ML20126F215

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Insp Rept 50-302/92-27 on 921018-1114.Violations Noted.Major Areas Inspected:Plant Operations,Security,Radiological Controls,Licensee Event Repts,Plant Mods & Licensee Action on Previous Insp Items
ML20126F215
Person / Time
Site: Crystal River Duke energy icon.png
Issue date: 12/11/1992
From: Freudenberger, Holmesray P, Landis K, Merriweather N
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20126F164 List:
References
50-302-92-27, NUDOCS 9212300151
Download: ML20126F215 (18)


See also: IR 05000302/1992027

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NUCLEAR REGULATORY COMMISSION

REGION 11

C 101 MARIETT A STREET, N.W.

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Report No.: 50-302/92-27

Licensee: Florida Power Corporation

3201 34th Street, South

St. Petersburg, FL 33733

Docket No.: 50-302 License No.: ORP-72

Facility Name: Crystal River 3

Inspection Conducted: October 18 - November 14, 1992

Inspector: 08 (cm fee 12f 11 M

P. Holmes-Ray, Senjor Resident Inspector Date Signed

Inspector: G . (2. [ce Poc l2 f 16 92

R. Freudenberger, Re5ident Inspector Date Signed

Inspector: .

ce M @ F1

FT-~Merriweather7Reaptor Inspector Date Signed

Approved by: 2/ h[uk

K. Landis, Section Chief

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Dat'e Signed

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Division of Reactor Projects

SUMMARY

Scope: -

This routine inspection was conducted by two resident inspectors and one

specialist inspector in the areas of plant operations, security, radiological

controls, Licensee Event Reports, plant modifications, and licensee action on

previous inspection items. Numerous facility tours were conducted and

facility operations observed. Backshift inspections were conducted on October

24, 25, 27, 31, and November 4, 6, 7, 11.

Results:

In the area of plant operations, the following violations were identified:

VIO 50-302/92-27-01: Failure to Follow Procedure Results in Valve

Misalignment and Reactor Building Spray (paragraph 3.a)

VIO 50-302/92-27-02: Failure to enter action statement 3.8.1.1 and

perform surveillance requirement 4.8.1.1.1.a with the "B" Emergency

Diesel Generator inoperable as the result of non-TS surveillance testing

(paragraph 4.a).

9212300151 921211

PDR

O ADOCK 05000302

PDR

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REPORT DETAILS

l. Persons Contacted

Licensee Employees

G. Boldt, Vice President Nuclear Production

  • J. Buckner, Nuclear Regulatory Specialist
  • R. Davis, Manager, Nuclear Plant Maintenance
  • E. Froats, Manager, Nuclear Compliance
  • A. Gelston, Manager, Site Nuclear Engineering Services (Acting)
  • G. Halnon, Manager, Nuclear Plant System Engineering

B. Hickle, Director, Nuclear Plant Operations

  • S. Johnson, Nuclear Chemistry and Radiation. Protection Superintendent
  • K. Lancaster, Nuclear Maintenance Work Controls Superintendent

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  • G. Longhouser, Nuclear Security Superintendent

W. Marshall, Nuclear Operations Superintendent *

  • P.-McKee, Director, Quality _ Programs
  • L. Moffatt, Nuclear Shift Manager

B. Moore, Manager, Nuclear' Integrated Scheduling

  • D. Porter, Nuclear Shif t Supervisor
  • S. Robinson, Manager, Nuclear Quality Assessments

~*W. Rossfeld, Manager, Site Nuclear Services

  • J. Terry, Supervisor, Site Nuclear Engineering Services
  • R. Widell, Director, Nuclear Operations Site Support

K. Wilson, Manager, Nuclear Licensing

Other licensee employees contacted included office, operations,

engineering,. maintenance, chemistry / radiation, and corporate personnel. ,

NRC Resident Inspectors

  • P. Holmes-Ray, Senior Resident Inspector
  • R. Freudenberger, Resident Inspector
  • Attended exit interview

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Acronyms and initialisms used throughout this report are listed in the

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last paragraph,

2. Plant Status and Activities

The plant 1 continued in power operation (Mode 1) for the duration of this

inspection period.

On October 21, the Chief of Region II Reactor Projects.Section 2B was on

site for a routine visit.

During the week of November 2, a specialist inspection was conducted to

observe the Emergency Drill. The results of this inspection were-

documented in NRC Inspection Report 50-302/92-26.

