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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:RO)
MONTHYEARML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17265A7601999-10-0505 October 1999 Part 21 Rept Re W2 Switch Supplied by W Drawn from Stock, Did Not Operate Properly After Being Installed on 990409. Switch Returned to W on 990514 for Evaluation & Root Cause Analysis ML17265A7621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Re Ginna Npp.With 991008 Ltr ML17265A7531999-09-23023 September 1999 Part 21 Rept Re Corrective Action & Closeout of 10CFR21 Rept of Noncompliance Re Unacceptable Part for 30-4 Connector. Unacceptable Parts Removed from Stock & Scrapped ML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7471999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Re Ginna Npp.With 990909 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7341999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Re Ginna Npp.With 990806 Ltr ML17265A7291999-07-29029 July 1999 Interim Part 21 Rept Re safety-related DB-25 Breaker Mechanism Procured from W Did Not Pas Degradatin Checks When Drawn from Stock to Be Installed Into BUS15/03A.Holes Did Not line-up & Tripper Pan Bent ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7131999-07-22022 July 1999 Special Rept:On 990407,radiation Monitor RM-14A Was Declared Inoperable.Caused by Failed Communication Link from TSC to Plant Process Computer Sys.Communication Link Was re-established & RM-14A Was Declaed Operable on 990521 ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7211999-07-19019 July 1999 ISI Rept for Third Interval (1990-1999) Third Period, Second Outage (1999) at Re Ginna Npp. ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A7661999-06-30030 June 1999 1999 Rept of Facility Changes,Tests & Experiments Conducted Without Prior NRC Approval for Jan 1998 Through June 1999, Per 10CFR50.59.With 991020 Ltr ML17265A7011999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Re Ginna Npp.With 990712 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6761999-06-16016 June 1999 Part 21 Rept Re Defects & noncompliances,10CFR21(d)(3)(ii), Which Requires Written Notification to NRC on Identification of Defect or Failure to Comply. Relays Were Returned to Eaton for Evaluation & Root Cause Analysis ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17265A6681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Re Ginna Nuclear Power Plant.With 990608 Ltr ML17265A6651999-05-27027 May 1999 Interim Rept Re W2 Control Switch,Procured from W,Did Not Operate Satisfactorily When Drawn from Stock to Be Installed in Main Control Board for 1C2 Safety Injection Pump. Estimated That Evaluation Will Be Completed by 991001 ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6591999-05-17017 May 1999 Part 21 Rept Re Relay Deficiency Detected During pre-installation Testing.Caused by Incorrectly Wired Relay Coil.Relays Were Returned to Eaton Corp for Investigation. Relays Were Repaired & Retested ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6381999-05-0707 May 1999 Part 21 Rept Re Replacement Turbocharger Exhaust Turbine Side Drain Port Not Functioning as Design Intended.Caused by Manufacturing Deficiency.Turbocharger Was Reaasembled & Reinstalled on B EDG ML17265A6391999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Re Ginna Nuclear Power Plant.With 990510 Ltr ML17265A6361999-04-23023 April 1999 Part 21 Rept Re Power Supply That Did Not Work Properly When Drawn from Stock & Installed in -25 Vdc Slot.Power Supply Will Be Sent to Vendor to Perform Failure Mode Assessment.Evaluation Will Be Completed by 991001 ML17265A6301999-04-18018 April 1999 Rev 1 to Cycle 28 COLR for Re Ginna Npp. ML17265A6251999-04-15015 April 1999 Special Rept:On 990309,halon Systems Were Removed from Svc & Fire Door F502 Was Blocked Open.Caused by Mods Being Made to CR Emergency Air Treatment Sys.Continuous Fire Watch Was Established with Backup Fire Suppression Equipment ML17265A6551999-04-0909 April 1999 Initial Part 21 Rept Re Mfg Deficiency in Replacement Turbocharger for B EDG Supplied by Coltec Industries. Deficiency Consisted of Missing Drain Port in Intermediate Casing.Required Oil Drain Port Machined Open ML17265A6291999-03-31031 March 1999 Rev 0 to Cycle 28 COLR for Re Ginna Npp. ML17265A6241999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Ginna Station.With 990409 Ltr ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A5661999-03-0101 March 1999 Rev 26 to QA Program for Station Operation. ML17265A5961999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Ginna Nuclear Power Plant.With 990310 Ltr ML17265A5371999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Re Ginna Nuclear Power Plant.With 990205 Ltr ML17265A5951998-12-31031 December 1998 Rg&E 1998 Annual Rept. ML17265A5001998-12-21021 December 1998 Rev 26 to QA Program for Station Operation. ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4761998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Re Ginna Nuclear Power Plant.With 981210 Ltr ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4531998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Re Ginna Nuclear Power Plant.With 981110 Ltr ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A4291998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Re Ginna Nuclear Power Plant.With 981009 Ltr 1999-09-30
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ACCELERATED DISTRIBUTION DEMONSTRATION SYSTEM~, I REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)ACCESSION NBR:9403110108 DOC.DATE: 94/03/04 NOTARIZED:
NO FACIL:50-244 Robert Emmet.Ginna Nuclear Plant, Unit 1, Rochester G AUTH.NAME AUTHOR AFFILIATION ST MARTIN,J.T.
