ML17263A563

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LER 94-005-00:on 940217,turbine Runback Occurred Due to Lost Offsite Power Circuit 751 Causing Low Voltage on Safeguard Busses 14 & 18.Circuit 751 Restored by Automatic Reclosure of Transformer breaker.W/940321 Ltr
ML17263A563
Person / Time
Site: Ginna Constellation icon.png
Issue date: 03/21/1994
From: MCCREDY R C, ST MARTIN J T
ROCHESTER GAS & ELECTRIC CORP.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
LER-94-005, LER-94-5, NUDOCS 9403290326
Download: ML17263A563 (12)


Text

ACCj"-'LBRA"I"BDDlSTRlBUTluNDEMON&"I'RA'i'losSYSl'UIvll,ttREGULATORYINFORMATIONDISTRIBUTIONSYSTEM(RIDS)ACCESSIONNBR:9403290326DOC.DATE:94/03/21NOTARIZED:NOFACIL:50-244RobertEmmetGinnaNuclearPlant,Unit1,RochesterGAUTH.NAMEAUTHORAFFILIATIONSTMARTIN,J.T.RochesterGas&Electric'Corp.MCCREDY,R.C.RochesterGas&ElectricCorp.RECIP.NAMERECIPIENTAFFILIATIONDOCKET05000244

SUBJECT:

LER94-005-00:on940217,turbinerunbackoccurredduetolostoffsitepowercircuit751causinglowvoltageonsafegaurdbusses14&18.Circuit751restoredbyautomaticreclosureoftransformerbreaker.940321ltr.DISTRIBUTIONCODE:IE22TCOPIESRECEIVED:LTRENCLSIZE:TITLE:50.73/50.9LicenseeEventReport(LER),IncidentRpt,etc.DNOTES:LicenseExpdateinaccordancewith10CFR2,2.109(9/19/72).05000244ADRECIPIENTIDCODE/NAMEPD1-3PDINTERNAL:AEOD/DOAAEOD/ROAB/DSPNRR/DE/EMEBNRR/DRCH/HHFBNRR/DRCH/HOLBNRR/DRSS/PRPBNRR/DSSA/SRXBRES/DSIR/EIBEXTERNALEG&GBRYCEgJ~HNRCPDRNSICPOORE,W.COPIESLTTRENCL111122111111221111221111RECIPIENTIDCODE/NAMEJOHNSON,AAEOD/DSP/TPABNRR/DE/EELBNRR/DORS/OEABNRR/DRCH/HICBNRR/DRIL/RPEBLSTLOBBYWARDNSICMURPHY,G.ANUDOCSFULLTXTCOPIESLTTRENCL111111111111111111111111DDS'OTETOALL"RIDS"RECIPIENTS:PLEASEHELPUSTOREDUCEWARMCONTACTTHEDOCUMENTCONTROLDESK,ROOMPl-37(EXT.20079)TOELIMINATEYOURNAMEFROMDISTRIBUTIONLISTSFORDOCUMENTSYOUDON'TNEED!DD'SFULLTEXTCONVERSIONREQUIREDTOTALNUMBEROFCOPIESREQUIRED:LTTR27ENCL27

'1ROCHESTERGASANDELECTRICCORPORATIONe89EASTAVENUE,ROCHESTERN.Y.14649-0001ROBERTCMECREDYVicePtetldentCinnatcvctearpcodoctionTEt.EPk<ONBaAEACOnE7te546-2700March21,1994U.S.NuclearRegulatoryCommissionDocumentControlDeskAttn:AllenR.JohnsonProjectDirectorateI-3Washington,D.C.20555

Subject:

