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Category:NOTICE OF VIOLATION OF A REGULATION
MONTHYEARML20196K6531999-06-29029 June 1999 Notice of Violation from NRC OI Investigation Conducted on 980701-1211.Violation Noted:For Approx Four Hours on 980616, with NMP1 at Full Power,Sro Assumed Assistant Shift Supervisor Position,Contrary to TS Requirements ML20196E5351998-11-19019 November 1998 Notice of Violation from Investigation on 980303-0930. Violation Noted:On 971224,individual Left Controls at NMP-2 Unattended for Six Minutes to Go Into Shift Supervisor Ofc, Area Not at Controls as Noted in NMPC UFSAR Figure 13.5-1 ML20248A8001998-05-20020 May 1998 Notice of Violation from Insp on 980406-0409.Violation Noted:During Insp,Inspectors Determined That Licensee Failed to Properly Store,Control & Classify Safeguards Info ML20199B8601998-01-22022 January 1998 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $55,000.Violation Noted:On 970925,package Containing Metal Samples Removed from Unit 1 Emergency Cooling Tube Sheet Was Sent to Listed Company,Not on List ML20198R4391997-11-0505 November 1997 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $50,000.Violations Noted:Listed non-safety Related SSCs Were Not Included in 10CFR50.65 Monitoring Program ML20137U8501997-04-10010 April 1997 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $200,000.Violation Noted:As of 961105,measures Were Not Established to Assure Condition Adverse to Quality Are Promptly Identified & Corrected ML20057G3271993-10-12012 October 1993 Notice of Violation from Insp on 930808-0918.Violation Noted:On 930803,inspector Discovered Individual That Required Escort in Protected Area W/O Escort for Approx 25 Minutes ML20056C1641993-03-23023 March 1993 Notice of Violation from Insp on 930124-0227.Violation Noted:I&C Technicians Performing N1-ISP-032-004 Failed to Correctly Perform Procedural Steps 7.2.1-7.2.5 Resulting in Automatic Reactor Scram Due to False High Neutron Flux ML20155F4171988-06-10010 June 1988 Notice of Violation from Insp on 880404-08.Violation Noted: Site Procedures CBI-SC 1,Rev 0 & NES-8042433,Rev 3 Did Not Establish Adequate Controls Over Nondestructive Testing Process for Making Precision Thickness Measurements ML20211A3971987-02-11011 February 1987 Notice of Violation from Insp on 861117-870104 ML20211A9671987-02-0404 February 1987 Notice of Violation from Insp on 861001-1116.Violations Noted:Source Range Monitor Downscale Rod Block Channels Inoperable During Refueling Mode & Not Placed in Tripped Condition & Failure to Notify NRC of Unplanned Actuation ML20207N4131986-12-23023 December 1986 Notice of Violation from Investigation Rept 1-84-014. Violations Noted:Qa Auditors Subj of Discrimination in That Lead Auditor Status Rescinded on 840405 in Retaliation for Making QA Findings Critical of QA Program IR 05000220/20050221985-07-11011 July 1985 Notice of Violation from Insp on 850621.Violations Noted: Failure to Test or Recertify Radiographer Assistant During 850220-0522 & Failure of Radiation Protection Officer to Perform Unannounced Insps During 840101-850621 ML20062E7971982-07-23023 July 1982 Notice of Violation from Insp on 820615-18 ML20062C9461978-09-26026 September 1978 Notice of Violation from Inspec on 780905-08 1999-06-29
[Table view] Category:TEXT-INSPECTION & AUDIT & I&E CIRCULARS