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3. Plant Operations (71707, 93702, 40500, & 82301)

Throughout the inspection period, facility tours were conducted to

observe operations and maintenance activities-in progress. The tours

included entries into the protected areas and the radiologically

controlled areas of the plant. During these inspections, discussions

were held with operators, health physics and instrument and controls

technicians, mechanics, security personnel, engineers, supervisors, and

plant management. Some operations and maintenance activity observations

were conducted during backshifts. Licensee meetings were attended by

the inspector to observe planning and management activities. The

inspections confirmed FPC's compliance with 10 CFR, Technical

Specifications, license Conditions, and Administrative Procedures,

a. Inadvertent Reactor Building Spray

On October 15, 1992, with the unit at full power and a quarterly

surveillance run of the "A" Building Spray Pump in progress, a valve

misalignment resulted in the discharge of borated water into the Reactor

Building. A detailed description of the event and licensee initial

actions was included in NRC Inspection Report 50-302/92-25, detail 3.a.

Unresolved Item 50-302/92-25-01 was identified pending the completion of

licensee evaluations and the planned submittal of a voluntary report on

the ;ent.

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Inspector review of the circumstances of the event concluded that the

root cause was licensed operator error. The surveillance flow path was

to be from the Borated Water Storage Tank (BWST) through the BSP-1A

recirculation line back to the BWST. Step 4.0.5 of SP-340B aligns

recirculation flow for testing the "A" Reactor Building Spray Pump,

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including prepositioning manual valve BSV-28 at approximately 7 and 1/2

turns open. After the pump has been started, step 4.7.1 states

" Establish flow at 1500 gpm (with allowable oscillation averaged value

between 1470 gpm and>1530 gpm), by throttling BSV-28." The licensed

operator mistakenly opened and throttled with BSV-3, the motor operated

valve to the spray nozzles, allowing flow to the Reactor Building spray

header.

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The licensed operator involved did not use proper self-checking

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techniques while performing the surveillance. Nevertheless, he

volunteered his error when he recognized it and candidly assessed his

I own performance. Contributing factors to the error included the wording

and structure of the procedure step and simulator training that

practiced throttling of Reactor Building spray flow using BSV-3 during

L accident conditions.

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l The licensee performed an immediate assessment of plant conditions and

developed an action plan to recover from the reactor building spray

l event. A preliminary evaluation was performed by the licensee in the

i following areas:

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Wetted areas of the RB

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- Metal corrosion, including galvanic corrosion, boron corrosion and

hydrogen production

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RB instrumentation condition

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Electric motors including:

RCP motors

AHF motors

Motor operated valves

CRDM stators

Cable issues

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Primary system thermal stress

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RB cranes

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Comparison to RB hydrolysing experiences

- Fan cooler effects of boron precipitation

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EQ equipment impact assessment

The NRC's overall conclusion was that no immediate safety concern

existed and that continued operation was justified. The short term

actions consisted primarily of increased monitoring of equipment and

instrumentation for indications of degradation caused by the spray, and

a RB entry to assess the condition of the RB and equipment. The

Resident Inspector participated in the RB entry. No damage to safety-

related equipment as a result of the spray was identified. The long

term actions required additional visual inspections of equipment for

signs of degradation due to spray.

A region-based inspector was dispatched to the site on October 16, to

aid in the review of licensee's actions to recover from the inadvertent

actuation of Building Spray. The inspector met with the Engineering

Manager to discuss the event and the licensee's action plan status. The

action plan contained 14 action items of which most were considered

complete. The open items were identified as follows:

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- Walkdown main control board thoroughly and frequently to look for

indication of failed instruments or components.

Status: Ongoing on October 16, now complete.

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Accumulate a list of known damage and effects.

Status: Ongoing. As of October 16, only two failures had

occurred and they were discussed in NRC Inspection Report

50-302/92-25. Two more Control Rod Drive Shroud Fans

subsequently failed, which might be attributable to the

spray event, as described below.

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Determine what actions were taken at other plants having similar

events.

Status: Ongoing on October 16, now complete.

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The licensee's action plan was_ judged to contain action items that_were

similar to those described in a Safety Evaluation (SE) developed by the

l NRC Division of Systems Technology concerning " Inadvertent' Containment

Spray Events at Commercial Nuclear Power Plants." The SE was issued by

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an NRC memorandum from Thomas Murley, Director, Office of Nuclear

Reactor Regulation, to all Regional Administrators, dated March 13,

1991. This SE was attachment A to NRC Inspection Report 50-302/92-25.

The safety evaluation indicated that continued reactor operation

following a spray event was acceptable if an immediate assessment of

plant conditions was performed and an action plan was developed to fully

evaluate the consequences of the event on plant systems and components.

Inspection of short term actions taken by the licensee was performed.

Increased surveillance of instruments and equipment for degradation were

observed and the engineering assessments of. potential problem areas were

evaluated. One licensee action item required operations to walk down

the main control board twice per shift to look for indication of failed

instruments or components. A Short Term Instruction (STI)92-019 was

issued which required performance of SP-300, Operating Daily

Surveillance Log, twice per shift for one week, until October 22, 1992.

