ML20127P257

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Notice of Violation from Insp on 850316-0510
ML20127P257
Person / Time
Site: Peach Bottom, Cook  Constellation icon.png
Issue date: 06/26/1985
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20127P150 List:
References
50-277-85-12, 50-278-85-12, NUDOCS 8507020360
Download: ML20127P257 (2)


See also: IR 05000316/2005010

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APPENDIX A

NOTICE OF VIOLATION

Philadelphia Electric Company Docket / License: 50-277/DRP-44

Peach Bottom Unit 2 50-278/DRP-56

As a result of the inspection conducted on March 16, 1985 - May 10, 1985, and in

accordance with the revised NRC Enforcement Policy (10 CFR 2, Appendix C)

published in the Federal Register on March 8, 1984 (49 FR 8583), the following

violation was identified:

A.1 Technical Specification 6.8.1 and Appendix A to Regulatory Guide

1.33, November 1972, require implementation of procedures for

surveillance testing and for the control of shift operations.

A.1.1 FSAR Section 10.14 indicates that the Emergency Ventilating systems

for the Emergency Switchgear and Battery Rooms are seismically

qualified. Surveillance Test Procedure ST 7.9.2, Daily Check of

Seismic Gas Supply Bottle Pressure, requires visual verification

that each bottle, including nitrogen bottle 0B55385, is seismically

restrained.

Contrary to the above from about March 5,1985, to April 8,1985,

seismic qualification of the nitrogen bottle 0855385 was invalidated

in that the bottle was out of its seismically designed restraint

rack, secured only by a piece of rope, and the ST 7.9.2 daily checks

did not identify this condition.

A.1.2 Administrative Procedure A-7, Shift Operations requires that when

the Control Room Supervisor is away from his post for more than

one-half hour, the on-coming Control Rcc= Supervisor receive a

verbal turnover report, review and sign the turnover check-off list

l completed by the Control Room Supervisor leaving the post, read the

l logs, and inspect the control panels.

Contrary to the above, on May 5, 1985 the Control Room Supervisor

position was changed four times to relieve the Senior Licensed

l Operator on the refuel floor with each change being longer than

one-half hour, and the turnover check-off list was not completed

for each change.

l This is a Severity Level IV Violation (Supplement I) applicable to

l DPR-44 and DPR-56.

8507020360 850626

PDR ADOCK 05000277

l G PDR

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l OFFICIAL RECORD COPY CIR PB 85-12 A - 0003.0.0

l 06/15/85

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Appendix A 2-

Pursuant to the provisions of 10 CFR 2.201, Philadelphia Electric Company is

hereby required to submit to this office within 30 days of the date of the

letter transmitting this Notice, a written statement or explanation of reply,

including: (1) the corrective steps which have been taken and the results

achieved; (2) the corrective steps which will be taken to avoid further viola-

tions, and (3) the date when full compliance will be achieved. Where good

cause is shown consideration will be given to extending the response time.

Because Violation A.1.2 was corrected during the inspection period and correc-

tive actions to avoid further violations were also made, no written response is

required for A.1.2.

OFFICIAL RECORD COPY CIR PB 85-12 A - 0004.0.0

06/14/85