Rochester Gas&Electric Corp.MECREDY,R.C.
Rochester Gas&Electric Corp.RECIP.NAME RECIPIENT AFFILIATION JOHNSON,A.R.
Project Directorate II-3 DOCKET g 05000244
SUBJECT:
LER 94-002-00:on 940202,discoverd Containment Pressure channels P-947&P-948 inoperable.
Caused by obstuction intr.comman containment pressure sensing line.Inoperable channels defeated,bistables in tripped condition.W/940304 ltr.DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR j ENCL/SIZE:/TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.D, NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72).
05000244 D RECIPIENT ID CODE/NAME PD1-3 PD INTERNAL: AEOD/DOA AEOD/ROAB/DSP NRR/DE/EMEB NRR/DRCH/HHFB NRR/DRCH/HOLB NRR/DRSS/PRPB NRR/DSSA/SRXB RES/DSIR/EIB EXTERNAL EG&G BRYCE F J~H NRC PDR NSIC POORE,W.COPIES LTTR ENCL 1 1 1 1 2 2 1 1 1 1 1 1 2 2 1 1 1 1 2 2 1 1 1 1 RECIPIENT ID CODE/NAME JOHNSON,A AEOD/DSP/TPAB NRR/DE/EELB NRR/DORS/OEAB NRR/DRCH/HICB NQR/DRIL/RPEB RR/ISSSA/PLB RGN1 FILE 01 L ST LOBBY WARD NSIC MURPHY,G.A NUDOCS FULL TXT COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 l.D D NOTE TO ALL"RIDS" RECIPIENTS:
D D PLEASE HELP US TO REDUCE WASTE!CONTACT THE DOCUMENT CONTROL DESK, ROOivI Pl-37 (EXT.20079)TO FLIMINATE YOUR NAME FROiil DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 27 ENCL 27 A ROCHESTER GAS AND ELECTRIC CORPORATION t~'~i e r~5 mart 51Att o 89 EAST AVENUE, ROCHESTER N.K 14649.0001 ROBERT C.MECREOY Vice President Oinna Nuclear Production TELEPHONE'REA CODE 716 546 2700 March 4, 1994 U.S.Nuclear Regulatory Commission Document Control Desk Attn: Allen R.Johnson Project Directorate I-3 Washington, D.C.20555
Subject:
LER 94-002, Containment Pressure Transmitters Inoperable, Due to Blockage of Sensing Line by Corrosion Products, Causes a Condition Prohibited by Technical Specifications R.E.Ginna Nuclear Power Plant Docket No.50-244 In accordance with 10 CFR 50.73, Licensee Event Report System, item (a)(2)(i)(B), which requires a report of,"Any operation or condition prohibited by the plant's Technical Specifications", the attached Licensee Event Report LER 94-002 is hereby submitted.
