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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEARML20203L0281986-04-25025 April 1986 Informs of Planned Site Visit to Obtain Info Supporting Implementation of Emergency Response Data Sys,Including Availability of PWR or BWR Parameters in Digital Form & Characterization of Available Data Feed Points 05000237/LER-1983-084, Updated LER 83-084/03X-1:on 831230,during Normal Operation, Primary Containment Oxygen Sample from Torus Alarmed on Low Level Sample Flow.Caused by Sample Line Moisture.Line Drained & Leads reconnected.W/840314 Ltr1984-03-14014 March 1984 Updated LER 83-084/03X-1:on 831230,during Normal Operation, Primary Containment Oxygen Sample from Torus Alarmed on Low Level Sample Flow.Caused by Sample Line Moisture.Line Drained & Leads reconnected.W/840314 Ltr 05000237/LER-1983-080, Supplemental LER 83-080/03X-1:on 831124,offgas Log Rad Monitor 2-1705-A Delivered Offgas High Alarm & High Alarm Spiked & Drifted Downscale.Caused by Burned Out Resistor. Power Supply Installed & Monitor Calibr1983-12-20020 December 1983 Supplemental LER 83-080/03X-1:on 831124,offgas Log Rad Monitor 2-1705-A Delivered Offgas High Alarm & High Alarm Spiked & Drifted Downscale.Caused by Burned Out Resistor. Power Supply Installed & Monitor Calibr ML20081M2021983-11-0202 November 1983 83-037/03L-0:on 831005,during Daily Battery Surveillance, 250-volt Battery Charger Float Voltage Indicated Improper Float Voltage.Caused by Defective Amplifier Board.Defective Board Replaced 05000237/LER-1982-023, Revised Deviation Rept for LER 82-023/03L-0:on 820623, Wrong Assumption Made for Drywell to Torus Differential Pressure.Caused by High Torus Pressure Transmitter 2-1673 Measurement1982-07-23023 July 1982 Revised Deviation Rept for LER 82-023/03L-0:on 820623, Wrong Assumption Made for Drywell to Torus Differential Pressure.Caused by High Torus Pressure Transmitter 2-1673 Measurement ML20147A9091978-09-0808 September 1978 /03L on 780821:during Survey,Dis 250-1,MSL Hi Flow Isolation Switch Psid 3-261-2C Tripped at 135.5 Psid.Caused by Bent Indicator Pointer Dragging Across Face Plate Prohibiting Proper Oper.(Encl to 7809220139) ML20147A9051978-09-0808 September 1978 /03L-0 on 780908:steam Leaking from Ventrom Vent Line.Caused by Cracked Weld.Repaired by Welding Externally. (Encl to 7809220138) ML20147A8941978-09-0808 September 1978 /03L on 780817:room Cooler Fans Failed to Start When Pumps 3B & 3C started.4KV Switchgear 33 & 34 Auxiliary Contacts Were Found Dirty.(Encl to 7809220129) ML20147A7211978-09-0808 September 1978 /01X-1 on 780320:Cracks Found on end-to-pipe Weld on CRD Return Line.Caused by Intermittent to Low Cooling Water Flow Leaving the CRD Nozzle.Pipe Was Removed & Replaced. (Encl to 7809180035) ML20147A7361978-09-0707 September 1978 /01T-0 on 780824:Unit 2 Diesel Failed W/ Diesel Generators 2 & 3 Out of Serv Because Pinion Gear on an Air Start Motor Did Not Engage W/ Diesel Ring Gear.Air Start Motor Replaced. (Encl to 7809180225) ML20147A7891978-08-25025 August 1978 /01X-1 on 780428:During Unit 2 Startup Opers, a LPCI & Core Spray Subsys Were Inadvertantly Rendered Inoper Because Personnel Had Closed LPCI Pump & Discharge Valves on Unit 2 Vice 3.(Encl to 7809180320) 05000237/LER-1950-237, Updated LER 50-237/75-048:on 751007,through-wall Crack Found in Drywell/Torus Nitrogen Purge Line 1604-18.Addl Mods, Including Temp Controlled Isolation Valve Installation, Delayed Until Proposal Review1977-06-10010 June 1977 Updated LER 50-237/75-048:on 751007,through-wall Crack Found in Drywell/Torus Nitrogen Purge Line 1604-18.Addl Mods, Including Temp Controlled Isolation Valve Installation, Delayed Until Proposal Review 05000237/LER-1976-066, Updated LER 76-066/01T-1:on 761113,during Maint Outage,Hpci Injection Valve M02-23018 Found in Closed Position W/Valve Stem Severed.Caused by Mechanical Overstress of Stem.Stem Replaced1977-05-13013 May 1977 Updated LER 76-066/01T-1:on 761113,during Maint Outage,Hpci Injection Valve M02-23018 Found in Closed Position W/Valve Stem Severed.Caused by Mechanical Overstress of Stem.Stem Replaced 05000237/LER-1976-063, Updated LER 76-063/03L-l:on 761003,stack Gas Sample Pump Flow Appeared Abnormally Low.Caused by Collection of Carbon Impeller Vane Products in Pump Cavity & Filter.Pump & Filter Replaced1977-03-0303 March 1977 Updated LER 76-063/03L-l:on 