LER94-005,LossofOffsitePowerCircuit751,DuetoLossofPowerto¹234.5KVBusatStation204,CausesAutomaticActuationofRPSSystem(TurbineRunback)R.E.GinnaNuclearPowerPlantDocketNo.50-244Inaccordancewith10CFR50.73,LicenseeEventReportSystem,item(a)(2)(iv),whichrequiresareportof,"Anyeventorconditionthatresultedinamanualorautomaticactuationofanyengineeredsafetyfeature(ESF),includingthereactorprotectionsystem(RPS)",theattachedLicenseeEventReportLER94-005isherebysubmitted.Thiseventhasinnowayaffectedthepublic'shealthandsafety.Verytrulyyours,go(RobertC.Mecredyxc:U.S.NuclearRegulatoryCommissionRegionI475AllendaleRoadKingofPrussia,PA19406GinnaSeniorResidentInspector940329032b940321PDRADOCKOS0002448PDR NRCFORH366(5-92)U.S.NUCLEARREGULATORYCOMMISSIONAPPROVEDBYOMBNO.31500104EXPIRES5/31/95LICENSEEEVENTREPORT(LER)(Seereverseforrequirednumberofdigits/charactersforeachblock)ESTIMATEDBURDENPERRESPONSETOCOMPLY'WITHTHISINFORHATIONCOLLECTIONREQUEST:50.0MRS.FORWARDCOMMENTSREGARDINGBURDENESTIHATETOTHEIHFORHATIONANDRECORDSHANAGEHENTBRANCH(HNBB7714),U.S.NUCLEARREGULATORYCOMHISSION,WASHINGTON,DC20555-0001,ANDTOTHEPAPERWORKREDUCTIONPROJECT(3150-0104),OFFICEOFHANAGEHENTANDBUDGETWASHINGTONDC20503.FACILITYNAME(1)R.E.GinnaNuclearPowerPlantDOCKETNUMBER(2)05000244PAGE(3)10F9TITLE(4)LossofOffsitePowerCircuit751,DuetoLossofPowerto¹234'KVBusatStation204,CausesAutomaticActuationofRPSSystem(TurbineRunback)LERNUHBER(6)SEQUENTIALNUHBER--005--EVENTDATE(5)REVISIONNUMBERYEARYEAR9494MONTHDAY0217OPERATINGHODE(9)00N20.402(b)THISREPORTISSUBMITTEDPURSUANTREPORTDATE(7)OTHERFACILITIESINVOLVED(B)HONTH03DAY21FACILITYNAHEYEARFACILITYNAHEDOCKETNUMBERDOCKETNUHBERTOTHEREQUIREMENTSOF10CFR5:(Checkoneormore)(ll)20.405(c)50.73(a)(2)(iv)73.71(b)XPOWERLEVEL(10)09B20'05(a)(1)(t)20.405(a)(1)(ii)20'05(a)(1)(iii)20.405(a)(1)(iv)20.405(a)(1)(v)50.36(c)(1)50.36(c)(2)50.73(a)(2)(i)50.73(a)(2)(ii)50.73(a)(2)(iii)50'3(a)(2)(v)50.73(a)(2)(vii)50'3(a)(2)(viii)(A)50.73(a)(2)(viii)(B)50.73(a)(2)(x)73.71(c)OTHER(ScifpeylnAbstractbelowandinText,NRCForm366A)LICENSEECONTACTFORTHISLER(12)NAHEJohnT~St.Martin-Director,OperatingExperienceTELEPHONENUMBER(IncludeAreaCode)(315)524-4446COHPLETEONELINEFOREACHCOMPONENTFAILUREDESCRIBEDINTHISREPORT(13)CAUSESYSTEMCOMPONENTMANUFACTURERREPORTABLETONPRDSCAUSESYSTEMCOMPONENTHANUFACTURERREPORTABLETONPRDSSUPPLEMENTALREPORTEXPECTED(14)YES(lfyes,completeEXPECTEDSUBHISSIONDATE).XNDEXPECTEDSUBHISSIONDATE(15)MONTHDAYYEARABSTRACT(Limitto1400spaces,i.e.,approximately15single-spacedtypewrittenlines)(16)OnFebruary17,1994,atapproximately1421EST,withthereactoratapproximately98l.steadystatepower,aturbinerunbackoccurredwhenoffsitepower34.5KVCircuit751waslost,causinglowvoltageonsafeguardsbusses14and18.TheControlRoomoperatorsperformedtheappropriateactionsofAP-TURB.2,"TurbineLoadReduction",andverifiedthattheplantwasstabilizedatapproximately93%poweraftertherunbacksignalcleared.Theunderlyingcauseofthelossofpowertooffsite34.5KVCircuit751waslossofpowertoN234.5KVBusatoffsiteStation204.(ThiseventisNUREG-1022(C)CauseCode.)CorrectiveactiontoprecluderepetitionisoutlinedinSectionV(B).NRCFORH366(5-92)