The NRC inspector toured the control room on October 17 and 18,1992,

attended shift turnover meetings, and witnessed the control room board

walkdowns at 8:00 a.m.,12:00 noon and 4:00 p.m. The data sheets for SP-

300, completed on October 17, 18 and 19, 1992, and the operating shift

log were reviewed to verify that no equipment failures had occurred that

could be attributed to the BS event. During the week of additional

monitoring, no other failures were identified. Other licensee action

items required engineering to perform evaluations of potential problem

areas as well as provide recommendations for 'short and_ long term action.

The preliminary evaluations performed by the licensee were reviewed and

found to be acceptable.

As discussed in NRC IR 50-302/92-25, immediately following the spray,

one of twelve control rod drive shroud exhaust fans (AHF-51A) and one

area radiation monitor (RMG-18) failed. Later in this report period,

two more of the control rod drive fans (AHF-51D & AHF-51K) failed. The

effect of these failures on reactor head service structure temperature

was negligible. Cause analysis of the recent failures was added to the

licensee's long term action plan, to determine if these failures were

the result of the spray.

The inspector confirmed that the licensee had a program in place to

perform increased surveillance of instruments to identify degradation of

components. The licensee's long term action plans, to assess equipment

for possible damage due to spray, appeared to be : appropriate. The plan

included such actions as visual inspections of selected plant equipment

and increased sensitivity to abnormal component conditions during

routine maintenance and calibration in future outages.

The licensee submitted a voluntary report on the event in a letter dated

November 4,1992, to the Regional Administrator, NRC, Region II. The

letter described the event and addressed the scope and sequence of

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licensee actions. Actions performed or planned included a human

performance evaluation and technical evaluation of the short and long

term affects. The licensee's human performance evaluation concluded

that the operator failed-to apply proper self-checking measures to

assure adequate comprehension and correct implementation of required

procedural guidance. The human performance evaluation proposed several

recommendations for consideration to prevent recurrence.

The operator's failure to properly implement the Step 4.7.1 of

Surveillance Procedure SP-340B was a violation, and was identified as

VIO 50-302/92-27-01: Failure to Follow Procedure Results in . Valve

Misalignment and Reactor Building Spray. Although the licensee promptly

initiated extensive corrective actions, as described in detail above,

the violation is being cited because of the inherent significance of an

operator error of this nature. Unresolved item 50-302/92-25--01 is

closed.

b. Emergency Drill Observation

On November 5, the licensee conducted an annual Emergency Preparedness

exercise. Specialist Inspectors from the Region II office of the NRC

were onsite to evaluate the exercise. The resident inspectors observed-

activities in the Simulator Control Room, The Technical Support Center,

and the Emergency Operations Facility.

This was the first occasion in which the control room simulator was used

to simulate accident conditions and provide realistic time frames for

emergency condition parameters.

Late in the scenario, the operators attempted to use a recently

installed high pressure auxiliary spray line to continue a rapid

cooldown and depressurization of the_ reactor coolant system following

the simulated steam-generator tube rupture. - Although the simulator had

been updated to provide simulation of use of the high pressure-auxiliary

spray, the operators identified that an out-of-date revision of

procedure OP-305, Operation of the Pressurizer, was in the simulator

control room and did not include a section for use of the high pressure

auxiliary spray. The procedure was replaced with a current revision.

The licensee's drill critique identified the deficiency and the_-

inspector verified that the correct revision of the procedure was in the

plant control room.

An assessment of the overall effectiveness of the exercise is documented

in NRC-Inspection' Report 50-302/92-26.

4. Maintenance and Surveillance Activities (62703 & 61726)

Surveillance tests were observed to verify that approved procedures were

being used; qualified personnel were conducting the tests; tests _were

adequate to verify equipment operability; calibrated equipment was

utilized; and TS requirements appropriately implemented.

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. The following tests were observed and/or data reviewedi

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SP-9078, Monthly Functional Test of 4160V ES Bus "B" Undervoltage

Relaying;

- SP-907A, Monthly Functional Test of 4160V ES Bus "A" Undervoltage

Relaying; and

- SP-317, Reactor Coolant Water Inventory Balance.

In addition, the inspector observed maintenance activities to verify

that correct equipment clearances were in effect; work requests and fire

prevention work. permits, as required, were issued and being followed;

quality control personnel performed inspection activities as required;

and TS requirements were being followed.