761003,stack Gas Sample Pump Flow Appeared Abnormally Low.Caused by Collection of Carbon Impeller Vane Products in Pump Cavity & Filter.Pump & Filter Replaced 05000237/LER-1976-053, Updated LER 76-053/01T-1:on 760803,util Advised by GE That MAPLHGR Limits in Effect No Longer Considered Sufficiently Conservative at Low Core Flow Rates.Problem Thought to Be ECCS Models Used to Determine Rates1977-01-0303 January 1977 Updated LER 76-053/01T-1:on 760803,util Advised by GE That MAPLHGR Limits in Effect No Longer Considered Sufficiently Conservative at Low Core Flow Rates.Problem Thought to Be ECCS Models Used to Determine Rates 05000000/LER-1950-237, Updated LER 50-237/01L:on 760406,unacceptable Ultrasonic Indication Found on Isolation Condenser safe-end.Caused by Cracks in safe-ends.Cracked safe-end Removed & Sent to Bmcl for Metallographic Analysis1976-07-13013 July 1976 Updated LER 50-237/01L:on 760406,unacceptable Ultrasonic Indication Found on Isolation Condenser safe-end.Caused by Cracks in safe-ends.Cracked safe-end Removed & Sent to Bmcl for Metallographic Analysis 1986-04-25
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20249C8491999-09-30030 September 1999 1999 Third Quarter Rept of Completed Changes,Tests & Experiments Evaluated,Per 10CFR50.59(b)(2), for Dresden Nuclear Power Station. with ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20210R6081999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Dresden Nuclear Power,Units 1,2 & 3.With ML20209E1291999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20209J3481999-06-30030 June 1999 1999 Second Quarter Rept of Completed Changes,Tests & Experiments, Per 10CFR50.59.With ML20210D3071999-06-30030 June 1999 Corrected Page 8 to MOR for June 1999 for DNPS Unit 3 ML20195G6381999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20195B2591999-05-19019 May 1999 Rev 66a to CE-1-A,consisting of Proposed Changes to QAP for Dnps,Qcs,Znps,Lcs,Byron & Braidwood Stations ML20206N2821999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20206B1901999-03-31031 March 1999 First Quarter Rept of Completed Changes,Tests & Experiments Per 10CFR50.59 for Dresden Nuclear Power Station. with ML20205N7491999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20207M6921999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20207E9311999-02-26026 February 1999 Part 21 Rept Re Sprague Model TE1302 Aluminum Electrolytic Capacitors with Date Code of 9322H.Caused by Aluminum Electrolytic Capacitors.Affected Capacitors Replaced ML20199M0891999-01-22022 January 1999 Part 21 Rept Re Failure of Square Root Converters.Caused by Failed Aluminum Electrolytic Capacitory Spargue Electric Co (Model Number TE1302 with Mfg Date Code 9322H).Sent Square Root Converters Back to Mfg,Barker Microfarads,Inc ML20199D3261998-12-31031 December 1998 10CFR50.59 SER for 1998-04 Quarter, of Changes,Tests & Experiments.With ML20199C8951998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Dnps,Units 1,2 & 3 ML20205M7061998-12-31031 December 1998 Unicom Corp 1998 Summary Annual Rept. with ML20197G8591998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Dresden Nuclear Power Station.With ML20196A4191998-11-19019 November 1998 Safety Evaluation Accepting QA TR CE-1-A,Rev 66 Re Changes in Independent & Onsite Review Organization by Creating NSRB ML20196J0061998-11-19019 November 1998 Rev 66 to Topical Rept CE-1-A, QA Program ML20195D2861998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Dresden Nuclear Power Station.With ML20154L3681998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20154N4131998-09-30030 September 1998 1998 Third Quarter 10CFR50.59 Rept, for Dresden Nuclear Power Station of Completed Changes,Tests & Experiments ML20153C5061998-09-21021 September 1998 SER Accepting Qualified Unit 1 Supervisor Initial & Continuing Training Program for Dresden Nuclear Power Station,Unit 1 ML20151Y2711998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20237E2331998-08-21021 August 1998 Revised Pages of Section 20 of Rev 66 to CE-1-A, QA Topical Rept ML20237A7161998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Dresden Nuclear Power Station,Units 1,2 & 3 ML20236Q5851998-06-30030 June 1998 1998 Second Quarter 10CFR50.59 Rept, for Dresden Nuclear Power Station of Completed Changes,Tests & Experiments ML20236F8131998-06-30030 June 1998 Rev 0 to Defueled SAR Dresden Nuclear