09-13-2016 | On March 19, 2016, at approximately 1024 Central Daylight Time ( CDT), the Unit 2 High Pressure Coolant Injection System ( HPCI) Steam Admission Valve failed to stroke due to a stuck contactor in the valve motor breaker. This rendered the Unit 2 HPCI inoperable, resulting in a Safety System Functional Failure; however the system had previously been declared inoperable for maintenance and the Unit 2 Reactor Core Isolation Cooling System had been verified as operable in accordance with Technical Specifications Limiting Conditions for Operation 3.5.1. On March 20, 2016, at approximately 1103 CDT, Maintenance personnel commenced work to repair the Unit 2 HPCI steam admission valve motor breaker. On March 21, 2016, at approximately 0245 CDT, Unit 2 HPCI was declared operable following completion of all required PMTS.
The cause of the stuck contactor was accelerated cyclic fatigue due to overheating of the motor starter during packing consolidation and MOVATS testing. Corrective actions were to replace the stuck contactor, to clean contactors in similar HPCI valve motor breakers for Units 1 and 3, to determine an allowable maximum number of valve cycles within a given time period , and to revise plant procedures based on the determined cycle limit in order to prevent contactors from sticking due to accelerated cyclic fatigue.
Subsequent review determined the identified condition to be reportable. |
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Category:Letter
MONTHYEARML24032A4762024-02-0101 February 2024 Final Report of a Part 21 Evaluation Associated with Starter Contactors for the BFN Unit 1 High Pressure Coolant Injection Suppression Pool Inboard Suction Valve ML24023A2802024-01-23023 January 2024 Final Report of a Deviation or Failure to Comply Associated with a Relay in the Reactor Core Isolation Cooling Condensate Pump CNL-24-017, Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure and Emergency Preparedness Department Procedure Revisions2024-01-17017 January 2024 Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure and Emergency Preparedness Department Procedure Revisions ML24016A3042024-01-16016 January 2024 Final Report of a Part 21 Evaluation Associated with Check Valve 0-CKV-023-0565 for D1 Residual Heat Removal Service Water Pump CNL-23-071, Response to Request for Additional Information Regarding Browns Ferry Nuclear Plant, Units 1, 2, and 3, Inservice Inspection and Augmented Program Interval Revised Request for Alternative 0-ISI-472024-01-11011 January 2024 Response to Request for Additional Information Regarding Browns Ferry Nuclear Plant, Units 1, 2, and 3, Inservice Inspection and Augmented Program Interval Revised Request for Alternative 0-ISI-47 ML24022A1732024-01-0303 January 2024 Receipt and Availability of the Subsequent License Renewal Application ML23319A1992024-01-0303 January 2024 Issuance of Amendment Nos. 333, 356, and 316 Regarding the Technical Specification Surveillance Requirements 3.4.3.2 and 3.5.1.11 Regarding Safety Relief Valves ML23355A2062023-12-21021 December 2023 Request for Exemption from Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Implementation ML23348A3942023-12-14014 December 2023 Interim Part 21 Report of a Potential Deviation or Failure to Comply Associated with Starter Contactors for the High Pressure Coolant Injection Suppression Pool Inboard Suction Valve IR 05000259/20230102023-12-11011 December 2023 Commercial Grade Dedication Inspection Report 05000259/2023010 and 05000260/2023010 and 05000296/2023010 ML23335A0722023-12-0101 December 2023 Interim Report of a Deviation or Failure to Comply Associated with a Relay in the Unit 2 Reactor Core Isolation Cooling Condensate Pump ML23334A2492023-11-30030 November 2023 Site Emergency