MONTHYEARPNO-I-99-046, on 991008,NMP,Unit 1 Declared Unusual Event,Due to Carbon Dioxide Discharge in Records Storage Room of Administration Bldg,Which Was Migrating Beyond Confines of Storage Room.Nrc Resident Inspector Staff Responded1999-10-0808 October 1999 PNO-I-99-046:on 991008,NMP,Unit 1 Declared Unusual Event,Due to Carbon Dioxide Discharge in Records Storage Room of Administration Bldg,Which Was Migrating Beyond Confines of Storage Room.Nrc Resident Inspector Staff Responded IR 05000220/19990061999-09-14014 September 1999 Insp Repts 50-220/99-06 & 50-410/99-06 on 990620-0731.NCVs Noted.Major Areas Inspected:Licensee Operations,Engineering, Maint & Plant Support ML20196K6531999-06-29029 June 1999 Notice of Violation from NRC OI Investigation Conducted on 980701-1211.Violation Noted:For Approx Four Hours on 980616, with NMP1 at Full Power,Sro Assumed Assistant Shift Supervisor Position,Contrary to TS Requirements IR 05000220/19990041999-06-21021 June 1999 Insp Repts 50-220/99-04 & 50-410/99-04 on 990328-0508.No Violations Noted.Major Areas Inspected:Aspects of Licensee Operations,Engineering,Maint & Plant Support PNO-I-99-023, on 990411,NMP Performed Insps That Identified Indications of Crack Growth Around Portion of One of Vertical Welds.Repair Mod for Shroud Vertical Welds Is Expected to Take Approx Five Days to Complete1999-05-12012 May 1999 PNO-I-99-023:on 990411,NMP Performed Insps That Identified Indications of Crack Growth Around Portion of One of Vertical Welds.Repair Mod for Shroud Vertical Welds Is Expected to Take Approx Five Days to Complete IR 05000220/19980151998-12-23023 December 1998 Insp Repts 50-220/98-15 & 50-410/98-15 on 980927-1121.No Violations Noted.Major Areas Inspected:Licensee Operations, Engineering,Maint & Plant Support ML20196E5351998-11-19019 November 1998 Notice of Violation from Investigation on 980303-0930. Violation Noted:On 971224,individual Left Controls at NMP-2 Unattended for Six Minutes to Go Into Shift Supervisor Ofc, Area Not at Controls as Noted in NMPC UFSAR Figure 13.5-1 IR 05000220/19980141998-10-26026 October 1998 Insp Repts 50-220/98-14 & 50-410/98-14 on 980816-0926.No Violations Noted.Major Areas Inspected:Reviews of Licensee Activities in Functional Areas of Operations,Engineering, Maint & Plant Support ML20248A8001998-05-20020 May 1998 Notice of Violation from Insp on 980406-0409.Violation Noted:During Insp,Inspectors Determined That Licensee Failed to Properly Store,Control & Classify Safeguards Info ML20217L9251998-04-28028 April 1998 Insp Repts 50-220/98-08 & 50-410/98-08 on 980406-21. Violations Noted.Major Areas Inspected:Licensee Security Force Capability to Protect Facility Against Radiological Sabotage & Compliance W/Safeguards Program Commitments ML20199B8601998-01-22022 January 1998 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $55,000.Violation Noted:On 970925,package Containing Metal Samples Removed from Unit 1 Emergency Cooling Tube Sheet Was Sent to Listed Company,Not on List ML20198R4391997-11-0505 November 1997 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $50,000.Violations Noted:Listed non-safety Related SSCs Were Not Included in 10CFR50.65 Monitoring Program ML20137U8501997-04-10010 April 1997 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $200,000.Violation Noted:As of 961105,measures Were Not Established to Assure Condition Adverse to Quality Are Promptly Identified & Corrected IR 05000220/19940011994-01-24024 January 1994 Insp Repts 50-220/94-01 & 50-410/94-01 on 940103-07.No Violations Noted.Major Areas Inspected:Mgt Support, Protected Area Barriers,Detection Aids & Assessment Aids, & Protected Area & Isolation Zone Lighting IR 05000220/19930221993-12-22022 December 1993 Insp Repts 50-220/93-22 & 50-410/93-22 on 931004-20.No Violations Noted.Major Areas Inspected:Mov Program Commitments & Enhancments Identified During Team Inspection in June 1992 Were Reviewed for Progress IR 05000220/19930011993-11-12012 November 1993 Insp Repts 50-220/93-01 & 50-410/93-01 on 930919-1030. Violations Noted.Major Areas Inspected:Major Components & Sys for Leakage,Alignment,Lubrication,Cooling Water Supply IR 05000220/19930231993-11-0505 November 1993 Insp Repts 50-220/93-23 & 50-410/93-22 on 931012-14.No Violations Noted.Major Areas Inspected:Mgt Support,Program