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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:RO)
MONTHYEARML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17265A7601999-10-0505 October 1999 Part 21 Rept Re W2 Switch Supplied by W Drawn from Stock, Did Not Operate Properly After Being Installed on 990409. Switch Returned to W on 990514 for Evaluation & Root Cause Analysis ML17265A7621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Re Ginna Npp.With 991008 Ltr ML17265A7531999-09-23023 September 1999 Part 21 Rept Re Corrective Action & Closeout of 10CFR21 Rept of Noncompliance Re Unacceptable Part for 30-4 Connector. Unacceptable Parts Removed from Stock & Scrapped ML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7471999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Re Ginna Npp.With 990909 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7341999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Re Ginna Npp.With 990806 Ltr ML17265A7291999-07-29029 July 1999 Interim Part 21 Rept Re safety-related DB-25 Breaker Mechanism Procured from W Did Not Pas Degradatin Checks When Drawn from Stock to Be Installed Into BUS15/03A.Holes Did Not line-up & Tripper Pan Bent ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7131999-07-22022 July 1999 Special Rept:On 990407,radiation Monitor RM-14A Was Declared Inoperable.Caused by Failed Communication Link from TSC to Plant Process Computer Sys.Communication Link Was re-established & RM-14A Was Declaed Operable on 990521 ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7211999-07-19019 July 1999 ISI Rept for Third Interval (1990-1999) Third Period, Second Outage (1999) at Re Ginna Npp. ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A7661999-06-30030 June 1999 1999 Rept of Facility Changes,Tests & Experiments Conducted Without Prior NRC Approval for Jan 1998 Through June 1999, Per 10CFR50.59.With 991020 Ltr ML17265A7011999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Re Ginna Npp.With 990712 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6761999-06-16016 June 1999 Part 21 Rept Re Defects & noncompliances,10CFR21(d)(3)(ii), Which Requires Written Notification to NRC on Identification of Defect or Failure to Comply. Relays Were Returned to Eaton for Evaluation & Root Cause Analysis ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17265A6681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Re Ginna Nuclear Power Plant.With 990608 Ltr ML17265A6651999-05-27027 May 1999 Interim Rept Re W2 Control Switch,Procured from W,Did Not Operate Satisfactorily When Drawn from Stock to Be Installed in Main Control Board for 1C2 Safety Injection Pump. Estimated That Evaluation Will Be Completed by 991001 ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6591999-05-17017 May 1999 Part 21 Rept Re Relay Deficiency Detected During pre-installation Testing.Caused by Incorrectly Wired Relay Coil.Relays Were Returned to Eaton Corp for Investigation. Relays Were Repaired & Retested ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6381999-05-0707 May 1999 Part 21 Rept Re Replacement Turbocharger Exhaust Turbine Side Drain Port Not Functioning as Design Intended.Caused by Manufacturing Deficiency.Turbocharger Was Reaasembled & Reinstalled on B EDG ML17265A6391999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Re Ginna Nuclear Power Plant.With 990510 Ltr ML17265A6361999-04-23023 April 1999 Part 21 Rept Re Power Supply That Did Not Work Properly When Drawn from Stock & Installed in -25 Vdc Slot.Power Supply Will Be Sent to Vendor to Perform Failure Mode Assessment.Evaluation Will Be Completed by 991001 ML17265A6301999-04-18018 April 1999 Rev 1 to Cycle 28 COLR for Re Ginna Npp. ML17265A6251999-04-15015 April 1999 Special Rept:On 990309,halon Systems Were Removed from Svc & Fire Door F502 Was Blocked Open.Caused by Mods Being Made to CR