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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:RO)
MONTHYEARML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17265A7601999-10-0505 October 1999 Part 21 Rept Re W2 Switch Supplied by W Drawn from Stock, Did Not Operate Properly After Being Installed on 990409. Switch Returned to W on 990514 for Evaluation & Root Cause Analysis ML17265A7621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Re Ginna Npp.With 991008 Ltr ML17265A7531999-09-23023 September 1999 Part 21 Rept Re Corrective Action & Closeout of 10CFR21 Rept of Noncompliance Re Unacceptable Part for 30-4 Connector. Unacceptable Parts Removed from Stock & Scrapped ML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7471999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Re Ginna Npp.With 990909 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7341999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Re Ginna Npp.With 990806 Ltr ML17265A7291999-07-29029 July 1999 Interim Part 21 Rept Re safety-related DB-25 Breaker Mechanism Procured from W Did Not Pas Degradatin Checks When Drawn from Stock to Be Installed Into BUS15/03A.Holes Did Not line-up & Tripper Pan Bent ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7131999-07-22022 July 1999 Special Rept:On 990407,radiation Monitor RM-14A Was Declared Inoperable.Caused by Failed Communication Link from TSC to Plant Process Computer Sys.Communication Link Was re-established & RM-14A Was Declaed Operable on 990521 ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7211999-07-19019 July 1999 ISI Rept for Third Interval (1990-1999) Third Period, Second Outage (1999) at Re Ginna Npp. ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A7661999-06-30030 June 1999 1999 Rept of Facility Changes,Tests & Experiments Conducted Without Prior NRC Approval for Jan 1998 Through June 1999, Per 10CFR50.59.With 991020 Ltr ML17265A7011999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Re Ginna Npp.With 990712 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6761999-06-16016 June 1999 Part 21 Rept Re Defects & noncompliances,10CFR21(d)(3)(ii), Which Requires Written Notification to NRC on Identification of Defect or Failure to Comply. Relays Were Returned to Eaton for Evaluation & Root Cause Analysis ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17265A6681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Re Ginna Nuclear Power Plant.With 990608 Ltr ML17265A6651999-05-27027 May 1999 Interim Rept Re W2 Control Switch,Procured from W,Did Not Operate Satisfactorily When Drawn from Stock to Be Installed in Main Control Board for 1C2 Safety Injection Pump. Estimated That Evaluation Will Be Completed by 991001 ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6591999-05-17017 May 1999 Part 21 Rept Re Relay Deficiency Detected During pre-installation Testing.Caused by Incorrectly Wired Relay Coil.Relays Were Returned to Eaton Corp for Investigation. Relays Were Repaired & Retested ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6381999-05-0707 May 1999 Part 21 Rept Re Replacement Turbocharger Exhaust Turbine Side Drain Port Not Functioning as Design Intended.Caused by Manufacturing Deficiency.Turbocharger Was Reaasembled & Reinstalled on B EDG ML17265A6391999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Re Ginna Nuclear Power Plant.With 990510 Ltr ML17265A6361999-04-23023 April 1999 Part 21 Rept Re Power Supply That Did Not Work Properly When Drawn from Stock & Installed in -25 Vdc Slot.Power Supply Will Be Sent to Vendor to Perform Failure Mode Assessment.Evaluation Will Be Completed by 991001 ML17265A6301999-04-18018 April 1999 Rev 1 to Cycle 28 COLR for Re Ginna Npp. ML17265A6251999-04-15015 April 1999 Special Rept:On 990309,halon Systems Were Removed from Svc & Fire Door F502 Was Blocked Open.Caused by Mods Being Made to CR Emergency Air Treatment Sys.Continuous Fire Watch Was Established with