Plans & Audits,Protected & Vital Area Physical Barriers, Detection & Assessment Aids PNO-I-93-058, on 931027,licensee Discovered Two Broken 100 Milliliter Vials of Yellow Powder (Believed to Be Yellowcake) at Corporate Ofc in Syracuse,Ny.No Personnel Contaminated.State of Ny Notified1993-10-28028 October 1993 PNO-I-93-058:on 931027,licensee Discovered Two Broken 100 Milliliter Vials of Yellow Powder (Believed to Be Yellowcake) at Corporate Ofc in Syracuse,Ny.No Personnel Contaminated.State of Ny Notified IR 05000220/19930241993-10-27027 October 1993 Insp Repts 50-220/93-24 & 50-410/93-23 on 931018-22.No Violations Noted.Major Areas Inspected:Exams of Procedures, Representative Records,Interviews W/Personnel & Observations by Inspectors IR 05000220/19930191993-10-18018 October 1993 Insp Rept 50-220/93-19 on 930823-27.No Violations Noted. Major Areas Inspected:Electrical Distribution Sys ML20057G3271993-10-12012 October 1993 Notice of Violation from Insp on 930808-0918.Violation Noted:On 930803,inspector Discovered Individual That Required Escort in Protected Area W/O Escort for Approx 25 Minutes IR 05000220/19930121993-10-0606 October 1993 Insp Repts 50-220/93-12 & 50-410/93-12 on 930615-18 & 0712-14.No Violations Noted.Major Areas inspected:930615-18 Emergency Preparedness Program & 930713 annual,full- Participation Emergency Preparedness Exercise IR 05000220/19930181993-10-0101 October 1993 Insp Repts 50-220/93-18 & 50-410/93-18 on 930808-0918. Violation Noted.Major Areas Inspected:Plant Operations, Maint & Surveillance Activities,Engineering & Plant Support, W/Regard to Radiological & Chemistry Controls & Security IR 05000220/19930131993-09-21021 September 1993 Insp Repts 50-220/93-13 & 50-410/93-13 on 930802-06.No Violations Noted.Major Areas Inspected:Design Changes & Mods,Installation & Testing of Mods,Interface/Communication, QA & Technical Support,Wrs & LERs IR 05000220/19930151993-09-16016 September 1993 Insp Repts 50-220/93-15 & 50-410/93-15 on 930719-23.No Violations or Deviations Noted.Major Areas Inspected:Offsite Power Supply Sources for Plant & to Review Licensees Corrective Action on Previously Identified Insp Findings IR 05000220/19930161993-08-0404 August 1993 Insp Repts 50-220/93-16 & 50-410/93-16 on 930426-30.No Violations Noted.Major Areas Inspected:Mgt Controls,Audits, Calibration of Effluent & Process Radiation Monitoring Sys, Air Cleaning Sys & Implementation of Previous Programs ML20056C1641993-03-23023 March 1993 Notice of Violation from Insp on 930124-0227.Violation Noted:I&C Technicians Performing N1-ISP-032-004 Failed to Correctly Perform Procedural Steps 7.2.1-7.2.5 Resulting in Automatic Reactor Scram Due to False High Neutron Flux ML20056C1661993-03-12012 March 1993 Insp Repts 50-220/93-01 & 50-410/93-01 on 930124-0227. Violations Noted.Major Areas Inspected:Plant Operations, Radiological Controls,Maintenance,Surveillance,Security & Safety Assessment/Quality Verification Activities PNO-I-90-092, on 901010,condensate Spill Occurred in Bldg. Caused by Malfunctioning Valve in Lineup for Transfer of New Resin from Mixing Tank to Condensate Demineralizer Bed. Excess Water Pumped Out sub-basement1990-10-11011 October 1990 PNO-I-90-092:on 901010,condensate Spill Occurred in Bldg. Caused by Malfunctioning Valve in Lineup for Transfer of New Resin from Mixing Tank to Condensate Demineralizer Bed. Excess Water Pumped Out sub-basement PNO-I-90-061, on 900806,plant Operators Manually Scrammed Reactor Due to High Vibration on Main Turbine Bearing.Caused by Blank Flange Left in Oil Supply Line to Bearing.Resident Inspectors Following Licensee Actions1990-08-0707 August 1990 PNO-I-90-061:on 900806,plant Operators Manually Scrammed Reactor Due to High Vibration on Main Turbine Bearing.Caused by Blank Flange Left in Oil Supply Line to Bearing.Resident