Emergency Air Treatment Sys.Continuous Fire Watch Was Established with Backup Fire Suppression Equipment ML17265A6551999-04-0909 April 1999 Initial Part 21 Rept Re Mfg Deficiency in Replacement Turbocharger for B EDG Supplied by Coltec Industries. Deficiency Consisted of Missing Drain Port in Intermediate Casing.Required Oil Drain Port Machined Open ML17265A6291999-03-31031 March 1999 Rev 0 to Cycle 28 COLR for Re Ginna Npp. ML17265A6241999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Ginna Station.With 990409 Ltr ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A5661999-03-0101 March 1999 Rev 26 to QA Program for Station Operation. ML17265A5961999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Ginna Nuclear Power Plant.With 990310 Ltr ML17265A5371999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Re Ginna Nuclear Power Plant.With 990205 Ltr ML17265A5951998-12-31031 December 1998 Rg&E 1998 Annual Rept. ML17265A5001998-12-21021 December 1998 Rev 26 to QA Program for Station Operation. ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4761998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Re Ginna Nuclear Power Plant.With 981210 Ltr ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4531998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Re Ginna Nuclear Power Plant.With 981110 Ltr ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A4291998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Re Ginna Nuclear Power Plant.With 981009 Ltr 1999-09-30
[Table view] |
Text
ACCEI.E ED DOCUMENT DIS OBVTION SYSTEM REGULA ORY INFORMATION DISTRIBUT 8 SYSTEM (RIDS)
ACCESSION NBR:9304160043 DOC.DATE: 93/04/12 NOTARIZED: NO DOCKET FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester G 05000244 AUTH. NAME AUTHOR AFFILIATION BACKUSgW HE Rochester Gas & Electric Corp.
MECREDY,R.C. Rochester Gas & Electric Corp.
RECIP.NAME RECIPIENT AFFILIATION S UBJECT: LER 93-001-00:on 930312,both source range detectors found inoperable during energization.Caused by center electrode degradation due to gamma corrosion. Failed detectors replaced w/qualified spares.W/930412 ltr.
DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE:
TITLE: 50.73/50.9 Licensee Event Report (LER), ncident Rpt, etc.
NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72). 05000244 RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD1-3 LA 1 1 PD1-3 PD 1 1 JOHNSONiA 1 1 INTERNAL: ACNW 2 2 AEOD/DOA 1 1 AEOD/DSP/TPAB 1 1 AEOD/ROAB/DSP 2 2 NRR/DE/EELB 1 1 NRR/DE/EMEB 1 1 NRR/DORS/OEAB 1 1 NRR/DRCH/HHFB 1 1 NRR/DRCH/HICB 1 1 NRR/DRCH/HOLB 1 1 NRR/DRIL/RPEB 1 1 NRR/DRSS/PRPB 2 2 RR7'DSSA/ PLB 1 1 NRR/DSSA/SRXB 1 1 G FILE 02 1 1 RES/DSIR/EIB 1 1 RGN E 01 1 1 EXTERNAL'G&G BRYCE g J ~ H 2 2 L ST LOBBY WARD 1 1 NRC PDR 1 1 NS IC MURPHY, G. A 1 1 NSIC POOREiW. 1 1 NUDOCS FULL TXT 1 1 f'23 7 4 pQg c 5 NOTE TO ALL"RIDS" RECIPIENTS:
$ 0- t DESK, PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL ROOM PI-37 (EXT. 504-2065) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!
FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 30 ENCL 30
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ROCHESTER GAS AND ELECTRIC CORPORATION 4 t~j 89 EAST AVENUE, ROCHESTER N.K 14649-0001 tE
'rOarr St Jlf ROBERT C. h1ECREDY TELEPHONE Vice President AREA CODE 7 i 6 546 2700 CrnnJ NucteJr Production April 12, 1993 U.S. Nuclear Regulatory Commission Document Control Desk Nashington, DC 20555
Subject:
LER 93-001, Loss of Source Range Detector Indication During Energization, Due to Faulty Detectors, Causes a Condition Prohibited by Plant Technical Specifica-tions.
R.E. Ginna Nuclear Power Plant Docket No. 50-244 In accordance with 10 CFR 50.73, Licensee Event Report System, item (a)(2)(i)(B), which requires a report of, "any operation prohibited by the plant's Technical Specifications",
the attached Licensee Event Report LER 93-001 is hereby submitted.
