02-05-2016 | system train "B" in support of planned maintenance on the non-safety related train "A". The CREV train "B" did not start. Once the CREV train "B" system failed to start, the non-safety related train "A" was restarted. Proper operation of the CREV system and CREV air conditioning (NC) systems could not be ensured, so both CREV and CREV AC system were declared inoperable. As a result, Technical Specification (TS) 3.7.4, Condition A, and TS 3.7.5, Condition A were entered.
The cause of the CREV train "B" system failure to start was the differential pressure switch, which is installed in a vibration susceptible location on the ductwork. This differential pressure switch makes up the interlock between the CREV train "B" system and the non-safety related Control Room HVAC train "A". The differential pressure switch's normally open contacts had temporarily welded together not allowing the starting signal to be received by the CREV train "B" system.
Corrective actions included replacing the differential pressure switch. A future corrective action will relocate the differential pressure switch off of the ductwork to minimize the vibration effects.
The safety significance of this event was minimal. Given the impact on the CREV system, which is common to both units, this report is submitted (for Units 1 and 2) in accordance with the requirements of 10 CFR 50.73 (a)(2)(v)(D), which requires the reporting of any event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident. |
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Category:Letter
MONTHYEARIR 05000254/20240112024-11-13013 November 2024 Biennial Problem Identification and Resolution Inspection Report 05000254/2024011 and 05000265/2024011 IR 05000254/20240032024-11-12012 November 2024 Integrated Inspection Report 05000254/2024003, 05000265/2024003 and 07200053/2024001 ML24317A1432024-11-0404 November 2024 Constellation Energy Generation, LLC, 2024 Annual Report - Guarantees of Payment of Deferred Premiums RS-24-101, License Amendment Request for One-Time Extension of Standby Gas Treatment System Technical Specifications Completion Time to Support Piping Repair2024-11-0404 November 2024 License Amendment Request for One-Time Extension of Standby Gas Treatment System Technical Specifications Completion Time to Support Piping Repair RS-24-126, Request to Replace Formerly Submitted Documents Available in the Agency Documents Access and Management System (ADAMS) with Documents Redacted in Accordance with 10 CFR 2.390(b)(4)2024-10-31031 October 2024 Request to Replace Formerly Submitted Documents Available in the Agency Documents Access and Management System (ADAMS) with Documents Redacted in Accordance with 10 CFR 2.390(b)(4) 05000265/LER-2024-002-01, Turbine Trip and Automatic Scram Due to Digital EHC Power Supply Intermittent Failure2024-10-30030 October 2024 Turbine Trip and Automatic Scram Due to Digital EHC Power Supply Intermittent Failure SVP-24-065, Offsite Dose Calculation Manual (ODCM) Section 12.2.2 Radioactive Gaseous Effluent Monitoring Instrumentation Report Main Chimney High Range Noble Gas Monitor2024-10-29029 October 2024 Offsite Dose Calculation Manual (ODCM) Section 12.2.2 Radioactive Gaseous Effluent Monitoring Instrumentation Report Main Chimney High Range Noble Gas Monitor IR 05000254/20240102024-10-28028 October 2024 Age Related Degradation Inspection Report 05000254/2024010 and 05000265/2024010 and Notice of Violation RS-24-080, Request to Replace Formerly Submitted Documents Available in the Agency Documents Access and Management System (ADAMS) with Documents Redacted in .2024-10-16016 October 2024 Request to Replace Formerly Submitted Documents Available in the Agency Documents Access and Management System (ADAMS) with Documents