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Category:ABNORMAL OCCURRENCE REPORTS (SEE ALSO LER & RO)
MONTHYEARML20084N6461977-03-31031 March 1977 Followup AO 50-249/75-44A:on 751125,offgas Activity Increased.Ge Insp Revealed Major Defect in Fuel Assembly DD-418.Assembly Removed from Reactor ML20084E3631976-06-29029 June 1976 Supplemental AO 50-237/75-11A:on 750127,core Spray Injection Line through-wall Cracks Discovered.Stainless Steel Portion of Core Spray Piping from Vessel Nozzle to Second Isolation Valve Replaced w/SA-333 Grade 6 Carbon Steel ML20084N6831976-06-29029 June 1976 Supplemental AO 50-249/1975-42A:motor Operated Valve 3-1501-5D Failed to Open During Testing Due to Thermal Overload Trip.Caused by Undersized Overload Heaters.Overload Heater Will Be Replaced W/Larger Capacity Unit ML20084D1191976-04-13013 April 1976 AO 50-237/75-39A:on 750612,diesel Generator Experienced Starting Failures.Possibly Caused by Two Gouged & Burred Areas on Ring Gear.Ring Gear Repaired ML20084D1541976-01-14014 January 1976 AO 50-237/75-38A Supplementing AO-50-237/75-38 Re Failure of MO-2-1301-2 Valve to Operate.Apparently Caused by Excessive Cycling of Valve.Valve Stem Probably Experienced Metal Fatigue Due to Multiple Actuations ML20090E4581975-12-17017 December 1975 Supplemental AO 50-237/75-44:diesel Generator Failed to Start.Caused by Air Relay Valve Failure Due to Sticking O-rings.O-rings Replaced ML20084N6541975-12-11011 December 1975 AO 50-249/75-44:on 751125,offgas Increase Exhibited Which May Have Represented Abnormal Degradation of Fuel Cladding.Cause Unknown.Investigation Underway ML20090E4321975-11-20020 November 1975 AO 50-237/75-52:on 751116,MSIV AO 2-203-1C Closing Time Found Below Tech Spec Section 3.7.D.1.Caused by Out of Adjustment Hydraulic Bleedoff Valve.Bleedoff Valve Readjusted ML20090E4751975-11-0606 November 1975 AO 50-237/75-51:on 751031,torus Water Level Exceeded Tech Spec Limit During HPCI Sys Surveillance.Caused by Operator Failure to Verify Proper Valve Lineup.Water Pumped from Torus Until Level Dropped Below Tech Spec Limits ML20084N6881975-10-20020 October 1975 AO 50-249/75-42:on 750920,motor Operated LPCI Suction Valve 3-1501-5D Failed to Open Twice During Testing. Apparently Caused by Defective Valve Motor.Valve Motor Will Be Replaced ML20090E4781975-10-17017 October 1975 AO 50-237/75-49:on 751009,LPCI Loop Selection Logic Circuitry Failed to Select Preferred B Loop.Caused by Out of Calibr Differential Switch 261-34 & Electrically Shorted Switch 261-34D.Mod to Provide Signal Dampening Initiated ML20090E4471975-10-17017 October 1975 AO 50-237/75-48:on 751007,through-wall Crack Discovered in Drywell/Torus Nitrogen Purge Line 1604-18.Caused by Rapid & Uneven Contraction of Line Tee Connection Due to Liquid Nitrogen Impingement Resulting from Boiler Failure ML20084N8331975-10-15015 October 1975 Supplemental AO 50-249/75-22:plant Mod Being Initiated to Eliminate Valve Seat Failures Due to Cryogenic Stress ML20090E4811975-10-0909 October 1975 AO 50-237/75-45:on 750929,HPCI Turbine Failed to Trip at Designated Reactor Coolant Level.Caused by Open Circuit in Turbine Trip Solenoid Valve Coil Due to Failure of Cold Solder Joint within Coil.Hpci Trip Solenoid Valve Replaced ML20090E4821975-10-0909 October 1975 AO 50-237/75-46:on 750929,reactor Scrammed on High Drywell Pressure During Drywell Inerting Process.Caused by Operator Valving Error,Allowing Nitrogen Flow to Bypass Inerting Pressure Control Valve Into Drywell.Operators Cautioned ML20084N6711975-10-0707 