This event has in no way affected the public's health and safety.
Very truly yours, Robert C. Me redy XCJ U.S. Nuclear Regulatory Commission Region I 475 Allendale Road King of Prussia, PA 19406 Ginna USNRC Senior Resident Inspector
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'9304160043 930412 PDR ADOCK 05000244 If S 'PDR
NAC FORM 300 US. NUCLEAR REGULATORY COMMISSI (Se)9) APPAOVED OMB NO. 3)500(OC EXP IRF5: C/30/92 ESTIMATED BURDEN PER RFSPONSE TO COMPLY WTH THIS INFORMATIOAI COLLKCTION AEOUESTI 50.0 HAS. FORWARD LICENSEE EVENT REPORT (LER) COMMENTS REGARDING BUADEN ESTIMATE TO THE RECORDS AND RFPORTS MANAGEMENT BRANCH (F030). U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON. DC 20555, AND TO THE PAPEAWORK ABDUCTION PROiECT (31500'IOe). OFFICE OF MANAGEMENTAND BUDGET. WASHINGTON, DC 20503.
FACILITY NAME (1) PA 4ioFll DOCKET NUMBER (2)
R. E. Ginna Nuclear Power Plant o 5 o o o 24 '
TITLE (e)
Loss of Source Range Detector Indication During Energization, Due to Faulty Detectors Causes a Condition Prohibited v Technical Snecifica io ~
y CC ~ 'VENT DATE (Sl LEA NUMBER (0)
SEQUENTIAL REVISION MONTH REPORT DATE (7 OTHER FACILITIES INVOLVED (0)
MONTH OAY YEAR YEAR Ig@ OAY YEAR FACILITYNAMES DOCKET NUMBFRISI NUMSER 0 5 0 0 0 0 312 93 93 001 0 0 0 4 1 2 9 3
~ ~
0 5 0 0 0 THIS REPORT IS SUBMITTED PURSUANT T 0 THE REDUIREMENTS OF 10 CFR (): (Check onr or more of the fo//owindi (11)
OPERATING MODE (0)
N 20.I02(0) 20.e05( ~ ) 50,7 3 le I (2) I Ir) 73.71(III POWER 20.e00( ~) IIIIII BOM(c) (I) 50.73(el(2) 4l 73.71(c)
LEVEL p p p 20A05(e l(1 ) (9) 50.30(cl(2) 50.73(e)(2) lrQ) OTHER ISptcify cn Atjttrect Orrow rot/ ln yrrt, /j/RC Form 20.005(e) ll 1(ill) 50.73(e I (2 I I II 50.73(e)(2)(rljj) (A) 300AI 20A05 4) ll)Grl 50.73(e) (2) IIII 50.73(el(2)(r(QI( ~ )
20.405( ~ Ill)4) 50.734)(2)(III) 50.73(e) (2) (el LICENSFE CONTACT FOA THIS LER (12)
NAME TELEPHONE NUMBER Wes1ey H. Backus AREA CODE Technical Assistant to the Ooerations Mana er 31 552 4-4 44 6 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE OKSCRIBED IN THIS REPORT ll3) C MANUFAC. REPORTABLE MANUFAC. EPOATABLE (c CAUSE SYSTEM COMPONENT TURER TO NPADS j~jPN~QQ cAUsE SYSTEM COMPONENT TURKR TO NPRDS Qt MY. 'NU wY, I G D T W 1 2 p kklk)MI.
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SUPPLEMKNTAL REPORl'XPECTED (IC) MONTH OAY YEAR EXPECTED SUBMISSION DATK (15)
YES IIIyrt, complrtt EXPECTED St/der/SSION DATEI NO ABSTRACT ILlmlt to Irdd tpecrt, I,r., rppror/mrtrfy Iiftten rindle.eptcr typrwrittrn /inrd I10)
On March 12, 1993, at 1425 EST, vith the reactor subcritical during planned shutdown, both source range detectors vere found a
inoperable with the reactor trip breakers closed.