Inspectors Following Licensee Actions IR 05000220/19890991990-08-0101 August 1990 Final SALP Repts 50-220/89-99 & 50-410/89-99 for Mar 1989 - Feb 1990 PNO-I-90-059, on 900730,plant Shut Down Due to Excessive RCS Leakage.Util Will Repair Plant Electromatic Relief Valves Found to Be Leaking During Startup.State of Ny Has Been Informed1990-07-30030 July 1990 PNO-I-90-059:on 900730,plant Shut Down Due to Excessive RCS Leakage.Util Will Repair Plant Electromatic Relief Valves Found to Be Leaking During Startup.State of Ny Has Been Informed PNO-I-90-057, on 900727,restart Authorized for Facility. Util Agreed to Perform Self Assessments of Performance & Inform NRC Restart Assessment Panel of Self Assessment Results1990-07-27027 July 1990 PNO-I-90-057:on 900727,restart Authorized for Facility. Util Agreed to Perform Self Assessments of Performance & Inform NRC Restart Assessment Panel of Self Assessment Results PNO-I-89-072A, on 890828,augmented Insp Team Exit Meeting Subsequent Press Conference Held at Plant Re Licensee Use of sub-basement for Storage of Solid & Liquid Radwaste.Two Violations Noted1989-08-29029 August 1989 PNO-I-89-072A:on 890828,augmented Insp Team Exit Meeting Subsequent Press Conference Held at Plant Re Licensee Use of sub-basement for Storage of Solid & Liquid Radwaste.Two Violations Noted ML20247D5991989-05-0202 May 1989 Investigation Rept 89-02 Re Misconduct of Ofc of Investigations Deputy Director,Ra Fortuna.Finding of No Misconduct or Dereliction of Duty Recommended IR 05000220/19880301988-11-16016 November 1988 Insp Repts 50-220/88-30 & 50-410/88-29 on 880926-30.No Violations Noted.Major Areas Inspected:Security Plan & Procedures,Mgt Organization,Audits,Records & Repts,Testing & Maint,Barriers,Security Power Supply & Assessment Aids IR 05000220/19860991988-07-0101 July 1988 Amended SALP Repts 50-220/86-99 & 50-410/87-99 for Nov 1986 - Feb 1988 & Feb 1987 - Feb 1988,respectively. Licensee Has Shown Limited Success W/Initiatives to Improve Previously Identified Weaknesses ML20155F4171988-06-10010 June 1988 Notice of Violation from Insp on 880404-08.Violation Noted: Site Procedures CBI-SC 1,Rev 0 & NES-8042433,Rev 3 Did Not Establish Adequate Controls Over Nondestructive Testing Process for Making Precision Thickness Measurements IR 05000220/19880091988-05-19019 May 1988 Insp Repts 50-220/88-09 & 50-410/88-09 on 880307-11 & 0404- 08.Violations Noted.Major Areas Inspected:Inservice Insp Program Re First 10-yr Insp Interval & Augmented Exams Conducted by Licensee,Including Procedures PNO-I-88-010, on 880120,reactor Scrammed from 42% Power Based on Low Reactor Vessel Water Level.Caused by Equipment Operator Error.Nrc Dispatched Augmented Insp Team to Site to Review Generic Safety Implications of Event1988-01-21021 January 1988 PNO-I-88-010:on 880120,reactor Scrammed from 42% Power Based on Low Reactor Vessel Water Level.Caused by Equipment Operator Error.Nrc Dispatched Augmented Insp Team to Site to Review Generic Safety Implications of Event PNO-I-88-009, on 880120,unusual Event Declared as Result of Worker Injured After Stepping Through Hole in Grating Between Reactor Vessel Flange & Refueling Cavity Floor.No Contamination Involved1988-01-21021 January 1988 PNO-I-88-009:on 880120,unusual Event Declared as Result of Worker Injured After Stepping Through Hole in Grating Between Reactor Vessel Flange & Refueling Cavity Floor.No Contamination Involved PNO-I-88-007, on 880115,present Unplanned Outage to Inspect & Repair Feedwater Sys Components & Supports Extended for Approx 3 Wks to Perform Insp of Bushings in Reactor Vessel Flange Which Hold 6-inch Diameter Reactor Vessel Head Studs1988-01-19019 January 1988 PNO-I-88-007:on 880115,present Unplanned Outage to Inspect & Repair Feedwater Sys Components & Supports Extended for Approx 3 Wks to Perform Insp