October 1975 AO 50-249/75-43:on 750927,leak Discovered in Drain Line from Feedwater Heater 3D3 to Heater 3C3.Caused by Poor Weld Installation of Drain Line Pipe Support.Crack Ground Out & Pipe Rewelded ML20090E4641975-10-0202 October 1975 AO 50-237/75-44:on 750923,diesel Generator Failed to Start.Caused by Operator Failure to Follow Monthly Insp Procedure & QC Procedure for safety-related Component Replacement.Air Start Sys Inspected & Seal Ring Replaced ML20090E4701975-09-19019 September 1975 AO 50-237/75-43:on 750911,diesel Generator Cooling Water Pump Main Breaker Tripped.Caused by Excessive Heat Buildup within Breaker Housing.Breakers on Buses Replaced & Cover Plates Removed for Ventilation ML20084N6911975-09-16016 September 1975 AO 50-249/75-41:on 750908,intermediate Range Monitors 11, 12,14,16 & 18 Failed to Respond During Plant Startup. Apparently Caused by Personnel Accidentally Loosening Cables.Cables Replaced ML20090E4911975-09-0808 September 1975 AO 50-237/75-42:on 750829,diesel Generator Cooling Water Pump Tripped,Followed by Diesel Generator Trip on High Temp. Cause Not Established.Investigation of Cooling Water Pump & Associated Breakers Continuing ML20084N7771975-09-0404 September 1975 AO 50-249/75-38:on 750826,pressure Switches 3-263-52A1 & 52A2 Found W/Setpoints Above Tech Spec Limit.Apparently Caused by Setpoint Drift Due to Long Periods of Inactivity. Switches Reset ML20084N8411975-09-0404 September 1975 AO 50-249/75-37:on 750826,pressure Switches PS3-263-53A,53B & 53C Had Setpoints Above Tech Spec Limit.Apparently Caused by Setpoint Drift Due to Long Periods at Zero Pressure. Setpoints Reset ML20084N7281975-09-0404 September 1975 AO 50-249/75-40:on 750827,during Routine Instrument Surveillance,Pressure Switches PS3-263-51A & 51B Had Setpoints Above Tech Spec Limit.Caused by Drifting Due to Long Periods at Zero Pressure.Switches Reset ML20084N7481975-09-0303 September 1975 AO 50-249/75-39:on 750826,overload Relay Tripped Twice on Motor Operated Isolation Valve 3-220-1.Caused by Defective Overload Relay.Relay Replaced ML20084N7941975-09-0202 September 1975 AO 50-249/75-36:on 750823,reactor High Pressure Sensors 263-55A,55B & 55C Found W/Setpoints Above Tech Spec Limit. Apparently Caused by Extended Periods at Zero Pressure. Switches Reset ML20084N8661975-08-29029 August 1975 AO 50-249/75-35:on 750821,circuit Breaker 152-3403 Failed to Trip During Breaker Trip Test.Caused by Failure of Trip Coil.Breaker Replaced ML20084N8821975-08-15015 August 1975 AO 50-249/75-34:on 750807,isolation Condenser High Flow Switches 1349A & B Exhibited Instrument Setpoint Drift.Cause Unknown.Switches Reset ML20084N9051975-07-31031 July 1975 AO 50-249/75-32:on 750721,clamp Bolt Keeper Tack Welds on Jet Pumps 6 & 17 Failed.Caused by Poor Tack Welding.Clamp Bolt Keepers Rewelded & Successfully Retested ML20084E0461975-07-0303 July 1975 AO 50-237/75-22:on 750507,vol Bounded by Valves 2-301-98 & 2-301-99 Exceeded Max Allowable Limits During Local Leak Rate Testing.Caused by Dirty Mating Surfaces of Disc & Seat. Seating Surfaces Cleaned & Valve Returned to Svc ML20084D2111975-07-0303 July 1975 AO 50-237/75-36:on 750606,MSIV-1C 10% Closure Limit Switch Failed.Caused by de-energized 10% Closure Relay.Switch Reassembled W/Less Torque Applied to Switch Contact Assembly Screws.Switch Operated Successfully ML20084N9141975-07-0303 July 1975 AO 50-249/1975-31:on 750626,cracks Discovered on Collet Housings of Control Rod Drives 984,883,1032 & 1099. Apparently Caused by Temp Cycles Drive