Backup Fire Suppression Equipment ML17265A6551999-04-0909 April 1999 Initial Part 21 Rept Re Mfg Deficiency in Replacement Turbocharger for B EDG Supplied by Coltec Industries. Deficiency Consisted of Missing Drain Port in Intermediate Casing.Required Oil Drain Port Machined Open ML17265A6291999-03-31031 March 1999 Rev 0 to Cycle 28 COLR for Re Ginna Npp. ML17265A6241999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Ginna Station.With 990409 Ltr ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A5661999-03-0101 March 1999 Rev 26 to QA Program for Station Operation. ML17265A5961999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Ginna Nuclear Power Plant.With 990310 Ltr ML17265A5371999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Re Ginna Nuclear Power Plant.With 990205 Ltr ML17265A5951998-12-31031 December 1998 Rg&E 1998 Annual Rept. ML17265A5001998-12-21021 December 1998 Rev 26 to QA Program for Station Operation. ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4761998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Re Ginna Nuclear Power Plant.With 981210 Ltr ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4531998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Re Ginna Nuclear Power Plant.With 981110 Ltr ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A4291998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Re Ginna Nuclear Power Plant.With 981009 Ltr 1999-09-30
[Table view] |
Text
ACCEI.ERAT@9 DOCUMENT DIST UTION SYSTEM REGULAT~ INFORMATION DISTRIBUTION STEM (RIDS)
ACCESSION NBR:9311170036 DOC.DATE: 93/11/10 ,NOTARIZED: NO DOCKET FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester G 05000244 AUTH. NAME AUTHOR AFFILIATION ST MARTIN,J.T. Rochester Gas a Electric Corp.
MECREDY,R.C. Rochester Gas & Electric Corp.
RECIP.NAME RECIPIENT AFFILIATION JOHNSON,A.R. Project Directorate I-3
SUBJECT:
LER 93-005-00:on 931011,due to misinterpretation of TS D 4.6.l.e.3.(a) requirements, verification of load shedding
'apability of safeguards loads not adequately performed.
Testing completed to verify capability.W/931110 ltr.
TITLE: 50.73/50.9 Licensee Event Report (LER),QIncidentQRpt, etc.
DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE: I ~
NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72). 05000244 D
RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL D PDl-3 LA 1 1 PD1-3 PD 1 1 JOHNSON,A 1 1 1
INTERNAL: AEOD/DOA 1 1 AEOD/DSP/TPAB 1 1 AEOD/ROAB/DSP 2 2 NRR/DE/EELB 1 1 NRR/DE/EMEB 1 1 NRR/DORS/OEAB 1 1 NRR/DRCH/HHFB 1 1 NRR/DRCH/HICB 1 1 NRR/DRCH/HOLB 1 1 NRR/DRZL/RPEB 1 1 NRR/DRSS/PRPB 2 2 BASSA SPLB 1 1 NRR/DSSA/SRXB 1 1 REG ILE 02 1 ~ 1 RES/DSIR/EIB 1 1 RG FILE 01 1 1 EXTERNAL: EGSG BRYCEPJ.H 2 2 L ST LOBBY WARD 1 1 NRC PDR 1 1 NSIC MURPHY,G.A 1 1 NSIC POOREPW. 1 1 NUDOCS FULL TXT 1 1 D
D NOTE TO ALL"RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTEl CONTACI'HE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT. 504-2065) TO, ELIMINATEYOUR NAME FROM DISTRIBUTION LISIS FOR DOCUMENTS YOU DON'T NEEDf r rvr r
FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 28 ENCL 28
'l jeylvm IgeZZaxri e ~ ~ ~ II C rrew "jr / 'g coen I]'jlj srArc j'J'ii'OCHESTER GAS AND ELECTRIC CORPORATION ~ 89 EAST AVENUE, ROCHESTER N. Y. 14649-0001 ROBERT C MECREDY TEi.EpHolr E Vice Preridenl AREA CODE 7 l6 546 2700 Cinna Nuclear Production November 10, 1993 U.S. Nuclear Regulatory Commission Attn: Allen R. Johnson Project Directorate I-3 Document Control Desk Nashington, DC 20555
Subject:
LER 93-005, Failure to Perform Surveillance, Due to Misinterpretation of Requirements, Causes a Condition Prohibited by Plant Technical Specifications R.E. Ginna Nuclear Power Plant Docket No. 50-244 In accordance with 10 CFR 50.73, Licensee Event Report System, item (a) (2) (i) (B), which requires a report of, "any operation or condition prohibited by the plant's Technical Specifications", the attached Licensee Event Report LER 93-005 is hereby submitted.
