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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217M3371999-10-20020 October 1999 Forwards Notice of Docketing of License SNM-2506 Amend Application.Notice Has Been Forwarded to Ofc of Fr for Publication ML20217M1111999-10-19019 October 1999 Forwards Insp Repts 50-282/99-14 & 50-306/99-14 on 990920- 22.One Violation Noted & Being Treated as Ncv.Insp Focused on Testing & Maint of Heat Exchangers in High Risk Sys ML20217F4331999-10-15015 October 1999 Forwards Rev 39 to Security Plan.Changes Do Not Decrease Effectiveness of Security Plan.Rev Withheld,Per 10CFR73.21 ML20217C2351999-10-0606 October 1999 Forwards Insp Repts 50-282/99-12 & 50-306/99-12 on 990823-0917.No Violations Noted.Insp Consisted of Selected Exam of Procedures & Representative Records,Observation of Activities & Interviews with Personnel ML20212J8811999-09-28028 September 1999 Forwards Preliminary Accident Sequence Precurson Analysis of Operational Event That Occurred at Plant,Unit 1 on 990105, for Review & Comment.Comment Requested within 30 Days of Receipt of Ltr IR 05000272/19990071999-09-28028 September 1999 Forwards Insp Repts 50-272/99-07 & 50-306/99-07 on 990721- 0831.One Potentially Safety Significant Issue Identified Dealing with Control Room Special Ventilation System.Four Addl Issues of Low Safety Significance Identified ML20212G7171999-09-24024 September 1999 Submits Semiannual Status Update on Project Plans for USAR Review Project & Conversion to Its.Conversion Package Submittal Continues to Be Targeted for Aug of 2000 ML20212G9801999-09-23023 September 1999 Refers to Resolution of Unresolved Items Identified Re Security Alarm Station Operations at Both Monitcello & Prairie Island ML20212F5121999-09-20020 September 1999 Forwards Response to NRC , Preparation & Scheduling of Operator Licensing Examinations ML20212D8401999-09-16016 September 1999 Discusses 990902 Telcon Between D Wesphal & R Bailey Re Administeration of Retake Exam at Prairie Island During Wk of 991206.NRC May Make Exam Validation Visit to Facility During Wk of 991116 ML20217H2331999-09-10010 September 1999 Forwards Security Insp Repts 50-282/99-10 & 50-306/99-10 on 990809-12.Two Findings,Each of Low Risk Significance Identified & Being Treated as non-cited Violations Consistent with App C of Enforcement Policy ML20217H5661999-09-0909 September 1999 Discusses 990907 Pilot Plan Mgt Meeting Re Results to-date of Pilot Implementation of NRC Revised Reactor Oversight Process at Prairie Island & Quad Cities.Agenda & Handouts Provided by Utils Encl ML20212A9241999-09-0909 September 1999 Discusses Plans Made During 990902 Telephone Conversation to Inspect Licensed Operator Requalification Program at Prairie Island During Weeks of 991101 & 991108.Requests That Written Exams & Operating Tests Be Submitted by 991022 ML20212B0511999-09-0909 September 1999 Forwards Insp Repts 50-282/99-11 & 50-306/99-11 on 990816-20.One Issue of Low Safety Significance Was Identified & Being Treated as Ncb ML20211Q7641999-09-0808 September 1999 Informs That NRC Tentatively Scheduled Initial Licensing Exam for Plant Operator License Applicants During Wk of 000515,in Response to D Westphal ML20211N8631999-09-0707 September 1999 Withdraws 970814 Request for Exemption from 10CFR50,App R, Section III.G.2, Fire Protection of Safe Shutdown Capabilities ML20211K5911999-09-0101 September 1999 Informs That Util Reviewed Rvid Data Base,As Requested in NRC .Summary of Proposed Changes & Observed Differences Are Included in Encl Tables ML20211L0211999-09-0101 September 1999 Provides Notification That License Amends 141 & 132 & Associated License Conditions 6 & 7 Have Been Fully Implemented ML20211K5931999-08-31031 August 1999 Forwards License Amend Request for License SNM-2506, Proposing Change to License Conditions 6,7 & 8 & TSs App a of License by Permitting Inclusion of Bpras & Thimble Plug Devices in Sf Assemblies Stored in TN-40 Casks ML20211Q6041999-08-31031 August 1999 Forwards Rev 19 to USAR for Pingp,Per 10CFR50.71(e).Rev Brings USAR up-to-date as of 990228,though Some Info Is More Recent.Attachment 1 Contains Descriptions & Summaries of SE for Changes,Tests & Experiments,Per 10CFR50.59 ML20211K2591999-08-27027 August 1999 Forwards NSP Co Fitness for Duty Program Performance Data for Six Month Period Ending 990630 ML20211D3541999-08-24024 August 1999 Discusses GL 95-07 Re Pressure Locking & Thermal Binding of