ML19339C602

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LER 80-036/03L-0:on 801017,standby Liquid Control Relief Valve Setpoints Found to Be Above Tech Spec 4.4.A Requirement of 1400 to 1490 Psig.Caused by Setpoint Drift. Relief Valves Adjusted,Bench Tested & Reinstalled
ML19339C602
Person / Time
Site: Vermont Yankee Entergy icon.png
Issue date: 11/14/1980
From: Murphy W
VERMONT YANKEE NUCLEAR POWER CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19339C593 List:
References
LER-80-036-03L, LER-80-36-3L, NUDOCS 8011180663
Download: ML19339C602 (1)


Text

NRC FOlM 366 U. S. NUCLEAR RESULATC~.Y COMMISSION

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LICENSEE EVENT REPORT LER 80-36/3L CONTAOL BLOCX
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ptEASE PRINT OR TYTE ALL REQUICED iNFORMATION) l0 l 18 l9 l V ILICENSEE

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7 6 6C 61 DOCKET NUMS E R 68 69 EVENT CATE 75 RE* ORT DATE EVENT DESCRIPTION AND PROB ABLE CONSECUENCES h j o !:; l During routine surveillance testing of the standby liquid control relief valves, thel toj3; lsetpoints were found to be above Tech. Spec. 4.4.A required setpoint of 1400 to 14901 l044 l lpsig.SR-39A setpoint was found to be 1550 psig while SR-39B was found at 1600 osie. I 1c;el l Since the system has been successfully hydrotested to 2250 psig, there were no I l o 16 l l Consequences to the public health and safety as a result of this event. Similar l lol2l [ occurrences were reported to the Corcission as LER 77-23/3L and 78-24/3L. 1

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7 8 9 80 SYSTEM CAUSE CAUSE COMP %ALvE CODE CODE SUSCCDE CCMPONENT CODE SUSCODE SU8CCOE loisi 7 8 l Pl Clh l Elh l Blh l VI A! L! V! El Xlh l Xlh l Blh 9 10 11 1: 13 1s te 20

. SE CU E NTI A L QCCURRENCE REPORT REvtsiON gg a raQ EVE F.T vf A R R EPORT NC. CODE TvPE NC.

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AK N A T N ON PL NT ME HOUR $ $8 i POR 6. S PPLIE MANUPACTURER lEl@lEl@ lZl@ lZl@ 1010l O! Ol lN l@ lY lh l43A l@ lCl7!1l0l@

3J 34 36 36 d, 40 en 42 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h 11 ioll The deviation from the recuired setpoint was attributed to setooint drift. The tue !

"iyl relief valves were properly adjusted, be.nch-tested, and reinstalled into the svstem!

, ,7i l SR-39A/B were manufactured by Crosby Valve and Gage Comnanv, Model JMWK. , I titall .

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(802) 257-7711 E, 8 0n18gN E O5 P AEPARER PHONE.