NRCFORH366A(5.92)U.S.NUCLEARREGULATORYCOHHISSIONLICENSEEEVENTREPORT(LER)TEXTCONTINUATIONAPPROVEDBYOMBNO.3150-0104EXPIRES5/31/95ESTIMATEDBURDENPERRESPONSETOCOHPLYWITHTHISINFORMATIONCOLLECTIONREQUEST:50.0HRS.FORWARDCOMMENTSREGARDIHGBURDENESTIHATETOTHEINFORHATIONANDRECORDSHANAGEMENTBRANCH(MNBB7714),U.STNUCLEARREGULATORYCOHMISSION,WASHINGTON,DC20555-0001ANDTOTHEPAPERWORKREDUCTIONPROJECT(31/0-0104),OFFICEOFMANAGEMENTANDBUDGETWASHINGTONDC20503.FACILITYNAME(1)R.E.GinnaNuclearPowerPlantDOCKETNUHBER(2)050002449400500LERNUMBER(6)YEARSEQUENTIALREVISIONPAGE(3)2OF9TEXT(Ifmorespaceisrequired,useadditionalcopiesofNRCForm366A)(17)I.PRE-EVENTPLANTCONDITIONSTheplantwasatapproximately98~steadystatereactorpower.The"A"emergencydieselgenerator(D/G)wasinoperationforthemonthlyperiodictestofD/Gperformance,procedurePT-12',"EmergencyDieselGeneratorlA."The"A"D/GwasinManualvoltagecontrol,'ndelectricallyloaded,perPT-12.1,toapproximatelytwothousand(2000)kilowatts(KW),supplyingpowerto480voltACsafeguardsbusses14and18.TheD/Gwassynchronizedtotheoffsitedistributionsystem,andwasbackfeedingsomepowertotheoffsiteelectricaldistributionsystem.Theoffsitepowertotheplantwasasfollows:~Offsitepower34.5KVCircuit751waslineduptosupplypowertosafeguardsbusses14and18through12A34.5KV/4160Vtransformerandthroughthesafeguardsbusses4160V/480Vtransformers.Inparallelwithoffsitepower,the"A"D/Gwasalsosupplyingpowertothesebusses.~Offsitepower34.5KVCircuit767wassupplyingpowertosafeguardsbusses16and17through12B34.5KV/4160Vtransformerandthroughthesafeguardsbusses4160V/480Vtransformers.NRCFORM366A(5-92)

NRCFORM366A(5-92)U.S.NUCLEARREGULATORYCOMMISSIONLICENSEEEVENTREPORT(LER)TEXTCONTINUATIONAPPROVEDBYOMBNO.3150~0104EXPIRES5/31/95ESTIMATEDBURDENPERRESPONSETOCOMPLYWITHTHISIHFORMATIONCOLLECTIONREQUEST:50.0HRS.FORWARDCOMMENTSREGARDIHGBURDENESTIMATETOTHEINFORMATIONANDRECORDSMANAGEMENTBRANCH(MNBB7714),U.S.NUCLEARREGULATORYCOMMISSION,WASHINGTON,DC20555-0001ANDTOTHEPAPERWORKREDUCTIONPROJECT(3110-0104),OFFICEOFMAHAGEMENTANDBUDGETWASHINGTONDC20503.FACILITYNAME(1)R.E.GinnaNuclearPowerPlantDOCKETNUMBER(2)05000244'EAR005--00LERNUMBER(6)SEQUENTIALREVISIONPAGE(3)3OF9TEXT(Ifmorespaceisrequired,useadditionalcopiesofNRCForm366A)(17)II.DESCRIPTIONOFEVENTA.DATESANDAPPROXIMATETIMESOFMAJOROCCURRENCES:~Februarystarted,P~Februaryisolated17,1994,1251EST:Monthlytestofthe"A"D/GwasperPT-12.117,1994,1421EST:Offsite34.5KVCircuit751wasfromtheelectricaldistributionsystem.~February17,1994,1421EST:Turbinerunback.Eventdateandtime.February17,1994,1421EST:Discoverydateandtime.VFebruary17,1994,1422EST:ControlRoomoperatorsperformedtheappropriateactionsofAP-TURB.2,"TurbineLoadReduction,"andstabilizedtheplant.~February17,1994,1444EST:Safeguardsbusses14and18resuppliedfromoffsitepower34.5KVCircuit751.~Febiuary17,1994,2210EST:Plantwasrestoredtoapproximately98~steadystatereactorpower.B.EVENT:OnFebruary17,1994,aproblemwasidentifiedintheRochesterGasandElectric(RGEE)electricaldistributionsystem.Anairtankona34.5KVcircuitbreakerwasleaking.Atapproximately1420EST,RGEEEnergyOperationscheckedthebusvoltagesattwooffsiteelectricaldistributionstations(Station204andStation13A)andopenedtheaffectedcircuitbreaker(5X20452).Thiswasastandardswitchingoperationthathasbeenperformedanumberoftimes.Uponopeningbreaker5X20452,¹234.5KVBusatStation204experiencedahighvoltagecondition.Afterreceivingthehighvoltagealarm,¹234.5KVBustransformerbreaker(2T20452)unexpectedlytripped,isolating¹234.5KVBusfromtherestoftheelectricaldistributionsystem.NRCFORM366A(5-92)