safety-related Power Operated Gate Valves.Forwards SE Re Response to GL 95-07 ML20211C7601999-08-19019 August 1999 Confirms NRC Intent to Meet with NSP & Ceco on 990807 in Lisle,Il to Discuss with Region III Pilot Plants,Any Observations,Feedback,Lessons Learned & Recommendations Relative to Implementation of Pilot Program ML20211B8311999-08-19019 August 1999 Forwards Request for Relief 8 Re Limited Exams Associated with Unit 1 Third ten-year Interval Inservice Insp Program. Licensee Requests Relief Due to Impractibility of Obtaining 100% Exam Coverage for Affected Items ML20211B5711999-08-19019 August 1999 Forwards Second 90-day Rept for Implementation of Voltage Based Repair Criteria at Prairie Island Unit 1.Rept Fulfills Requirements of Section 6.b of Attachment 1 to GL 95-05 ML20211C2311999-08-19019 August 1999 Forwards Unit 1 ISI Summary Rept,Interval 3,Period 2 Refueling Outage Dates 990425-0526,Cycle 19 971212-990526. Rept Identifies Components Examined,Exam Methods Used,Exam Number & Summarizes Results ML20211B0561999-08-18018 August 1999 Provides Addl Info on Proposed Rev to Main Steam Line Break Methodology ,in Response to NRC Staff Request Made in 990416 Telcon.Nuclear Svcs Corp Rept PIO-01-06, Analysis Rept Structural Analyses of Main Steam Check... Encl ML20211B2621999-08-17017 August 1999 Forwards Insp Repts 50-282/99-09 & 50-306/99-09 on 990719-22.No Violations Noted.Insp Included Review & Evaluation of Current Emergency Preparedness Performance Indicators ML20211C7371999-08-17017 August 1999 Discusses Closure of Staff Review Re Generic Implication of Part Length Control Rod Drive Mechanism Housing Leak on 980123.Enclosed NRC 980811 & 1223 Ltrs Responded to WOG Positions Re Corrective Actions ML20210T5661999-08-12012 August 1999 Forwards RAI Re & Suppl ,which Requested Exemptions from TSs of Section III.G.2 of 10CFR50 App R,To Extent That Specifies Separation of Certain Redundant Safe Shutdown Circuits with fire-related Barriers ML20210R7021999-08-12012 August 1999 Forwards Insp Repts 50-282/99-06 & 50-306/99-06 on 990601- 0720.One NCV Occurred,Consistent with App C of Enforcement Policy ML20210P5191999-08-11011 August 1999 Discusses GL 92-01,Rev 1,Supp 1, Rv Integrity, Issued by NRC on 950519 & NSP Responses for PINGP & 951117. Staff Reviewed Info in Rvid & Released Info as Rvid Version 2.Requests Submittal of Comments Re Revised Rvid by 990901 ML20210G5061999-07-30030 July 1999 Responds to Administrative Ltr 99-02, Operating Reactor Licensing Action Estimates 05000282/LER-1999-007, Forwards LER 99-007-00,re Loss of CR Special Ventilation Function.One New Commitment Was Made in Rept as Indicated in Corrective Action Section Statement in Bold Italics1999-07-23023 July 1999 Forwards LER 99-007-00,re Loss of CR Special Ventilation Function.One New Commitment Was Made in Rept as Indicated in Corrective Action Section Statement in Bold Italics ML20210J4991999-07-22022 July 1999 Forwards Rev 18 to USAR for Pingp,Bringing USAR up-to-date as of 990228,though Some Info More Recent.Safety Evaluation Summaries Also Encl ML20209J0941999-07-15015 July 1999 Forwards SER Finding Rev 7 to Topical Rept NSPNAD-8102, Reload Safety Evaluation Methods for Application to PI Units, Acceptable for Ref in Plant Licensing Actions ML20209H8051999-07-14014 July 1999 Forwards Summary of non-modification Safety Evaluation Number 515 Re Storage of Fuel Inserts,Per Insp Rept 72-0010/99-201 ML20209D4181999-07-0707 July 1999 Informs That Util Has Changed Listed TS Bases Pages Attached for NRC Use.Util Made No New Commitments in Ltr ML20209H8361999-07-0202 July 1999 Forwards Operator Licensing Exam Repts 50-282/99-301(OL) & 50-306/99-301(OL) for Tests Administered During Week of 990517-21.Two Applicants Passed All Sections of Exam & Issued Reactor Operator Licenses to Operate Pings ML20196J9681999-07-0101 July 1999 Informs That in Sept 1998,Region III Received Rev 20 to Portions of Util Emergency Plan Under 10CFR50.54(q).Based on Determination That Changes Do Not Decrease Effectiveness of Licensee Emergency Plan,No NRC Approval Required ML20209C3951999-07-0101 July 1999 Forwards Supplemental Response to GL 95-07, Pressure Locking & Thermal Binding of SR Power-Operated Gate Valves ML20209B7541999-07-0101 July 1999 Final Response to GL 98-01,Suppl 1 Re Y2K Readiness of Computer Sys.Sys Remediated as Required for Plant Operation. Contingency Plans Developed to Mitigate Impact of Y2K-induced Events at