Semantic search

Jump to navigation Jump to search
 Issue dateTitleTopic
ML20203L02825 April 1986Informs of Planned Site Visit to Obtain Info Supporting Implementation of Emergency Response Data Sys,Including Availability of PWR or BWR Parameters in Digital Form & Characterization of Available Data Feed PointsBackfit
05000237/LER-1983-084, Updated LER 83-084/03X-1:on 831230,during Normal Operation, Primary Containment Oxygen Sample from Torus Alarmed on Low Level Sample Flow.Caused by Sample Line Moisture.Line Drained & Leads reconnected.W/840314 Ltr14 March 1984Updated LER 83-084/03X-1:on 831230,during Normal Operation, Primary Containment Oxygen Sample from Torus Alarmed on Low Level Sample Flow.Caused by Sample Line Moisture.Line Drained & Leads reconnected.W/840314 Ltr
05000237/LER-1983-080, Supplemental LER 83-080/03X-1:on 831124,offgas Log Rad Monitor 2-1705-A Delivered Offgas High Alarm & High Alarm Spiked & Drifted Downscale.Caused by Burned Out Resistor. Power Supply Installed & Monitor Calibr20 December 1983Supplemental LER 83-080/03X-1:on 831124,offgas Log Rad Monitor 2-1705-A Delivered Offgas High Alarm & High Alarm Spiked & Drifted Downscale.Caused by Burned Out Resistor. Power Supply Installed & Monitor Calibr
ML20081M2022 November 198383-037/03L-0:on 831005,during Daily Battery Surveillance, 250-volt Battery Charger Float Voltage Indicated Improper Float Voltage.Caused by Defective Amplifier Board.Defective Board Replaced
05000237/LER-1982-023, Revised Deviation Rept for LER 82-023/03L-0:on 820623, Wrong Assumption Made for Drywell to Torus Differential Pressure.Caused by High Torus Pressure Transmitter 2-1673 Measurement23 July 1982Revised Deviation Rept for LER 82-023/03L-0:on 820623, Wrong Assumption Made for Drywell to Torus Differential Pressure.Caused by High Torus Pressure Transmitter 2-1673 Measurement
ML20147A9098 September 1978/03L on 780821:during Survey,Dis 250-1,MSL Hi Flow Isolation Switch Psid 3-261-2C Tripped at 135.5 Psid.Caused by Bent Indicator Pointer Dragging Across Face Plate Prohibiting Proper Oper.(Encl to 7809220139)
ML20147A9058 September 1978/03L-0 on 780908:steam Leaking from Ventrom Vent Line.Caused by Cracked Weld.Repaired by Welding Externally. (Encl to 7809220138)
ML20147A8948 September 1978/03L on 780817:room Cooler Fans Failed to Start When Pumps 3B & 3C started.4KV Switchgear 33 & 34 Auxiliary Contacts Were Found Dirty.(Encl to 7809220129)
ML20147A7218 September 1978/01X-1 on 780320:Cracks Found on end-to-pipe Weld on CRD Return Line.Caused by Intermittent to Low Cooling Water Flow Leaving the CRD Nozzle.Pipe Was Removed & Replaced. (Encl to 7809180035)
ML20147A7367 September 1978/01T-0 on 780824:Unit 2 Diesel Failed W/ Diesel Generators 2 & 3 Out of Serv Because Pinion Gear on an Air Start Motor Did Not Engage W/ Diesel Ring Gear.Air Start Motor Replaced. (Encl to 7809180225)
ML20147A78925 August 1978/01X-1 on 780428:During Unit 2 Startup Opers, a LPCI & Core Spray Subsys Were Inadvertantly Rendered Inoper Because Personnel Had Closed LPCI Pump & Discharge Valves on Unit 2 Vice 3.(Encl to 7809180320)
05000237/LER-1950-237, Updated LER 50-237/75-048:on 751007,through-wall Crack Found in Drywell/Torus Nitrogen Purge Line 1604-18.Addl Mods, Including Temp Controlled Isolation Valve Installation, Delayed Until Proposal Review10 June 1977Updated LER 50-237/75-048:on 751007,through-wall Crack Found in Drywell/Torus Nitrogen Purge Line 1604-18.Addl Mods, Including Temp Controlled Isolation Valve Installation, Delayed Until Proposal Review
05000237/LER-1976-066, Updated LER 76-066/01T-1:on 761113,during Maint Outage,Hpci Injection Valve M02-23018 Found in Closed Position W/Valve Stem Severed.Caused by Mechanical Overstress of Stem.Stem Replaced13 May 1977Updated LER 76-066/01T-1:on 761113,during Maint Outage,Hpci Injection Valve M02-23018 Found in Closed Position W/Valve Stem Severed.Caused by Mechanical Overstress of Stem.Stem Replaced
05000237/LER-1976-063, Updated LER 76-063/03L-l:on 761003,stack Gas Sample Pump Flow Appeared Abnormally Low.Caused by Collection of Carbon Impeller Vane Products in Pump Cavity & Filter.Pump & Filter Replaced3 March 1977Updated LER 76-063/03L-l:on 761003,stack Gas Sample Pump Flow Appeared Abnormally Low.Caused by Collection of Carbon Impeller Vane Products in Pump Cavity & Filter.Pump & Filter Replaced
05000237/LER-1976-053, Updated LER 76-053/01T-1:on 760803,util Advised by GE That MAPLHGR Limits in Effect No Longer Considered Sufficiently Conservative at Low Core Flow Rates.Problem Thought to Be ECCS Models Used to Determine Rates3 January 1977Updated LER 76-053/01T-1:on 760803,util Advised by GE That MAPLHGR Limits in Effect No Longer Considered Sufficiently Conservative at Low Core Flow Rates.Problem Thought to Be ECCS Models Used to Determine Rates
05000000/LER-1950-237, Updated LER 50-237/01L:on 760406,unacceptable Ultrasonic Indication Found on Isolation Condenser safe-end.Caused by Cracks in safe-ends.Cracked safe-end Removed & Sent to Bmcl for Metallographic Analysis13 July 1976Updated LER 50-237/01L:on 760406,unacceptable Ultrasonic Indication Found on Isolation Condenser safe-end.Caused by Cracks in safe-ends.Cracked safe-end Removed & Sent to Bmcl for Metallographic Analysis