of Bushings in Reactor Vessel Flange Which Hold 6-inch Diameter Reactor Vessel Head Studs PNO-I-87-120, on 871226,reactor Scram Occurred from Approx 25% Power Due to Turbine Trip on Low Condenser Vacuum Caused by Crack in Condenser Pipe Penetration.Pentration Seal Weld Repaired1987-12-29029 December 1987 PNO-I-87-120:on 871226,reactor Scram Occurred from Approx 25% Power Due to Turbine Trip on Low Condenser Vacuum Caused by Crack in Condenser Pipe Penetration.Pentration Seal Weld Repaired PNO-I-87-117, on 871219,reactor Manually Scrammed After Mechanical Vibrations from Turbine Bldg Felt in Control Room.Caused by Feedwater Control Valve Stem Separation from Disc.Outage Dependent on Availability of Repair Parts1987-12-21021 December 1987 PNO-I-87-117:on 871219,reactor Manually Scrammed After Mechanical Vibrations from Turbine Bldg Felt in Control Room.Caused by Feedwater Control Valve Stem Separation from Disc.Outage Dependent on Availability of Repair Parts PNO-I-87-114, on 871207,reactor Scrammed from Approx 96% Power Due to Low Reactor Vessel Water Level.Caused by Malfunction of Feedwater Control Valves 13A & 13B.Preventive & Corrective Maint Underway1987-12-10010 December 1987 PNO-I-87-114:on 871207,reactor Scrammed from Approx 96% Power Due to Low Reactor Vessel Water Level.Caused by Malfunction of Feedwater Control Valves 13A & 13B.Preventive & Corrective Maint Underway IR 05000220/19870221987-12-0909 December 1987 Insp Rept 50-220/87-22 on 871019-23.No Violations Noted. Major Areas Inspected:Design Change/Mods,Maint & Previously Identified Items PNO-I-87-113, on 871128,condensate Storage Tank Ruptured Spilling Over 260,000 Gallons Nonradioactive Demineralized Water.Caused by Break in Seam Between Tank Sidewall & Floor. Vendor Onsite Inspecting Cause.Plant in Cold Shutdown1987-12-0202 December 1987 PNO-I-87-113:on 871128,condensate Storage Tank Ruptured Spilling Over 260,000 Gallons Nonradioactive Demineralized Water.Caused by Break in Seam Between Tank Sidewall & Floor. Vendor Onsite Inspecting Cause.Plant in Cold Shutdown PNO-I-87-096, on 871016,plant Scrammed on High Neutron Flux from 89% Power During Testing Causing Main Steam Pressure Oscillations Triggering APRM High Flux Scram.Crd Stub Tube Leakage Identified.Hydrostatic Tests Performed1987-10-19019 October 1987 PNO-I-87-096:on 871016,plant Scrammed on High Neutron Flux from 89% Power During Testing Causing Main Steam Pressure Oscillations Triggering APRM High Flux Scram.Crd Stub Tube Leakage Identified.Hydrostatic Tests Performed IR 05000220/19870161987-10-15015 October 1987 Exam Rept 50-220/87-16OL on 870804-06.Exam Results:All Three Senior Reactor Operator Candidates Passed Written & Operating Exams.Exam Key Encl IR 05000410/19870181987-10-0101 October 1987 Requalification & Replacement Exam Rept 50-410/87-18OL on 870707-07.Exam Results:Two of Four Senior Reactor Operator Candidates & Three of Four Reactor Operator Candidates Passed Exam.Exams Encl 1999-09-14
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9 ENCLOSURE NOTICE OF VIOLATION i j AND :
- t PROPOSED IMPOSITION OF civil PENALTIES I
Niagara Mohawk Power Corporation (NMPC) Docket Nos. 50-220/50-410 Nine Mile Point, Units 1 and 2 License Nos. DPR-63/NPF-69 - t EA Nos.96-474; 96-475; '
l 96-494; 96-541
! During three separate NRC inspections conducted between October 7 and November 30,1996 ;
for which several exit meetings were held (the last of which was on December 20,1996),
i violations of NRC requirements were identified. In accordance with the " General Statement ,
- - of Policy and Procedure for NRC Enforcement Actions," NUREG-1600, the NRC proposes to 1 impose civil penalties pursuant to Section 234 of the Atomic Energy Act of 1954, as amended ,
(Act),42 U.S.C. 2282, and 10 CFR 2.205. The particular violations and associated civil !