Experiences During Reactor Scram.Analyses Initiated ML20084D1771975-06-25025 June 1975 AO 50-237/75-58:on 750615,isolation Condensor Outboard Steam Supply Valve MO-2-1301-2 Found W/Bent Stem.Possibly Caused by Combination of Excessive Cycling of Valve 1301-2 & Maladjustment of Limit Switches for Valve Travel ML20084D0381975-06-23023 June 1975 AO 50-237/75-41:on 750613,electromatic Relief Valve 2-203-3C Failed to Operate During Test at Rated Pressure.Apparently Caused by Leaking Seal Rings in Valve.Valves Replaced by Rebuilt Valves & Successfully Tested ML20084N7741975-06-20020 June 1975 Followup to AO Rept Re Correlation of Fuel Failures, Identified by Wet Sipping Tests to Calcualted Violations of GE Pciomr ML20084D0531975-06-20020 June 1975 AO 50-237/75-40:on 750611,five Arrays Exhibited 5% Scram Times Exceeding Tech Specs Limits During 2x2 Array Test. Caused by High Regulated Pressure in Scram Valve Air Header. Regulator Reset to Correct Pressure ML20084D1411975-06-18018 June 1975 AO 50-237/75-39:on 750612,diesel Generator Failed to Start During Surveillance Run.Cause Not Known.Suitable Action to Be Taken When Cause Determined ML20084N9751975-06-13013 June 1975 AO 50-249/1975-30:on 750605,standby Liquid Control Pump Discharge Relief Valves Found at Setpoints Lower than Tech Spec Limits.Caused by Setpoint Drift.Valves Cleaned & Reset ML20084D1911975-06-13013 June 1975 AO 50-237/75-37:on 750604,diesel Generator Failed to Start on First Attempt.Cause Undetermined.Suitable Action Will Be Taken When Cause Determined ML20084D2161975-06-0505 June 1975 AO 50-237/75-35:on 750526,explosion Occurred in B Offgas Sys.Cause Not Determined.Load Drop to Minimize Releases Into Bldg Started ML20084D2211975-06-0505 June 1975 AO 50-237/75-33:on 750526,torus Level Found to Be Low.Caused by Personnel Error.Water Pumped from Condensate Storage Into Torus Via HPCI Min Flow Line.Importance of Card Tagging Procedures Emphasized ML20084D2251975-06-0303 June 1975 AO 50-237/75-32:on 750526,electromagnetic Relief Valve 203-3B Failed to Open During post-maint Testing of Valves. Cause Unknown.Corrective Actions to Be Determined When Cause Discovered ML20084D4121975-05-30030 May 1975 AO 50-237/75-31:on 750522,containment Cooling Svc Water Valve MO-1501-3A Failed to Control Flow During Scheduled Surverillance.Cause Not Determined.Design Mods for Valves Being Evaluated ML20084D4271975-05-30030 May 1975 Ao:On 750520,electromagnetic Relief Valve 2-203-3C Failed to Open During Scheduled Surveillance.Caused by Adjustment Problem in Pilot Valve Linkage.Capscrew Out of Adjustment. All Electromagnetic Relief Valves Adjusted ML20084D4321975-05-29029 May 1975 AO 50-237/75-29:on 750519,limit Switch Indicating 10% Closure on 1C MSIV Failed During Startup.Caused by Failure to Reinstall 1C Limit Switch & to Perform Tests.Switch Reinstalled ML20084D8811975-05-27027 May 1975 AO 50-237/75-27:on 750421,control Rod Withdrawn for Friction Testing While Both GE & Util Employees within Direct Line of Sight of Core.Caused by Disregard of Master Procedure & Failure of Testing Procedure to Include Precaution ML20084D3781975-05-23023 May 1975 AO 50-237/75-25:on 750116,Noshua Silver Duct Tape Dropped Into Reactor Vessel Annulus from Feedwater Sparger Work Platform.On 750516,decision Made to Start Reactor W/O Recovering Tape Rendering Tape Drop Reportable ML20084D4411975-05-23023 May 1975 AO 50-237/75-28:on 750506,containment Cooling Svc Water Valves MO-1501-3A & 3B Failed to Control Flow During Lpci/ Containment Cooling Logic