This event has in no way affected the public's health and safety.Very truly yours, Robert C.Mecredy xc: U.S.Nuclear Regulatory Commission Region I 475 Allendale Road King of Prussia, PA 19406 Ginna Senior Resident Inspector Zip&9403110108 940304 PDR ADOCK 05000244 8 PDR f NRC FORH 366 (5.92)U.S.NUCLEAR REGULATORY COHHISSIOH APPROVED BY QGI NO.3150-0104 EXPIRES 5/31/95 LICENSEE EVENT REPORT (LER)(See reverse for required number of digits/characters for each block)EST IHATED BURDEN PER RESPONSE TO COHPLY WITH THIS INFORHATION COLLECTION REQUEST: 50.0 HRS.FORWARD COMHENTS REGARDING BURDEH EST I HATE TO THE INFORMATION AND RECORDS-MANAGEHENT BRANCH (MNBB 7714), U.S.NUCLEAR REGULATORY COMMISSION/
WASHINGTON, DC 20555-0001 AND TO THE PAPERWORK REDUCTION PROJECT (3110-0104), OFFICE OF MANAGEMENT AND BUDGET WASHINGTON DC 20503.FAcILITY NAME (1)R.E~Ginna Nuclear Power Plant DOCKET IRNIBER (2)05000244 PAGE (3)10F 10 TITLE (4)Contaiwent Pressure Transmitters Inoperable, Due to Blockage of Sensing Line by Corrosion Products, Causes a Condition Prohibited by Technical Specifications EVENT DATE 5 LER NUIBER 6 REPORT DATE 7 OTHER FACILITIES INVOLVED 8 HONTH DAY 02 02 YEAR 94 YEAR 94 SEQUENTIAL NUMBER-002--REVISION NUHBER 00 HONTH 03 DAY YEAR 04 94 FACILITY NAME FACILITY NAHE DOCKET NUHBER DOCKET NUHBER OPERATING HODE (9)POWER LEVEL (10)N 098 THIS REPORT IS SUBHITTED PURSUANT 20.402(b)20.405(a)(1)(i)20.405(a)(1)(ii) 20.405(a)(1)(iii) 20.405(a)(1)(iv) 20.405(a)(1)(v) 20.405(c)50.36(c)(1) 50.36(c)(2) 50.73(a)(2)(i) 50.73(a)(2)(ii) 50.73(a)(2)(iii) 50.73(a)(2)(iv) 50.73(a)(2)(v) 50.73(a)(2)(vii) 50.73(a)(2)(viii)(A) 50.73(a)(2)(viii)(B) 50'3(a)(2)(x) 73.71(b)73.71(c)OTHER (Specify in Abstract below and in Text, NRC Form 366A TO THE REQUIREMENTS OF 10 CFR: Check one or mor e 11 LICENSEE CONTACT FOR THIS LER 12 NAHE John T~St.Hartin-Director, Operating Experience TELEPHONE NUMBER (Include Area Code)(315)524-4446 CQIPLETE ONE LINE FOR EACH C(NPONENT FAILURE DESCRIBED IN THIS REPORT 13 CAUSE SYSTEH COMPONENT MANUFACTURER REPORTABLE TO NPRDS CAUSE SYSTEM COMPONENT HANUFACTURER REPORTABLE TO NPRDS SUPPLEMENTAL REPORT EXPECTED 14 YES (If yes, complete EXPECTED SUBHISSION DATE).X NO EXPECTED SUBHISSION DATE (15)HONTH DAY YEAR ABSTRACT (Limit to 1400 spaces, i'.e., approximately 15 single-spaced typewritten lines)(16)On February 2, 1994, at approximately 1642 EST, with the reactor at approximately 98%steady state power, Control Room operators determined that Containment Pressure channels P-947 and P-948 were inoperable.
Based on post-event review of computer data, this condition was in violation of Technical Specification Table 3.5-2 Action Statements.
Immediate corrective action was to defeat the inoperable channels by placing the affected bistables in the tripped condition.