Key Rollover Dates ML20196J8941999-06-30030 June 1999 Transmits Util Comments on Draft Regulatory Guide DG-1074, Steam Generator Tube Integrity. Licensee Recommends That NRC Focus on Several Important Listed Areas Considered Principal Concerns & Contentions ML20209F0391999-06-30030 June 1999 Forwards Insp Repts 50-282/99-04 & 50-306/99-04 on 990407-0531.Violation Noted.Notice of Violation or Civil Penalty Will Not Be Issued,Based on NRC Listed Decision to Exercise Discretion ML20209C3011999-06-29029 June 1999 Forwards Annual Rept of Corrections to NSP ECCS Evaluation Models,Iaw 10CFR50.46.Since All Analyses Remain in Compliance,No Reanalysis Is Required or Planned ML20209B5751999-06-24024 June 1999 Submits Revised Relief Request for Limited Examinations Associated with Third 10-yr ISI Examination Plan.Attached Is Unit 1 Relief Request 7,rev 1 Which Addresses Limited Examinations ML20196F3871999-06-23023 June 1999 Forwards Revised Pages 71,72 & 298 of Rev 7 to NSPNAD-8102, Prairie Island Nuclear Power Plant Reload Safety Evaluation Methods for Application to PI Units, Per Discussions with Nrc.Approved Version of Rept Will Be Issued 05000282/LER-1999-006, Forwards LER 99-006-00 Re Discovery That Manual SI Actuation Switch Had Not Been Tested on Staggered Basis During Integrated SI Test.Two New Commitments Are Indicated in Corrective Action Section Statement in Bold Italics1999-06-18018 June 1999 Forwards LER 99-006-00 Re Discovery That Manual SI Actuation Switch Had Not Been Tested on Staggered Basis During Integrated SI Test.Two New Commitments Are Indicated in Corrective Action Section Statement in Bold Italics ML20196D5501999-06-18018 June 1999 Forwards Individual Exam Results for Licensee Applicants Who Took May 1999 Initial License Exam.In Accordance with 10CFR2.790,info Considered, Proprietary. Without Encls ML20196A6741999-06-17017 June 1999 Refers to 990517-20 Meeting with Util in Welch,Minnesota Re Licensee Initiatives in Risk Area & to Establish Dialog Between SRAs & Licensee PRA Staff 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217F4331999-10-15015 October 1999 Forwards Rev 39 to Security Plan.Changes Do Not Decrease Effectiveness of Security Plan.Rev Withheld,Per 10CFR73.21 ML20212G7171999-09-24024 September 1999 Submits Semiannual Status Update on Project Plans for USAR Review Project & Conversion to Its.Conversion Package Submittal Continues to Be Targeted for Aug of 2000 ML20212F5121999-09-20020 September 1999 Forwards Response to NRC , Preparation & Scheduling of Operator Licensing Examinations ML20211N8631999-09-0707 September 1999 Withdraws 970814 Request for Exemption from 10CFR50,App R, Section III.G.2, Fire Protection of Safe Shutdown Capabilities ML20211K5911999-09-0101 September 1999 Informs That Util Reviewed Rvid Data Base,As Requested in NRC .Summary of Proposed Changes & Observed Differences Are Included in Encl Tables ML20211L0211999-09-0101 September 1999 Provides Notification That License Amends 141 & 132 & Associated License Conditions 6 & 7 Have Been Fully Implemented ML20211Q6041999-08-31031 August 1999 Forwards Rev 19 to USAR for Pingp,Per 10CFR50.71(e).Rev Brings USAR up-to-date as of 990228,though Some Info Is More Recent.Attachment 1 Contains Descriptions & Summaries of SE for Changes,Tests & Experiments,Per 10CFR50.59 ML20211K5931999-08-31031 August 1999 Forwards License Amend Request for License SNM-2506, Proposing Change to License Conditions 6,7 & 8 & TSs App a of License by Permitting Inclusion of Bpras & Thimble Plug Devices in Sf Assemblies Stored in TN-40 Casks ML20211K2591999-08-27027 August 1999 Forwards NSP Co Fitness for Duty Program Performance Data for Six Month Period Ending 990630 ML20211C2311999-08-19019 August 1999 Forwards Unit 1 ISI Summary Rept,Interval 3,Period 2 Refueling Outage Dates 990425-0526,Cycle 19 971212-990526. Rept Identifies Components Examined,Exam Methods Used,Exam Number & Summarizes Results ML20211B8311999-08-19019 August 1999 Forwards Request for Relief 8 Re Limited Exams Associated with Unit 1 Third ten-year Interval Inservice Insp Program. Licensee Requests Relief Due to Impractibility of Obtaining 100% Exam Coverage for Affected Items ML20211B5711999-08-19019 August 1999 Forwards Second 90-day Rept for Implementation of Voltage Based Repair Criteria at Prairie Island Unit 1.Rept Fulfills Requirements of Section 6.b of Attachment 1 to GL 95-05 ML20211B0561999-08-18018 August 1999 Provides Addl