The Control Room operators immediately entered and performed the applicable actions of equipment restoration procedure ER-NZSe1 (SR Malfunction). The reactor trip breakers vere opened vithin five (5) minutes of the event.
The most likely cause of the source range detector failures was center electrode degradation due to gamma corrosion of the bare tungsten center ~ e"trode (center wire). (This event is NUREG--
1022 (B) cause code).
Corrective action was to replace the failed detectors vith qualified spares. Corrective action to prevent recurrence is outlined in section V(B).
NRC Form 300 (509)
NRC FORM 3SSA US, NUCLEAR REGULATORY COMMISSION (649) APPROVED OMB NO,3150010S EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY IYTH THIS LlCENSEE EVENT REPORT (LER) INFORMATION COLLECTION REOUEST: 500 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATlON AND REPORTS MANAGEMENT BRANCH (F430), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO SHE PAPERWORK REDUCTION PROJECT (31500)04), OFFICE OF MANAGEMENTAND BUDGET,WASHINGTON. DC 20503.
FACILITYNAME (1) DOCKET NUMBER (2) LER NUMBER (8) PAGE (3)
YEAR ??o SEOUCNTIAL >5~ REVrdr0N
?.'/1/ NUMddA SP/r) NUM EA R.E. Glnna Nuclear Power Plant o s o o o 24 493 0 0 1 0 0 02 oF l 1 TEXT ///more d/rdee /d //r/rer/ ude/(r)roe/ir//IC Form 3//S42/(12)
PRE- PMNT CONDIT ONS A plant shutdown was in progress per operating procedure 0-2.1 (Normal Shutdown to Hot Shutdown) for the annual refueling and maintenance outage. The turbine generator had gust. been taken off the line and Control Room operators
'were in the process of shutting the reactor down and inserting all control and shutdown rods.
DESCRIPTION OF EVENT DATES AND APPROXIMATE TIMES OF MAZOR OCCURRENCES o March 12, 1993, 1425 EST: Event date and time o March 12, 1993, 1425, EST: Event discovery date and time o March 12, 1993, 1430 EST: Control Room operators complete inserting all control and shutdown rods and open the reactor trip breakers.
o March 12, 1993, 1435 EST: Plant stabilized at hot shutdown.
o March 12, 1993, 1501 EST: Source Range NIS N-31 and NIS N-32 declared inoperable.
o March 12, 1993, 1730 EST: Source Range NIS N-32 declared operable using the installed spare source range detector.
o March 16, 1993, 1747 EST: Source Range NIS N-31 declared operable.
o March 17, 1993, 2040 EST: Source Range NIS N-32 declared operable, using its normal source range detector.
NRC Penn 388A (589)
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (689) APPROVED OM 6 NO. 31500106 EXPIRES: 6/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE EVENT REPORT (LER) LNFORMATION COLLECTION REGUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE To THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT SRANCH (PJ)30). U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO 1HE PAPERWORK REDUCTION PROJECT (3)500106), OFFICE OF MANAGEMENTANO BUDGET, WASHINGTON. DC 20503.
FACILITYNAME (I) DOCKET NUMBER (2) LER NUMBER (6) I'AGE I3)
YEAR O~>: SSOUSNTIAI v~4'EVISION NVM66R '&- NUMFSA R.E. Ginna Nuclear Paver Plant 0 s 0 0 02 ~ ~93 p 01 0 0 0 3 DF 1 1 TEXT lllmoto tptcoitttquia/, utt At//oont/P/RC%%dmt36SA't/(IT)
B. EVENT-On March 12, 1993 at approximately 1425 EST with the reactor subcritical during a planned shutdown, source range (SR) Nuclear Instrumentation System (NIS)
Channel N-31 and Channel N-32 automatically energized at the normal setpoint of </= 5E-11 amps on the two intermediate range (IR) NIS channels. The Control
.Room operators were closely monitoring the decay of the intermediate range currents, and were anticipating the 'reset level for the .source ranges. At the time of automatic energization of the source range detec-tors, there was no count rate indication on Channel N-31 or Channel N-32. Seeing no indication of count rate, the Control Room operators, in accordance with plant procedures and training guidance, immediately attempted to manually energize the source range detectors using the P-6 defeat pushbuttons. The source range detectors still did not indicate counts.