The underlying cause of the event was an obstruction in the common containment pressure sensing line for P-947 and P-948.Corrective action was taken to clear the obstruction from the affected tubing, leak test the penetration piping and transmitter tubing, and verify the proper operation of P-947 and P-948.Corrective action to preclude repetition is outlined in Section V (B).NRC FORM 366 (5 92)
NRC FORM 366A (5-92)U.S.NUCLEAR REGULATORY CQIIISSION LICENSEE EVENT REPORT (LER)TEXT CONTINUATION APPROVED BY QGI NO.3150-0104 EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS.FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMEN'I BRANCH (MNBB 7714), U.S.NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555-0001 AND TO THE PAPERWORK REDUCTION PROJECT (31i0.0104), OFFICE OF MANAGEMENT AND BUDGET WASHINGTON DC 20503.FACILITY NAME 1 DOCKET NLNBER 2 LER NUMBER 6 SEQUENTIAL REVISION PAGE 3 R.E.Ginna Nuclear Power Plant 05000244 94--002-00 2 OF 10 TEXT (If more space is required, use additional copies of HRC Form 366A)(17)PRE-EVENT PLANT CONDITIONS The plant was at approximately 984 steady state reactor power with no major activities in progress.Instrument and Control (I&C)Department personnel were investigating Containment Pressure channel P-947.This investigation was initiated by a Maintenance Work Request/Trouble Report (MWR/TR)written January 20, 1994 by Control Room operators because the Main Control Board pressure indication for P-947 (PI-947)was observed to be reading slightly lower than the indication for Containment Pressure channels P-945 and P-949 (PI-945 and PI-949), which are also on the Main Control Board.II.DESCRIPTION OF EVENT A.DATES AND APPROXIMATE TIMES OF MAJOR OCCURRENCES:
o June 24, 1992, 1500 EDST: Containment (CNMT)pressure channel P-947 output indication starts to become inconsistent with channels P-945 and P-949, as monitored on the Plant Process Computer System (PPCS).(This is based on post-event review of archived data on the PPCS.)Event date and time.o January 20, 1994: Control Room operators submit MWR/TR on PI-947 Main Control Board indication.
o February 2, 1994, 1642 EST: Discovery date and time.o February 4, 1994, 0007 EST: Containment Pressure channel P-947 is restored to operable status.o February 4, 1994, 1536 EST: Containment Pressure channel P-948 is restored to operable status.HRC FORM 366A (5 9?)
NRC FORM 366A (5-92)U S NUCLEAR REGULATORY CQIIISSION LICENSEE EVENT REPORT (LER)TEXT CONTINUATION APPROVED BZ CHB NO.3150-0104 EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECT ION REQUEST: 50.0 HRS.FORWARD COMMENTS REGARDING BURDEH ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRANCH (MNBB 7714), U.S.NUCLEAR REGULATORY COMMISSION, WASHIHGTON, DC 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150 0104), OFFICE OF MANAGEMENT AND BUDGET WASHINGTON DC 20503.FACILITY NAME 1 R.E.Ginna Nuclear Power Plant DOCKET NMBER 2 05000244 YEAR LER NINBER 6 SEQUENTIAL M R 94-002--REVISION M 00 PAGE 3 3 OF 10 TEXT (If more space is required, use additional copies of NRC Form 366A)(17)B.EVENT: On January 20, 1994, Control Room operators observed that one Main Control Board indication for CNMT pressure, PI-947,"was reading slightly lower than the other two indicators, PI-945 and PI-949.They initiated a MWR/TR, for I&C personnel to investigate the difference in readings.On January 21, I&C performed the annual calibration of the channel.The channel (P-947)responded properly to both the electronic checks and,to actual pressure signals inserted into the transmitter (PT-947).After reviewing post-calibration trending data and archived PPCS computer traces of CNMT pressure, I&C noticed that channel P-947 was still not tracking consistent with channels P-945 and P-949.Further investigation was conducted on February 2, 1994, to identify if there could be any possible mechanical and/or electrical problems with P-947.On February 2, 1994, at approximately 1612, EST, with the reactor at approximately 98%,steady state reactor power, Control Room operators declared channel P-947 inoperable.
The affected bistables were placed in the tripped condition.
To verify the operability of the redundant CNMT pressure channels, the operators then caused a small change in CNMT pressure by depressurizing CNMT per operating procedure 0-11,"Control of Mini Purge Exhaust Valves While Depressurizing Containment".
I&C personnel monitored test points for CNMT pressure channels P-945, P-947, P-948, and P-949 with a digital multimeter.
During this depressurization, at approximately 1642 EST, two channels (P-947 and P-948)did not show any response to the small change in CNMT pressure.The'Control Room operators formally declared P-948 inoperable at approximately 1658 EST.The affected bistables were placed in the tripped condition per emergency restoration procedure ER-INST.1,"Reactor Protection Bistable Defeat After Instrumentation Loop Failure".P-947 and P-948 sense CNMT pressure via a common line (CNMT Penetration 203A).A CNMT entry was made to verify that this sensing line for PT-947 and PT-948, (Pen.203A)was not mechanically blocked.Pen.203A was visually verified not to be externally obstructed.