Info on Proposed Rev to Main Steam Line Break Methodology ,in Response to NRC Staff Request Made in 990416 Telcon.Nuclear Svcs Corp Rept PIO-01-06, Analysis Rept Structural Analyses of Main Steam Check... Encl ML20210G5061999-07-30030 July 1999 Responds to Administrative Ltr 99-02, Operating Reactor Licensing Action Estimates 05000282/LER-1999-007, Forwards LER 99-007-00,re Loss of CR Special Ventilation Function.One New Commitment Was Made in Rept as Indicated in Corrective Action Section Statement in Bold Italics1999-07-23023 July 1999 Forwards LER 99-007-00,re Loss of CR Special Ventilation Function.One New Commitment Was Made in Rept as Indicated in Corrective Action Section Statement in Bold Italics ML20210J4991999-07-22022 July 1999 Forwards Rev 18 to USAR for Pingp,Bringing USAR up-to-date as of 990228,though Some Info More Recent.Safety Evaluation Summaries Also Encl ML20209H8051999-07-14014 July 1999 Forwards Summary of non-modification Safety Evaluation Number 515 Re Storage of Fuel Inserts,Per Insp Rept 72-0010/99-201 ML20209D4181999-07-0707 July 1999 Informs That Util Has Changed Listed TS Bases Pages Attached for NRC Use.Util Made No New Commitments in Ltr ML20209C3951999-07-0101 July 1999 Forwards Supplemental Response to GL 95-07, Pressure Locking & Thermal Binding of SR Power-Operated Gate Valves ML20209B7541999-07-0101 July 1999 Final Response to GL 98-01,Suppl 1 Re Y2K Readiness of Computer Sys.Sys Remediated as Required for Plant Operation. Contingency Plans Developed to Mitigate Impact of Y2K-induced Events at Key Rollover Dates ML20196J8941999-06-30030 June 1999 Transmits Util Comments on Draft Regulatory Guide DG-1074, Steam Generator Tube Integrity. Licensee Recommends That NRC Focus on Several Important Listed Areas Considered Principal Concerns & Contentions ML20209C3011999-06-29029 June 1999 Forwards Annual Rept of Corrections to NSP ECCS Evaluation Models,Iaw 10CFR50.46.Since All Analyses Remain in Compliance,No Reanalysis Is Required or Planned ML20209B5751999-06-24024 June 1999 Submits Revised Relief Request for Limited Examinations Associated with Third 10-yr ISI Examination Plan.Attached Is Unit 1 Relief Request 7,rev 1 Which Addresses Limited Examinations ML20196F3871999-06-23023 June 1999 Forwards Revised Pages 71,72 & 298 of Rev 7 to NSPNAD-8102, Prairie Island Nuclear Power Plant Reload Safety Evaluation Methods for Application to PI Units, Per Discussions with Nrc.Approved Version of Rept Will Be Issued 05000282/LER-1999-006, Forwards LER 99-006-00 Re Discovery That Manual SI Actuation Switch Had Not Been Tested on Staggered Basis During Integrated SI Test.Two New Commitments Are Indicated in Corrective Action Section Statement in Bold Italics1999-06-18018 June 1999 Forwards LER 99-006-00 Re Discovery That Manual SI Actuation Switch Had Not Been Tested on Staggered Basis During Integrated SI Test.Two New Commitments Are Indicated in Corrective Action Section Statement in Bold Italics ML20195G4281999-06-0909 June 1999 Notifies That Amsac/Dss Mods Completed & TS 138/129 Has Been Fully Implemented 05000282/LER-1999-005, Forwards LER 99-005-00 Re Containment Inservice Purge Sys Not Isolated During Heavy Load Movement Over Fuel.Event Has Indicated That Level of Performance Expected by Mgt Has Not Yet Been Achieved1999-06-0707 June 1999 Forwards LER 99-005-00 Re Containment Inservice Purge Sys Not Isolated During Heavy Load Movement Over Fuel.Event Has Indicated That Level of Performance Expected by Mgt Has Not Yet Been Achieved ML20207F4301999-06-0101 June 1999 Forwards 1999 Unit 1 SG Insp Results,Per TS 4.12.E.1. Following Insp 84 Tubes Were Plugged for First Time ML20196L2461999-05-21021 May 1999 Forwards Rev 0 to COLR for Pingp,Unit 1 Cycle 20, IAW TS Section 6.7.A.6 ML20195C6861999-05-21021 May 1999 Forwards Rev 17 to USAR for Prairie Island Nuclear Generating Plant.Attachment 1 Contains Descriptions & Summaries of SEs for Changes,Tests & Experiments Made Under Provisions of 10CFR50.59 During Period Since Last Update ML20206U6781999-05-17017 May 1999 Forwards Revised Emergency Response Plan Implementing Procedures,Including Rev 15 to F3-3,rev 15 to F3-16,rev 14 to F3-22 & Table of Contents ML20206U7131999-05-17017 May 1999 Forwards Revised EOF Emergency Plan Implementing Procedures, Including Table of Contents & Rev 2 to F8-10, Record Keeping in Eof. with Updating Instructions ML20206T2461999-05-17017 May 1999 Forwards Off-Site Radiation Dose