Plan Implementing Procedure Revision CNL-23-070, Submittal of Fifth 10-Year Interval Inservice Testing Program Plan2023-11-29029 November 2023 Submittal of Fifth 10-Year Interval Inservice Testing Program Plan ML23331A2532023-11-27027 November 2023 Summary Report for 10 CFR 50.9 Evaluations, Technical Specifications Bases Changes, Technical Requirement Manual Changes, and NRC Commitment Revisions CNL-23-067, Central Emergency Control Center Emergency Plan Implementing Procedure Revisions2023-11-27027 November 2023 Central Emergency Control Center Emergency Plan Implementing Procedure Revisions ML23325A1102023-11-21021 November 2023 Anchor Darling Double Disc Gate Valve Commitment Revision ML23320A2542023-11-16016 November 2023 Interim Part 21 Report of a Deviation or Failure to Comply Associated with Check Valve 0-CKV-023-0565 for D1 Residual Heat Removal Service Water Pump IR 05000259/20230032023-11-13013 November 2023 Integrated Inspection Report 05000259/2023003, 05000260/2023003 and 05000296/2023003 IR 05000259/20230402023-11-0202 November 2023 Supplemental Inspection Supplemental Report 05000259 2023040 and Follow-Up Assessment Letter ML23292A2532023-10-18018 October 2023 BFN 2024-301, Corporate Notification Letter (210-day Ltr) ML23282A0022023-10-0606 October 2023 Interim Part 21 Report of a Deviation or Failure to Comply Associated with Check Valve 0-CKV-023-0565 for D1 Residual Heat Removal Service Water Pump ML23278A0122023-10-0505 October 2023 Updated Final Safety Analysis Report, Amendment 30 ML23271A1702023-09-28028 September 2023 Site Emergency Plan Implementing Procedure Revision ML23270A0702023-09-26026 September 2023 SLRA Pre-Application Meeting Summary 09-13-2023 ML23257A1232023-09-22022 September 2023 Administrative Changes to Technical Specification Pages Issued for License Amendment Nos. 332, 355, and 315 CNL-23-061, Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure Revision2023-09-20020 September 2023 Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure Revision ML23263B1042023-09-20020 September 2023 Special Report 260/2023-001 for Inoperable Post Accident Monitoring (PAM) Instrumentation ML23205A2132023-09-0808 September 2023 Issuance of Amendment Nos. 332, 355, and 315 Regarding the Revision of Technical Specifications to Adopt TSTF-566-A and TSTF-580-A, Rev. 1 CNL-23-057, Central Emergency Control Center Emergency Plan Implementing Procedure Revisions. Includes CECC-EPIP-1, Revision 76 and CECC-EPIP-9, Revision 642023-09-0505 September 2023 Central Emergency Control Center Emergency Plan Implementing Procedure Revisions. Includes CECC-EPIP-1, Revision 76 and CECC-EPIP-9, Revision 64 IR 05000259/20230052023-08-29029 August 2023 Updated Inspection Plan for Browns Ferry Nuclear Plant, Units 1, 2 and 3 - Report 05000259/2023005, 05000260/2023005 and 05000296/2023005 ML23233A0432023-08-18018 August 2023 Enforcement Action EA-22-122 Inspection Readiness Notification ML23219A1542023-08-17017 August 2023 Request to Use Later Edition of ASME Code for Operation and Maintenance and Alternative Requests BFN-IST-01 Through 05 for the Fifth 10-Year Interval Inservice Testing Program ML23228A1642023-08-16016 August 2023 Site Emergency Plan Implementing Procedure Revision ML23228A0202023-08-15015 August 2023 (BFN) Unit 1 - Special Report 259/2023-001 for Inoperable Post Accident Monitoring (PAM) Instrumentation IR 05000259/20230022023-08-10010 August 2023 Integrated Inspection Report 05000259/2023002, 05000260/2023002, 05000296/2023002 and 07200052/2023001 ML23192A4472023-07-31031 July 2023 Staff Assessment of Updated Seismic Hazards at TVA Sites Following the NRC Process for the Ongoing Assessment of Natural Hazards Information CNL-23-055, Tennessee Valley Authority - Emergency Preparedness