The valve lineups for the pressure transmitters (PT-947 and PT-948)were verified to be correct.HRC FORM 366A (5-92)
NRC FORM 366A (5-92)U.S.NUCLEAR REGULATORY CQIII SSI ON LICENSEE EVENT REPORT (LER)TEXT CONTINUATION APPROVED BY CSQ NO.3150-0104 EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPOHSE TO COMPLY MITH THIS INFORMATION COLLECTIOH REQUES'I: 50.0 HRS.FORllARD COMMENTS REGARDIHG BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRANCH (MNBB 7714), U.ST NUCLEAR REGULATORY COMMISSIONS HASHIHGTOH, DC 20555-0001 AHD TO THE PAPERIJORK REDUCTION PROJECT (3140-0104), OFFICE OF MANAGEMENT AND BUDGET'WASHINGTON DC 20503.FACILITY NAME 1 R.E.Ginna Nuclear Power Plant DOCKET NtMBER 2 05000244 94--002--00 LER NINBER 6 YEAR SEOUEHTIAL REVISION PAGE 3 4 OF 10 TEXT (If more space is required, use additional copies of HRC Form 366A)(17)On February 3, 1994, a work package for troubleshooting and repair of the CNMT penetration line was prepared.A CNMT entry was made and Pen.203A was pressurized to thirty (30)pounds per square inches above atmospheric pressure (PSIG), using surveillance test procedure PTT-23.17B,"Containment Isolation Valve Leak Rate Testing Containment Pressure Transmitters PT-947 and PT-948 Pen 203A".PT-947 and PT-948 did not respond to this pressure, which indicated a blockage in the piping for Pen.203A or in the common instrument tubing line.Backflushing with one-hundred-twenty (120)PSIG air supply to clear the blockage was unsuccessful.
Pen.203A was isolated inside CNMT to provide double barrier isolation for CNMT integrity.
The instrument tubing was disconnected outside CNMT.The instrument tubing was found to contain water, but.this water was not the source of the blockage.The 1/t2 inch carbon steel tubing for Pen.203A was found to be mechanically blocked with a thick sludge.The blockage was removed.The tubing was reassembled and preparations were made to test the tubing.I On February.3, 1994, at approximately 2207 EST, Pen.203A was declared inoperable to perform required Appendix J testing.The Limiting Condition for Operation (LCO)for Technical Specification (TS)3.6.3.1.was entered.Pen.203A was tested in accordance with surveillance test procedure PTT-23.17B,"Containment Isolation Valve Leak Rate Testing Containment Pressure Transmitters PT-947 and PT-948 Pen 203A".It was documented in PTT-23.17B that PT-947 and PT-948 now accurately responded when the penetration was pressurized to 60 PSIG.PTT-23.17B was successfully completed at approximately 2336 EST and Pen.203A was declared operable at approximately 2340 EST.OnFebruary 4, 1994, at approximately 0007 EST, P-947 was declared operable.The transmitter and rack calibration procedure for channel P-948 was performed later in the day on February 4, and P-948 was declared operable at approximately 1536 EST on February 4, 1994.C~I NOPERABLE'TRUCTURES i COMPONENTS i OR SYSTEMS THAT CONTRI BUTED TO THE EVENT: None NRC FORM 366A (5 92)
HRC FORH 366A (5-92)U.S NUCLEAR REGULATORY CQIII SSIOH LICENSEE EVENT REPORT (LER)TEXT CONTINUATION APPROVED BY QGI NO.3150-0104 EXPIRES 5/31/95 ESTIHATED BURDEN PER RESPONSE TO COMPLY MITH THIS INFORHATIOH COLLECTION REQUEST: 50.0 HRS.FORNARD COHMENI'S REGARDIHG BURDEN ESTIHATE TO THE INFORMATION AND RECORDS HANAGEHEHT BRAHCH (MHBB 7714), U.S.NUCLEAR REGULATORY COMHISSION, llASHINGTOH, DC 20555-0001 AND TO THE PAPERNORK REDUCTION PROJECT (3140-0104), OFFICE OF HANAGEMENI'ND BUDGET LIASHINGTON DC 20503.FACILITY NAHE 1 R.E.Ginna Nuclear Power Plant DOCKET NINBER 2 05000244 94--002--00 LER HI%GER 6 YEAR SEQUENTIAL REVISION PAGE 3 5 OF 10 TEXT (If more space is required, use additional copies of NRC Form 366A)(17)D.OTHER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED: Engineered Safety Features that rely on CNMT pressure inputs are Safety Injection Actuation (SI), Steam Line Isolation, and Containment Spray Actuation (CNMT Spray).None of these features was affected by the inoperability of P-947 and P-948, because at no time, from'June 24, 1992, to February 4, 1994, was CNMT pressure at or near the actuation setpoints (4 PSIG for SI, 18 PSIG for Steam Line Isolation, and 28 PSIG for CNMT Spray).During this period, the redundant channels (for P-94'7 the channels are P-945 and P-949;for P-948 the channels are P-946 and P-950)were in service and were not taken out of service unless the affected bistables were placed in the tripped condition.