Assessment for Jan-Dec 1998, Rev 0 to Annual Radiactive Effluent Rept for 980105- 990103 & Effluent & Waste Disposal Annual Rept Solid Waste & Irradiated Fuel Shipments,Jan-Dec 1998 ML20206R0401999-05-13013 May 1999 Forwards Application for Amends to Licenses DPR-42 & DPR-60, Removing Plant Organization Requirement,Imposed in Amend 141/132 That Plant Manager,Who Has Responsibility for Overall Safe Operation of Plant,Report to Corporate Officer ML20206Q0871999-05-13013 May 1999 Forwards Result of Evaluation Re Ultrasonic Exams of SG Number 22 Performed in Accordance with ASME Boiler & Pressure Vessel Code Section Xi.Procedure Used for Evaluation Contained in WCAP-14166,submitted for Review ML20206F9381999-05-0303 May 1999 Forwards Response to NRC 990304 RAI Re GL 96-05 Program at Pingp.Licensee Commitments Are Identified in Encl as Statements in Italics ML20206J3851999-05-0303 May 1999 Forwards 1998 Annual Radiological Environmental Monitoring Rept 05000282/LER-1999-004, Forwards LER 99-004-00 Re Discovery of Inadequate Sp That Demonstrates Operability of SFP Special Ventilation Sys.Two New NRC Commitments Are Contained in Corrective Action Section of Rept in Bold Italics1999-05-0303 May 1999 Forwards LER 99-004-00 Re Discovery of Inadequate Sp That Demonstrates Operability of SFP Special Ventilation Sys.Two New NRC Commitments Are Contained in Corrective Action Section of Rept in Bold Italics ML20206E1761999-04-28028 April 1999 Forwards Revised TS Pages for Amends 144 & 135 to Licenses DPR-42 & DPR-60,respectively,to Update Controlled Manual or File ML20205S3221999-04-20020 April 1999 Forwards Application for Amends to Licenses DPR-42 & DPR-60, Changing Implementation Date for Relocation from TS to UFSAR of Requirements in TS 3.1.E & Flooding Shutdown Requirements of TS 5.1 ML20205P9891999-04-12012 April 1999 Requests Approval for Proposed Alternatives to Liquid Penetrant Requirements of N-518.4 of 1968 ASME Boiler & Pressure Vessel Code.Results of Analysis & Summary of Tests Performed & Tests Results Are Encl ML20205Q0191999-04-12012 April 1999 Forwards Application for Amend to License DPR-42 & DPR-60, Relocating Shutdown Margin Requirements from TS to COLR 05000282/LER-1998-010, Forwards LER 98-010-01 Re Discovery That 32 App R Related MOVs Are Susceptible to Physical Damage by Fire Induced Hot Shorts.Rept Provides Addl Details on Current Plans for Completing C/As Committed to in Original LER1999-04-0808 April 1999 Forwards LER 98-010-01 Re Discovery That 32 App R Related MOVs Are Susceptible to Physical Damage by Fire Induced Hot Shorts.Rept Provides Addl Details on Current Plans for Completing C/As Committed to in Original LER ML20205P9221999-04-0101 April 1999 Submits Relief Request 8,rev 0 Which Addresses Limited Exams Associated with Unit 2 Third ten-year Interval Inservice Insp Program.Util Requests Relief Per 10CFR50.55a(q)(5)(iii) Due to Impracticality of Obtaining 100% Exam Coverage ML20205E8371999-03-31031 March 1999 Submits Four Copies of Rev 38 to Prairie Island Security Plan,Per 10CFR50.54(p).Changes Do Not Decrease Effectiveness of Security Plan.Encl Withheld,Per 10CFR73.21 ML20196K7831999-03-31031 March 1999 Forwards Decommissioning Funding Status Rept for Monticello & Prairie Island Nuclear Generating Plants,Per Requirements of 10CFR50.75(f)(1) ML20205Q5051999-03-30030 March 1999 Forwards Inservice Insp Summary Rept Interval 3,Period 1 & 2 Refueling Outage Dates 981109-1229 Cycle 19,970327- 981229. Rept Identifies Components Examined,Exam Methods Used,Exam Number & Summarized Results ML20205H5731999-03-29029 March 1999 Submits Required 1998 Actual & 1999 Projected Cash Flow Statements for Monticello Nuclear Generating Plant & PINGP, Units 1 & 2.Encl Contains Proprietary Info.Proprietary Info Withheld,Per 10CFR2.790(b)(1) ML20205C6561999-03-26026 March 1999 Submits Semiannual Update on Project Plans for USAR Review Project & Conversion to ITS ML20204H3371999-03-19019 March 1999 Forwards Application for Amend to Licenses DPR-42 & DPR-60, Removing Dates of Two NRC SERs & Correcting Date of One SER Listed in Section 2.C.4, Fire Protection 1999-09-07
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Northern States Power Company Prairie Island Nuclear Generating Plant 1717 Wakonade Dr. East Welch, Minnesota 55089 June 2,1997 10 CFR Pad 2 U S Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555 PRAIRIE ISLAND NUCLEAR GENERATING PLANT Docket Nos. 50-282 License Nos. DPR-42 l 50-306 DPR-60 72-10 SNM-2506 Reply to Notice of Violation (Inspection Report 97005),