Department Procedure Revision. Includes EPDP-3, Revision 3, Emergency Plan Exercises and Preparedness Drills2023-07-25025 July 2023 Tennessee Valley Authority - Emergency Preparedness Department Procedure Revision. Includes EPDP-3, Revision 3, Emergency Plan Exercises and Preparedness Drills ML23171A8862023-07-24024 July 2023 Issuance of Amend. Nos. 331, 354, and 314; 365 and 359 Regarding Adoption of TSTF-541-A, Add Exceptions to Surveillance Requirements for Valves and Dampers Locked in the Actuated Position ML23201A2182023-07-20020 July 2023 Registration of Use of Cask to Store Spent Fuel (MPC-298 and -299) ML23159A2552023-07-20020 July 2023 Proposed Alternative to the Requirements of the ASME Code Regarding Volumetric Inspection of Standby Liquid Control Nozzles ML23199A3072023-07-18018 July 2023 Site Emergency Plan Implementing Procedure Revision CNL-23-053, Tennessee Valley Authority - Radiological Emergency Plan Revisions2023-07-18018 July 2023 Tennessee Valley Authority - Radiological Emergency Plan Revisions IR 05000259/20233012023-07-18018 July 2023 NRC Operator License Examination Report Nos. 05000259/2023301, 05000260/2023301, and 05000296/2023301 2024-02-01
[Table view] Category:Licensee Event Report (LER)
MONTHYEARML20160A0232020-06-0404 June 2020 SR 2020-001-00 for Browns Ferry Nuclear Plant (Bfn),Inoperable Oscillating Power Range Monitor (OPRM) Instrumentation 05000296/LER-2017-0022017-12-29029 December 2017 4kV Shutdown Board Potential Transformer Primary Fuses Do Not Coordinate with Secondary Fuses, LER 17-002-00 for Browns Ferry Nuclear Plant, Unit 3 Regarding 4kV Shutdown Board Potential Transformer Primary Fuses Do Not Coordinate with Secondary Fuses 05000296/LER-2017-0012017-10-31031 October 2017 Inoperable Residual Heat Removal Pump Results in Condition Prohibited by Technical Specifications, LER 17-001-00 for Browns Ferry Nuclear Plant, Unit 3, Regarding Inoperable Residual Heat Removal Pump Results in Condition Prohibited by Technical Specifications 05000260/LER-2017-0042017-07-0707 July 2017 Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints, LER 17-004-00 for Browns Ferry, Unit 2, Regarding Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints 05000260/LER-2017-0032017-05-30030 May 2017 Manual Reactor Scram Initiated During Startup Due to Multiple Rods Inserting, LER 17-003-00 for Browns Ferry Nuclear Plant, Unit 2 Regarding Manual Reactor Scram Initiated During Startup Due to Multiple Rods Inserting 05000259/LER-2017-0022017-04-27027 April 2017 Unauthorized Firearm Introduced into the Protected Area, LER 17-002-00 for Browns Ferry, Unit 1, Regarding Unauthorized Firearm Introduced into the Protected Area 05000260/LER-2017-0022017-04-24024 April 2017 Inoperable Primary Containment Isolation Valve Resulting in Condition Prohibited by Technical Specifications, LER 17-002-00 for Browns Ferry, Unit 2, Regarding Inoperable Primary Containment Isolation Valve Resulting in Condition Prohibited by Technical Specifications 05000260/LER-2017-0012017-04-14014 April 2017 High Pressure Coolant Injection Safety System Functional Failure Due to a Blown Fuse, LER 17-001-00 for Browns Ferry, Unit 2, Regarding High Pressure Coolant Injection Safety System Functional Failure Due to a Blown Fuse 05000259/LER-2016-0022016-09-19019 September 2016 High Pressure Coolant Injection Safety System Functional Failure due to Inoperability of Primary Containment Isolation Valve, LER 16-002-00 for Browns Ferry, Unit 1, Regarding High Pressure Coolant Injection Safety System Functional Failure Due to Inoperability of Primary Containment Isolation Valve 05000260/LER-2016-0022016-09-13013 September 2016 High Pressure Coolant Injection System Failure Due To Stuck Contactor, LER 16-002-00 for Browns Ferry