This event has in no way affected the public's health and safety.
Very truly yours, Robert C. Me redy xc: U.S. Nuclear Regulatory Commission Region I 475 Allendale Road King of Prussia, PA 19406 Ginna USNRC Senior Resident Inspector 931117003b '7i31110 PDR ADOCK 05000244 S PDR
NRC FORH 366 U.S NUCLEAR REGULATORY COHHISSI ON APPROVED BY QLB NO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIHATED BURDEN PER RESPONSE TO COHPLY WITH THIS INFORHATION COLLECTION REOUEST: 50.0 HRS.
LICENSEE EVENT REPORT (LER) FORWARD COHMENTS REGARDING BURDEN ESTIHATE TO THE IHFORHATION AND RECORDS MANAGEHENT BRANCH (HNBB 7714), U.S. NUCLEAR REGULATORY COHHISSION, (See reverse for required number of digits/characters for each block) WASHIHGTON, DC 20555-0001 AND TO THE PAPERWORK REDUCTION PROJECT (3150 0104), OFFICE OF HANAGEMENT AND BUDGET WASHINGTON DC 20503.
FAcILITY NAME (1) R. E ~ Ginna Nuclear Power Plant DOCKET NQSER (2) PAGE (3) 05000244 1 OF 9 TITLE (4) Failure to Perform Surveillance, Due to Misinterpretation of Requirements, Causes a Condition Prohibited by Plant Technical Specifications EVENT DATE 5 LER NINBER 6 REPORT DATE 7 OTHER FACILITIES INVOLVED 8 SEQUENTIAL REVISION FACILITY NAME DOCKET NUMBER HONTH DAY YEAR YEAR NUMBER NUMBER HONTH DAY YEAR 05000 10 11 93 93 005 00 10 93 FACILITY NAME DOCKET NUMBER 05000 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR: Check one or more 11 M<X)E (9) N 20.402<b) 20.405(c) 50 '3(a)(2)(iv) 73.71(b)
POWER 20.405(a )(1)(i) 50.36< c) (1) 50.73(a)(2)(v) 73.71(c) 097 LEVEL (10) 20.405(a)(1)<ii) 50.36(c)(2) 50.73(a)(2)(vii) OTHER 20.405(a)(1)(iii) )( 50.73(a)(2)(i) 50.73(a)(2)(viii)(A) (Specify in 20.405(a)(1)(iv) 50.73(a)(2)(ii) 50 '3(a)(2)(viii)(B)
Abstract below and in Text, 20.405(a)(1)(v) 50.73(a)(2)(iii) 50.73(a)(2)(x) NRC Form 366A LICENSEE CONTACT FOR THIS LER 12 NAHE John T. St. Hartin - Director, Operating Experience TELEPHONE NUHBER (Include Area Code)
(315) 524-4446 C<NPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT 13 REPORTABLE REPORTABLE CAUSE SYSTEH COMPONENT HANUFACTURER SYSTEH COMPONENT HANUFACTURER TO NPRDS TO NPRDS
';;ip:4:+I PQ+IPqx".'AUSE SUPPLEMENTAL REPORT EXPECTED 14 EXPECTED HONTH DAY YEAR YES SUBMISSION (I f yes, complete EXPECTED SUBMISSION DATE). X NO DATE (15)
ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) (16)
On October 11, 1993, at 1330 EDST, with the reactor at approximately 97'.
full power, evaluation of surveillance testing procedures determined that Technical Specification 4.6.1.e.3.(a) requirements were misinterpreted.