Redacted in . RS-24-093, Response to Request for Additional Information - Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests2024-10-10010 October 2024 Response to Request for Additional Information - Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests SVP-24-059, Correction to Registration of Use of Casks to Store Spent Fuel2024-10-0404 October 2024 Correction to Registration of Use of Casks to Store Spent Fuel ML24275A2442024-10-0303 October 2024 Reassignment of the U.S. Nuclear Regulatory Commission Branch Chief, Division of Operating Reactor Licensing ML24247A1642024-09-30030 September 2024 Alternative Request RP-01 IR 05000254/20244022024-09-12012 September 2024 Material Control and Accounting Program Inspection Report 05000254/2024402 and 05000265/2024402 (Public) SVP-24-054, Deviation from BWR Vessel and Internals Project (BWRVIP) Guidelines - Inspection of Top Guide Rim Welds2024-09-11011 September 2024 Deviation from BWR Vessel and Internals Project (BWRVIP) Guidelines - Inspection of Top Guide Rim Welds ML24249A1362024-09-0404 September 2024 EN 57304 - Westinghouse Electric Company, LLC, Final Report - No Embedded Files. Notification of the Potential Existence of Defects Pursuant to 10 CFR Part 21 IR 05000254/20240052024-08-28028 August 2024 Updated Inspection Plan and Assessment Follow-Up Letter for Quad Cities Nuclear Power Station (Report 05000254/2024005; 05000265/2024005) RS-24-078, Alternative Request RV-08, Revision 1, Associated with Safety Relief Valve Testing Interval2024-08-20020 August 2024 Alternative Request RV-08, Revision 1, Associated with Safety Relief Valve Testing Interval ML24183A1082024-08-0808 August 2024 – Issuance of Amendment Nos. 302 and 298 Adoption of Tstf-505, Provide Risk Informed Extended Completion Times – RITSTF Initiative 4b SVP-24-049, Owners Activity Report Submittal Sixth 10-Year Interval 2024 Refueling Outage Activities2024-08-0707 August 2024 Owners Activity Report Submittal Sixth 10-Year Interval 2024 Refueling Outage Activities IR 05000254/20243012024-08-0101 August 2024 NRC Initial License Examination Report 05000254/2024301; 05000265/2024301 SVP-24-048, Registration of Use of Casks to Store Spent Fuel2024-07-31031 July 2024 Registration of Use of Casks to Store Spent Fuel 05000265/LER-2024-002, Turbine Trip and Automatic Scram Due to Digital EHC Power Supply Intermittent Failure2024-07-22022 July 2024 Turbine Trip and Automatic Scram Due to Digital EHC Power Supply Intermittent Failure RS-24-070, Independent Spent Fuel Storage Installation, Nine Mile Point, Units 1 and 2, Quad Cities, Units 1 and 2, R. E. Ginna - Nuclear Radiological Emergency Plan Document Revisions2024-07-12012 July 2024 Independent Spent Fuel Storage Installation, Nine Mile Point, Units 1 and 2, Quad Cities, Units 1 and 2, R. E. Ginna - Nuclear Radiological Emergency Plan Document Revisions SVP-24-041, Regulatory Commitment Change Summary Report2024-07-0505 July 2024 Regulatory Commitment Change Summary Report SVP-24-043, Registration of Use of Casks to Store Spent Fuel2024-07-0505 July 2024 Registration of Use of Casks to Store Spent Fuel ML24162A0982024-07-0303 July 2024 – Issuance of Amendment Nos. 301 and 297 Adoption of 10 CFR 50.69 Risk Informed Categorization and Treatment of Structures, Systems, and Components for Nuclear Power Reactors SVP-24-040, Registration of Use of Casks to Store Spent Fuel2024-06-25025 June 2024 Registration of Use of Casks to Store Spent Fuel RS-24-061, Constellation Energy Generation, LLC, Response to NRC Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations2024-06-14014 June 2024 Constellation Energy Generation, LLC, Response to NRC Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations SVP-24-039, Ile Post Exam Package Letter2024-06-12012 