penalties are set forth below:
1 i 1. Violations Related to Corrective Actions i
10 CFR Part 50, Appendix B, " Quality Assurance Criteria for Nuclear Power Plants,"
. Criterion XVI, " Corrective Action," requires, in part, that measures he established to ,
assure that conditions adverse to quality are promptly identified and corrected, in the
- case of significant conditions adverse to quality, the measures shall assure that the i
cause of the condition is determined and that corrective actions are taken to preclude l
j recurrence.
i A. Contrary to the above, as of November 5,1996, measures were not established l to assure a condition adverse to quality, namely, potential overfill of the Unit 1 l reactor pressure vessel (RPV), was promptly identified and corrected despite several opportunities to do so, as evidenced by the following examples.
j Specifically:
- 1. Following a reactor scram on November 5,1996, the system for overfill ;
l protection failed to prevent FW injection on high water level due to leakage past the FW flow control valve. Additionally, the procedure for response to a reactor scram (N1-SOP-1, Revision 5) did not provide l direction to verify that the overfill automatic protective actions occurred nor direction to take manual action if those actions did not occur, and i training did not reinforce the actions necessary to prevent an overfill event.
4 2. Deviation / event report (DER) 1-92-3353 was initiated on August 27, 1992, to document that the wide range reactor water level indication read lower than expected during power operations. The condition was evaluated to be acceptable and it was determined that no equipment 4
modifications were required. However, the corrective action was 4
deficient because the operators in the control room were not made 1 aware of the discrepancy to ensure correct interpretation of RPV level 9704170124 970410 PDR ADOCK 05000220 G PDR ,
Enclosure 2 indication so as to prevent an overfill event.
- 3. On July 29,1996, following a Unit 1 normal plant shutdown with a manual reactor scram, the operators allowed RPV water level to remain 1 above the high level setpoint (95 inches) for approximately 15 minutes l before taking action to lower level, a condition adverse to quality. !
Subsequent to the shutdown, the licensee's corrective actions were l narrowly focused in that training was provided and procedure changes l were made to address the assumed cause of the high level, but no 1 action was taken to identify why the operators did not recognize the need to take prompt action to restore level to less than 95 inches, as !
specified by N1-SOP-1. )
As a melt, operators allowed FW injection to continue for approximately 50 :
minutes when FW injection was not stopped automatically after the high level !
trip setpoint was exceeded due to leakage past the FW flow control valves following'a scram on November 5,1996. As a result, approximately 30,000 gallons of water entered the main steam lines. (01013)
Violation I.A is a Severity Level lli violation. (Supplement 1)
Civil Penalty - $100,000.
B. Contrary to the above, prior to September 1996, measures were not established to assure that conditions adverse to quality were promptly identified and corrected. Specifically, the pressure control valve (2lCS'PCV115) for the Unit 2 reactor core isolation cooling (RCIC) turbine lube oil conter was failed in the open position on January 26,1991. However, this failure, constituted a condition adverse to quality because the downstream piping and lube oil cooler were routinely operated above their design pressure of 150 psig. This resulted in system degradation and could have adversely affected the RCIC operability.
This condition adverse to quality was not corrected until September,1996.
(02013)
I C. Contrary to the above, prior to August 14, 1996, measures were not established to assure that conditions adverse to quality were promptly identified and corrected. Specifically, in 1992, NMPC reviewed the control room chiller condenser water low flow trip setpoint following cancellation of Modification PN2Y87MXO57 and concluded that the setpoint was conservative. In September 1995, the Unit 2 Division 11 control room chiller tripped twice due to low condenser flow concurrent with the start of the emergency dieselgenerator ]
(EDG). The evaluation of these events and the 1992 review failed to recognize that,in response to a postulated design basis condition, the EDGs are expected to start, resulting in service water pressure and flow transients; and that sufficient margin was not provided for the control room chiller low flow trip setpoint to compensate for these transients. This constituted a condition adverse to quality because the CR chillers could trip following a postulated design basis accident. As a result of the narrowly focused evaluations, the l licensee did not identify this condition adverse to quality until August 14,1996. !