NRCFORH366A(5-92)U.S.NUCLEARREGULATORYCOHHISSIONLICENSEEEVENTREPORT(LER)TEXTCONTINUATIONAPPROVEOBYOHBNO.3150-0104EXPIRES5/31/95ESTIHATEDBURDENPERRESPONSETOCOHPLYWITHTHISINFORMATIONCOLLECTIOHREQUEST:50.0HRS~FORWARDCOMMENTSREGARDINGBURDENESTIHATETOTHEINFORMATIONANDRECORDSHANAGEHENTBRANCH(HNBB7714),U.S.NUCLEARREGULATORYCOMMISSION,WASHINGTON,DC20555-0001ANDTOTHEPAPERWORKREDUCTIONPROJECT(3140-0104),OFFICEOFMANAGEMENTANDBUDGETWASHINGTONDC20503.FACILITYNAME(1)R.E.GinnaNuclearPowerPlantDOCKETNUMBER(2)YEAR0500024494LERNUHBER(6)SEQUENTIAL--005--REVISION00PAGE(3)4OF9TEXT(Ifmorespaceisrequired,useadditionalcopiesofNRCForm366A)(17)Theg234.5KVBussuppliesCircuit751,oneofthetwo34.5KVtransmissioncircuitsthatsuppliesoffsitepowertoGinnaStation.Therefore,apartiallossofoffsitepowertoGinnaoccurred,asCircuit751wasnowisolatedfromtherestoftheelectricaldistributionsystem.Theotheroffsitepowersupply,from34.5KVCircuit767,wasunaffectedandcontinuedtosupplypowerto480Vsafeguardsbusses16and17.Circuit751andtheN234.5KVBuswiththeirconnectedloadsremainedenergizedbytheGinna"A"D/G,sincetheD/GhadbeenparalleledtotheoffsiteelectricaldistributionsystemviaCircuit751.However,withthe"A"D/GinManualvoltagecontrol,the"A"D/GvoltageoutputwasreducedbytheelectricalloadsonN234.5KVbus,whichresultedinalowvoltageconditiononbusses14and18.Thisvoltagereductionresultedinactuationofundervoltagerelays,whichtrippedthenormalsupplybreakersto480Vbusses14and18.Trippingofthenormalsupplybreakerstobusses14and18isolatedthe"A"D/Gandbusses14and18fromCircuit751.The"A"D/Gvoltage(andthevoltageonbusses14and18)recoveredtoabovetheundervoltagerelayactuationsetpoints.Coincidentwiththelowvoltageonbus14,lowvoltageoccurredonthe"B"InstrumentBus.Lowvoltageonthe"B"InstrumentBusexistedforapproximatelyfour(4)seconds.IAtapproximately1421EST,withthereactoratapproximately98%steadystatereactorpowerandlowvoltageonthe"B"InstrumentBus,theControlRoomreceivednumerousannunciatoralarms.TheControlRoomoperatorsimmediatelydeterminedthataturbinerunbackhadoccurred.ThisrunbackwascausedbyoneoffourOvertemperatureDeltaTemperature(OTDeltaT)channelsandoneoffourOverpowerDeltaTemperature(OPDeltaT)channelsrunback'signals.Thisrunbackdecreasesturbineloadwhentherelaysdropout.TheControlRoomoperatorsrespondedtotheannunciators,andimmediatelyperformedtheappropriateactionsofabnormaloperatingprocedureAP-TURB.2,"TurbineLoadReduction".Theoperatorsobservedthatthenormalsupplybreakersforbusses14and18hadopened,andthatthe"A"D/Gwassupplyingpowertobusses14and18.Loadonthe"A"D/Gstabilizedatapproximately500KW.NRCFORH366A(592) l NRCFORM366A(5-92)U.S.NUCLEARREGULATORYCOMMISSIONLICENSEEEVENTREPORT(LER)TEXTCONTINUATIONAPPROVEDBYOMBNO.3150.0104EXPIRES5/3'1/95ESTIMATEDBURDENPERRESPONSETOCOMPLYWITHTHISINFORMATIONCOLLECTIONREQUEST:50.0HRS.FORWARDCOMMENTSREGARDINGBURDENESTIMATETOTHEINFORMATIONANDRECORDSMANAGEMENTBRANCH(MHBB7714),U.S.NUCLEARREGULATORYCOMMISSION,WASHINGTON,DC20555-0001ANDTOTHEPAPERWORKREDUCTIONPROJECT(3140-0104),OFFICEOFMANAGEMENTANDBUDGETWASHINGTONDC20503.FACILITYNAME(1)DOCKETNUMBER(2)LERNUMBER(6)YEARSEQUENTIALREVISIONPAGE(3)R.E.GinnaNuclearPowerPlant0500024494--005--005OF9TEXT(Ifmorespaceisrequired,useadditionalcopiesofHRCForm366A)(17)Atapproximately1422EST,EnergyOperationspersonneltelephonedtheGinnaControlRoom,andnotifiedtheOperationsShiftSupervisoroftheswitchingoperationsthathadoccurredatStation204andoftheunexpectedlossofpowertoCircuit751.Circuit751hadbeenisolatedforapproximatelyninety(90)seconds.TheControlRoomoperatorsstabilizedtheplantatapproximately93%reactorpoweraftertherunbacksignalcleared.Atapproximately1439EST,theoperatorsreferredtoemergencyrestorationprocedureER-ELEC.1,"RestorationofOffsitePower".Atapproximately1444EST,usingthisprocedure,theControlRoomoperatorsclosedthenormalsupplybreakerstobusses14and18,restoringoffsitepowertobusses14and'18.The"A"D/Gwasthenshutdownandreturnedtonormalstandbystatus.Duetothereactorpowerdecreasefromtheturbinerunback,axialfluxdifferenceinthereactorcoreexceeded"penalty"limitsofTechnicalSpecification(TS)3.10.2.Theoperatorssubsequentlyreducedreactorpowertobelow90~tocomplywiththeactionrequirementsofTS3.10.2forlimitsonaxialfluxdifference.Atapproximately1511EST,apowerincreasebackto98'.reactorpowerwasinitiated,andthereactorwasatapproximately98~steadystatereactorpoweratapproximately2210ESTonFebruary17,1994'INOPERABLESTRUCTURESiCOMPONENTSORSYSTEMSTHATCONTRIBUTEDTOTHEEVENT:NoneD.OTHERSYSTEMSORSECONDARYFUNCTIONSAFFECTED:NoneE.METHODOFDISCOVERY:ThiseventwasimmediatelyapparentduetoMainControlBoardannunciatoralarmsandotherindicationsintheControlRoom.NRCFORM366A(5-92)