June 2024 Ile Post Exam Package Letter RS-24-053, Response to Request for Additional Information Related to License Amendment Request to Revise Technical Specifications to Adopt Risk Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed2024-06-0606 June 2024 Response to Request for Additional Information Related to License Amendment Request to Revise Technical Specifications to Adopt Risk Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed ML24110A0492024-05-28028 May 2024 Audit Report Related to the TSTF-505 and 10 CFR 50.59 Amendments ML24079A0762024-05-23023 May 2024 Issuance of Amendments to Adopt TSTF 264 ML24142A3352024-05-21021 May 2024 Quad Cities—Information Request to Support the NRC Annual Baseline Emergency Action Level and Emergency Plan Changes ML24141A2102024-05-20020 May 2024 Operator Licensing Examination Approval - Quad Cities Nuclear Power Station, May 2024 RS-24-055, 2023 Corporate Regulatory Commitment Change Summary Report2024-05-17017 May 2024 2023 Corporate Regulatory Commitment Change Summary Report IR 05000254/20240012024-05-14014 May 2024 Integrated Inspection Report Nos. 05000254/2024001 and 05000265/2024001 RS-24-042, Response to Request for Additional Information Related to License Amendment Request to Revise Technical Specifications to Adopt Risk Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed Extended Completion2024-05-10010 May 2024 Response to Request for Additional Information Related to License Amendment Request to Revise Technical Specifications to Adopt Risk Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed Extended Completion 05000265/LER-2024-001, Automatic Actuation of Reactor Protection System During Scram Discharge Volume Leak Rate Testing2024-05-10010 May 2024 Automatic Actuation of Reactor Protection System During Scram Discharge Volume Leak Rate Testing SVP-24-034, Annual Radiological Environmental Operating Report2024-05-10010 May 2024 Annual Radiological Environmental Operating Report RS-24-046, 10 CFR 50.46 Annual Report2024-05-0606 May 2024 10 CFR 50.46 Annual Report ML24109A0662024-05-0202 May 2024 – Relief Request I5R-26, Revision 0 RS-24-041, Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests2024-04-30030 April 2024 Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests SVP-24-028, Independent Spent Fuel Storage Installation Annual Radioactive Effluent Release Report2024-04-26026 April 2024 Independent Spent Fuel Storage Installation Annual Radioactive Effluent Release Report SVP-24-029, Radioactive Effluent Release Report for 20232024-04-26026 April 2024 Radioactive Effluent Release Report for 2023 ML24114A1712024-04-23023 April 2024 State of Illinois (IEMA-OHS) Comment Quad Cities HI-STORM Exemption Environmental Assessment SVP-24-024, Corrected Radioactive Effluent Release Report for 20222024-04-0505 April 2024 Corrected Radioactive Effluent Release Report for 2022 IR 05000254/20245012024-04-0505 April 2024 Emergency Preparedness Biennial Exercise Inspection Report 05000254/2024501 and 05000265/2024501 RS-24-032, Response to Request for Additional Information Related to License Amendment Request to Revise Technical Specifications to Adopt Risk Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed Extended Completion2024-04-0505 April 2024 Response to Request for Additional Information Related to License Amendment Request to Revise Technical Specifications to Adopt Risk Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed Extended Completion RS-24-002, Constellation Energy Generation, LLC - Annual Property Insurance Status Report2024-04-0101 April 2024 Constellation Energy Generation, LLC - Annual Property Insurance Status Report 2024-09-04