Therefore, it was concluded that verification of load shedding capability of safeguards loads had not been adequately performed.
Immediate corrective action was initiated to complete testing that would verify this load shedding capability. This testing was completed within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> of discovery, achieving compliance with Technical Specification 4.6.1.e.3.(a) requirements.
The underlying cause of the failure to perform this surveillance was a misinterpretation of Technical Specification surveillance requirements.
(This event is NUREG-1220 (E) cause code.)
Corrective action was to perform the testing. Corrective action to preclude repetition is outlined in Section V (B).
NRC FORM 366 (5-92)
'
NRC FORM 366A U.S. NUCLEAR REGULATORY COHIISSION APPROVED BY OMB NO 3150-0104 (5-92) EXPIRES 5/31/95 ESTIHATED BURDEN PER RESPONSE TO COHPLY WITH THIS INFORHATION COLLECTION REQUEST: 50.0 HRS.
FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO LICENSEE EVENT REPORT (LER) THE INFORMATION AND RECORDS HANAGEHEHT BRANCH TEXT CONTINUATION (MNBB 7714), U.S. NUCLEAR REGULATORY COHMISSION, WASHINGTON, DC 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150.0104), OFFICE OF MAHAGEHENT AND BUDGET WASHINGTOH DC 20503.
FACILITY NAME 1 DOCKET NUMBER 2 LER HIMBER 6 PAGE 3 YEAR SEQUENTIAL REVISION R.E. Ginna Nuclear Power Plant 05000244 93 -- 005-- 00 2 OF 9 t
TEXT (If more space is required, use additional copies of HRC Form 366A) (17)
PRE-EVENT PLANT CONDITIONS The plant was at approximately 979. steady state reactor power. An evaluation of surveillance test procedures was in progress, to address potential non-compliance with Technical Specification 4.6.1.e.3.(a) surveillance requirements to verify load shedding from the emergency buses.
II. DESCRIPTION OF EVENT A. DATES AND APPROXIMATE TIMES OF MAJOR OCCURRENCES:
- 1. October 11, 1993, 1330 EDST: Event date and approximate time.
- 2. October 11, 1993, 1330 EDST: Discovery date and approximate time.
- 3. October 11, 1993, 2037 EDST: Initiated testing to verify load shedding capability for loads on emergency bus 14.
- 4. October 12, 1993, 0441 EDST: Initiated testing to verify load shedding capability for loads on emergency bus 18.
- 5. October 12, 1993, 0447 EDST: Completed testing of load shedding for safeguards loads from emergency bus 14.
- 6. October 12, 1993, 0539 EDST: Completed testing of load shedding for safeguards loads from emergency bus 18. Load shedding was satisfactorily verified for the "A" train of safeguards equipment.
- 7. October 12, 1993, 0540 EDST: Initiated testing to verify load shedding capability for loads on emergency bus 17.
- 8. October 12, 1993, 0625 EDST: Completed testing to verify load shedding for safeguards loads from emergency bus 17.
- 9. October 12, 1993, 0626 EDST: Initiated testing to verify load shedding capability for loads on emergency bus 16.
NRC FORH 366A (5-92)
NRC FORM 366A U.S. NUCLEAR REGULATORY CQIIISSION APPROVED BY MB NO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY lllTH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS.
FORNARD COMMENTS REGARDING BURDEN ESTIMATE TO LICENSEE EVENT REPORT (LER) THE INFORHATION AND RECORDS MANAGEMENT BRANCH TEXT CONTINUATION (MNBB 7714), U.S. NUCLEAR REGULATORY COMHISSION, NASHINGTOH, DC 20555-0001 AND TO THE PAPERNORK REDUCTION PROJECT (3140-0104), OFFICE OF MANAGEMENT AND BUDGET IJASHINGTON DC 20503.