Procedural Adherence issues and Security Log Falsification Your letter of May 1,1997, which transmitted Inspection Report No. 97005, required a
- response to a Notice of Violation. Our response to the notice is contained in the attachment to this letter.
In this response we have made one new Nuclear Regulatory Commission commitment, the corrective action for Violation 1.b in italics. Commitments have previously been made, for Violation 1.a, in the Unit 2 Licensee Event Report 97-02, dated April 17,
- 1997. !
Please contact Jack Leveille (612-388-1121, Ext. 4662) if you have any questions f, i
related to this letter. //
mw Joel P Sorensen -
Plant Manager :
Prairie Island Nuclear Generating Plant ;
c: Regional Administrator - Region 111, NRC Senior Resident inspector, NRC NRR Project Manager, NRC J E Silberg
Attachment:
RESPONSE TO NOTICE OF VIOLATION 9706050246 970602
{DR ADOCK 0500 2 ((((\\kh\g}((,(( k
o i t i L -
RESPONSE TO NOTICE OF VIOLATION . !
t l
VIOLATION 1.a l 10 CFR 50, Appendix B, Criterion V, " Instructions, Procedures, and Drawings," required, in part, that activities affecting quality shall be prescribed by documented instructions, procedures, or drawings of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or drawings.
. Procedure C18, " Engineered Safeguards System," Revision 34, Section 5.2, !
" Raising Accumulator Level (Cold or Refueling Shutdown)," required that the plant be in the Cold or Refueling Shutdown Mode when the accumulators were filled.
1 Surveillance Procedure SP 1001AA, " Reactor Coolant System Leakage Test,"
Revision 24, did not address manipulation of valve CV-31205. ;
Contrary to the above:
- a. On March 18,1997, the licensee used Procedure C18, Section 5.2 to fill l the Unit 2 accumulators and the plant was not in the Cold or Refueling :
Shutdown Mode.
- b. ...
)
i This is a Severity Level IV Violation (Supplement 1). ;
, BESPDNSE TOYJOLATION 1a Background Niolation 1.a)
On March 18,1997, Unit 2 was above cold shutdown, with the reactor coolant system (RCS) at approximately 335 degrees F and 360 psig, during startup evolution from a refueling outage. Following an outage, each safeguards accumulator (tank containing borated water pressurized with nitrogen that provides a passive means of injecting into the RCS in the event that the RCS pressure drops below the pressure of the accumulator) needs to be filled. in order to accomplish this, a safety injection pump is normally used to deliver water to an accumulator through the accumulator fill line (see Figure 1); during the filling, the valves to the RCS cold legs, 8801A and 8801B, must be closed to prevent flow to the RCS when RCS pressure is below shutoff head of the safety injection pump. This evolution is normally done prior to heating the RCS above 200 degrees F (and the normal pre-conditions are a gas bubble in the pressurizer and a containment air temperature of greater than 70 degrees F).
l
Attachment June 2,1997 a
- Page 2 Prior to exceeding an RCS temperature of 200 degrees F, the procedure requires the accumulators to be filled with borated water and pressurized with nitrogen. However, there is a restriction in another procedure against pressurizing the accumulators when the containment air temperature is less than 70 degrees F. Since the containment air temperature was below 70 degrees F and the accumulators are not required to be in service by Technical Specifications until the RCS pressure is greater than 1000 psig, it was decided to make a temporary change to the procedure to delay filling of the accumulators until later in the startup evolution. There was another reason not to fill at this time: the RCS was filled and solid whereas the Technical Specifications require both SI pumps' control switches to be in pullout with the RCS below 200 degrees F and no bubble in the pressurizer. The accumulators could have physically been filled by gravity supplying borated water from the RWST except that there is an Updated Safety Analysis Report statement that the accumulators are filled by the use of an Si pump and, therefore, there were no procedures supporting a gravity feed fill of the accumulators. It is believed that the Updated Safety Analysis Report statement was not intended to be prescriptive but it was conservatively decided not to fill in this manner without evaluating per 10CFR50.59.