The Control Room operators continued to expeditiously insert control and shutdown rods per 0-2.1 and at approximately 1430 EST the reactor trip breakers were opened. The plant,was subsequently stabilized in hot shutdown at approximately 1435 EST.
NRC Form 366A (649)
NRC FORM 366A US. NUCLEAR REGULATORY COMMISSION (64)9) APPROVED OMB NO.3ISOOI04 EXPIRESI 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE EVENT REPORT (LER) INFORMATION COLLECTION REOUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (P4)30), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (31504)104). OFFICE OF MANAGEMFNTAND BUDGET, WASHINGTON,OC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)
YEAR SEOUENZIAL,Oi)i AEVISION NUMB%4 NUMO64 R.E. Glnna Nuclear Power Plant o s o o o 24 49 3 001 00 0 40F TEXT ///mom 4/>>oo JF
~os, uoo d/d/ooo/ NRC FomI 35549/ ()7)
~ Subsequently the Control Room operators notified higher supervision and the Instrument & Control (I&C)
Department of the event and at approximately 1501 EST declared source range NIS N-31 and N-32 inoperable.
The Plant Operation Review Committee (PORC) was convened to review the actions taken, conformance to Technical Specifications, event classification and reportability. PORC directed that access to the Containment Building (CNMT) be prohibited until one source range channel was restored to operable status.
In addition PORC confirmed that actions were taken to ensure plant cooldown would not occur, and that dilution of boron concentration would not occur. The Control Room operators entered and performed the applicable actions of equipment, restoration procedure ER-NIS.1 (SR Malfunction) including continued boration to greater than 54 shutdown margin .and sampling the Reactor Coolant System (RCS). for boron concentration on a periodic basis during the boration.
C. INOPERABLE STRUCTUEUKSF COMPONENTS, OR SYSTEMS THAT CONTRIBUTED TO THE 15TENT:
None.
D. OTE&R SYSTEMS OR SECONDARY FUNCTIONS AFFECTED:
None.
E METHOD OP DISCOVERY The event was immediately apparent due to indications in the Control Room.
NRC FoIm 366A (64)9)
NRC FORM 366A US. NUCLEAR REGULATORY COMMISSION (689) ~ APPROVED OMB NO, 31500106 5 XP IR ES: 6/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE EVENT REPORT (LER) INFOAMATION COLLECTION REQUEST: 500 HRS. FORWARD COMMENTS REGARDING BUAOEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (P430), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON. DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (31500106). OFFICE OF MANAGEMENTAND BUDGET. WASHINGTON, OC 20503.
FACILITY NAME n) DOCKET NUMBER (2) LER NUMBER (6) PAGE D))
SEQUENTIAI. REVISION YEAR LPNL I+I: NUMEER 4.'UM
+WC:
ER R.E. Ginna Nuclear PoT6er Plant o s o o o 24 493 0 1 0 0 0 5 OF JEXT ///6NKE Epecr is>>6U9od. u>> >>M/6'one/N/IC Form 35569) nl)
P OPERATOR ACTION The Control Room operators, after recognizing that there were no indicated count rates on either of the source range detectors, immediately attempted to manually energize the- source range detectors using the P-6 defeat pushbuttons. The operators entered ER-NIS.1 and performed the applicable actions, including pulling the fuses for Instrument Power, in another attempt to reinstate, the source'anges.
Subsequently, the Control Room operators notified higher supervision 'and the I&C Department and declared source range NIS N-31 and N-32 inoperable.