Nuclear Plant, Unit 2, Regarding High Pressure Coolant Injection System Failure Due To Stuck Contactor 05000260/LER-2016-0012016-08-16016 August 2016 High Pressure Coolant Injection Safety System Functional Failure due to a Blown Fuse and a Failed Relay, LER 16-001-00 for Browns Ferry, Unit 2, Regarding High Pressure Coolant Injection Safety System Functional Failure Due to a Blown Fuse and a Failed Relay 05000296/LER-2016-0062016-08-0505 August 2016 1 OF 8, LER 16-006-00 for Browns Ferry Nuclear Plant, Unit 3, Regarding High Pressure Coolant Injection System Found to be Inoperable During Testing 05000259/LER-2016-0012016-06-21021 June 2016 Failure of 4kV Shutdown Board Normal Feeder Breaker Results in Actuations of Emergency Diesel Generators and Containment Isolation Valves, LER 16-001-00 for Browns Ferry, Unit 1, Regarding Failure of 4kV Shutdown Board Normal Feeder Breaker Results in Actuations of Emergency Diesel Generators and Containment Isolation Valves 05000296/LER-2016-0052016-06-17017 June 2016 Automatic Depressurization System Valve Inoperability Exceeded Technical Specification Limits, LER 16-005-00 for Browns Ferry, Unit 3, Regarding Automatic Depressurization System Valve Inoperability Exceeded Technical Specification Limits 05000296/LER-2016-0042016-06-0606 June 2016 Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints, LER 16-004-00 for Browns Ferry, Unit 3, Regarding Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints 05000296/LER-2016-0032016-04-25025 April 2016 Main Steam Isolation Valve Leaking in Excess of Technical Specification Requirements, LER 16-003-00 for Browns Ferry Nuclear Plant Unit 3 Regarding Main Steam Isolation Valve Leaking in Excess of Technical Specification Requirements 05000296/LER-2016-0022016-04-22022 April 2016 Improperly Installed Switch Results in Condition Prohibited by Technical Specifications, LER 16-002-00 for Browns Ferry Nuclear Plant, Unit 3, Regarding Improperly Installed Switch Results in Condition Prohibited by Technical Specifications 05000296/LER-2016-0012016-03-21021 March 2016 Inoperable Residual Heat Removal Pump Results in Condition Prohibited by Technical Specifications and Safety System Functional Failure, LER 16-001-00 for Browns Ferry, Unit 3, Regarding Inoperable Residual Heat Removal Pump Results in Condition Prohibited by Technical Specifications and Safety System Functional Failure 05000260/LER-2015-0022016-03-17017 March 2016 High Pressure Coolant Injection System Inoperable due to Manual Isolation of Steam Leak I, LER 15-002-01 for Browns Ferry, Unit 2, Regarding High Pressure Coolant Injection System Inoperable Due to Manual Isolation of Steam Leak ML1108400352011-03-22022 March 2011 Letter Re Licensee Event Report Which Occurred on December 22, 2010, Concerning Low Pressure Coolant Injection Operability, TVA Expects to Submit a Revised LER by April 15, 2011 ML1015505752010-04-0707 April 2010 Event Notification for Browns Ferry on Spill of Water Containing Tritium ML1015505632008-01-10010 January 2008 Event Notification for Browns Ferry on Offsite Notification - Spill of Water Containing Tritium ML18283B3261978-09-29029 September 1978 LER 1978-205-01 for Browns Ferry, Unit 3 Four Main Steam Isolation Valves Which Exceeded the Leakage Limits of Technical Specification 4.7.A.2.i While Performing Local Leak Rate Testing During Refueling ML18283B3391978-07-25025 July 1978 Licensee Event Report Concerning Excessive Drywell Floor Drain Leak Rate Observed During Normal Operation ML18283B3411978-07-18018 July 1978 Licensee Event Report Concerning an Abnormal Indication on a 4-kV Standby Power Circuit Breaker During Normal Operation ML18283B3401978-07-18018 July 1978 Licensee Event Report Concerning an Outboard Main Steam Isolation Valve, Which