E.METHOD OF DISCOVERY:
This event was first identified due to the astute observation of a Control Room operator on January 20, 1994, who questioned a slight difference in indications for CNMT pressure.The small deviation between redundant channels was within the tolerance of Main Control Board instrumentation channel checks.The monthly Channel Functional Tests and annual Channel Calibrations associated with these channels (as required by TS Table 4.1-1 for units f17 and f25)did not detect the obstructed tubing line due to the location of the obstruction.
The sludge was located between CNMT and the root isolation valves for PT-947 and PT-948.These root isolation valves are closed during performance of the necessary tests and calibrations, in order to pressurize the volume between the valve and the pressure transmitter.
This method of testing is consistent with the definition of Channel Functional Testing, as defined in TS 1~7~3~a~The fact that this event affected both channels P-947 and P-948 was identified as a result of the investigations performed by I&C personnel on February 2, 1994.A more detailed review of the archived PPCS records of CNMT pressure concluded that channel P-947 had not responded to changes in CNMT pressure since June 24, 1992, beginning at approximately 1500 EDST.HRC FORH 366A (5-92)
NRC FORH 366A (5-92)U.S.NUCLEAR REGULATORY CQOII SSION LICENSEE EVENT REPORT (LER)TEXT CONTINUATION APPROVED BY 0KB NO.3150-0104 EXPIRES 5/31/95 ESTIHATED BURDEN PER RESPOHSE TO COHPLY WITH THIS IHFORHATION COLLECTIOH REQUEST: 50.0 HRS.FORWARD CONNENTS REGARDING BURDEN ESTIHATE TO THE IHFORHATIOH AND RECORDS NANAGEHEHT BRANCH (HHBB 7714), U.S.NUCLEAR REGULATORY CONHISSIONg WASHINGTON, DC 20555-0001 AND TO THE PAPERWORK REDUCTION PROJECT (3140.0104), OFFICE OF NANAGENENT AND BUDGET WASHINGTON DC 20503.FACILITY NANE 1 R.E.Ginna Nuclear Power Plant DOCKET NIMBER 2 05000244 94--002--00 LER NIMBER 6 YEAR SEQUENTIAL REVISION PAGE 3 6 OF 10 TEXT (If more space is required, use additionnI copies of NRC Form 366A)(17)Note that while CNMT pressure channel P-947 is monitored by the PPCS, channel P-948 is not.In addition, PI-948 (and also PI-946 and PI-950)have a scale of 10 to 200 PSIA (absolute pressure).
By comparison, PI-947 (and also PI-945 and PI-949)have a scale of 0 to 60 PSIG.It is assumed that P-948 had not responded to changes in CNMT pressure for the same amount of time as P-947.F.OPERATOR ACTION: The Control Room operators observed that the PI-947 reading was inconsistent on January 20, 1994, and initiated'a MWR/TR.After both channels P-947 and P-948 were discovered to be inoperable, the Control Room operators performed emergency restoration procedure ER-INST.1 and placed the affected bistables in the tripped condition.
