ML19341A254

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LER 80-043/03L-0:on 801220,reactor Core Isolation Cooling Valve 15 Had Seat Leakage of 1.531 Lbm/Hr,Exceeding Tech Specs.No Cause Noted.Valve Seating Surfaces Lapped & Valve Retested
ML19341A254
Person / Time
Site: Vermont Yankee File:NorthStar Vermont Yankee icon.png
Issue date: 01/16/1981
From: Murphy W
VERMONT YANKEE NUCLEAR POWER CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19341A253 List:
References
LER-80-043-03L, LER-80-43-3L, NUDOCS 8101220462
Download: ML19341A254 (1)


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