Closed Faster than Allowed by Technical Specifications ML18283B3421978-05-31031 May 1978 Licensee Event Report Concerning MSIV 1-38 Which Closed in 1 Second Exceeding Limiting Condition of Operation ML18283A9901978-05-30030 May 1978 LER 1978-010-00 for Browns Ferry Nuclear Plant, Unit 2, Relief Valve on Standby Liquid Control Pump B Opened at 900 Psig (Which Is Lower than Designed Setting of 1425 +/- 75 Psig as Designated by Tech Spec 4.4.A.2.A) During Surveillance Tes ML18283A9911978-05-0909 May 1978 LER 1978-008-00 for Browns Ferry Nuclear Plant, Unit 2, Reactor Building Ventilation Radiation Monitoring Channel Failed During Refueling Outage ML18283A9941978-05-0505 May 1978 LER 1978-009-00 for Browns Ferry Nuclear Plant, Unit 2, Local Leak Rate Tests of All Containment Isolation Valves Where Leak Rate Exceeded Allowable Leak Rate of 60 Percent of La Per 24 Hours or 707.1 Scfh ML18283A9921978-05-0505 May 1978 LER 1978-006-00 for Browns Ferry Nuclear Plant, Unit 2, Check Valve 2-73-603 in High-Pressure Coolant Injection System Was Found in Open Position During Maintenance Inspection After Failing Local Leak Rate Test ML18283B4001978-05-0101 May 1978 LER 1978-010-00 for Browns Ferry Nuclear Plant, Unit 3, Both RBM Channels Which Became Continuously Bypassed During Power Ascension ML18283B4011978-04-28028 April 1978 LER 1978-009-00 for Browns Ferry Nuclear Plant, Unit 3, Smoke Alarm Which Would Not Clear & Was Received for Preaction Sprinkler Zone in Reactor Building During Normal Operation ML18283B4021978-04-28028 April 1978 LER 1978-008-00 for Browns Ferry Nuclear Plant, Unit 3, Relief Valve 3-1-31 Which Failed to Reseat Until Reactor Pressure Reached 280 Psig During Reactor Scram ML18283B4041978-04-24024 April 1978 LER 1978-001-00 for Browns Ferry Nuclear Plant, Unit 3, Torus Oxygen Sensor O2M-76-42, Found to Be Erratic & Did Not Meet Requirements of Tech Spec 4.7.II During Normal Operation, Which Is Superseding Previous Letter of 2/8/1978 ML18283B4031978-04-24024 April 1978 LER 1978-006-00 for Browns Ferry Nuclear Plant, Unit 3, Electrical Connector Carrying Thermocouple Circuits Monitoring Primary Containment Atmospheric Temperature Not Included as Part of Modification Which Qualified Connector Assemblies for ML18283B4051978-04-0404 April 1978 LER 1978-005-00 for Browns Ferry Nuclear Plant, Unit 3, Six CRD Accumulator Level Switches Which Would Not Alarm with Level Increases During Plant Operation While Performing Electrical Maintenance Instruction 50 ML18283B4061978-03-30030 March 1978 LER 1977-012-00 for Browns Ferry Nuclear Plant, Unit 3, Temperature Transients Which Were Experienced with Six Charcoal Adsorber Beds in Offgas System During Normal Operation, Which Is Supplementing Previous Letter of 7/29/1977 ML18283A9951978-03-29029 March 1978 LER 1978-005-00 for Browns Ferry Nuclear Plant, Unit 2, Unidentified Coolant Leakage in Drywall Was Found to Be 9.5 Gpm & Exceeded 5 Gpm Limit of Technical Specification 3.6.C.1. During Normal Operation ML18283B4091978-03-28028 March 1978 LER 1978-004-00 for Browns Ferry Nuclear Plant, Unit 3, Three of Five Test Specimens Failed During Simulated LOCA Conditions & During Qualification Testing of Bendix Electrical Connectors Identical to Those Used in Primary Containment ML18283B4101978-03-22022 March 1978 LER 1977-005-00 for Browns Ferry Nuclear Plant, Unit 3, RPS MG Set a Which Continued Running & MG Set B Output Breaker Which Did Not Trip During Startup Test STI-31, Which Is Supplementing Previous Letter of 3/24/1977 ML18283B4111978-03-10010 March 1978 LER 1978-003-00 for Browns Ferry Nuclear Plant, Unit 3, Valve FCV 3-74-52 Was Found Inoperable During Performance of Surveillance Instruction 4.5.B.1.C ML18283A9961978-02-28028 February 1978 LER 1978-004-00 for