Subsequently, the Control Room operators ensured that higher supervision and the NRC Resident Inspector had been notified of this event.G.SAFETY SYSTEM RESPONSES:
None III.CAUSE OF EVENT A.IMMEDIATE CAUSE: The immediate cause of the event was the failure of P-947 and P-948 to respond to changes in CNMT pressure due to obstruction of the common pressure sensing line.B.INTERMEDIATE CAUSE: The intermediate cause of the obstruction of the common pressure sensing line at Pen.203A was a buildup of corrosion products in this line, which is 1/2 inch OD, 0.065 inch wall thickness, carbon steel tubing.These corrosion products were visually examined and found to be reddish brown/black in color, visually resembling iron oxide scale.HRC FORH 366A (5-92)
NRC FORM 366A (5-92)U.S NUCLEAR REGULATORY C(NHISSIOH LICENSEE EVENT REPORT (LER)TEXT CONTINUATION APPROVED BY INIB NO.3'150-0104 EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY IJITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS.FORIJARD COMMENTS REGARDING BURDEN ESTIMATE TO THE IHFORMATIOH AHD RECORDS MANAGEMENT BRANCH (MHBB 7714), U.S+NUCLEAR REGULATORY COMMISSIOH, IJASHINGTOH, DC 20555-0001 AND TO THE PAPERIJORK REDUCTION PROJECT (31(0-0104), OFFICE OF MANAGEMENT AHD BUDGET IJASHIHGTON DC 20503.FACILITY NAME 1 R.E.Ginna Nuclear Power Plant DOCKET HINBER 2 05000244 YEAR 94 LER HINBER 6 SEQUENTIAL M--002-REVISION 00 PAGE 3 7 OF 10 TEXT (If more space is required, use additional copies of HRC Form 366A)(17)C.ROOT CAUSE: The underlying cause of the buildup of corrosion products (iron oxide scale)was the method of transmitter calibration coupled with sensing line configuration.
I&C personnel have calibrated these transmitters with a water-filled deadweight tester for many years.The configuration of the transmitter and sensing line prevented the drainage of all the water after calibration.
After the transmitter was unisolated as part of the calibration process, the trapped water traveled down to the low portion of the sensing line.Stagnant water has remained in the carbon steel sensing lines for a substantial period of time.Under such conditions, sig-nificant corrosion of the carbon steel material can occur.The corrosion product, hydrated iron oxide (common rust)is voluminous, occupying many times the volume of the material lost to the corrosion process.Sufficient corrosion product accumulated to block the sensing line tubing, resulting in the inoperability of P-947 and P-948.IV.ANALYSIS OF EVENT This event is reportable in accordance with 10 CFR 50.73, Licensee Event Report System, item (a)(2)(i)(B), which requires a report of,"Any operation or condition prohibited by the plant's'Technical Specifications".
CNMT pressure channels P-947 and P-948 were inoperable for a considerable length of time, in violation of TS Table 3.5-2, units g 1.b., 2.b., and 5.c.Operation in this condition since June 24, 1992 is a condition prohibited by TS.An assessment was performed considering both the safety consequen-ces and implications of this event.The results of this assessment are that there were no operational or safety consequences or implications attributed to the inoperability of P-947 and P-948 because: o A review of plant history and preventive maintenance history files has shown that the redundant CNMT pressure channels (P-945, P-946, P-949, and P-950)have been either operable or placed in the conservative tripped state from the Event date to the Discovery date.NRC FORM 366A (5-92)
NRC FORM 366A (5-92)U.S NUCLEAR REGULATORY COtlISSIOH LICENSEE EVENT REPORT (LER)TEXT CONTINUATION APPROVED BT QQ NO.3150-0104 EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY IIITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS~FORIJARD COMMENTS REGARDIHG BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRANCH (HHBB 7714), U.S.NUCLEAR REGULATORY COMMISSION,'MASHIHGTON, DC 20555-0001 AHD TO THE PAPERWORK REDUCTION PROJECT (3140-0104), OFFICE OF MANAGEMENT AND BUDGET IIASHINGTON DC 20503.R.E.Ginna FACILITY NAME 1 Nuclear Power Plant DOCKET NINBER 2 05000244 YEAR 94 LER HINIBER 6 SEQUENTIAL