Test.Caused by Bent Valve Stems. Increased Size Stem Valves on Order ML20084D8831975-05-23023 May 1975 AO 50-237/75-26:on 750415,diesel Generator Starting Air Motors Failed to Start Diesel Engine.Caused by Motor Pinion Gears Jamming Against Teeth of Ring Gear Preventing Proper Engagement.Vendor Suggested Mod to Regulate Pressure ML20084D8881975-05-21021 May 1975 AO 50-237/75-34:on 750513,drywell Equipment Drain Sump Pump Discharge Valve AO-2001-5 Failed to Close.Possibly Caused by Dirt on Solenoid Diaphragms.Valve Disassembled & Cleaned & Electric Conduit Insulation Repaired ML20084E0431975-05-21021 May 1975 AO 50-237/75-23:on 750511,diesel Generator Overheated After Inadvertent Fast Start & ECCS Inadvertently Initiated. Overheating Caused by Loss of Cooling Water Pump Suction. ECCS Initiation Caused by Valving Out Flow Check Valve 1977-03-31
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20249C8491999-09-30030 September 1999 1999 Third Quarter Rept of Completed Changes,Tests & Experiments Evaluated,Per 10CFR50.59(b)(2), for Dresden Nuclear Power Station. with ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20210R6081999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Dresden Nuclear Power,Units 1,2 & 3.With ML20209E1291999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20209J3481999-06-30030 June 1999 1999 Second Quarter Rept of Completed Changes,Tests & Experiments, Per 10CFR50.59.With ML20210D3071999-06-30030 June 1999 Corrected Page 8 to MOR for June 1999 for DNPS Unit 3 ML20195G6381999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20195B2591999-05-19019 May 1999 Rev 66a to CE-1-A,consisting of Proposed Changes to QAP for Dnps,Qcs,Znps,Lcs,Byron & Braidwood Stations ML20206N2821999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20206B1901999-03-31031 March 1999 First Quarter Rept of Completed Changes,Tests & Experiments Per 10CFR50.59 for Dresden Nuclear Power Station. with ML20205N7491999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20207M6921999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20207E9311999-02-26026 February 1999 Part 21 Rept Re Sprague Model TE1302 Aluminum Electrolytic Capacitors with Date Code of 9322H.Caused by Aluminum Electrolytic Capacitors.Affected Capacitors Replaced ML20199M0891999-01-22022 January 1999 Part 21 Rept Re Failure of Square Root Converters.Caused by Failed Aluminum Electrolytic Capacitory Spargue Electric Co (Model Number TE1302 with Mfg Date Code 9322H).Sent Square Root Converters Back to Mfg,Barker Microfarads,Inc ML20199D3261998-12-31031 December 1998 10CFR50.59 SER for 1998-04 Quarter, of Changes,Tests & Experiments.With ML20199C8951998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Dnps,Units 1,2 & 3 ML20205M7061998-12-31031 December 1998 Unicom Corp 1998 Summary Annual Rept. with ML20197G8591998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Dresden Nuclear Power Station.With ML20196A4191998-11-19019 November 1998 Safety Evaluation Accepting QA TR CE-1-A,Rev 66 Re Changes in Independent & Onsite Review Organization by Creating NSRB ML20196J0061998-11-19019 November 1998 Rev 66 to Topical Rept CE-1-A, QA Program ML20195D2861998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Dresden Nuclear Power Station.With ML20154L3681998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20154N4131998-09-30030 September 1998 1998 Third Quarter 10CFR50.59 Rept, for Dresden Nuclear Power Station of Completed Changes,Tests & Experiments ML20153C5061998-09-21021 September 1998 SER Accepting