Maintenance was observed and work packages were reviewed for the

following maintenance activities:

- WR 302973, Installation:of Phase Gating Unit for Phase B for

Control Rod Group 6A Power Supply;

- WR 262140 & 299344, Preventive Maintenance on Inverter 1A;

- WR 302712 Troutteshooting Inverter 1E intermittent output voltage

fluctuation;

- WR 303112 & 303086, Cleaning and Ultrasonic Inspection of Nuclear-

Services Closed Cycle Cooling System Suction Header; and

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WR 290604, Prefabrication of Replacement Nuclear Services Closed

Cycle Cooling Suction Header Piping.

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The following items were considered noteworthy:

a. Technical Specification' Action Statement Applicability During

Surveillance Testing

On October.27,'1992, the -licensee performed SP-907B, Monthly

Functional Test of 4160V ES Bus "B" Undervoltage Relaying. The

purpose of the procedure was to demonstrate operability of the

4160V ES Bus B undervoltage protection scheme. The undervoltage

protection scheme is comprised of three undervoltage modes: First

Level Undervoltage Relays (loss of voltage); Second Level

Undervoltage Relays (degraded voltage); and Second Level

Undervoltage with an ES actuation. Each mode is capable of

stripping the 4160V ES Bus B and initiating a start-of Emergency

Diesel Generator 3B. The performance of SP-907B is not required

by TS.

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Performance of the procedure included disabling the Emergency

Diesel Generator by tripping the fuel rack and isolating starting

air to prevent an inadvertent start. Degraded voltage conditions

were then simulated to actuate the FLUR and SLUR relays and

measure their response time. The inspector observe 6 tae test and

equipment restoration, which was performed satisfactorily.

The inspectot noted that although the "B" Emergency Diesel

Generator was disabled for approximately two hours as directed by

the procedure, the licensee did not enter TS action statement

3.8.1.1 nor perform action b, performance of surveillance

requirement 4.0.1.1.1.a, which requires verification of the

breaker alignments and indicated power availability to the offsite

circuits within one hour. This was identified as VIO S0-302/92-

27-02: Failure to enter action statement 3.8.1.1 and perform

surveillance requirement 4.8.1.1.1.a with the "B" Emergency Diese'

Generator inoperable as the result of non-TS eJrveillance testing.

The safety sigr.ificance of this violation was minor because

offsite power circuits remained operable throughout the

performance of the SP. In addition, the Emergency Diesel Generator

was inoperable for significantly less than the 72-hour time period

allowed by the action statement before shutdown must be initiated.

Review of the circumstances of the above violation revealed that

historically, the licensee has not entered TS action statements

when TS related equipment became inoperable as the result of

performing SPs. It was recognized that this practice was not

consistent e ' the NRC staff's position stated in Part 9900:

Technical f.1.nce - Operability of the NRC Inspection Manual

published in Generic Letter 91-18 "Information to Licensee's

Regarding Two %"C Inspection Manual Sections on Resolution of

Degraded and F._ conforming Conditions and on Operability " dated

November 7, 1991. This guidance states "If TS surveillances

require that safety equipment be removed from service and rendered

incapable of performing its safety function, the equipment is

inoperable. The LC0 accion statement shall be entered unless the

TS explicitly direct otherwise." However, some surveillance

requirements such as RPS testing which removes a RPS channel fr;m

service cannot be completed within the action statement time

al'. owanc e .

FPC is currently examining their position on entering the required

actions of TS when equipment is rendered inoperable as a direct

result of periodic surveillance testing based on their review of

WRC GL 91-18 and implementation of the Revised Standard Technical

Specifications (RSTS).

A licensee written positien or, the issue provided to the

inspectors following discussions with FPC management states that

FPC " understands this issue was discussed at the Region 1

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NRC/Public workshop on GL 91-18 and that as the result of issues

identified at that time, it it the NRC Staff's intent to further

discuss it at subsequent GL 91-18 workshops. FPC intends to

remain involved in these discussions and work, together with other

utilities, towards a resolution that provides adequate operational

latitude while maintaining full cognizance of equipment

availability / operability." RSTS accommodates implementation of the

NRC Staff's position and is currently scheduled for implementation

in the Fall of 1993.

b. Reactor Coolant Water Inventory Balance

The reactor coolant drain tank level indicator (WD-23-LT).has

experianced sporadic perturbations in indication since startup -

from the 1992 refueling outage. Due primarily to inaccessibility

of the components during power operations, troubleshooting

activities have not been successful at identifjing and correcting

the cause of the indicated perturbations.

The level change in the reactor coolant dra?n tank is monitored

during the performance of SP-317, Reactor Coolant Water Inventory

Balance, to determine the identified leakage in accordance with TS 3.4.6.2. Leakage from the reactor coolant system to the reactor

coolant drain tank would originate from the pressurizer power

operated relief valve, code safeties, core flood tank drains or

reactor coolant system vents and drains. During initial -

troubleshooting efforts, reactor coolant leakage to the reactor ,

coolant drain tank was considered in the unidentified leakage

calculation.