NRCFORM366A(5-92)U.S.NUCLEARREGULATORYCOHHISSIONLICENSEEEVENTREPORT(LER)TEXTCONTINUATIONAPPROVEDBYOHBNO.3150-0104EXPIRES5/31/95ESI'IMATEDBURDENPERRESPONSETOCOMPLYWITHTHISINFORMATIONCOLLECTIONREOUEST:50.0HRS.FORWARDCOMMENTSREGARDINGBURDENESTIHATETOTHEIHFORHATIONAHDRECORDSMANAGEMENTBRANCH(MHBB7714),U.STNUCLEARREGULATORYCOMMISSION,WASHINGTON,DC20555-0001,ANDTOTHEPAPERWORKREDUCTIONPROJECT(3150-0'104),OFFICEOFMANAGEMENTANDBUDGETWASHINGTOHDC20503.FACILITYNAHE(1)R.E.GinnaNuclearPowerPlantDOCKETNUMBER(2)05000244LERNUMBER(6)YEARSEOUEHTIAL94--005REVISION00PAGE(3)6OF9TEXT(Ifmorespaceisrequired,useedditionatcopiesofHRCForm366A)(17)F.OPERATORACTION:TheControlRoomoperatorsimmediatelyperformedtheappropriateactionsofAP-TURB.2andverifiedthatthe"A"D/Gwasoperatingproperlyandthatbusses14and18wereenergizedfromtheD/G.Theoperatorsrestartednecessaryequipment,includingthe"A"servicewaterpump.TheoperatorsnotifiedhighersupervisionandtheNRCResidentInspector.Subsequently,theoperatorsrestoredoffsitepowertobusses14and18.Theytransitionedtoprocedure0-5.1,"LoadReductions,"andreducedpowerbelow90'duetoaxialfluxdifferenceinthereactorcore.Theoperatorsterminatedthetestofthe"A"D/G,andthe."A"D/GwasshutdownandreturnedtonormalstandbystatusperprocedureT-27.4,"DieselGeneratorOperation."G.SAFETYSYSTEMRESPONSES:Electricalloadsonbusses14and18deenergizedasdesigned,duetoanundervoltageconditiononthebusses.Theoperatorsmanuallyrestartednecessaryloads,includingthe"A"servicewaterpump,atapproximately1422EST.The"A"D/Gcontinuedtosupplypowertobusses14and18untilrestorationofoffsitepowertobusses14and18.Offsite34.5KVCircuit767continuedtosupplypowertosafeguardsbusses16and17duringtheevent.CAUSEOFEVENTA.IMMEDIATECAUSE:TheimmediatecauseoftheturbinerunbackwasreceiptofturbinerunbacksignalsfromoneoffourOTDeltaTandOPDeltaTchannels.B.INTERMEDIATECAUSE:Theintermediatecauseofreceiptofturbinerunbacksignalswaslowvoltageonthe"B"InstrumentBus,whichcausedtheturbinerunbackrelaysassociatedwiththe"B"InstrumentBustodropout.Thelowvoltageonthe"B"InstrumentBuswasduetolowvoltageonMCC-1C,whichsuppliespowertothe"B"InstrumentBus.ThelowvoltageonMCC-1CwasduetolowvoltageonBus14,whichsuppliesMCC-1C.HRCFORH366A(5-92)

