. Johnson, Vice President — Farley Mr. D. H. Jones, Vice President — Engineering RTYPE: CFA04.054; LC # 14596 U. S. Nuclear Regulatory Commission Dr. W. D. Travers, Regional Administrator Ms. K. R. Cotton, NRR Project Manager — Farley Mr. E. L. Crowe, Senior Resident Inspector— Farley NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104 EXPIRES: 06/30/2007 (6-2004) Estimated burden per response to comply with this mandatory collection request: 50 hours. Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F52), U.S. Nudear Regulatory Commission, Washington, DC 2055570001, or by InternetLICENSEE EVENT REPORT (LER) e-mail to infocolledsanrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information(See reverse for required number of collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, thedigits/characters for each block) information collection. 1. FACILITY NAME 2. DOCKET NUMBER 3. PAGE Joseph M. Farley Nuclear Plant - Unit 1 05000 348 1 OF 4 4. TITLE Technical Specification 3.8.1 Violation Due to Failure of Breaker / Mechanism-Operated Cell (MOC) Switch | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000316/LER-2007-001 | As-Found Local Leak Rate Tests Not Performed | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000456/LER-2007-001 | Unit 1 Reactor Trip Following a 345 Kv Transmission Line Lightning Strike | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000333/LER-2007-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000254/LER-2007-001 | Quad Cities Nuclear Power Station Unit 1 05000254 1 of 3 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000389/LER-2007-001 | S, Reactor Shutdown Due to Unidentified RCS Leakage | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000255/LER-2007-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000369/LER-2007-001 | 369 5McGuire Nuclear Station Unit 1 05000 1 OF5 | | 05000335/LER-2007-001 | Mispositioned Service Air Containment Isolation Valves | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000362/LER-2007-001 | Failure to declare Emergency Diesel Generator Inoperable and enter TS Action | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000353/LER-2007-001 | Scram Discharge Volume Vent and Drain Valves Opened Due To Fuse Removal | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | 05000400/LER-2007-001 | Control Rod Shutdown Bank Anomaly Causes Entry into Technical Specification 3.0.3 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000261/LER-2007-001 | Reactor Trip Due to a Loose Wire in the Main Transformer Monitoring Circuitry | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000389/LER-2007-002 | 2B2 Reactor Coolant Pump (RCP) Seal Housing Leakage | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000255/LER-2007-002 | | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material | 05000395/LER-2007-002 | Failure to Follow Administrative Controls Results in LCO 3.6.4 Violation | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000306/LER-2007-002 | | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000440/LER-2007-002 | Shutdown Cooling Pump Trip Results in Operation Prohibited by Technical Specifications | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) | 05000414/LER-2007-002 | Technical Specification Violation Associated with Containment Valve Injection Water System | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000416/LER-2007-002 | Reactor SCRAM due to Turbine Trip caused by Loss of Condenser Vacuum | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(iv), System Actuation | 05000423/LER-2007-002 | Loss of Offsite Power Caused by Transmission System Operator While Defueled | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(iv), System Actuation | 05000311/LER-2007-002 | RReactor Trip Due to a Breach in the Condensate System | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000369/LER-2007-002 | | | 05000454/LER-2007-002 | Technical Specification Required Shutdown of Unit 1 and Unit 2 Due to an Ultimate Heat Sink Pipe Leak Common to Both Units | | 05000282/LER-2007-002 | | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | 05000315/LER-2007-002 | Failure to Declare Essential Service Water Inoperable | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000247/LER-2007-002 | Technical Specification Prohibited Condition Due to Exceeding Containment Air Temperature Limit Allowed Outage Time as a Result of Changes in Instrument Uncertainty | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000250/LER-2007-002 | Completion of Shutdown Required by Technical Specifications due to Inoperable Rod Position Indication for Two Control Rods in the Same Control Bank | 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000353/LER-2007-002 | Automatic Actuation of Main Condenser Low Vacuum Isolation Logic During Refueling Outage | 10 CFR 50.73(a)(2)(iv), System Actuation | 05000272/LER-2007-002 | MManual Reactor Trips Due to Degraded Condenser Heat Removal | 10 CFR 50.73(a)(2)(iv)(A), System Actuation |
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