--002--REVISION PAGE 3 pp 8 OF 10 TEXT (lf more space is required, use additional copies of NRC Form 366A)(17)o A review of PPCS data has shown that the redundant pressure channels have responded to pressurization of the sensing lines and pressure changes in CNMT.Thus, these redundant channels did not exhibit the same failure mode as P-947 and P-948.0 0 The 2 out of 3 logic (2/3)required for actuation of SI was reduced to'a 2/2 logic with the inoperability of P-947.Thus SI actuation from high CNMT pressure (4 PSIG)would have occurred as assumed in the design basis.The diverse actuation circuitry for SI has three additional means of actuation (steam generator low steam pressure, pressurizer low pressure, and Manual).None of these diverse means was affected by the inoperability of P-947.The 2/3 logic required for Steam Line Isolation actuation was reduced to a 2/2 logic with the inoperability of P-948.Thus, Steam Line Isolation actuation from high-high CNMT pressure (18 PSIG)would'have occurred as assumed in the design basis.0 The diverse actuation circuitry for Steam Line Isolation has three additional means of actuation (hi-hi steam flow with safety injection, hi steam flow and 2/4 low Tavg with safety injection, and Manual).None of these diverse means was affected by the inoperability of P-948.o The 2/3 plus 2/3 logic required for CNMT Spray actuation was reduced to a 2/2 plus 2/2 logic with the inoperability of P-947 and P-948.Thus, CNMT Spray actuation from high-high CNMT pressure (28 PSIG)would have occurred as assumed in the design basis.o The alternate actuation circuitry for CNMT Spray (Manual)was not affected by the inoperability of P-947 and P-948.Based on the above, it can be concluded that the public's health and safety was assured at all times.NRC FORM 366A (5-92)
NRC FORM 366A (5.92)U.S.NUCLEAR REGULATORY CQOIISSION LICENSEE EVENT REPORT (LER)TEXT CONTINUATION APPROVED BY QQ NO.3150-0104 EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY lllTH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS.FORNARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION AHD RECORDS MANAGEMENT BRANCH (MHBB 7714), U.S.NUCLEAR REGULATORY COMMISSION/
WASHINGTON, DC 20555-0001 AHD TO THE PAPERNORK REDUC'TIOH PROJECT (3140-0104), OFFICE OF MANAGEMENT AND BUDGET IIASHINGTON DC 20503.FACILITY NAME 1 R.E.Ginna Nuclear Power Plant DOCKET NNSER 2 YEAR 05000244 94 LER NHIBER 6 SEQUENTIAL
-002 RE VIS IOH PAGE 3 pp 9 OF 10 TEXT (If more space is required, use additional copies of NRC Form 366A)(17)V.CORRECTIVE ACTION A.ACTION TAKEN TO RETURN AFFECTED SYSTEMS TO PRE-EVENT NORMAL STATUS: o The iron oxide scale was removed from the obstructed'enetration sensing line and P-947 and P-948 were restored to operable status.o The other channels that monitor CNMT pressure were verified to respond to small changes in CNMT pressure.B.ACTION TAKEN OR PLANNED TO PREVENT RECURRENCE:
o PPCS computer points for CNMT pressure will be archived daily until the 1994 refueling outage to verify channel operability.
o The sensing lines for all CNMT pressure channels will be inspected and cleaned out during the 1994 refueling outage.o The method of calibration of the CNMT pressure transmitters has been changed to use gas (instead of water)as the test medium.o Testing these containment penetrations has been enhanced to include formal documentation of pressure channel response.HRC FORM 366A (5 92)
NRC FORM 366A (5-92)U.S.NUCLEAR REGULATORY CQIIISSION LICENSEE EVENT REPORT (LER)TEXT CONTINUATION APPROVED BY QUI NO.3150-0104 EXPIRES 5/31/95 ES'IIMATED BURDEN PER RESPONSE TO COMPLY lllTH THIS INFORMATION COLLECTIOH REOUEST: 50.0 MRS.FORNARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRANCH (MHBB 7714), U.S.NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555-0001 AND TO THE PAPERMORK REDUCTION PROJECT (3110-0104), OFFICE OF MAHAGEHEHT AHD BUDGET WASHINGTON DC 20503.FACILITY NAME 1 DOCKET NUMBER 2 LER NMBER 6 PAGE 3 R.E.Ginna Nuclear Power Plant 05000244 YEAR 94--002-pp 10 OF 10 SEQUENTIAL REVISIOH TEXT (lf more space is required, use additional copies of HRC Form 366A)(17)VI.ADDITIONAL INFORMATION A.FAILED COMPONENTS:
There were no failed components.
The obstructed sensing line is 1/2 inch OD, 0.065 inch wall thickness, carbon steel tubing.Information about the vendor and manufacturer is not relevant to this event.B.PREVIOUS LERs ON SIMILAR EVENTS: A similar LER event historical search was conducted with the following results: LER 92-003 was also an event caused by an obstructed pressure sensing line.However, the obstruction was caused by buildup of sludge from normal impurities in the process fluid (feedwater).
The obstruction referred to in LER 94-002 was caused by corrosion from the interaction of the test medium and the sensing line materials.
C.SPECIAL COMMENTS: None NRC FORM 366A (5-92)