STI 92-0021 was issued on October 19, 1992, after long term

trending of the WD-23-LT indication. The STI allows use of

WD-23-LT level indication for the calculation of identified

leakage provided a review of the history of the output of WD-23-LT

for a period including one hour before and after the collection of

SP-317 data is reviewed and no perturbations exist.  :

Plans were established to conduct further troubleshooting in the .

event of an unplanned octage. The inspector reviewed SP-317 data

from throughout the report period. Reactor coolant- system leakage

has remained stable and low following the 1992 refueling outage.

The inspector considered the licensee's actions to address this

issue to be acceptable,

c. Nuclear-Services Closed Cycle Cooling Suction Header Degradation

On November 5,-a maintenance planner performing a walkdown of a WR

for replacement of the Nuclear Services Closed Cycle Cor' + (SW)

suction header identified leakage from the header in the v:,inity

of the joint of the six inch surge line to the eighteen inen

suction header.

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The suction header and the surge line are located in a trench in

the floor of the Seawater Room in the Auxiliary Building. The

suction header is common to three SW system circulating pumps.

One pump is the normal duty pump, with two ES pumps normally in

standby. The SW system provides cooling to safety related

components such as; high pressure injection pumps, letdown

coolers, reactor building coolers, spent fuel pool coolers,

reactor coolant pumps, and control rod drive mechanism coolers.

Decay Heat Removal is supplied by separate closed cycle cooling

systems.

On November 6, the licensee performed a detailed visual inspection

of the leaking section of pipe. Two additional pin hole type

leaks were identified on the bottom of the suction header. A

temporary non-rode repair was designed and installed to reinforce

the structural integrity of the leaking section adjacent to hanger

SWH-18. The repair consisted of encasing approximately three feet

of the surge line and suction header in high density grout,

filling the trench in the area of the hanger SWH-18. The repair

was installed in accordance with a temporary modification, MAR

number T92-11-02-01. The MAR was reviewed and the PRC meeting

that approved the MAR was attended by the inspector. Prior to

installation of the temporary non-code repair, the NRC reviewed

and approved the installation in accordance with GL 90-05,

" Guidance For Performing Temporary Non-Code Repair of ASME Code 1,

2, and 3 Piping."

During the week of November 9, an ultrasonic inspection to

characterize the condition of the remainder of the surge line and

suction header, including the two additional leaks, was perf ormed.

Portions of this inspection were observed by the inspectors.

Inspection results indicated that significant external corrosion

had caused general wall thinning on the lower third of the

eighteer-inch portion of the header and the full circumference of

the six inch surge line in the trench. A stress analysis of the

piping was completed by the licensee which indicated the piping

remained operable and the leaks did not compromise the structural

integrity of 'Se piping. The inspectors reviewed the analysis and

provided the information to NRC personnel involved in approval of

the temporary non-code repairs. It was determined that the

analysis provided sufficient justification that the piping

remained operable with minimal margin for further degradation.

The licensee submitted a request for approval of non-code repairs

for the remaining leaks in a letter dated November 13.

An operations STI was issued on November 9, which directed the

Primary Plant Operator to monitor the suction header at least

twice per shift for any change in leakage. The STI remains

effective until December 1, 1992.

Prefabrication of permanent replacement piping for the affected

areas was ongoing at the end of the inspection period. The

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licensee's actions to monitor the condition of the SW will be

assessed in future inspections.

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5. Review o' '< ensee Event Reports (92700)

LERs we 9m iewed for potential generic impact, to detect trends, and

to detero.ne whether corrective actions appeared appropriate. Events

that were reported immediately were reviewed as they occurred to

determine if the IS were satisfied. LERs were also reviewed in

accordance with the current NRC Enforcement Policy,

a. (Closed) LER 91-04: Personnel error caused reactor vessel level

required for inadequate core cooling to be incorrectly calibrated.

See paragraph 6.b for details.

b. (Closed) LER 91-05: ECCS pump and flow paths were secured due to ,

valve leak resulting in a condition outside the plant design

basis.

Crystal River Unit 3 was operating at 100 percent ful? power on

May 30, 1991. Between 9:00 p.m. and 9:07 p.m., operators received

indications of leakage from the Makeup and Purification system in-

- the Auxiliary Building. Operators located the leakage source by

visual observations and by measuring piping surface temperatures.

Leakage was originating from the inter-stage packing leakoff

connection on MVP discharge crosstie valve, MUV-3. The leak was

stopped at 10:23 p.m. by backseating the valve.