I I
Enclosure 3 l l
(02023)
D. Contrary to the above, prior to October 1996, measures were not established to assure that conditions adverse to quality were promptly identified and corrected. Specifically, while cleaning the Unit 2 suppression pool during a refueling outage (RF04) in 1995, NMPC recognized and documented in a deviation / event report (DER) that most of the foreign material removed from the suppression pool must have entered through the downcomers. Despite this recognition, NMPC did not examine the downcomers. As a result of this failure to identify and correct a condition adverse to quality, a significant amount of debris was left in the downcomer from June 1995 until October 1996. The foreign material could have adversely affected the performance of the emergency core cooling system pumps by clogging the suction strainers.
(02033)
Vio!ations 1.B, l.C, and I.D are classified in the aggregate as a Severity Level lit problem (Supplement 1).
Civil Penalty - $50,000.
II. Violations Related to Desian Control 10 CFR Part 50, Appendix B, Criterion Ill, " Design Control," requires that measures be established to assure that applicable regulatory requirements and design basis for structures, systems, and components are correctly translated into specifications, drawings, and procedures. These measures shall include provisions to assure that appropriate quality standards are specified and included in design documents and that deviations from such standards are controlled. The design control measures shall provide for verifying or checking the adequacy of design, such as by the performance of design reviews. Design changes, including field changes, shall be subject to design control measures commensurate with those applied to the original design.
The NMPC Quality Assurance Topical Report (QATR), Section B.3, states that station ,
modifications are accomplished in accordance with approved designs and procedures. l The design controls apply to preparation, review and revision of design documents, ;
including the correct translation of applicable regulatory requirements and design bases into those documents.
i l
. l Enclosure 4 !
l 4
Nuclear Engineering Procedure NEP-DES-340," Design Calculations," Step 2.1, requires the discipline supervisor to review calculation assumptions, and the validity of their application. Step 2.3 requires the calculation reviewer to check the calculation !
assumptions. ;
A. Contrary to the above, as of October 11,1996, regulatory requirements and design basis were not correctly translated into specifications, and calculation assumptions were not reviewed at Unit 2. Specifically, NMPC did not l adequately verify or check the adequacy of design for motor-operated valves i 2CHS
- MOV25B in the high pressure core spray, RCIC, and containment spray systems. Motor-actuator run efficiency was utilized as a design input without verifying the validity of the application. Consequently, the functionality of the valves under design-basis pressure locking conditions was not adequately assured. (03013)
B. Contrary to the above, as of November 1,1996, regulatory requirements and design basis were not correctly translated into specifications, and calculation assumptions were not reviewed at Unit 2. Specifically, the calculation entitled
- "RCIC pump cooler differential pressure evaluation", dated June 15,1992,was ,
incorrect in that it did not include the suction pressure of the RCIC pump when calculating the downstream pressure of 21CS*PCV115, assuming the relief valve failed to open. Also, this calculation was not reviewed by the discipline '
supervisor. The calculation was used as the basis for two operability determinations for the RCIC system dated June 16,1992, and i August 24,1993. As a result of the incorrect calculation, the operability determinations incorrectly concluded that the downstream pressure would not ,
exceed the hydrostatic test pressure for the piping if the relief valve failed to open. Consequently, the RCIC system was operated with 2lCS* PCV115 failed l open which had the potential to exceed the design of the system if the relief !
valve failed to open. (03023) )
l C. Contrary to the above, as of November 1,1996, regulatory requirements and j design basis were not correctly translated into specifications, and calculation ;
assumptions were not reviewed at Unit 2. Specifically, calculation A10.1-H- i 005 dated September 23,1996, used an incorrect pressure input in determining i the required size for the RCIC turbine lube oil cooler restricting orifice l (2lCS'RO207). The independent review and the station operation review l committee review failed to ident'ify the incorrect design input. As a result, ]
when 2lCS*RO207 was rebored in support of the design chhnge to replace 2lCS*PCV115, the resulting orifice size was too small. With the incorrect orifice size, the RCIC turbine lube oil cooler and its associated piping could be operated at a pressure exceeding their design pressure and the relief valve could continuously lift during RCIC operation. (03033) e __ _____ .