NRCFORH366A(5-92)U.S.NUCLEARREGULATORYCOHHISSIONL'ICENSEEEVENTREPORT(LER)TEXTCONTINUATIONAPPROVEDBYOHBNO.3150-0104EXPIRES5/31/95ESTIMATEDBURDENPERRESPONSETOCOHPLYlllTHTHISINFORMATIONCOLLECTIONREQUEST:50.0HRS.FORllARDCOMMENI'SREGARDINGBURDENESTIMATETOTHEINFORMATIONANDRECORDSHANAGEMENTBRANCH(HNBB7714),U.S.NUCLEARREGULATORYCOHHISSION,IIASHINGTON,DC20555-0001ANDTOTHEPAPERllORKREDUCTIONPROJECT(3140-0104),OFFICEOFHANAGEMENTANDBUDGETlJASHINGTONDC20503.FACILITYNAME(1)DOCKETNUHBER(2)LERNUHBER(6)YEARSEQUENTIALREVISIONPAGE(3)R.E.GinnaNuclearPowerPlant0500024494--005--007OF9TEXT(Ifmorespaceisrequired,useadditionalcopiesofNRCForm366A)(17)C.ROOTCAUSE:TheunderlyingcauseofthelowvoltageonBus14(andBus18)waslossofpowerto34.5KVCircuit751,duetolossofpowertog234.5KVbusatStation204.(ThiseventisNUREG-1022(C)CauseCode,ExternalCause.)IV.ANALYSISOFEVENTThiseventisreportableinaccordancewith10CFR50.73,LicenseeEventReportSystem,item(a)(2)(iv),whichrequiresareportof,"Anyeventorconditionthatresultedinamanualorautomaticactuationofanyengineeredsafetyfeature(ESF),includingthereactorprotectionsystem(RPS)~"TheturbinerunbackwasanautomaticactuationoftheRPS,andthemanualstartofthe"A"servicewaterpumpwasanactuationofanESF.Anassessmentwasperformedconsideringboththesafetyconsequencesandimplicationsofthiseventwiththefollowingresultsandconclusions:~Allreactorcontrolandprotectionsystemsperformedasdesigned,thuslimitingtheoveralleffectsoftheturbinerunbacktransient.~The"A"D/Goperatedasdesignedbysupplyingpowertosafeguardsbusses14and18.~TheControlRoomoperatorsexpeditiouslystabilizedtheplantafterthetransient.~Offsitepower34.5KVCircuit767wasstillinoperationsupplyingpowertosafeguardsbusses16and17.Basedontheabove,itcanbeconcludedthatthepublic'shealthandsafetywasassuredatalltimes.NRCFORH366A(5-92)