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000265/LER-2024-002-01, Turbine Trip and Automatic Scram Due to Digital EHC Power Supply Intermittent Failure2024-10-30030 October 2024 Turbine Trip and Automatic Scram Due to Digital EHC Power Supply Intermittent Failure 05000265/LER-2024-002, Turbine Trip and Automatic Scram Due to Digital EHC Power Supply Intermittent Failure2024-07-22022 July 2024 Turbine Trip and Automatic Scram Due to Digital EHC Power Supply Intermittent Failure 05000265/LER-2024-001, Automatic Actuation of Reactor Protection System During Scram Discharge Volume Leak Rate Testing2024-05-10010 May 2024 Automatic Actuation of Reactor Protection System During Scram Discharge Volume Leak Rate Testing 05000265/LER-2023-001-01, Turbine Trip and Automatic Reactor Scram Due to High Moisture Separator Level2023-11-30030 November 2023 Turbine Trip and Automatic Reactor Scram Due to High Moisture Separator Level 05000265/LER-2023-001, Turbine Trip and Automatic Reactor Scram Due to High Moisture Separator Level2023-10-10010 October 2023 Turbine Trip and Automatic Reactor Scram Due to High Moisture Separator Level SVP-22-072, Manual Scram Due to Feedwater Regulator Valve Failure Increasing Reactor Water Level2022-12-30030 December 2022 Manual Scram Due to Feedwater Regulator Valve Failure Increasing Reactor Water Level 05000265/LER-2022-002, Manual Scram Due to Feedwater Regulator Valve Failure Decreasing Reactor Water Level2022-09-0101 September 2022 Manual Scram Due to Feedwater Regulator Valve Failure Decreasing Reactor Water Level 05000254/LER-2022-003, Both Trains of Standby Gas Treatment Inoperable Due to Blockage in the Common Discharge Line2022-09-0101 September 2022 Both Trains of Standby Gas Treatment Inoperable Due to Blockage in the Common Discharge Line 05000254/LER-2022-002, Low Pressure Coolant Injection Manually Isolated Due to Valve Test Equipment Issue2022-07-0808 July 2022 Low Pressure Coolant Injection Manually Isolated Due to Valve Test Equipment Issue 05000265/LER-2022-001, Electromatic Relief Valve 3B Did Not Actuate Due to Incorrectly Oriented Plunger Well Plastic Guides2022-05-20020 May 2022 Electromatic Relief Valve 3B Did Not Actuate Due to Incorrectly Oriented Plunger Well Plastic Guides 05000254/LER-2022-001, Regarding High Pressure Coolant Injection System Inoperable Due to Gland Seal System Malfunction2022-01-26026 January 2022 Regarding High Pressure Coolant Injection System Inoperable Due to Gland Seal System Malfunction 05000254/LER-2021-001, Automatic Actuation of Emergency Diesel Generator Due to Transformer Maintenance2021-05-18018 May 2021 Automatic Actuation of Emergency Diesel Generator Due to Transformer Maintenance 05000254/LER-2020-002, Main Steam Line Drain Valve Declared Inoperable Due to Improper Torque Switch Setting2020-11-10010 November 2020 Main Steam Line Drain Valve Declared Inoperable Due to Improper Torque Switch Setting 05000265/LER-2020-003, Oscillation Power Range Monitors (Oprms) Count Setpoint Discrepancy Due to Inadequate Instructions2020-09-17017 September 2020 Oscillation Power Range Monitors (Oprms) Count Setpoint Discrepancy Due to Inadequate Instructions 05000265/LER-2020-002, Electromatic Relief Valve 3D Did Not Actuate Due to Out of Specification Plunger2020-05-28028 May 2020 Electromatic Relief Valve 3D Did Not Actuate Due to Out of Specification Plunger 05000265/LER-2020-001, Loss of Both Divisions of Residual Heat Removal Low Pressure Coolant Injection Due to Swing Bus Failure to Transfer2020-05-19019 May 2020 Loss of Both Divisions of Residual Heat Removal Low Pressure Coolant Injection Due to Swing Bus Failure to Transfer 05000254/LER-2017-0042018-01-0505 January 2018 Unit 1 HPCI Did Not Trip Due to Wear Debris in the Turbine Stop Valve Oil Resetting Solenoid, LER 17-004-00 For Quad Cities Nuclear Power Station, Unit 1 re: Unit 1 HPCI Did Not Trip Due to Wear Debris in the Turbine Stop Valve Oil Resetting Solenoid 05000254/LER-2017-0032017-11-17017 November 2017 Control Room Emergency Ventilation Air Conditioning Piping Refrigerant Leak Due to High Cycle Fatigue, LER 17-003-00 for Quad Cities, Unit 1, Regarding Control Room Emergency Ventilation Air Conditioning Piping Refrigerant Leak Due to High Cycle Fatigue 05000265/LER-2017-0012017-07-13013 July 2017 High Pressure Coolant Injection Minimum Flow Valve Failed to Open, LER 17-001-00 for Quad Cities, Unit 2, Regarding High Pressure Coolant Injection Minimum Flow Valve Failed to Open 05000254/LER-2017-0022017-05-26026 May 2017 Four Main Steam Isolation Valves (MSIVs) Closure Times Exceeded, LER 17-002-00 for Quad Cities, Unit 1, Regarding Four Main Steam Isolation Valves (MSIVs) Closure Times Exceeded 05000254/LER-2017-0012017-03-22022 March 2017 Secondary Containment Interlock Doors Opened Simultaneously, LER 17-001-00 for Quad Cities, Unit 1, Regarding Secondary Containment Interlock Doors Opened Simultaneously 05000265/LER-2016-0022016-06-24024 June 2016 High Pressure Coolant Injection System Declared Inoperable Due to Valve Packing Leak, LER 16-002-00 for Quad Cities Nuclear Power Station Unit 2 - RE: High Pressure Coolant Injection System Declared Inoperable Due to Valve Packing Leak 05000265/LER-2016-0012016-05-19019 May 2016 Main Steam Isolation Valve Local Leak Rate Tests Exceed Technical Specification Limits, LER 2016-001-00 for Quad Cities Nuclear Power Station, Unit 2 Regarding Main Steam Isolation Valve Local Leak Rate Tests Exceed Technical Specification Limits 05000254/LER-2016-0022016-03-14014 March 2016 Secondary Containment Differential Pressure Momentarily Lost Due to Air Line Failure (RWCU Pump Rm), LER 16-002-00 for Quad Cities Units 1 and 2, Regarding Secondary Containment Different Pressure Momentarily Lost due to Air Failure (RWCU pump Rm) 05000254/LER-2016-0012016-03-10010 March 2016 Secondary Containment Differential Pressure Momentarily Lost Due to Air Line Failure (RWCU Hx Rm), LER 16-001-00 for Quad Cities, Unit 1, Regarding Secondary Containment Differential Pressure Momentarily Lost Due to Air Line Failure (RWCU Hx Rm) 05000254/LER-2015-0102016-02-0505 February 2016 Loss of Control Room Emergency Ventilation System Due to Differential Pressure Switch Failure, LER 15-010-00 for Quad Cities, Unit 1, Regarding Loss of Control Room Emergency Ventilation System Due to Differential Pressure Switch Failure SVP-03-036, LER 03-S01-00, Security Event Report for Quad Cities, Unescorted Protected Area Access Granted Based on Falsified Information and Inadequate Screening Caused by a Failure of Administrative Controls.2003-03-0303 March 2003 LER 03-S01-00, Security Event Report for Quad Cities, Unescorted Protected Area Access Granted Based on Falsified Information and Inadequate Screening Caused by a Failure of Administrative Controls. ML17252B4771976-09-15015 September 1976 LER 76-059-00 for Dresden, Units 2 and 3 Re Review of Quad-Cities Unusual Event Letter Led to Discovery That Dresden'S Standby Gas Treatment System Deviated from Single Failure Criteria That Disabled the SBGT System ML18348A2401976-08-0606 August 1976 LER 1976-027-00, Reportable Occurrence of Control Rods for Quad-Cities, Unit 1 ML18348A2391976-08-0404 August 1976 LER 1976-026-00, Reportable Occurrence of Control Rods for Quad-Cities, Unit 1 2024-07-22
[Table view] |
PLANT AND SYSTEM IDENTIFICATION
General Electric - Boiling Water Reactor, 2957 Megawatts Thermal Rated Core Power Energy Industry Identification System (EIIS) codes are identified in the text as [XX].
EVENT IDENTIFICATION
The Control Room Emergency Ventilation (CREV) system failed to start due to a failed differential pressure switch.