~
Enclosure 5 D. Contrary to the above, as of August 14,1996, regulatory requirements and design basis were not correctly translated into specifications, and calculation assumptions were not reviewed at Unit 2. Specifically, a 1988 setpoint calculation for the low condenser flow trip of the control room chillers, had failed to consider the effects of the service water pressure and flow transients that would be expected to occur when the EDGs started following a postulated design basis accident. As a result, when the setpoint change was implemented in 1989, the low flow trip setpoint was set excessively high. This resulted in both control room chillers being inoperable, contrary to Technical Specification 3.7.3 which requires two independent control room chiller subsystems to be operable when the plant is in operational conditions 1,2,3, and when irradiated ,
fuelis being handled in the reactor building, during core alterations, and during operations with a potential for draining the reactor vessel and uncovering irradiated fuel. With the excessively high setpoint, the control room chillers could have inadvertently tripped when the EDGs started following a postulated design basis accident rendering them unable to perform their intended safety function without operator action. (03043)
Violations ll.A - II.D are classified in the aggregate as a Severity Level lil problem ,
(Supplement 1).
Civil Penalty - $50,000.
Pursuant to the provisions of 10 CFR 2.201, Niagara Mohawk Power Corporation (Licensee) is hereby required to submit a written statement or explanation to the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, within 30 days of the date of this Notice of Violation and Proposed imposition of Civil Penalties (Notice). This reply should be clearly marked as a " Reply to a Notice of Violation" and should include for each alleged violation:
(1) admission or denial of the alleged violation, (2) the reasons for the violation if admitted, and if denied, the reasons why, (3) the corrective steps that have been taken and the results achieved, (4) the corrective steps that will be taken to avoid further violations, and (5) the date when full compliance will be achieved. If an adequate reply is not received within the time specified in this Notice, an Order or a Demand for Information may be issued as to why the license should not be modified, suspended, or revoked or why such other action as may be proper should not be taken. Consideration may be given to extending the response time for good cause shown. Under the authority of Section 182 of the Act,42 U.S.C. 2232, this response shall be submitted under oath or affirmation.
Within the same time as provided for the response required above under 10 CFR 2.201, the Licensee may pay the civil penalties by letter addressed to the Director, Of fice of Enforcement, U.S. Nuclear Regulatory Commission, with a check, draft, money order, or electronic transfer payable to the Treasurer of the United States in the amount of the civil penalty proposed above, or the cumulative amount of the civil penalties if more than one civil penalty is proposed, or may protest imposition of the civil penalties, in whole or in part, by a written answer addressed to the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission. Should the Licensee fail to answer within the time specified, an order imposing the civil penalties will be issued. Should the Licensee elect to file an answer in accordance with 10 CFR 2.205 protesting the civil penalties, in whole or in part, such answer should be
i o
Enclosure 6 clearly marked as an " Answer to a Notice of Violation" and may: (1) deny the violations listed
- in this Notice, in whole or in part, (2) demonstrate extenuating circumstances, (3) show error j
! in this Notice, or (4) show other reasons why the penalties should not be imposed. In addition :
1-to protesting the civil penalties, in whole or in part, such answer may request remission or mitigation of the penalties. )
i
- in requesting mitigation of the proposed penalties, the f actors addressed in Section VI.B.2 of l l the Enforcement Policy should be addressed. Any written answer in accordance with 10 CFR L 2.205 should be set forth separately from the statement or explanation in reply pursuant to f j 10 CFR 2.201, but may incorporate parts of the 10 CFR 2.201 reply by specific reference <
t' (e.g., citing page and paragraph numbers) to avoid repetition. The attention of the Licensee 1
is directed to the other provisions of 10 CFR 2.205, regarding the procedure for imposing civil i
- penalties. l l
! Upon failure to pay any civil penalties due which subsequently have been determined in !
] accordance with the applicable provisions of 10 CFR 2.205, this matter may be referred to the s
.~ Attorney General, and the penalties, unless compromised, remitted, or mitigated, may be t
- collected by civil action pursuant to Section 234(c) of the Act,42 U.S.C. 2282c. j
. t The response noted above (Reply to Notice of Violation, letter with payment of civil penalties, ,
and Answer to a Notice of Violation) should be addressed to: Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Wsshington, D.C.
20555 with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission, ,
Region I and a copy to the NRC Resident inspector at the facility that is the subject of this :
Notice. t Because your response will be placed in the NRC Public Document Room (PDR), to the extent ;
possible, it should not include any personal privacy, proprietary, or safeguards information so :
that it can be placed in the PDR without redaction. However, if you find it necessary to include such information, you should clearly indicate the specific information that you desire not to be placed in the PDR, and provide the legal basis to support your request for I withholding the information from the public. f Dated at King of Prussia, Pennsylvania this 10th day of April,1997 l I
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