G. SAFETY SYSTEM RESPONSES None.
III. CAUSE OF OSTENT A. IMMEDIATE CAUSE The cause of the failure of source range detectors N-31 and N-32 to indicate counts was detector failure due to center electrode degradation. Specific measurements indicate that the center electrode to shield had become short circuited on source range detector N-31, most, likely due to the electrode breaking at the bottom of the detector. Source range detector N-32 was found to be open circuited, possibly due to the electrode breaking at the top of the detector.
NAC Form 366A (689)
NRC FORM 366A US. NUCLEAR REGULATORY COMMISSION ISS9) APPROVED OMS NO. 31600104 EXPIRES: E/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE EVENT REPORT (LER) INFORMATION COLLECTION REOUESTI 603) HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH IF@30), U,S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20655, AND TO 1HE PAPERWORK REDUCTION PROJECT 131600)04), OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, DC 20603.
FACILITY NAME 11) DOCKET NUMBER 12) LER NUMBER IS) PAGE 13)
YEAR X6% SEOUENTIAI. REVISION NUMBER NUMSER R.E. Gonna Nuclear Power Plant o s o o o 24 493 0 0 1 00 06 OF TEXT illmoro EPoco lr rorlrr/rod, Irw oddldorM/ll/IC Forrrr 366AS/)17)
B ROOT CAUSE:
After consulting with Westinghouse Electric Corporation (the manufacturer and vendor for these detectors), it was concluded that the underlying cause of the center electrode degradation of source range detectors N-31 and N-32 is most likely due to gamma corrosion of the bare tungsten center electrode (center wire). This effect occurs whenever the source range detector is energized.
ANALYSIS Op EVENT The event is reportable in accordance with 10 CFR 50.73, Licensee Event Report System, item (a)(2)(i)(B), which requires a report of, "any operation prohibited by the plant's Technical Specification", in that the failure of source range detectors N-31 and N-32 to indicate counts at
</= 1E-10 amps on the two intermediate range NIS channels was an operation prohibited by the plant Technical Specifications as follows:
o Specification 3.5.1.1 states, "The Protection System Instrumentation shown on Table 3.5-1 shall be operable whenever the conditions specified in Column 6 are exceeded". For the source range instruments, column 6 refers to Note 2, which states, "Channels should be operable at all modes below the bypass condition with the reactor trip system breakers in the closed position and control rod drive system capable of rod withdrawal". Contrary to the above, source range channels N-31 and N-32 were inoperable below the bypass condition of </= 1E-10 on both IR NIS channels with the reactor trip breakers closed and the control rod drive system capable of rod withdrawal. This condition existed for approximately five (5) minutes until the reactor trip breakers were opened. While an Action Statement exists for one source detector inoperable, there is no stated action requirement for two, detectors inoperable with the Reactor Trip breakers closed. Therefore, a condition prohibited by the plant's Technical Specifications existed.
NRC Form 366A )689)
NRC FORM 366A 2~ U.S. NUCLEAR REGULATORY COMMISSION (669) APPROVED OMB NO. 3(600104 EXPIRES: A/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE EVENT REPORT (LER) INFORMATION COLLECTION REOUESTI 500 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE To THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (P430), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND To 1HE PAPERWORK REDUCTION PROJECT (3150010I), OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (11 DOCKET NUMBER (2) PAGE (3)
LER NUMBER (6)
<~~ REVISION YEAR ~rA SEOUENTIAL NUMSER ..IH: NUM ER R.E. Ginna Nuclear Power Plant 0 s 0 0 0 244 93 0 0 1 0 0 070F1 1 TEXT /I/mom H>>ce /t >>I)r/irer/ Ir>> pr/r//I/orN/HRC Form 366AB/ (17)
Once the trip breakers are open, the minimum operable channels required reduces to one (1) instead of two (2) and the action statement states in part as follows:
With the number of operable channels one less than the minimum operable channels requirement, suspend all operations involving positive reactivity changes.