Between 9:42 p.m. and 9:55 p.m., while attempting the isolate the

leaking valve, operators stopped all makeup flow, closed another

discharge crosstie valve, MUV-4, the recirculation valve, MUV-264,

and removed control power to the circuit breaker for one of the

MVP/HPI Pumps. These actions placed the plant in a condition

outside the design basis. This condition existed from 9:42 p.m.

until approximately 11:05 p.m.. At this time, operators opened

the valves and restored control power to the pump circuit breaker.

The FSAR for CR-3 discusses combinations of operable MVPs and HPI

valves necessary to ensure adequate HPI flow in the event-of an

accident. With control power removed from-the MVP-1C circuit

breaker, the pump could not be started. -Since_MVP-1B was not

aligned to automatically start, only one pump was available to

provide HPI flow. With MUV-4 closed, only two nozzles were

available. Based on information in the FSAR, it is not clear that

this pump / valve combination would have provided adequate HPI- r' low

under certain accident scenarios. Control Room personnel did not

initially consider that these actions placed the unit in a

condition outside the plant design basis. During subsequent

review of the event, plant personnel determined that the unit was

temporarily outside the plant design basis.

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The licensee developed detailed guidance regarding HPI flow path

operability documented in TSI 92-02. The failed valve packing was

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replaced during the 1991 maintenance outage with an improved

design packing arrangement. This LER is closed.

c. (Closed) LER 91-10: Wiring problem causes transformer breakers-to

open actuating the emergency diesel generator.

On October 20, 1991 CR-3 was in Mode 5 (COLD SHUTDOWN) for a

scheduled maintenance outage. At 2:43 p.m. the breakers for the

offsite power transformer opened, disconnecting the ES busses from

the offsite power supply. Decay heat cooling was interrupted for

less than a minute while the emergency diesel generator loaded the

ES bus and operators restarted the DHP. Upon starting the DHP, a

purification relief valve lifted causing a drop in pressurizer

level. Operators quickly identified the source and isolated the

purification system. At 2:47 p.m., the oparators manually

energized the remaining ES bus via the CR-3 startup transformer.

This event was caused by a pre-existing wire installation which

inadvertently applied 115V AC to the CR-3 battery bus.

The improperly installed wire was removed by WR 0289924. The

breaker relays were replaced with less sensitive ones by WR 0289619 to reduce the possibility of repeating this_ event. An

Operations Study Book entry describing this event and lessons

learned was issued November 7,1991, and was signed off by all

active operators. Procedure AP-770, Emergency Diesel Generator

Actuation, was revised to address restarting the DHP if required

following 4160V bus undervoltage. This LER is closed.

d. (Closed) LER 91-12: Procedure deficiency leads to inadvertent

emergency diesel generator actuation during engineered safeguards

testing.

The procedure inadequai.y in SP-457, Refueling Interval ECCS

Response to a Safety Iajection Test Signal, was corrected by

Revision 10 which was affective July 22, 1992. Some test switches

are spring loaded to return to normal position some are not. The

revision clearly required placing the test switches back to pre-

test positions verses releasing the test switches. This LER is

closed.

e. (Closed) LER 92-21: Lack of Required Lube Oil Leakage Collection

Tank Reserve Capacity For Reactor Coolant Pumps Violates 10 CFR 50

Appendix R Design Criteria

The issue described in this LER was the subject of a violation

detailed in NRC Inspection Report 50-302/92-25, detail 3.b.

Corrective actions will be reviewed as part of the violation

followup VIO 50-302/92-25-02, therefore this LER is closed.

Violations or deviations were not identified.

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6. Licensee Action on Previously Identified Inspection Findings (92702 &

92701)

a. (Closed) NCV 50-302/90-32-02: Failure to provide adequate design

control measures as required by 10 CFR 50, Appendix B, Criterion

III.

On September 24, 1990, with the reactor at full power, the " area

owner" was making a walkdown of the "B" decay heat pit. He

noticed that the guard encapsulation for DHV-43 was not leak tight

in that two small diameter pipe nipples did not contain plugs.

The area owner, an operations assistant shift supervisor, wrote a

memorandum to engineering requesting information as to whether the

nipples should be open or plugged. On September 25,1990, the

system engineer, accompanied by a senior reactor operator,

examined the guard enclosure for both decay heat trains and found

the plugs missing on both decay heat train encapsulations. The

system engineer referred operations to the FSAR chapter 5 which

stated:

" Penetrations 345 and 346 have only one containment isolation

valve etch. The second barrier, which is required in order to

meet the CR-3 containment isolation derign basis, is provided by-  ;

an encal sulation around each recirculation.line from the

containment to beyond the first isolation valve. This

encapsulation is leak-tight at containment design pressure and is

not directly connected to the containment sump or atmosphere. A

single passive or active failure in these lines or encapsulations

will not provide a path for leakage to the environment."