Power Station Unit 1 Commonwealth Edison Co ML20236T8331998-06-30030 June 1998 COLR for Dresden Station Unit 3,Cycle 15 ML20236T8391998-06-30030 June 1998 Rev 1 to EMF-96-141, Dresden Unit 3 Cycle 15 Reload Analysis Rept ML20236M6041998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Dresden Nuclear Power Station,Units 1,2 & 3 ML20248M3021998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Dresden Nuclear Power Station,Units 1,2 & 3 ML20248F3531998-05-21021 May 1998 Part 21 Rept Re Electronic Equipment Repaired or Reworked by Integrated Resources,Inc from Approx 930101-980501.Caused by 1 Capacitor in Each Unit Being Installed W/Reverse Polarity. Policy of Second Checking All Capacitors Is Being Adopted ML20247F3391998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Dresden Nuclear Power Station,Units 1,2 & 3 ML20217D0281998-04-22022 April 1998 Part 21 Rept Re Additive Constants Used in MCPR Determination for Siemens ATRIUM-9B Fuel by Core Monitoring Sys Were Found to Be non-conservative.SPC Personnel Notified All Customers w/ATRIUM-9B Lead Test Assemblies ML20216D4411998-03-31031 March 1998 First Quarter Rept of Completed Changes,Tests & Experiments for 10CFR5059 ML20216C9651998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Dresden Nuclear Power Station,Units 1,2 & 3 ML20216E2531998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Dresden Nuclear Power Station ML20202F7831998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Dresden Nuclear Power Station ML20199K1651998-01-23023 January 1998 Rev 65h to Topical Rept CE-1-A, Comm Ed QA Tr ML20198P5321997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Dresden Nuclear Power Station ML20198P7021997-12-31031 December 1997 Fourth Quarter Rept of Completed Changes,Tests & Experiments Per 10CFR50.59 ML20216D3611997-12-31031 December 1997 Unicom Corp 1997 Summary Annual Rept ML20203F8781997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Dresden Nuclear Power Station ML20199B0701997-10-31031 October 1997 Monthly Operating Repts for Oct 1997 for Dresden Nuclear Power Station ML20217H7201997-09-30030 September 1997 Monthly Operating Repts for Sept 1997 for Dresden Nuclear Power Station,Units 1,2 & 3 ML20210V2401997-09-19019 September 1997 Rev 65g to Topical Rept CE-1-A, Comm Ed QA Manual ML20216J3781997-08-31031 August 1997 Monthly Operating Repts for Aug 1997 for DNPS ML20210H5511997-07-31031 July 1997 Monthly Operating Repts for July 1997 for DNPS IAW RG 1.16 & GL 97-02 1999-09-30
[Table view] |
LER-2076-066, Updated LER 76-066/01T-1:on 761113,during Maint Outage,Hpci Injection Valve M02-23018 Found in Closed Position W/Valve Stem Severed.Caused by Mechanical Overstress of Stem.Stem Replaced |
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2372076066R00 - NRC Website |
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CONTROL BLOCC
. . Previous Report Date: 11/23/76
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EVENT DESCR;PTION
- HE I During a weekend maintenance outage, HPCI injection valve M02-2301-8 was found to be in -
7 89 Q l the closed position with its valve stem severed. The valve was last observed to '
7 89 g l function properly during the previous refueling outage. The valve is located in the b 7 89 gg l "X-Area", which is not routinely accessible during operation. From the beginning of "
7 89 Ql this fuel cycle until 10/12/76, the valve was cycled on a monthly basis with proper sYsTEu ' cAust couEmf (continued) C CCCE CCMacumi CCCE COMPCNENT CODE SUPPUER MANUNTurut VOLATON
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[ Cl 6l 6l 5l 47 lN l 48 CAUSE DESCR;PTION l The original Licensee Event Report described the failure of the HPCI M0-2-2301-8 ,
7 89 g l valve stem and the immediate corrective ae_ tion associated with the event. This 65 7 89 Ml supplemental report documents the results of tests performed on the damaged valve '{
7 89 sacuTY 60 STATUS 4 POWER OTHEA STATUS utTuoO cr - (continued)
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l l EVENT DESCRIPTION (continued) i control room position indication. On 10/12/76, valve 2301-8 was taken out of service in the open position (according to position Indication) In order to isolate a 250V DC ground which was present only when the valve was closed. The HPCI pump discharge line was then isolated by closing valve 2301-9 This is not a repetitive occurrence.