FACILITY NAME 1 DOCKET NINBER 2 LER NNBER 6 PAGE 3 YEAR SEQUENTIAL REVISION R.E. Ginna Nuclear Power Plant 05000244 M
93 -- 005-- 00 3 OF 9 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)
- 10. October 12, 1993, 0716 EDST: "B" component cooling water (CCW) pump operability was indeterminate. The pump was declared inoperable and removed from service.
- 11. October 12, 1993, 0950 EDST: Completed testing of load shedding for safeguards loads from emergency bus 16. Load shedding was satisfactorily verified for the "B" train of safeguards equipment, except for the "B" CCW pump.
- 12. October 12, 1993, 1003 EDST: With the completion of testing for the "A" and "B" trains of safeguards equipment, compliance with Technical Specification 4.6.1.e.3.(a) was achieved.
- 13. October 12, 1993, 1939 EDST: "B" CCW pump declared operable.
B. EVENT:
On October 11, 1993, at approximately 1330 EDST, station and engineering staff confirmed that surveillance test procedures had not fully complied with the requirements of Technical Specification (TS) 4.6.1.e.3.(a), in that verification of load shedding of safeguards loads powered from the emergency buses (buses 14, 16, 17, and 18), while simulating a loss of offsite power in conjunction with a safety injection (SI) test signal, had not been performed as required. The guidance of NRC Generic Letter (GL) 87-09, entitled "Sections 3.0 and 4.0 of the Standard Technical Specifications (STS) on the Applicability of Limiting Conditions for Operation and Surveillance Requirements", was followed. Both the "A" and "B""
diesel generators (D/Gs) were available to perform all intended functions. Failure to perform the surveillance within the specified time interval constituted a non-compliance with the Operability Requirements of the Limiting Conditions for Operation (LCO).
NRC FORH 366A (5-92)
NRC FORM 366A U.S. NUCLEAR REGULATORY CQIIISSION APPROVED BY OMB NO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COHPLY NITH THIS INFORMATION COLLECTIOH REQUEST: 50.0 HRS.
FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO LICENSEE EVENT REPORT (LER) THE IHFORMATIOH AND RECORDS MANAGEMENT BRANCH TEXT CONTINUATION (MHBB 7714), U.S. NUCLEAR REGULATORY COMMISSION, MASHINGTON, DC 20555-0001 AND TO THE PAPERNORK REDUCTION PROJECT (3110-0104), OFFICE OF MANAGEMENT AND BUDGET NASHINGTON DC 20503.
FACILITY NAME DOCKET NUMBER 2 LER NINIBER 6 PAGE 3 SEQUENTIAL REVISION YEAR R.E. Ginna Nuclear Power Plant 005--
M M 05000244 93 00 4 OF 9 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)
Surveillance testing to verify compliance with TS 4.6.1.e.3.(a) was initiated on October 11, 1993, at approximately 2037 EDST, with each emergency bus being tested sequentially. Testing for the "A" train of safeguards equipment (emergency buses 14 and
- 18) was completed at approximately 0539 EDST (on October 12, 1993), and testing for the "B" train (emergency buses 16 and
- 17) was completed at approximately 0950 EDST. Technical Specification compliance was achieved at approximately 1003 EDST.
During testing of the "B" train, resistance reading of a relay contact associated with the "B" CCW pump breaker Undervoltage Trip circuitry did not meet the specified acceptance criteria.
Despite having confidence that the higher resistance did not impede the "B" CCW pump load shedding feature, the station staff elected to declare the "B" CCW pump inoperable. The "B" CCW pump was removed from service, and the appropriate TS LCO was entered, until functional testing and/or corrective maintenance could verify acceptable circuit operation.
Subsequently, the "B" CCW pump breaker was racked into the test position, closed from the Main Control Board, and successfully trip tested by actuating the undervoltage circuitry. This test demonstrated acceptable load shedding capability. Following this verification of circuit operability, corrective maintenance was performed to improve circuit performance.