Qualified Unit 1 Supervisor Initial & Continuing Training Program for Dresden Nuclear Power Station,Unit 1 ML20151Y2711998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20237E2331998-08-21021 August 1998 Revised Pages of Section 20 of Rev 66 to CE-1-A, QA Topical Rept ML20237A7161998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Dresden Nuclear Power Station,Units 1,2 & 3 ML20236Q5851998-06-30030 June 1998 1998 Second Quarter 10CFR50.59 Rept, for Dresden Nuclear Power Station of Completed Changes,Tests & Experiments ML20236F8131998-06-30030 June 1998 Rev 0 to Defueled SAR Dresden Nuclear Power Station Unit 1 Commonwealth Edison Co ML20236T8331998-06-30030 June 1998 COLR for Dresden Station Unit 3,Cycle 15 ML20236T8391998-06-30030 June 1998 Rev 1 to EMF-96-141, Dresden Unit 3 Cycle 15 Reload Analysis Rept ML20236M6041998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Dresden Nuclear Power Station,Units 1,2 & 3 ML20248M3021998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Dresden Nuclear Power Station,Units 1,2 & 3 ML20248F3531998-05-21021 May 1998 Part 21 Rept Re Electronic Equipment Repaired or Reworked by Integrated Resources,Inc from Approx 930101-980501.Caused by 1 Capacitor in Each Unit Being Installed W/Reverse Polarity. Policy of Second Checking All Capacitors Is Being Adopted ML20247F3391998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Dresden Nuclear Power Station,Units 1,2 & 3 ML20217D0281998-04-22022 April 1998 Part 21 Rept Re Additive Constants Used in MCPR Determination for Siemens ATRIUM-9B Fuel by Core Monitoring Sys Were Found to Be non-conservative.SPC Personnel Notified All Customers w/ATRIUM-9B Lead Test Assemblies ML20216D4411998-03-31031 March 1998 First Quarter Rept of Completed Changes,Tests & Experiments for 10CFR5059 ML20216C9651998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Dresden Nuclear Power Station,Units 1,2 & 3 ML20216E2531998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Dresden Nuclear Power Station ML20202F7831998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Dresden Nuclear Power Station ML20199K1651998-01-23023 January 1998 Rev 65h to Topical Rept CE-1-A, Comm Ed QA Tr ML20198P5321997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Dresden Nuclear Power Station ML20198P7021997-12-31031 December 1997 Fourth Quarter Rept of Completed Changes,Tests & Experiments Per 10CFR50.59 ML20216D3611997-12-31031 December 1997 Unicom Corp 1997 Summary Annual Rept ML20203F8781997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Dresden Nuclear Power Station ML20199B0701997-10-31031 October 1997 Monthly Operating Repts for Oct 1997 for Dresden Nuclear Power Station ML20217H7201997-09-30030 September 1997 Monthly Operating Repts for Sept 1997 for Dresden Nuclear Power Station,Units 1,2 & 3 ML20210V2401997-09-19019 September 1997 Rev 65g to Topical Rept CE-1-A, Comm Ed QA Manual ML20216J3781997-08-31031 August 1997 Monthly Operating Repts for Aug 1997 for DNPS ML20210H5511997-07-31031 July 1997 Monthly Operating Repts for July 1997 for DNPS IAW RG 1.16 & GL 97-02 1999-09-30
[Table view] |
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~P one FiscNational Ptara. Chicago. Ithnois yby Address Heply to: Post Othce Box 767 7' Chicago. Ilknois 60690 BBS Ltr # 194-75 Dresden Nuclear Power Station R. R. #1 ,
Morris, Illinois 60450 'N Ihroh 27, 1975 '
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lir. James G. Koppler, Regional Director '
Directorate of Regulatory Operation-Region III 9.\ ..,- s.