(50-237/1976-66) l l CAUSE DESCRIPTION (continued) stem by Commonwealth Edison's Operational Analysis Department and the final corrective action taken to repair the valve.
Examination of the Dresden Unit 2 HPCI valve stem (M0' 2-2301-8) indicates that the failure was not material-related but was a one time mechanical overstress of the stem. Utilizing macro-photographic and electron microscope fractographic techniques, coupled with a chemical analysis of the valve stem, it was determined that approximately sixty (60) percent of the.facture surface separated by the quasi-cleavage mode, and forty (40) percent failed in shear. The shear portion of the fracture is thought to have occurred during bending of the valve stem when the torque switch momentarily remained energized, after the valve seated. Because of moisture accumulation in the valve operator, with 40% of the cross section fractured and the valve stem severely bent, final through-fracture occurred during the next attempted backseat cycle.
During a planned 5 day Unit 2 outage beginning on March 16, 1977, the HPCI M02-2301-8 valve was disassembled and the failed valve stem was replaced. While the valve was disassembled, a visual code examination of the valve body and internals, including the seating faces, was satisfactorily canpleted. The examined components were found free of any detectable erosion, corrosion, or mechanical adamage. In addition, during the same outage period tr.e junction boxes and conduits in the "X-Area: were sealed to prevent a possible recurrence. '
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. SUPPLEMENT TO DVR -
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.: STA utilT. YEAR NO.
- D- 12 - 2 - 76 - 102 PART l l TITLE OF EVEtiT OCCU?. RED 11/13/76 0930 Failure of 2-2301-8 Valve stem DATE TIME ,
REASON FOR SUPPLEME 4TAL REPORT To report results of ter.ts or. valve stem and to document final corrective action to repair the va'Ive.
PART 2 l J
ACCEPTANCE BY STAT 10tl REVIEV @j ,f wp ,)
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/ '.>-1 DATE 6h ot [ l') /
p,y , , . .
.$[Q !77, SUPPLEttENTAL REPORT APPROVED ,
AllD AUTHORIZED FOR DISTRIBUT10tl f /,,~d fgj ff ).
. NTATIOWSUPERitiTE!GEtiT / 'DATE O
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Comman$lth Edison (
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.. Dresden Nuclear Power St: tion ,
I .- R.R. #1 Morris, i;tinois 60450 Telephone 815/942-2920 BBS Ltr. No.77-424 May 9, 1977 Mr. James G. Keppler, Regional Director Directorate of Regulatory Operations - Region lli JEgmg U. 3. Nuclear Regulatory Commiss!on 799 Roosevelt Road Glen Ellyn, Illinois 6013/
Enclosed please find an update report to Repo,rtable Occurrence report number 50-237/1976-66. This report is being submitted to your office in accordance with the Dresden Nuclear Power Station Technical Specifications, Section 6.6.B.
/A r
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- f M
. . Stephenson Station Superintendent Dresden Nuclear Power Station BBS:sm Enclosure cc: Director of Inspection & Enforcement Director of Management i nformation & Program Control File /NRC -
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05000237/LER-1976-053, Updated LER 76-053/01T-1:on 760803,util Advised by GE That MAPLHGR Limits in Effect No Longer Considered Sufficiently Conservative at Low Core Flow Rates.Problem Thought to Be ECCS Models Used to Determine Rates | Updated LER 76-053/01T-1:on 760803,util Advised by GE That MAPLHGR Limits in Effect No Longer Considered Sufficiently Conservative at Low Core Flow Rates.Problem Thought to Be ECCS Models Used to Determine Rates | | 05000237/LER-1976-063, Updated LER 76-063/03L-l:on 761003,stack Gas Sample Pump Flow Appeared Abnormally Low.Caused by Collection of Carbon Impeller Vane Products in Pump Cavity & Filter.Pump & Filter Replaced | Updated LER 76-063/03L-l:on 761003,stack Gas Sample Pump Flow Appeared Abnormally Low.Caused by Collection of Carbon Impeller Vane Products in Pump Cavity & Filter.Pump & Filter Replaced | | 05000237/LER-1976-066, Updated LER 76-066/01T-1:on 761113,during Maint Outage,Hpci Injection Valve M02-23018 Found in Closed Position W/Valve Stem Severed.Caused by Mechanical Overstress of Stem.Stem Replaced | Updated LER 76-066/01T-1:on 761113,during Maint Outage,Hpci Injection Valve M02-23018 Found in Closed Position W/Valve Stem Severed.Caused by Mechanical Overstress of Stem.Stem Replaced | |
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