The corrective maintenance consisted of burnishing of an auxiliary relay contact in the pump trip circuitry. The corrective maintenance proved successful, with subsequent resistance readings meeting the acceptance criteria. The "B" CCW pump was restored to service and declared operable.
the functional trip test, 'which was successfully performed Note'hat prior to the corrective maintenance, demonstrated acceptable load shedding capability for the "B" CCW pump.
HRC FORM 366A (5-92)
lf NRC FORM 366A U.S. NUCLEAR REGULATORY CNHIISSIOH APPROVED BY W HO. 3150-0104 (5-92) EXP I RES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS.
FORMARD COMMENTS REGARD IHG BURDEH ESTIMATE TO LICENSEE EVENT REPORT (LER) THE INFORMATION AHD RECORDS MANAGEMENT BRANCH TEXT CONTINUATION (MHBB 7714), U.S. NUCLEAR REGULATORY COMMISSION, IIASHINGTON, DC 20555-0001 AHD TO THE PAPERISRK REDUCI'ION PROJECT (3140-0104), OFFICE OF MAHAGEMENT AHD BUDGET UASHIHGTON DC 20503.
FACILITY NAME 1 DOCKET NINSER 2 LER NIMBER 6 PAGE 3 YEAR SEQUENTIAL REVISION R.E. Ginna Nuclear Power Plant 05000244 93 005-- 00 5 OF 9 TEXT (If more space is required, use additional copies of HRC Form 366A) (17)
C~ INOPERABLE STRUCTURES i COMPONENTS i OR SYSTEMS THAT CONTRI BUTED TO THE EVENT:
None.
D. OTHER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED:
None.
E. METHOD OF DISCOVERY:
This event was apparent after completion of an evaluation of TS RSSP 2 'i 4.6.1.e.3.(a) and RSSP 2 'Ai RSSP 2 'i surveillance test procedures (procedures PT-9.1.16, PT-9.1.17, and PT-9.1.18). This evaluation RSSP 19'SSP 20i PT 9 ' '4i determined that verification of load shedding capability of safeguards loads from the emergency buses had not been adequately performed.
F. OPERATOR ACTION:
The Control Room operators were notified of the failure to fully comply with the requirements of TS, and that the guidance of NRC GL 87-09 provided a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> period to complete the required surveillance testing.
G. SAFETY SYSTEM RESPONSE:
None.
HRC FORM 366A (5-92)
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY m5/31/95 NO. 3150-0104 (5-92) EXPIRES ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECT ION REQUEST: 50.0 HRS.
FORWARD COMMENTS REGARD IHG BURDEN ESTIMATE TO LICENSEE EVENT REPORT (LER) THE INFORMATION AND RECORDS MANAGEMENT BRANCH TEXT CONTINUATION (MHBB 7714), U.ST NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555-0001 AHD TO THE PAPERWORK REDUCTION PROJECT (3140-0104), OFFICE OF MANAGEMENT AND BUDGET WASHINGTON DC 20503.
FACILITY NAME 1 DOCKET HLNBER 2 LER NUMBER 6 PAGE 3 YEAR SEQUENTIAL REVI SION R.E. Ginna Nuclear Power Plant 05000244 93 -- 005-- 00 6 OF 9 TEXT (lf more space is required, use additional copies of, NRC Form 366A) (17)
III. CAUSE OF EVENT A. IMMEDIATE CAUSE:
The immediate cause for failure to fully comply with requirements of TS was procedural deficiency, in that surveillance test procedures did not completely reflect the requirements of TS 4.6.1.e.3.(a).
B. ROOT CAUSE:
The underlying cause of the procedural deficiencies was a misinterpretation of TS surveillance requirements. TS 4.6.1.e.3.(a) had been previously interpreted that the load shedding capabilities required to be verified were for the non-essential loads powered from the emergency buses. This capability (for non-essential loads) has been tested by simulating a SI signal during performance of procedures RSSP-2.1 and RSSP-2.1A, which are performed each refueling outage.