After a bubble had been established in the pressurizer and the containment air temperature had warmed to greater than 70 degrees F, it was intended to fill the accumulators. The RCS was at approximately 335 degrees F and 360 psig. In order to fill the accumulators, the two cold leg injection isolation valves 8801 A and 8801B needed to be closed to prevent flow to the RCS. However, the Technical Specifications require that, when the RCS temperature is greater than 200 degrees F, these valves be
. . . locked in the open position by having the motor control center supply breakers physically locked in the off position." Recognizing this restriction, shift management thought that it would be legitimate to close the valves for a short period of time under !
direct supervision because the filling could be accomplished in less than an hour and 1 Technical Specification 3.0.C. (commonly referred to as the " motherhood clause")
states:
When a Limiting Condition for Operation is not met, and required action is not specified or cannot be satisfied, within one hour initiate the action necessary to place the affected unit in a condition in which the equipment is not required to be OPERABLE.
Since a required action is not specified for the condition where these two valves are closed above cold shutdown, shift management assumed that they could enter this condition, fill the accumulators and pressurize them, return the valves to their required positions and be within the intent of Technical Specification 3.0.C if they could accomplish the operation within one hour. in addition, it was thought that this would be a more prudent course of action than cycling the RCS through the process of returning to cold shutdown, filling the accumulators, and returning to the heatup process (for IR97005. DOC
s
- j. Attachment s .
- June 2,1997 Page 3 example, the concern about low temperature overpressurization of the RCS was
- - already past).
i
!o The operation was accomplished in 44 minutes and was done with an operator
- - stationed at the control switches for the subject valves prepared to open them if j necessary (the breakers were on). The valves were retumed to the Technical
- Specification required locked open position when the operation was completed.
t i
Reason for the Violation Niolation 1.a)
The cause of the event was that shift management assumed that Technical i Specification 3.0.C could be used as a normal Technical Specification required action
- when a limiting condition for operation is not met. It was thought that it would be similar
! to removing one safety injection pump from service with a 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> return to. service
- requirement. The limit in Technical Specification 3.0.C is one hour, which is a very i
short time limit but that seemed appropriate for an action where both paths of injoction
. to the cold legs are isolated. That is, the time limit seemed proportionate to the
[
i condition in which the plant was being placed.
l It was not understood that Technical Specification 3.0.C is intended to provide time to I orderly place the plant in the required mode when a limiting condition for operation is j found not met and no required action is specified in the corresponding specification.
4 Plant management had the proper understanding of Technical Specification 3.0.C but that understanding was not effectively communicated to the operauons shift staff.
Corrective Stens Taken and Results Achieved Niolation 1.a) 5 l The plant was restored to compliance with the Technical Specification requirements L prior to the shift staff becoming aware that the plant had been out of compliance, f
Corrective Steos To Avoid Further Violations Niolation 1.a)
! On March 18,1997, the General Superintendent of Operations sent a message to all
, operations perconnel with a discussion of the significance of entering Technical i Specification 3.0.C.
l The licensee event report for this event has been " required reading" for all operators.
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Attachment June 2,1997 j Page 4 '
Training on the intent of Techriical Specification 3.0.C will be made a part of the routine training provided to all operators. l l
An evaluation will be performed to determine if the Updated Safety Analysis Report can :
be changed te allow gravity filling of the accumulators from the refueling water storage ;
tank. >
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The Date When Full Comoliance Will be Achieved (Violation 1.a)
Full comp!!ance has been achieved.
VIOLATION 1.b 10 CFR 50, Appendix B, Criterion V, " Instructions, Procedures, and Drawings," required, in part, that activities affecting quality shall be prescribed by documented instructions, procedures, or drawings of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or drawings.
Procedure C18, " Engineered Safeguards System," Revision 34, Section 5.2,
. " Raising Accumulator Level (Cold or Refueling Shutdown)," required that the plant be in the Cold or Refueling Shutdown Mode when the accumulators were filled.
Surveillance Procedure SP 1001 AA, " Reactor Coolant S / stem Leakage Test," 1 Revision 24, did not address manipulation of valve CV-31205.
1 Contrary to the above:
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- b. Operators occasiona':y manipulated valve CV-31205 during the
- performance of SP 1001AA to preclude diversion ofletdown to the holdup tanks and subsequent voiding of the surveillance.