Browns Ferry Nuclear Plant, Unit 2, Relief Valve 2-1-5 Opened and Failed to Reseat During Steady State Operation ML18283B4141978-02-28028 February 1978 LER 1978-002-00 for Browns Ferry Nuclear Plant, Unit 3, Bendix Connectors of Type Used Inside Primary Containment Have Failed a Post-Aging Environmental Test at Wyle Laboratory Testing Facility ML18283A9971978-02-15015 February 1978 LER 1978-003-00 for Browns Ferry Nuclear Plant, Unit 2, Relief Valve 2-1-41 Opened and Failed to Reseat During Steady State Operation ML18283B0001978-02-13013 February 1978 LER 1978-002-00 for Browns Ferry Nuclear Plant, Unit 2, Reactor Pressure Switch PS-68-95 Not Functioning as Required by Tech Spec Table 4.2.B During Normal Operation While Performing Surveillance Instruction ST 4.2.B-7 ML18283A9991978-02-0606 February 1978 LER 1978-001-00 for Browns Ferry Nuclear Plant, Unit 2, Surveillance Samples Were Taken from Charcoal in Unit 2 Primary Containment Purge System Following Maintenance Outage ML18283B4161978-02-0606 February 1978 LER 1978-001-00 for Browns Ferry Nuclear Plant, Unit 3, Torus Oxygen Sensor O2M-76-42 Found to Be Erratic & Did Not Meet Requirements of Technical Specification 4.7.H During Normal Operation ML18283B4071977-10-0505 October 1977 LER 1977-012-00 for Browns Ferry Nuclear Plant, Unit 3, Temperature Transients Were Experienced with Six Charcoal Adsorber Beds in Offgas System ML18283B4171977-09-26026 September 1977 LER 1977-017-00 for Browns Ferry Nuclear Plant, Unit 3, Primary Containment Isolation Valve 3-FCV-77-2A on Drywell Floor Drain Sump Pump Discharge Line Would Not Operate as Required by Tech Spec 3.7.D.L During Routine Operability Checks 2020-06-04
[Table view] |
MR!` FARM "ARRA II C NI1119 FAR 12Fa.III ATt112V ratININIICCIAN APPROVED BY OMB: NO. 3150-0104 EXPIRES: 10/31/2018 comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by intemet e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
3. LER NUMBER
2016 - 00 002
I. Plant Operating Conditions Before the Event
At the time of discovery, Browns Ferry Nuclear Plant (BFN), Unit 2, was operating in Mode 1 at approximately 100 percent rated thermal power. BFN, Units 1 and 3, were unaffected by this event.
A. Event:
On March 19, 2016, at approximately 0004 Central Daylight Time (CDT), BFN Operations personnel received a 2-EA-57-117 ground alarm [ALM] during performance of valve diagnostic (MOVATS) testing on the Unit 2 High Pressure Coolant Injection System (HPCI)[BJ] Steam Admission Valve 2-FCV-073-0016. The valve motor breaker [BKR] 2-BKR-073-0016 was opened at 250VDC RMOV Board [ECBD] 2A, Compartment 3D, and the alarm cleared. The thermal overload relay was found tripped, resulting in the alarm, and was reset. At 1024 CDT, Operations attempted to stroke the valve from the Control Room for post-maintenance testing (PMT) using hand switch [HS] 2-HS-073-0016A, and the valve failed to stroke due to a stuck contactor [CNTR] in the breaker.
BFN, Unit 2, had previously entered Technical Specifications (TS) Limiting Conditions for Operation (LCO) 3.5.1, Emergency Core Cooling Systems (ECCS) — Operating. Condition C was entered due to HPCI inoperability for repack of the steam admission valve, with required actions to immediately verify Reactor Core Isolation Cooling (RCIC)[BN] operable by administrative means and restore HPCI to operable status within 14 days. LCO 3.5.1 requires each ECCS injection/spray subsystem and the Automatic Depressurization System (ADS)[SB] function of six safety/relief valves to be operable in reactor Modes 1, 2, and 3 except when HPCI and ADS valves are not required to be operable with reactor steam dome pressure less than or equal to 150 pounds per square inch, gauge (psig). RCIC was verified operable by Operations personnel.