The need to verify load shedding capabilities for safeguards loads, with both undervoltage and SI present, had not been considered in this interpretation. (This event is NUREG-1220 (E) cause code, Management/Quality Assurance Deficiency).
IV. ANALYSIS OF EVENT:
I This event is reportable in accordance with 10 CFR 50 Licensee Event Report System, item (a) (2) (i) (B), which
'3i requires a report of, "Any operation or condition prohibited by the plant's Technical Specifications". Failure to perform the surveillance to verify load shedding from the emergency buses for greater than 18 months is a condition prohibited by Ginna Technical Specifications.
NRC FORM 366A (5-92)
- NRC FORM 366A U S. NUCLEAR REGULATORY CQNIISSION APPROVED BY W NO. 3150-0104 (5-92) EXP IRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORHATION COLLECTION REQUEST: 50.0 HRS.
FORWARD COMMENTS REGARDING BURDEN ESTIHATE TO LICENSEE EVENT REPORT (LER) THE INFORHATION AND RECORDS MANAGEHENT BRANCH TEXT CONTINUATION (MNBB 7714), U.S. NUCLEAR REGULATORY COMHISSION, WASHINGTON, DC 20555-0001 AND TO THE PAPERWORK REDUCTION PROJECT (3140-0104), OFFICE OF MANAGEMENT AND BUDGET WASHIHGTON DC 20503.
FACILITY NAME 1 DOCKET NUHBER 2 LER NIMBER 6 PAGE 3 SEQUENTIAL REVISION YEAR R.E. Ginna Nuclear Power Plant 05000244 93 005-- 00 7 OF 9 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)
As stated in NRC GL 87-09, "Failure to perform a Surveillance Requirement within the allowed surveillance interval, defined by Specification 4.0.2, shall constitute non-compliance with the OPERABILITY requirements for a Limiting Condition for Operation.
The time limits of the ACTION requirements are applicable at the time it is identified that a Surveillance Requirement has not been performed. The ACTION requirements may be delayed for up to 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> to permit the completion of the surveillance when the allowable outage time limits of the ACTION requirements are less than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />."
An assessment was performed considering both the safety consequences and implications of this event with the following results and conclusions:
The requirement of TS 4.6.1.e.3.(a) is to simulate a loss of offsite power in conjunction with a safety injection test signal and verify de-energization of the emergency buses and load shedding from the emergency buses.
Performance of this surveillance is accomplished through a number of shutdown procedures: RSSP-2.1, RSSP-2.1A, RSSP-2.2, RSSP-19, RSSP-20, PT-9.1.14, PT-9.1.16, PT-9.1.17, and PT-9.1.18. An evaluation of these procedures indicated that the undervoltage load shedding of the following safeguards equipment was not being performed: safety injection (SI) pumps, residual heat removal (RHR) pumps, service water (SW) pumps, containment recirculation fans, and auxiliary feedwater (AFW) pumps. In addition, the undervoltage (in conjunction with SI signal) load shedding of the CCW pumps was not being performed. The procedures did verify the operability of the undervoltage relays, undervoltage system logic, and partially verified the operability of the undervoltage auxiliary relays. The procedures also verified the load shedding of all other emergency bus loads.
NRC FORM 366A (5-92)
NRC FORM 366A U.S. NUCLEAR REGULATORY CQOIISSION APPROVED BY QQI NO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY 'WITH THIS INFORMATION COLLECTIOH REQUEST: 50.0 HRS.
FORWARD COMMENTS REGARDIHG BURDEN ESTIMATE TO LICENSEE EVENT REPORT (LER) THE INFORMATION AND RECORDS MANAGEMENT BRANCH TEXT CONTINUATION (MHBB 7714), U.S. NUCLEAR REGULATORY COMMISSION@
WASHINGTON, DC 20555 0001 AHD TO THE PAPERWORK REDUCTION PROJECT (3140 0104), OFFICE OF MANAGEMENT AND BUDGET WASHINGTON DC 20503.