A. CONDITION PRIOR TO EVENT
Unit: 1 / 2 Event Date: December 7, 2015 Event Time: 0825 hours0.00955 days <br />0.229 hours <br />0.00136 weeks <br />3.139125e-4 months <br /> Reactor Mode: 1 / 1 Mode Name: Power Operation / Power Operation Power Level: 100% / 100%
B. DESCRIPTION OF EVENT
On December 7, 2015, at 0825 hours0.00955 days <br />0.229 hours <br />0.00136 weeks <br />3.139125e-4 months <br />, Operations attempted to start the safety related Control Room Emergency Ventilation (CREV) [VI] system train "B" in support of planned maintenance on the non-safety related train "A". The CREV train "B" did not start. Once the CREV train "B" system failed to start, the non-safety related train "A" was restarted. Proper operation of the CREV train "B" system and CREV train "B" air conditioning (NC) system could not be ensured, so both CREV and CREV AC system were declared inoperable. As a result, Technical Specification 3.7.4, Condition A, and Technical Specification 3.7.5, Condition A were entered.
On December 7, 2015, at 1402 hours0.0162 days <br />0.389 hours <br />0.00232 weeks <br />5.33461e-4 months <br />, ENS#51589 was made to the NRC under 10 CFR 50.72(b)(3)(v)(D) to report this event as an event or condition that could have prevented the fulfillment of the safety function.
Operations restarted the Train "A" Control Room HVAC system and began troubleshooting. Differential Pressure Switch [PDS] 0-5795-50 and Relay [RLY] 0-9400-105-CR5ISO were replaced and sent to Powerlabs for further analysis. On December 8, 2015, at 2201 hours0.0255 days <br />0.611 hours <br />0.00364 weeks <br />8.374805e-4 months <br />, Operations successfully completed the Post Maintenance Testing on the CREV and CREV AC Systems and exited TS 3.7.4, Condition A and TS 3.7.5 Condition A.
Given the impact on the CREV system, which is common to both Units, this report is submitted (for Units 1 and 2) in accordance with the requirements of 10 CFR 50.73 (a)(2)(v)(D), which requires the reporting of any event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident.
C. CAUSE OF EVENT
The apparent cause for the CREV train "B" system failure to start was identified as the differential pressure switch, which is installed on a vibration susceptible location of the ductwork [DUCT]. This differential pressure switch makes up the interlock between the CREV train "B" system and the non-safety related Control Room HVAC train "A". The differential pressure switch was susceptible to vibrations and was installed on the air handling unit ductwork. These vibrations caused the differential pressure switch's normally open contacts to temporarily weld together, which did not allow the CREV train "B" system to automatically start or manually start either locally or remotely.
D. SAFETY ANALYSIS
System Design Habitability systems are provided to ensure that control room operators are able to remain in the Main Control Room (MCR) [NA] and operate the plant safely under normal conditions and to maintain the plant in a safe condition under accident conditions. The worst-case design basis accident (DBA) for habitability considerations is postulated as a loss of coolant accident (LOCA) with main steam [SB] isolation valve [ISV] leakage at TS limits.
Per Updated Final Safety Analysis Report (UFSAR) Section 6.4.2, the Control Room HVAC systems are capable of maintaining the control room atmosphere suitable for occupancy throughout the duration of a DBA. The HVAC systems are capable of both automatic and manual transfer from the normal operating mode to the isolation mode.
Transfer of the Control Room HVAC systems to the emergency (pressurization) mode of operation is not a fully automatic operation, since some Control Room HVAC system components must be manually started to operate the Control Room HVAC systems in the emergency (pressurization) mode. The manual actions required when placing the Control Room HVAC system into the pressurization mode following an accident include: (1) starting the refrigeration compressor unit; and (2) starting one Air Filtration Unit (AFU) booster fan.
Per UFSAR Section 6.4.2.1, the Control Room Emergency Zone (Control Room Envelope) is defined as the following areas: the main control room, the cable spreading room, the auxiliary electrical equipment room, which surrounds the old computer room; and the Train "B" HVAC equipment room. The Control Room Envelope boundary is the combination of walls, floor, roof, ducting, doors, penetrations and equipment that physically form the Control Room Envelope. The operability of the Control Room Envelope boundary must be maintained to ensure that the in-leakage of unfiltered air into the Control Room Envelope will not exceed the in-leakage assumed in the DBA analysis for the main control room occupants.