On March 20, 2016, at approximately 1103 CDT, Maintenance personnel commenced work to repair the Unit 2 HPCI steam admission valve motor breaker. Both the 1C and 2C contactors were replaced.
On March 21, 2016, at approximately 0245 CDT, Unit 2 HPCI was declared operable following successful completion of all required PMTS.
II. Description of Events
B. Status of structures, components, or systems that were inoperable at the start of the event and that contributed to the event:
No inoperable systems, structures, or components contributed to this event.
comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by intemet e-mail to Inf000llects.Resource@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
3. LER NUMBER
2016 - 002 - 00
C. Dates and approximate times of occurrences:
March 17, 2016, at 2300 CDT Declared Unit 2 HPCI inoperable for repacking of HPCI steam admission valve.
March 19, 2016, at 1024 CDT Operations personnel unsuccessfully attempted to stroke open Unit 2 HPCI steam admission valve.
March 20, 2016, at 1103 CDT Maintenance personnel commenced work to repair a stuck contactor in the Unit 2 HPCI steam admission valve motor breaker.
March 20, 2016, at 2205 CDT Declared Unit 2 HPCI available. Troubleshooting showed no grounds on Battery Board 2 and the valve opened and closed as expected.
March 21, 2016, at 0245 CDT Declared Unit 2 HPCI operable following successful completion of all required PMTS D. Manufacturer and model number (or other identification) of each component that failed during the event:
The breaker containing the failed contactor was manufactured by General Electric Co.
The manufacturer's part number is THEF124040.
E. Other systems or secondary functions affected:
There were no other systems or secondary systems affected.
F. Method of discovery of each component or system failure or procedural error:
The stuck contactor was discovered when the valve failed to open during MOVATS testing.
G. The failure mode, mechanism, and effect of each failed component, if known:
The 2C contactor in 2-BKR-073-0016 failed due to accelerated cyclic fatigue as a result of overheating of the motor starter during packing consolidation and MOVATS testing.
H. Operator actions:
Operations personnel stationed an Assistant Unit Operator to operate the supply breaker for 2-FCV-73-16 to maintain HPCI available while maintenance personnel performed a ground inspection.
I. Automatically and manually initiated safety system responses:
There were no automatic or manual safety responses associated with this event.
MR!` FARM "ARRA II C NI1119 FAR 12Fa.III ATt112V ratININIICCIAN APPROVED BY OMB: NO. 3150-0104 EXPIRES: 10/31/2018 comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by intemet e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
3. LER NUMBER
2016 - 00 002 Ill. Cause of the event A. The cause of each component or system failure or personnel error, if known:
The cause of the stuck contactor was accelerated cyclic fatigue due to overheating of the motor starter during packing consolidation and MOVATS testing.
B. The cause(s) and circumstances for each human performance related root cause:
No human performance related cause has been identified.
IV. Analysis of the event:
The Tennessee Valley Authority (WA) is submitting this report in accordance with Title 10 of the Code of Federal Regulations (10 CFR) 50.73(a)(2)(v)(D), as any event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident.
This event was the result of accelerated cyclic fatigue due to overheating of the motor starter.
The valve had stroked multiple times for packing consolidation and MOVATS testing prior to the failure. Each valve cycle results in arcing between the motor starter contact surfaces, which causes pitting and burning of the contact surface. Excessive pitting of the contact surfaces can lead to stuck contacts.
The safety function of HPCI is to assure that the reactor is adequately cooled to limit fuel cladding temperature in the event of a small break in the nuclear system and loss of coolant which does not result in rapid depressurization of the reactor vessel.
