ML17309A124

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LER 81-002/03L-0:on 810109,safety Injection Pump C Did Not Start W/Bus Breaker 16.Probable Cause Due to Breaker in off-set Position.Personnel to Be Instructed in Proper Breaker Alignment
ML17309A124
Person / Time
Site: Ginna Constellation icon.png
Issue date: 01/30/1981
From: BELUKE S R
ROCHESTER GAS & ELECTRIC CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML17258A757 List:
References
LER-81-002-03L, LER-81-2-3L, NUDOCS 8102050598
Download: ML17309A124 (2)


Text

NRC FOQM 366 I7.77)2~o 7 8 CON'T~01 1 QB 0 1 3 0 8 1 OB 74 75 REPORT DATE 80~LQR 0 8 0 0 0 2 4 4 Q2 0 1 0 9 8~60 61 DOCKET NUMBER 68 69 EVENT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q10 During test C SL pŽp did not start with bus 16 breaker.(T.S.3.3.l.1c).The C pump 7 8 U.S.NUCLEAR REGULATORY COMMISSION 8 1-002/03 L-0 QL[CENSEE EVENT REPORT((BR 1228)CONTROL BLOCK: Q1 (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)

I 6 N Y R 8 G 1 Q2 0 0-0 0 0 0 0-0 0 Q3 4 1 1 1 1QR~QR 9 LICENSEE CODE 14 15 LICENSE NUMBER 25 26 LICENSE TYPE 30 57 CAT 58 had been proven operable using bus 14 breaker during this test as well as the other 2 4 pumps~After examining breaker for position breaker was fully racked out, then fully racked in, and operation proved successful.

~OB~O7 I~OB 7 8 9 80 l jzz 7;8 SYSTEM~CAUSE CAUSE COMP.VALVE CODE CODE SUBCODE COMPONENTCODE SUBCODE SUBCODE~SF Q>>E Q12~Q13 C K T 8 K R Q4~BQ>>~2Q18 9 10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION LF RIRD EVENT YEAR REPORT NO.CODE TYPE NO.Q12 RRRRRR~81 Q~00 2 QZ~03 QL I=I 0 21 22 23 24 26 27 28 29 30 31 32 ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT NPRDX PRIME COMP.COMPONENT TAKEN ACTION ON PLANT METHOD HOURS O22 SUBMITTED FORM SUB.SUPPLIER MANUFACTURER

~ROIS~HOB~ZO20 gJO2'~023~O24~026 33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS 027 o Breaker possibly in"off-set" position indicated by positioning device pin not moving freely in positioning stop bracket fully-racked-in slot~At next test electricians to examine breaker before closing and after opening.Training in proper breaker align-I~12 3 ment and reporting rack-in problems will be emphasized.

Breaker is Westinghouse 4 DB-50 air circuit breaker, 500 amp.80 DISCOVERY DESCRIPTION Q32 Surveillance test 80 LOCATION OF RELEASE Q NA 80 80 80 80 NRC USE ONLY 68 69 80 o PHDNE 315/524-4446, ext.318 NAME oF PREPARER Stuart R.Beluke 7 8 9 FACILITY~30-METHOD OF STATUS%POWER OTHERSTATUS

~DISCOVERY~15 8 Q28~0Q28 N8~~Q31 7 8 9 10 12 13 44 45 46 ACTIVITY CONTENT RELEASED OF RELEASE AMOUNT OF ACTIVITY Q 6~Z Q33~ZO34 NA 7 8 9 10 44 45 PERSONNEL EXPOSURES NUMBER~TYPE DESCRIPTION O39 1~00 0Q32 ZQ38.N8 7 8 9 11 12 13 PERSONNEL INJURIES 7 8 9 11 12 LOSS OF-OR DAMAGE TO FACILITY Q43 4 TYPE DESCRIPTION 9~Z 042 NA 8 9 10 PUBLICITY ISSUED DESCRIPTION

~B ego so5 o~'4 NA 7 8 9 10 (L J 1