UFSAR Section 6.4.2.4 provides that potential adverse interactions between the Control Room Emergency Zone and adjacent zones that may allow the transfer of toxic or radioactive gases into the control room are minimized by maintaining the control room at a slightly positive pressure with respect to adjacent areas during normal conditions.
Safety Impact The primary purpose of the CREV train "B" system is to provide a protected environment from which occupants can control the unit following an uncontrolled release of radioactivity, hazardous chemicals or smoke. The CREV function was restored when the differential pressure switch was replaced and the CREV system ran when called upon. Since the differential pressure switch had failed and one of its functions is to allow the CREV train "B" system to operate, a safety system functional failure occurred.
Per TS Bases 3.7.4, the CREV train "B" system is considered operable when the train "B" air handling unit is operable along with the AFU and the outside air ventilation intake. Since the train "B" Control Room HVAC system would not start, the system was inoperable and TS 3.7.4 Condition A was entered.
Per TS Bases 3.7.5, the CREV AC system is considered operable when the individual components necessary to maintain the Control Room Emergency Zone temperature are operable. The CREV train "B" air handling unit is necessary to deliver the conditioned air to the Control Room Emergency Zone. Since the train "B" CREV system would not start to all the condition air to be delivered, the CREV AC system was inoperable and TS 3.7.5 Condition A was entered.
Risk Insights The plant Probabilistic Risk Assessment (PRA) model gives no credit to the Control Room Envelope (CRE) and does not include it in the model; hence, the CREV train "B" Fan failing to operate did not contribute to an increase in risk.
In conclusion, the overall safety significance and impact on risk of this event were minimal.
E. CORRECTIVE ACTIONS
Immediate:
The differential pressure switch was replaced.
Follow-up:
The differential pressure switch will be relocated to a non-vibration susceptible area. The failed switch had been in service for 5 years with no issues prior to the failure.
F. PREVIOUS OCCURRENCES
The station events database, LERs, and INPO Consolidated Event System (ICES) were reviewed for similar events at the Quad Cities Nuclear Power Station. This event was attributed to incorrect installation location of the differential pressure switch. Based on the cause of this event and the associated corrective actions, the events listed below, although similar in topic, are not considered significant station experiences that would have directly contributed to preventing this event.
- Station Issue Report (IR) 01067025, "0-9400-105 A-3 Invalid Alarm AFU Post HEPA Filter DP Hi," (05/08/2010) — the local panel for the B Train of Control Room HVAC had tile A-3 lit on panel 0-9400-105 for "AFU Post HEPA Filter DP Hi." The alarm was present when the B Train of Control Room HVAC was not running and differential pressure indication switch DPIS 0-5795-311 was reading 0 inches of water column. The cause of the alarm was a degraded differential pressure indication switch, which was replaced. This previous event, although similar to this LER event was caused by a different failure mode. Both switches were manufactured by the same vendor, but DPIS 0-5795-311 was installed at a location free from excessive vibrations. This is not considered a significant station experience that would have directly contributed to preventing the event of this current LER based on the different failure modes.
- LER 254/2007-003-00, 01/18/08, Safety Function Not Met Due to Control Room Emergency Ventilation System Air Filtration Unit Heater Flow Switch Failure (11/20/07) — Operation's surveillances determined that the CREV Air Filtration Unit (AFU) heaters were not operating as required. Troubleshooting of the AFU heater found that a flow switch had an open contact that was preventing the heater from energizing as required. The previous event was caused by infant mortality of the flow switch, whereas this current LER was caused by improper mounting location of the differential pressure switch.
G. COMPONENT FAILURE DATA
Failed Equipment: Control Room HVAC Differential Pressure Switch (DPS 0-5795-50) Component Manufacturer: Dwyer Instrument Inc.
Component Model Number: 1910-1 Component Part Number: N/A This event has been reported to ICES as Failure Report No. 320582