NRCFORM366A(5-92)U.S.NUCLEARREGULATORYCOMMISSIONLICENSEEEVENTREPORT(LER)TEXTCONTINUATIONAPPROVEDBYOHBNO.3150.0104EXPIRES5/31/95ESTIMATEDBURDENPERRESPONSETOCOMPLYWITHTHISINFORMATIOHCOLLECTIONREQUEST:50.0HRS.FORWARDCOMMENTSREGARDIHGBURDENESTIMATETOTHEINFORMATIONAHDRECORDSMANAGEMENTBRANCH(MHBB7714),U.S.NUCLEARREGULATORYCOMMISSION,WASHINGTON,DC20555.0001ANDTOTHEPAPERWORKREDUCTIONPROJECT(3140-0104),OFFICEOFMAHAGEMEHTANDBUDGETWASHINGTONDC20503.FACILITYNAME(1)R.E.GinnaNuclearPowerPlantDOCKETNUMBER(2)05000244LERNUMBER(6)YEARSEOUEHTIAL94005REVISION00PAGE(3)8OF9TEXT(Ifmorespaceisrequired,useadditionalcopiesofHRCForm366A)(17)V.CORRECTIVEACTIONA.ACTIONTAKENTORETURNAFFECTEDSYSTEMSTOPRE-EVENTNORMALSTATUS:~Offsitepower34.5KVCircuit751wasrestoredbyautomaticreclosureoftransformerbreaker2T20452atStation204'TheGinnaControlRoomoperatorsrestoredoffsitepowertosafeguardsbusses14and18from34.5KVCircuit751.~The"A"D/Gwasshutdownandreturnedtonormalstandbystatus.~Reactorpowerwasrestoredtoapproximately98~steadystatereactorpowerafterrestoringaxialfluxdifferencetowithinoperatinglimits.B.ACTIONTAKENORPLANNEDTOPREVENTRECURRENCE:~EnergyOperationshasreviewedtheapplicableoffsiteelectricaldistributiondrawingsandswitchingorders.~EnergyOperationshasmadechangesintheswitchingorderstominimizetheprobabilityofalossofpowertoCircuit751'EnergyOperationshasmadechangestothenotificationproceduresoftheswitchingorderstoensuretheseactivitiesarecommunicatedtotheGinnaOperationsShiftSupervisor.~ProceduresaffectingCircuit767and/orCircuit751willbeidentifiedandrevised,asnecessary,toensureappropriateactivitiesarecommunicatedtoEnergyOperations.NRCFORM366A(5-92)

NRCFORH366A(5-92)U.S.NUCLEARREGULATORYCOMMISSIONLICENSEEEVENTREPORT(LER)TEXTCONTINUATIONAPPROVEDBYOMBNO.3150.0104EXPIRES5/31/95ESTIMATEDBURDENPERRESPONSETOCOHPLYWITHTHISINFORMATIONCOLLECTIOHREQUEST:50.0HRS.FORWARDCOMMENTSREGARDIHGBURDENESTIHATETOTHEINFORMATIONAHDRECORDSMAHAGEMEHTBRANCH(HHBB7714),U.S.NUCLEARREGULATORYCOHMISSION,WASHINGTOH,DC20555-0001,ANDTOTHEPAPERWORKREDUCTIONPROJECT(3150-0104),OFFICEOFHANAGEHENTAHDBUDGETWASHINGTONDC20503.FACILITYNAHE(1)R.E.GinnaNuclearPowerPlantDOCKETNUHBER(2)05000244LERNUHBER(6)YEARSEQUENTIAL94005REVISION00PAGE(3)9OF9TEXT(Ifmorespaceisrequired,useadditionalcopiesofHRCForm366A)(17)VI.ADDITIONALINFORMATIONA.FAILEDCOMPONENTS:TherewerenofailedcomponentsatGinnaStation.B.PREVIOUSLERsONSIMILAREVENTS:AsimilarLEReventhistoricalsearchwasconductedwiththefollowingresults:NodocumentationofsimilarLEReventswiththesamerootcauseatGinnaNuclearPowerPlantcouldbeidentified.However,LER92-007andLER91-002weresimilareventswithdifferentrootcauses.C.SPECIALCOMMENTS:NoneHRCFORH366A(5-92)