FACILITY NAME 1 DOCKET HIMBER 2 LER HIHIBER 6 PAGE 3 YEAR SEQUENTIAL REVISION R.E. Ginna Nuclear Power Plant 05000244 93 -- 005 00 8 OF 9 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)
The testing performed on October 11 and 12, 1993 demonstrated end-to-end operability of the undervoltage protection system.
This testing verified undervoltage signals to all safeguards equipment, and undervoltage in conjunction with SI signals to the CCW pumps. This testing also verified full operability of the undervoltage auxiliary relays.
The testing, in combination with the surveillance tests conducted during the 1993 outage,.met the requirements of TS 4.6.1.e.3.(a). Based on the above, public's health and safety was assured at all times.
it can be concluded that the V. CORRECTIVE ACTION A. ACTION TAKEN TO RETURN AFFECTED SYSTEMS TO PRE-EVENT NORMAL STATUS:
O Testing was performed within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> of discovery, and compliance with the requirements of TS 4.6.1.e.3.(a) was achieved.
B. ACTION TAKEN OR PLANNED TO PREVENT RECURRENCE:
o Procedures that verify load shedding capability will be upgraded to include safeguards loads, for conditions of undervoltage and SI, prior to the next scheduled refueling outage.
O The requirements of TS 4.6.1 have been reviewed and compared with surveillance procedures. No non-compliances were identified.
O A review of Section 4 of the Ginna Technical Specifications will be performed, to ensure that there are implementing procedures for every surveillance required by TS.
NRC FORM 366A (5-92)
NRC FORM 366A U.S. NUCLEAR REGULATORY C(NHISSIOH APPROVED BY OMB NO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY 'NITN THIS IHFORMATIOH COLLECTIOH REOUEST: 50.0 NRS.
FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO LICENSEE EVENT REPORT (LER) THE INFORMATION AND RECORDS MANAGEMENT BRANCH TEXT CONTINUATION (MHBB 7714), U.S. NUCLEAR REGULATORY COMHISSIOH ~
IJASHINGTON, DC 20555-0001 AHD TO THE PAPERMORK REDUCTION PROJECT (3140-0104), OFFICE OF MANAGEMENT AND BUDGET NASHIHGTON DC 20503.
FACI LIT'Y NAME 1 DOCKET NUMBER 2 LER NUMBER 6 PAGE 3 YEAR SEQUENTIAL REVISION R.E. Ginna Nuclear Power Plant 05000244 93 005-- 00 9 OF 9 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)
VI. ADDITIONAL INFORMATION A. FAILED COMPONENTS:
None.
B. PREVIOUS LERs ON SIMILAR EVENTS.
A similar LER event historical search was conducted with the following results: No documentation of similar LER events with the same root cause at Ginna Nuclear Power Plant could be identified.
C. SPECIAL COMMENTS:
NRC GL 87-09 allows 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> to perform a missed surveillance test, if the allowable outage time (AOT) of the LCO Action Requirements are less than this 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> time limit, or when shutdown Action Requirements apply. This time limit is based balancing the risks between completing the required testing
'n and potentially challenging safety systems while performing shutdown actions. TS 4.6.1.e.3.(a) is normally required to be performed during shutdown conditions, since performing this surveillance removes the normal source of offsite power, which may cause electrical system disturbances. Rochester Gas &
Electric (RG&E) elected to perform the necessary testing at power, after evaluating the potential risks.
A review of existing testing procedures indicated that only specific portions of the load shedding capabilities were not being tested. RG&E determined that performance of the necessary voltage and continuity tests to verify these untested capabilities could be safely conducted at power. This is due to the fact that no safeguards loads on the buses would have to be declared inoperable, and no offsite power source would have to be removed from service to perform the tests. Therefore, performance of the necessary tests (at power) within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> of discovery was deemed appropriate.
HRC FORM 366A (5.92)