The drawings for the encapsulation (FPC Drawing Number P0-301-621)

details the two socket weld adapters but does-not show any

attachment or closure devices. Therefore, the encapsulations are

in accordance with the drawings. There is no test data, readily

available, to indicate that the encapsulation is capable of

withstanding containment design pressure. The licensee has

plugged the openings but has not tested the encapsulation. .

A violation was considered for this issue because the fact that

the encapsulations in the plant were in accordance with plant

drawings but not in accordance with the design basis indicated

that the design control measures required by 10 CFR 50, Appendix

B, Criterion III were not effective.

This was one of the issues discussed during an Enforcement

Conference at the NRC Region 11 Office on October 31, 1990. The

licensee presented information that-the design basis of the

encapsulations was different from that described in the current

revision of the FSAR. Information from B&W correspondence'from

1971 stated:

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"

... the intent of the guard pipe is to prevent excessive '

quantities of fluid escaping from the Reactor Building sump in the

unlikely event a LOCA and subsequent rupture of this Decay Heat

line were to occur."

B&W correspondence in 1987, relative to the-function of

encapsulations stated:

"The function of the piping jacket is to prevent drainage of the

RB sump in the event of failure or breakage of the piping between

the RB penetration and the isolation valves."

ANSI N271-1976 states the following relative to these containment

penetrations:

3.6.4 Sinale valve and closed system outside containment:

"The single valve and piping between the containment and the

valve shall be enclosed in a protective leak tight p_r

controlled leakane housina to prevent leakage to the

atmosphere."

Inaccurate information relative to the definition of this type

penetration was included in the 1989 revision of the FSAR.

Based on the information presented at the Enforcement Conference, *

the issue was categorized as a non-cited violation. The violation

was held open to verify the revision of the FSAR to accurately. .

i

describe the design basis of the encapsulations,

The current FSAR description of the design basis-of the

encapsulatiuns was reviewed. It accurately described the design

basis. This-item is closed.

b. (Closed) URI 50-302/91-04-01: Review and approval of inadequate .

procedure steps for calibration of reactor vessel level

instruments.

On April 24, 1991, after licensee followup of NRC questions,

errors were identified in the calibration data sheets for reactor

1

level instruments RC-163A-LT and RC-163B-LT, RC-164A-LT-and RC-

l 164B-LT, and RC-201-LT and RC-202-LT. The errors associated with

the calibration status of reactor vessel head level instruments

(RC-164A-LT and RC-164B-LT) was evaluated to be a condition

outside the design basis as referenced in FSAR section 7.3.4.2.1

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and TMI Action Plan item II.F.2. Therefore, the licensee made a

one hour ENS call on May 14,.1991, and submitted LER 91-04 on June

13, 1991.

The licensee attributed the calibration errors to FPC engineering

l personnel who incorrectly transposed calibration data from a

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contractor instrument data sheet. The document apparently did not j

clearly indicate instrument zero. This resulted in the RC-164A-LT

and RC-164B LT level devices measuring the reactor vessel head

stand pipe level rather than the level from hot leg to reactor

head. A modification was implemented in August 1985, (MAR 83-03-

04-02) to meet NRC Order requirements which added these new  :

reactor vessel level monitoring devices.

The licensee verified the instrument calculations and data sheets,

and revised the appropriate SPs (SP-144A, RCITS Reactor Vessel and

Hot Leg Level Channel Calibration; and SP-195, Remote Reactor

Vessel Level Instrumentation Calibration). WRs 283679 and 283680

recalibrated the affected instruments on May 17, 1991 and May 18,

1991, respectively.

Problem Report SYPR-91-0012 was issued to document this issue, to

determine root.cause and to recommend corrective actions. The

licensee determined the level instruments to be operable and

therefore the associated TS action statements (TS 3.3.3.6.b and c

for TS Table 3.3-10 items 21 and 22) were not entered. In

addition, a PRC meeting on May 13, 1991,- reviewed operability and

concluded these in.ctruments to be operable. The basis for this

determination was that tne RC-164A-LT and RC-164B-LT devices would ,

still measure a 'ressel voiding condition as they were monitoring '

the reactor vessel stand pipe level. Also, other instrumentation

was available t<s the operator (e.g., void monitor, core exit

thermocouples and h'st leg level monitor).

The inspector reviewed the LER, the PR, the SPs and WRs, and the

FSAR. The '.nspectJr also discussed this item with licensee

engineerir.g, maintenance, operations and management personnel.