U. S. Nonlene Femtlatory Cenniction h,\ ' '
799 Roosevolt Road \y Glen Ellyn, Illinois 60137 ' p([.h/
\
SUBJECT:
REPORT OF APNORMAL OCCURRENCE PER SFITION 6.6.A 0F THE TIIHNICAL Sr?EIFICf.TIONS MAIR STEEi LIRE IMW PRESSURE INSTRUN?7P DRIPP Roforencoa 1) Regulatory Guide 1.16 Rev. 1 Appendix A
- 2) Notification of Region III of U. S. Naclear Regulatory Co:nniosion Tolophones P. Johnson, 1430 hours0.0166 days <br />0.397 hours <br />0.00236 weeks <br />5.44115e-4 months <br /> on March 18, 1975 Telegrem: J. Koppler, 1430 hours0.0166 days <br />0.397 hours <br />0.00236 weeks <br />5.44115e-4 months <br /> on thrch 18, 1975 neport namoort 50-2f//19 /5-17 Report Datos Pa.rch 27, 1975 Occurrence Date Parch 17, 1975 Facility: Droeden Nuclear Power Station, Morrio, Illinois 60450 IDB7PIFICATION OF OCCURRE"CE Ihin Steam Lino Low Proscure Switches 261-30A-D wore found to have trip netpoints from 835 to 845. The trip aetting is identified by table 3 2.a of the technical epecification no croater than or equal to 855 pai (includco 5 pai head pressuro).
_CONDITICN PRIOR TO OCCURRDEE Dresden Unit 2 was in the cold shutdown scode with zero power (!Gt and IGo). Routine instrument surveillance was in progrecs. Droeden Unit 2 has been shutdown i since Noycober 2, 1974 for refueling.
DESCRIPTION OP OCCURRD!CE During routine surveillance of the main steam lino low pressure switchen 261-30A, B, C and D on thrch 17, 1975, the cidtch notpoints ware found to exceed the
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Q technical specification limit. The switch setpoints were innediately reset within Dresden setpoint limit of 871 1 4 pai. l DESIGNATION OF APPARENP CAUSE OP OCCURRENCE (Equipment Failure)
- The apparent cause of this occurrence is instrument drift which probably occurred between the time Dresden Unit 2 was shutdown on November 2, 1974
- for refueling and March 17, 1975 when instrument surveinance was accomplished.
! The most recent instrument surveillance, prior to March 17, 1975, was October 26, .
1974, prior to the Unit 2 shutdown for refueling on November 2, 1974.
i ANALYSIS OP OCCURRDT,E <
i i
The 1\tnction of these pressure switches is to initiate a main steam isolation ;
(Group 1) in the event of a break in the main stcasa line. Previous surveillance, ,
performed on October 26, 1974 (7 days prior,to start of refueling outage), j showed the switch setpoints to be within Dresden setpoint limits. Evaluation i
of the change in the month to month surveillance readings for the Barksdale j precycled pressure switch typo B27-A12SS (GE) from the installation date on January 12, 1974, to October 26, 1974, indicates the switch has not exceeded a 10 poi drift per month. Using a 10 pai per month drift rate, a setpoint of {
! 871 psi minus 10 pai = 861 psi which is within the Technical specification l i limit of 855 psi. It is concluded therefore, that the switch setpoint had j
) not exceeded technical specification limits between the time of October 26, :'
- 1974 and the refueling shutdown date of November 2,1974. Since the Unit has
)
been in the shutdown mode since November 2, 1974 and the present date it is .
c a lal d timt, w wick,im - d io iluu laulullaLiva persvunwl or to the pdulic !
i resulted from this deviation from Technical Specification. !
