ML20028F374

From kanterella
Revision as of 15:36, 19 February 2020 by StriderTol (talk | contribs) (StriderTol Bot insert)
(diff) ← Older revision | Latest revision (diff) | Newer revision → (diff)
Jump to navigation Jump to search
LER 83-002/02T-0:on 830108,discovered Leak in 2-inch Stainless Steel Schedule 160 Isolable Section of Reactor Drain Line.Cause Unknown.Leaking Elbow Replaced w/304L Type Stainless Steel Matl Per NUREG-0313 Requirements
ML20028F374
Person / Time
Site: Vermont Yankee Entergy icon.png
Issue date: 01/21/1983
From: Pelletier J
VERMONT YANKEE NUCLEAR POWER CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20028F371 List:
References
LER-83-002-02T, LER-83-2-2T, NUDOCS 8302010297
Download: ML20028F374 (2)


Text

r NjCrowan u.s. NuctEAxE:utATonY Commission I LER 83-02/1T

. . LidENSEE EVENT REPORT CONTROL f LOCK: l l l l l l l (PLEAss PRINT OR TYPE ALL REQUIRED .NPORMATIONI i .@

FoTil 7 8 WI v ! LICENSEE Tl v i CODE Yi SI ll@l 0101 -1 0ILICENSE 14 15 01 01 NUMBER 01 01 -1010 ;@l 21 26 4 LICENSE l 1l 1lTYPE 1l J01lgl_ l lg 61 CAT SS CCN'T I,0 I I8 sour $63 l Ll@l015 l0 61 l0 l0 l 217 l1 68l@l690 l 1EVENT DOCKET NUM8 ER l 0OlATE8 l 8 l 3 l@l 0lREPORT 74 76 1l 2lDATE 1l 8l 3l@ 80 EVENT OESCRIPTION AND PROBABLE CONSEQUENCES h Iol2l l While performing routine surveillance of the drywell during shutdown, indication ,

i

[Oi3l l of a leak in a 2" SS schedule 160 isolable section of the reactor drain line was ,

I j lo l4 l l discovered. lais leak is contrary to Tech. Spec. 3.6.E. There were no adverse l I

l o I s l I consequences to the public health an_d safety.  ;

lo is i i 1

. 10171i l 1 L9.J!O I I

7 8 9 80
*$'E "#'dE C0 stsEE COMPONENT CODE SUS ODE 5 10191 7 8 9 lclGlh (2Jh W h lPlIlPlElXlXl@ W @ W @

to 11 12 12 14 19 10 UEQUE NTI AL OCCURRENCE REPORT REVISION EVENTvEAR REPORT NO. CODE TYPE NO.

C")..,at;g LE R RO , l 010 l 2 I 1012l i u lJ1 al22al l-l 23 24 J6 l/l lT I l-j [0_j

._ 27 24 29 30 31 JJ AK N AC ON CNPLANT ' HOUR $ 22 38 IT PO b u. UPPLI MANUPACTURER i

W@lX JJ J4 l@ l Z l@

J3 l36Z l@ l0l0l0lUl 3J 40 W@

41 l42Y l@ l A lg l E l 0 l 6 l 5 l@

43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h 11 I o l IThe exact cause of the pipe crack is unknown at present. The leaking elbow was l LL.L.' ] l replaced with a 304L type stainless steel material which meets the intent of NUREG I iii:.i 10313. Additional examinations of the vessel drain line were performed to verify the l lil3; l integrity of the pressure boundary. l L.'_L4 ] I I 7 8 9 80

! sTA 5  % POWE R OTHER STATUS bis O RY DISCOVERY DESCRIPTION

! 11 isI W @ l0l0l0l@l NA l l B l@l Routine Surveillance l AdTIVITY CC TENT aELEAsEo OP RELEASE AMOUNT OP ACTiviTV LOCATION OF RELEASE l1 l6I W h,lzl@l '

NA l

l NA l l

PERsosNEt ExPOsuSEs suveE R TvPE OEsCArPTiON@

l 1 l il' l' 01 O l 0' l@l Zl@l NA l PERsOsse'L iN;u'd'Es '

i NuveER oEsCRiPTiONh I

11 Isll0l0l0l@l 7 8 9 11 12 NA 80 l

'M*E * "oEs'C$^IT ON'''**h l 1 l 9d 3l l Z l@l NA l 7 1 'J SO NRC USE ONLY ,

[ 2 [o,LJ ,ssuE @loEsCRiPTiON O NA l- lllllllllllll{

7 8 3 to 68 69 80 3 t 8302010297 830121, James P. Pelletier PHONE: (802) 257-7711 2

' PDR ABCCK 05000274 s PDR

_ _. ~.

.>- -=

=

, .. o '

1 VTVYS1 05000271 LER 83-2/1T CAUSE DESCRIPTION AND CORRECTIVE ACTION The exact cause of the pipe crack is unknown at present. The leaking elbow was replaced with a 304L type stainless steel material which meets the intent of NUREG 0313. Additional examinations of the vessel drain line were performed to verify the integrity of the pressure boundary. This included 4 welds PT'd and 6 welds VT'd and no-further leaks were discovered. An additional walk down of the nonisolable portion of the piping was. conducted and inspection was performed for evidence of leakage. No additional evidence of leakage was found. .

i The failed elbow was sent to the Battelle Laboratories for analysis 'and failure mode determination. Upon receiving the Battelle Report, a cause description and summary of the corrective actions taken will be provided in a follow up report.

i

,