ML18348A239
ML18348A239 | |
Person / Time | |
---|---|
Site: | Quad Cities |
Issue date: | 08/04/1976 |
From: | Kalivianakis N Commonwealth Edison Co |
To: | James Keppler NRC/IE, NRC/RGN-III |
References | |
LER 1976-026-00 | |
Download: ML18348A239 (1) | |
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.,.. . COJntMnwea*e~ .
Quad-Cities Nliclee Po'$t0ffic:e Box.2'\6
- Cordova. Illinois Gt242
- weF Station*
. .. Tti~ophone 300/sa4;...2241 Tel~.; Region U~t;:*. At:ten1'ion:: Hr.~ . C.. Feier.abemf*.
August 4~ . l97a.,
- J.;;. Keppler~. keglonal' nf,rec:tor.
. Offi.ce of. ln,;,pect.f.on. and Enfor--eement RegfOn-. UI: . .
U;. 5,;,. Nilc..J~ar.* Reg~let:orr-y**COmniss_ian.-
7.99 Roosevet t: Road
- Glen:~ EHyn*** U linois 60l'J7;
Reference:
Q.uad-C-iti'es Nuclear. Power- St:at:ion-~-- Unit* f"..
~k.et N6~ 5~254*~, OPR~29*' * .
.* Appendix .. A,.. Sections 3 .. ) .. ~l~b-. 6.6.a~ l'~ti _*
Dear Hr. Keppler:
The purpose* of thls *letter.- is to*:provitie*you w.i'th: noclficatl0n: of* a*
, . Repot.itable* Occurrence as l".1M1Uh"ff. by**Tedmh:;eJ. Sp,eciificatJOrt. 6~6-.. 8-. f .
.w.lthtn.. 2~, hours of the* occurrenu.. *
- At 8*: JS> p.;m*. on. August 3
- 1976* wbHe
- cont*rol ** rods ware* being wi thdr-awn towards: crft:i-Ca1 fty;.. the contro:J.* room operator.: observed* 'that. the Rod.*.
Worth* Kintmizer. was dispta.ying the sl.xth-. rod of* the first group *. yet:*:
50 rods had been: wi thdr:awn at tha1: time. AU rnds. were verified to ..
- have. been w.ithdrawn in*, sequence. The f'ul I core display. was checked' and al I cont:roF rods were verified to -be in, thei*r c:or:reet pt>sitions *.
tnvestigatibRs are underway* at present: to dete-r.mt*ne the cause *of .th.ls*
problem..
- This: occurrence was d.lscussed* by**t~te"'hone w.ith: Hr.-. Feier.abend of. your
. office on August: 4, 1976.. Further information. will be provi4ed by Rep-or.table. Occurrence Report NO. S0-2Sft/76 which will. be. submitted*
within* Jlf* day.s of th~ date: of thi's* occurrence.
Very* truly yours.*
COMMOWEAt:TW EO f SON. COMPANY QUAD-CITIES NUCLEAA.POVER. STATION
'.r N..fkllFG/Jk:
cc:. G. A--AbreJl
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