05000244/LER-1981-002-03, /03L-0:on 810109,safety Injection Pump C Did Not Start W/Bus Breaker 16.Probable Cause Due to Breaker in off-set Position.Personnel to Be Instructed in Proper Breaker Alignment

From kanterella
(Redirected from ML17309A124)
Jump to navigation Jump to search
/03L-0:on 810109,safety Injection Pump C Did Not Start W/Bus Breaker 16.Probable Cause Due to Breaker in off-set Position.Personnel to Be Instructed in Proper Breaker Alignment
ML17309A124
Person / Time
Site: Ginna Constellation icon.png
Issue date: 01/30/1981
From: Beluke S
ROCHESTER GAS & ELECTRIC CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML17258A757 List:
References
LER-81-002-03L, LER-81-2-3L, NUDOCS 8102050598
Download: ML17309A124 (2)


LER-1981-002, /03L-0:on 810109,safety Injection Pump C Did Not Start W/Bus Breaker 16.Probable Cause Due to Breaker in off-set Position.Personnel to Be Instructed in Proper Breaker Alignment
Event date:
Report date:
2441981002R03 - NRC Website

text

NRC FOQM 366 I7.77) 2

~o 7

8 CON'T

~01 1

QB 0

1 3

0 8

1 OB 74 75 REPORT DATE 80

~LQR 0

8 0

0 0

2 4

4 Q2 0

1 0

9 8

~

60 61 DOCKET NUMBER 68 69 EVENT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q10 During test C SL p'pdid not start with bus 16 breaker.

(T.S. 3. 3. l. 1c).

The C pump 7

8 U. S. NUCLEAR REGULATORY COMMISSION 8 1-002/03 L-0 QL[CENSEE EVENT REPORT

(( BR 1228)

CONTROL BLOCK:

Q1 (PLEASE PRINT OR TYPE ALLREQUIRED INFORMATION)

I 6

N Y R

8 G

1 Q2 0

0

0 0

0 0

0

0 0

Q3 4

1 1

1 1QR~QR 9

LICENSEE CODE 14 15 LICENSE NUMBER 25 26 LICENSE TYPE 30 57 CAT 58 had been proven operable using bus 14 breaker during this test as well as the other 2 4

pumps

~

After examining breaker for position breaker was fully racked out, then fully racked in, and operation proved successful.

~OB

~O7 I ~OB 7

8 9

80 ljzz 7;

8 SYSTEM

~

CAUSE

CAUSE COMP.

VALVE CODE CODE SUBCODE COMPONENTCODE SUBCODE SUBCODE

~SF Q>>

E Q12

~Q13 C

K T

8 K

R Q4

~BQ>>

~2Q18 9

10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION LF RIRD EVENT YEAR REPORT NO.

CODE TYPE NO.

Q12 RRRRRR ~81 Q

~00 2

QZ

~03 QL I=I 0

21 22 23 24 26 27 28 29 30 31 32 ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT NPRDX PRIME COMP.

COMPONENT TAKEN ACTION ON PLANT METHOD HOURS O22 SUBMITTED FORM SUB.

SUPPLIER MANUFACTURER

~ROIS ~HOB

~ZO20 gJO2'

~ 023

~O24 ~ 026 33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS 027 o

Breaker possibly in "off-set" position indicated by positioning device pin not moving freely in positioning stop bracket fully-racked-in slot ~

At next test electricians to examine breaker before closing and after opening.

Training in proper breaker align-I ~12 3

ment and reporting rack-in problems will be emphasized.

Breaker is Westinghouse 4

DB-50 air circuit breaker, 500 amp.

80 DISCOVERY DESCRIPTION Q32 Surveillance test 80 LOCATIONOF RELEASE Q NA 80 80 80 80 NRC USE ONLY 68 69 80 o

PHDNE 315/524-4446, ext. 318 NAME oF PREPARER Stuart R. Beluke 7

8 9

FACILITY

~30

- METHOD OF STATUS

% POWER OTHERSTATUS ~

DISCOVERY

~15 8

Q28 ~0Q28 N8

~~Q31 7

8 9

10 12 13 44 45 46 ACTIVITY CONTENT RELEASED OF RELEASE AMOUNTOF ACTIVITYQ 6

~Z Q33

~ZO34 NA 7

8 9

10 44 45 PERSONNEL EXPOSURES NUMBER

~

TYPE DESCRIPTION O39 1 ~00 0Q32 ZQ38 N8 7

8 9

11 12 13 PERSONNEL INJURIES 7

8 9

11 12 LOSS OF-OR DAMAGETO FACILITYQ43 4

TYPE

DESCRIPTION

9

~Z 042 NA 8

9 10 PUBLICITY ISSUED DESCRIPTION ~B ego so5 o ~'4 NA 7

8 9

10

(L J

1