The inspector questioned the licensee's operability determination

since tne licens'se concluded the RC-164A-LT and RC-164B-LT -

instrument calibration was outside the design basis. The design

basis as state 6 in the FSAR and in the THI Action Plan Item II.F.2

was that the level from the reactor vessel hot leg to the vessel

head was to be the measured range. Also, the LER appeared

deficient in that it did not address the related TS issues nor

provide the basis for instrument operability determination. This

issue appears to be mitigated based on the licensee corrective -

actions including instrument re-calibration with four days of

identifying the condition, (well within the seven day TS Action

Statement) and the availability of redundant monitors for

potential core voiding. In addition, this instrument provides an

indication function only and operator implementation -of E0Ps would

direct them to successfully assess a condition of inadequate core

cooling. Also, the licensee was proactive in their corrective

actions in that they reviewed all safety related and NRC

Regulatory Guide 1.97 level instruments for similar type . errors

and none were found. All system engineers were required to review

l this event.

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Based on the above actions, URI 50-302/91-04-01 and LER 91-04 are

considered closed.

Violations or deviations were not identified.

7. Exit Interview

The inspection scope and findings were summarized on November 16, 1992,

with those persons indicated in paragraph 1. The inspectors described

the areas inspected and discussed in detail the inspection results

listed below. Proprietary information is not contained in this report.

Dissenting comments were not received from the licensee.

Item Number Status (Lescrintion and Reference

VIO 50-302/92-27-01 Open Failure to Follow Procedure Results

in Valve Misalignment and Reactor

Building Spray (paragraph 3.a)

VIO 50-302/92-27-02 Open Failure to enter action statement

3.8.1.1 and perform surveillance

requirement 4.8.1.1.1.a with the "B"

emergency diesel generator

inoperable as the result of non-TS

surveillance testing (paragraph 4.a)

UNR 50-302/92-25-01 Closed Followup of inadvertent Actuation of

Reactor Building Spray (paragraph

3.a)

LER 50-302/91-04 Closed Personnel error caused reactor

vessel level required for inadequate

core cooling to be incorrectly

calibrated (paragraph 5.a, 6.b)

LER 50-302/91-05 Closed ECCS pump and flow paths were

secured due to valve leak resulting

in a condition outside the plant

design basis (paragraph 5.b)

LER 50-302/91-10 Closed Wiring problem causes transformer

breakers to open actuating the

emergency diesel generator

(paragraph 5.c)

LER 50-302/91-12 Closed Procedure deficiency leads to

inadvertent emergency diesel

generator actuation during

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engineered safeguards testing

(paragraph 5.d)

.

LER 50-302/92-21 Closed Lack of Required Lube Oil Leakage

Collection lank Reserve Capacity For

Reactor Coolant Pumps Violates 10

CFR 50 Appendix R Design Criteria

(paragraph 5.e)

NCV 50-302/90-32-02 Closed failure to provide adequate design

control measures as required by 10

CFR 50, Aapendix B, Criterinn 111

(paragrap16.a)

URI 50-302/91-04-01 Closed Review and approval of inadequate

procedure steps for calibration of

reactor vessel level instruments

(paragraph 6.b)

8. Acronyms and Abbreviations

AHF - Air Handling fan

ANSI - American National Standards Institute

a.m. - ante meridiem

AP - Administrative Procedure

ASME - American Society of Mechanical Engineers

BS - Reactor Building Spray

B&W - Babcock & Wilcox

BWST - Borated Water Storage Tank

CFR - Code of Federal Regulations

CRDM - Control Rod Drive Motor

DHP - Decay Heat Pump

ECCS - Emergency Core Cooling System (s)

ENS - Emergency Notification System

E0P - Emergency Operating Procedure

EQ - Environmental Qualification

ES - Engineered Safeguards

FPC - Florida Power Corporation

FSAR - Final Safety Analysis Report

gpm - gallons per minute

HPI - High Pressure Injection System

LC0 - Limiting Condition for Operation

LER - Licensee Event Report

MAR - Modification Approval Record

MVP - Makeup and Purification System

NCV - Non-cited Violation

NRC - Nuclear Regulatory Commission

OP - Operating Procedure

p.m. - post meridiem

PR - Problem Report

PRC - Plant Review Committee

RB - Reactor Building

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RCP

- Reactor Coolant Pump

RPS

- Reactor Protection System

RSTS

- Revised Standard Technical Specifications

SE - Safety Evaluation

SP r

- Surveillance Procedure

STI

SW - Short Term Instruction (

TMI - Nuclear Services Closed Cycle Cooling System

TS

- Three Mile Island

- Technical Specification

TSI

URI - Technical Specification Interpretation

- Unresolved Item

V - volt

VIO - Violation

WR - Work Request

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