An assessment was performed considering both the safety consequences and implications of this event with the following results and conclusions:
The safety significance of the failure of both source range channels is the loss of detection of subcritical neutron flux in the core and the function those channels provide for both automatic actuation of the reactor protection system and the prompting of operator action to protect shutdown margin. However, this significance is minimized in this instance for the following reasons:
0 The failure occurred completely within the sequence of shutting down the-reactor in accordance with plant procedure 0-2.1 in that the operators were closely monitoring the decay of the intermediate range currents and were anticipating the reset level for the source ranges.
ln accordance with 0-2.1 the operators were ex-peditiously inserting the control and shutdown rods to five steps prior to manually opening the reactor trip breakers. This sequence, simultaneous with injecting boric acid to achieve the required RCS cold shutdown boron concentration insured that shutdown margin was maintained greater than the requirements of Technical Specifications, and that shutdown margin did not decrease during this event.
NRC Form 366A (BJ)9)
J NRC FORM 355A U.S. NUCLEAR REGULATORY COMMISSION (689) APPROVED OMB NO. 31600104 EXPIRES: 4/30JS2 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE EYENT REPORT ILER) INFORMATION COLLECTION REQUESTI 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (P430), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO 1HE PAPERWORK REDUCTION PROJECT (31504104). OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, OC 20503.
FACILITY NAME (1) DOCKET NUMBER (21 LER NUMBER (5) PAGE (3)
YEAR(PSEQUENTIALS)I(REVISION M3 NUMSEA 'P..: NUMBER R.E. Ginna Nuclear Power Plant s o2 44 93 00 0 0 0 8Oi TEXT FIT mo>> ~ JJ>>ookod, u>> aktJNeal HRC Ann 35543) (IT) o o o 1 o After immediately recognizing that the source range channels did not indicate counts at the intermediate range reset point, the operators took appropriate actions in attempting- to reinstate source range -
detectors. They continued to expeditiously insert control and shutdown rods, and within five minutes, opened the reactor trip breakers. The operator continued boration to the cold shutdown, xenon free concentration required by procedure for RCS cooldown below 500 degrees. There was no decrease in shutdown margin, from the time'of failure of both source range channels until the time the spare source range detector was used to declare Channel N-32 operable.
All operations involving positive reactivity changes were suspenders until after the spare source range detector was declared operable.
Based on the above, it health and safety was assured at all times.
can be concluded that the public's V CORRECTIVE ACTION A ACTION TAKEN TO RETURN AFFECTED SYST1963 TO PRE-EVENT NORMAL STATUS:
0, The detector installed in source range channel N-32 was disconnected and the previously installed spare source range detector was connected to source range channel N-32. NIS N-32 high voltage setting and the pulse height discriminator (PHD) bias setting were ad)usted to conform to the data for the spare detector. At approxi-mately 1730 EST on March 12, 1993, source range Channel N-32 was declared operable.
NRC Form 365A (SSS)
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (669) APPROVED 0MB NO. 31500)04 EXPIRES: 6/30)92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE EVENT REPORT (LER) INFORMATION COLLECTION REQUEST: 500 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (P630), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, OC 20555, AND TO 1'HE PAPERWORK REDUCTION PROJECT (31500106), OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, DC 20503, FACILITY NAME (I) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)
YEAR S~y SEQVSNTIAL REVISION
- ~ 2 NUMSSII NUM SA R.E. Gonna Nuclear Power Plant 2 44 3 001 0 0 0 9 oF 11 TEXT Nmon JIMce ls ~, VJP ~HRC Form 35663) (IT) p p p p p The detector installed in source range channel N-31 was replaced with a detector withdrawn from stock. Subsequently, for source range channel N-31 the high voltage power supply was replaced.