1 i
I CORRECTIVE ACTION l The immediate corrective action was to adjust the switch setpoints within !
Dresden setpoint limit of 871 i pai.
r
- It has been concluded from the data analyzed, that increasing the Dresden '
setpoint in November 1972 and monthly surveillances have prevented Technical {
Specification setpoint violations for the cain steam low pressure switch. i
- and that the out-of-specification readings obtained on March 17, 1975, can. !
, be attributed to instrument drift during the period of reactor shutdown when monthly curve 111ances were not m4ntained.
l !
r Corrective action taken to prevent repetition of the occurrence will be to l
maintain monthly surveillance during reactor operation until a suitable !
replacement pressure switch with =4=4m=1 drift characteristics can be obtained. !
During extended periods of shutdowns, such as refueling outages, infrequent- !
surveillances will be conducted.
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[ Mr.JamesG.Khcr March 27, 1975 FAII)JRE DATA ,
i The instrument which drifted below the technical specification value was Barksdale pre-cycled pressure switch type B27-A12 SS (GE).
Review of the instrument surveillance data shows this occurrence to be the only deviation from Technical specification limits on Dresden Unit 2 Barksdale pressure switchen 261-30A-D frca November 20, 1972, through January 12, 1974, when Barksdale precycled switch was installed, to October 26, 1974, when the j last surveillance prior to shutdown for refueling was accomplished. The latest deviation for the same typo Dresden Unit 3 pressure switch 261-30 A-D, l
(pre-cycled switch installed on June 31,1974) was April 19, 1973.
From the time of 11 April 1972, to the time of installation of the pre-cycled i Barksdale pressure switch there had been 11 times during which similar type
! switches have deviated bolow the technical cpecification limit. Since tho i
installation of the pre-cycled Barksdale pressure switch (January 12, 1974 j for Unit 2 and June 31, 1974 for Unit 3) this has been the first occurrence of this type of switch deviating below the technical specification 1:Imit.
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Sincerely, wh &'
l . B. Stophenson i
f Superintendent BBSSTDI:smp File /AEC l
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j 8159424449 TDBN MORRIS IL 124 03- 18 035 8P EST V/
PMS JAMES G KEPPLER, REG IONAL DIRECTOR, DIRECTORATE OF REGULATORY OPERATIONS REG ION 5, WUX $
l US NUCLEAR REGULATORY COMMISSION 799 ROOSEVELT RD d \
I GLEN ELLYN IL 6013 7 i P
SUBJECT:
D PR- 19, DRESDEN N UCLE AR POWER STATION, UN IT 2.
! THIS WILL CONFIRM THE CONVERSAT ION WITH MR JOHNSON OF YOUR OFFICE AT ~
i 1430 HOURS THIS D ATE CONCERNING ITEM 1. DRIFT OF PRESSURE SWITCHES 2-261-50A, B, C, AND D WHICH ISOL ATE MAIN STEAM LINES ON LOW PRESSURE. ALL SWITCHES WERE PRECOND IT 10NED TYPE. SWITCHES WERE 1
IMMEDIATELY RESET TO PROPER VALUES. SWITCHES HAVE SEEN O PRESSURE FOR ALMOST 5 MONTHS AND THIS MAY BE FACTOR IN THE DRIFT. ITEM 2. -
i i 1 FAILURE OF UNIT 2 D IESEL GENER ATOR TO ST ART FOLLOWING MINOR sr mi MAINTEN ANCE WHEN ST ARTING AIR SOLENOID ST UCK. STRUCK SOLONOID AND IT i
j POSITIONED TO START THE D IESEL. SOLON0!D BEING INSPECTED NOW.
l B B STEPHENSON SUPERINTENDENT DRESDEN NUCLEAR POWER STATION l COMMONWEALTH EDISON COMPANY RR I MORRIS ILLINOIS 60450 i NNNN i
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