ML20084A215

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RO 50-237/76-66:on 761113,HPCI Sys Injection Valve 2-2301-8 Failed.Valve Repairs to Be Completed at Next Outage
ML20084A215
Person / Time
Site: Dresden Constellation icon.png
Issue date: 12/13/1976
From: Abrell G
COMMONWEALTH EDISON CO.
To: Ziemann D
Office of Nuclear Reactor Regulation
Shared Package
ML20084A199 List:
References
RO-50-237-76-66, NUDOCS 8304050131
Download: ML20084A215 (2)


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December 13, 1976 i

111 SEC N C -20 p'O Q]%[fkID%

Director of Nuclear Reactor Regulation C

11 Attn:

Mr. Dennis L. Ziemann, Chief Operating Reactors - Branch 2 Division of Operating Reactors

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U.S. Nuclear Regulatory Commission

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Washington, D.C.

20555

Subject:

Dresden Station Unit 2 High Pressure Coolant Injection (HPCI)

System Flow Testing 7

NRC Docket No. 50-237 OQ<

p Reference (a) :

Dresden Station Reportable Occurrence No. 50-237/76-66.

Daar Mr. Ziemann:

Reference (a) reported the failure of the high pressure coolant injection (HPCI) system injection valve 2-2301-8.

In order to maintain the HPCI system operability, this valve has been placed in the open po-sition.

Although thic line-up maintains the injection capability of the HPCI system, it makes more difficult the complete surveillance flow testing.

Section 4.5.C.1 requires flow testing at reactor vessel pressure between 1150 and 150 psig.

Although no interval is specified for this flow testing in the Technical Specifications, this flow testing has b een conducted routinely on a quarterly basis.

The flow test conducted during this quarter included the usual run at 900 psig vessel pressure but the 1150 psig test was deferred.

This test was not conducted at this time in order to avoid the possibility of injecting the HPCI into the vessel.

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The HPCI water supply is from the storage tank and is cold, oxygenated 88 water.

Although of react'or quality in terms of its chemistry, it is y

not desirable to inject this water into the vessel under operating con-

,o ditions considering feedwater thermal cycles, accelerated corrosion due gg to oxygenated water, and the potantial for a flux spike.

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Conducting the flow test at 900 psig provides adequate assurance om of the HPCI operability when the measured parameters of pump flow, pump OOm pressure, and turbine speed are compared to previous test results.

This shows that the pump is operating on its established performance curve.

I Past operating history reveals no significant deterioration of the pump and turbine performance since 1970, certainly no deteriora &on, ti fo COPY SENT REGION + ~

12835 N

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(] Comm:nwrith Edison C y

Mr. Dennis L.

Ziemann December 13, 1976 1

is to be expected in the interim period until full pressure testing is resumed.

Repairs of the 2-2301-8 motor operated valve is to be completed at the next outage of approximately three days duration which will This occur in any case in late April at a hydraulic snubber inspection.

means that possibly one additional abbreviated flow test will be conducted prior to complete the restoration of the system on our present quarterly flow testing schedule.

One (1) signed original and 39 copies are provided for your use.

Very truly yours, b

Q'

~ G. A. Abrell Nuclear Licensing Administrator Boiling Water Reactors

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