This is a Severity Level IV Violation (Supplement 1).
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June 2,1997 i Page 5 RESPONSE TO VIOLATION 1.b -
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- t i Reason for the Vioistion (Violation 1.b) !
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! As discussed in the inspection report, we, too, believe that the valve CV-31205 was !
mis-positioned during the performance of the daily RCS leak rate surveillance, SP i
, . 1001aa. The test requires stable conditions including constant volume control tank i' level during the two hours data is collected. To avoid any diverting of letdown to the - j CVCS holdup tanks and thus voiding the surveillance, some Operators have placed the j l control switch to the VC TNK position. The action is taken without benefit of procedure l steps to initiate the action or to retum the switch to the AUTO position. On this - i occasion, it appears that the operator positioned the wrong valve, failing to adequately i
, self-check. Sehequently, the operator failed to do an adequate control board l walkdown, not noticing the valve out of its normal position. ;
j Further investigation via interviews revealed that secondary causes of the mis-
' I positioned valve were:
l l e The modified mirror image conventien used in the control room contributes to !
! positioning of the wrong divert valve; j
. The dual red light convention (a reo Mrs is illuminated for either position of
, tha valve) contributes to a poor discover / mechanism to find mispositioned j
- c'ivert valves. :
3
. The small tag depicting a lit light bulb over the normal position of the divert valve is not seen by some Operators and contributes little to a discovery
{
j method.
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e Corrective Steos Taken and Results Achieved (Violation 1.b)
Upon review, the mis-positioned valve was returned to its normal position.
Corrective Steos To Avoid Further Violations (Violation 1.b)
There are four procedures to perform the RCS daily RCS leakage rate; these have all been revised to include steps M position the valve when required and to return the valve to its normal position wh?n done.
A solution being considered is to replace the redlenses over the off normalposition with white lenses. It is believed that the white lenses would be thought of as
-" disagreement" as are other white lenses and would draw more attention to the valves if !
in an off normal position. A decision regarding human factors improvement to the l control board will be made by September 1,1997.
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Attachment 4 June 2,1997 I Page 6 The Date When Full Comoliance Will be Achieved Niolation 1.b) t i
Full compliance has been achieved.
J VIOLATION 2 Section 13 of Amendment 2 of Materials License No. SNM-2506, dated February 1,1996, requires the licensee to comply with all provisions of the Independent Spent Fuel Storage Installation (ISFSI) security plan. Section 6.2 of the ISFSI security plan requires visitors entry to be logged before entering the ISFSI protected area.
10 CFR 50.9 (a) requires information required by the Commission's regulations, orders, or license conditions to be complete and accurate in all material respects.
i
, 10 CFR 50.5 (a) prohibits an individual (s) from engaging in deliberate j misconduct that could cause a licensee to be in violation of any rule, regulation, or order issued by the Commission.
Contrary to the above, on February 24,1996, the junior day shift security shift supervisor removed a visitor sign in log sheet (required by Section 6.2 of the Independent Spent Fuel Storage Installation (ISFSI) security plan) that correctly j showed that visitors had entered the ISFSI on February 23,1996, and replaced it
, with an altered visitor log sheet that incorrectly showed that no visitors had
- entered the ISFSI on February 23,1996. The actions taken by the security supervisor caused the licensee to be in violation of Section 6.2 of the ISFSI security plan. The record (ISFSI visitor log) was material to the NRC in that such records are routinely reviewed to confirm compliance with requirements of the ISFSI security plan.
This is a Severity Level IV violation (Supplement Vil D.2).
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Page 7 j RESPONSE TO VIOLATION 2 Reason for the Violation Niolation 2)
The record (ISFSI visitor log) was material to the NRC in that such records are routinely
. reviewed to confirm compliance with requirements of the ISFSI security plan. Removal ,
and falsification of this record by the supervisor constitutes a violation of the ISFSI l security plan. Discussion of the potential reasons that the security supervisor falsified l the record are included in our April 15,1996 letter to the NRC transmitting a copy of our {
l investigative report.
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Corrective Steos Taken and Results Achieved and Corrective Steosjo Avoid Further i Violations Niolation 21 l
A full investigation of the activities surrounding this event was immediately conducted by the security contractor, under the supervision of the licensee. During the investigation, on February 29,1996, the two shift supervisors involved resigned. The !
licensee considered the resignations as "for cause" and their unescorted access !
authorization was subsequently denied. ,
- The original visitor log page was returned to the log book and the log book changed to '
a bound book vice the three-ring binder previously used. The security staff changed l
protected and vital area security locks and keys. Discussion of this event with all !
members of the security team verify that this was an isolated instance involving only l these two supervisors. A " Lessons Learned" document was reviewed with all members of the security team.
-t The Date When Full Comoliance Will be Achieved Niolation 2)
Full compliance has been achieved.
IR97005, DOC
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