V. Assessment of Safety Consequences
This event resulted in additional, unplanned inoperability and unavailability of the single train of the BFN, Unit 2, HPCI system. This resulted in the inability of the HPCI system to perform its safety functions, for mitigation of the consequences of an accident, longer than the planned system outage duration. In the event of an emergency, the RCIC system remained operable, and all other ECCS and ADS systems were available during this event to facilitate core cooling. Additionally, this event did not result in BFN, Unit 2, exceeding the fourteen-day limit for HPCI inoperability given in TS LCO 3.5.1.C. Therefore, during the time period that the HPCI system was inoperable, sufficient systems were available to provide the required safety functions to protect the health and safety of the public.
A. Availability of systems or components that could have performed the same function as the components and systems that failed during the event:
During this event, RCIC was verified as operable by Operations personnel. Additionally, all other ECCS and ADS systems remained operable.
MR!` FARM "ARRA II C NI1119 FAR 12Fa.III ATt112V ratININIICCIAN APPROVED BY OMB: NO. 3150-0104 EXPIRES: 10/31/2018 comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by intemet e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
3. LER NUMBER
2016 - 00 002 B. For events that occurred when the reactor was shut down, availability of safety- related systems or components:
This event did not occur when the reactor was shut down.
C. For failure that rendered a train of a safety system inoperable, an estimate of the elapsed time from discovery of the failure until the train was returned to service:
The Unit 2 HPCI system was inoperable due to failure of the contactor from 0004 on March 19, 2016, when the failure was discovered, to 0245 on March 21, 2016, when the system was declared operable following successful completion of all required PMTS for 2-FCV-73-16 and MOVAT testing. This event did not result in BFN, Unit 2, exceeding the fourteen-day limit for HPCI inoperability given in TS LCO 3.5.1.C.
VI. Corrective Actions:
Corrective actions are being managed by TVA's Corrective Action Program (CAP) under Condition Reports (CR) 1160196 and 1199462.
The following corrective actions have been completed:
1. Replaced the stuck contactor for breaker 2-BKR-73-16.
2. Revised MCI-0-000-PCK001 (Generic Maintenance Instructions for Valve Packing) to add the following note:
"If DC MOVs are cycled electrically for packing consolidation, then the starter contactors are to be inspected and burnished (as necessary) prior to returning the valve to service. (This may be conducted following as-left MOVATS testing.) EPI-0-000-MCC001 is to be referred to for guidance on starter contactor inspection and burnishing.
The following corrective actions are in progress:
1. Determine an allowable maximum number of cycles within a given time period to prevent cyclic fatigue of Motor Starters.
2. Revise ECI-0-000-MOV009 (Testing of Motor Operated Valves Using Viper 20) to add a step to this procedure to not exceed the maximum allowable number of cycles within a given period.
3. Revise MCI-0-000-PCK001 to add a step to this procedure to not exceed the maximum allowable number of cycles within a given period.
4. Clean the open and close contactors in 1-BKR-73-16 and 3-BKR-73-16 per EPI-0-000-MCC001 (Maintenance and Inspection of 480V AC and 250V DC Motor Control Centers).
MR!` FARM "ARRA II C NI1119 FAR 12Fa.III ATt112V ratININIICCIAN APPROVED BY OMB: NO. 3150-0104 EXPIRES: 10/31/2018 comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by intemet e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
3. LER NUMBER
2016 - 00 002
VII. Additional Information:
A. Previous Similar Events:
A review of the BFN CAP and Licensee Event Reports (LERs) for Units 1, 2, and 3 revealed no contactor failures resulting in the inoperability of BFN HPCI systems for the last three years.
B. Additional Information:
There is no additional information.
C. Safety System Functional Failure Consideration:
The failed contactor was not part of the planned maintenance being performed during the scheduled LCO. Due to the additional, unplanned inoperability of the HPCI system resulting from the failed contactor, this system was unable to perform its safety function while in a mode of applicability for HPCI.
This event resulted in the inability of the BFN, Unit 2, HPCI system to perform its safety function for mitigation of the consequences of an accident. In accordance with NUREG-1022, this event is considered a safety system functional failure.
D. Scram with Complications Consideration:
This event did not result in a reactor scram.
VIII. COMMITMENTS
There are no new commitments.
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