The detector anode voltage curve (also referred to as the plateau curve). was obtained, and the PHD bias setting was adjusted. At approximately 1747 EST on March 16, 1993, source range Channel N-31 was declared operable.
o The detector installed in source range channel N-32 was replaced with a detector withdrawn from stock. For this newly installed detector, the plateau curve was obtained and the PHD bias setting was adjusted. The installed spare source range detector was then disconnected from source range channel N-32 and this newly installed source range detector was connected to source range channel N-32. .The channel operability test was completed, and at approximately 2040 EST on March 17, 1993 source range Channel N-32 was declared operable, using its normal source range detector.
B ACTION TAKEN OR PLANN19) TO NUGENT REC&tRENCE:
To minimize future source range detector failures, the following actions are being planned:
0 A periodic replacement interval for BF~ filled source range detectors will be established, based upon time in service or number of ener-gizations of the detectors.
NRC Form 366A (689)
NRC FORM 366A UE. NUCLEAR REGULATORY COMMISSION APPROVED OM 8 NO. 31600104 (689)
E XP I R ES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE EVENT REPORT tLER) INFORMATION COLLECTION REQUEST: 50/) HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (P830), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (31500104). OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (8) PAGE (3)
YEAR P444 SEQUENTIAL .Ay REVISION NUMSSR NUMSER R.E. Gonna Nuclear Power Plane TEXT /// mare S>>ce JI re/Ir/red, Iree edd/dar>>/N/IC %%drm 38642/ ((7) ps ppp24 493 0 0 1 00 10 OF o A new Westinghouse design for these BF3 filled source range detectors incorporates low voltage source range detectors with gold-plated tungsten center wire conductor material. Detectors of this new design will be procured. When detectors of this new design are installed, as part of a planned detector upgrade schedule, as replace-ments for existing detectors, the periodic replacement interval will be re-evaluated.
0 Existing calibration procedures will be revised,
" or new procedures developed, to include steps to perform time domain reflectometry (TDR) measure-ments on N-31, N-32 and spare detector, prior to scheduled refueling outages. (TDR measurements can determine wire is broken, if the shorted detector out or center electrode if it has high or low resistance) .
0 A trending program to detect potential degradation of source range detectors will be established, for the following data:
- 1) Detector plateau curve data will be trended.
As the BF3 gas in the detector dissociates over time, the high voltage will be adjusted higher each time until set on the plateau.
it can no longer be
- 2) PHD bias curves will be trended.
RMAT ON A PAXLED COMPONENTS:
The faulty detectors were BF3 filled, source range detector proportional counters, Part No. WL-24182 manufactured by Westinghouse Electric Corporation.
NRC Form 388A (889)
NRC FORM 366A (SJ)9) t LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION US. NUCLEAR REGULATORY COMMISSION APPROVEO OMB NO, 31500104 EXPIRES: EI30(92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REQUEST: 500 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (F430). U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON. OC 20555, AND TO 1HE PAPERWORK REDUCTION PROJECT (31500104). OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1I DOCKET NUMBER (2) LER NUMBER (SI I'AGE (3)
YEAR SEQUENTIAL REVISION NVMSER NVMSER R.E. Ginna Nuclear Power Plant o s o o o 2 449 3 001 0 0 1 1 OF RJOOOOPooo (ssoSs(INL goo oddlooIMI HRC %%dmI 36643) (17)
B. PREVXOUS LERs ON SIMILAR KGFNTS.
A similar LER event historical search was conducted with the following results: LER 90-003 (Higher Than Normal Count Rate on Source Range NIS, Due to a Faulty Detector, Causes a Reactor Trip During Source Range Re-energization) was a similar event with the same root cause. The corrective action to prevent recur-rence, of the event described in LER 90-003, was to initiate a evaluation which will ultimately result in procurement and installation of detectors, of a new Westinghouse design. It should be noted that even if the evaluation had been completed, and detectors of a new design had been procured and were in stock, these detectors would not have been installed prior to the 1993 outage.
C SPECIAL COMMENTS None.
NRC FoIm 366A (SJ)9)