ML17264A994

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LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr
ML17264A994
Person / Time
Site: Ginna Constellation icon.png
Issue date: 08/19/1997
From: MECREDY R C, ST MARTIN J T
ROCHESTER GAS & ELECTRIC CORP.
To: VISSING G
NRC (Affiliation Not Assigned), NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
LER-97-002, LER-97-2, NUDOCS 9708270015
Download: ML17264A994 (16)


Text

0CATEGORY1REGULATORY INFORMATION DISTRIBUTION SYSTEM(RIDS)ACCESSION NBR:9708270015 DOC.DATE:

97/08/19NOTARIZED:

NODOCKETFACIL:50-244 RobertEmmetGinnaNuclearPlant,Unit1,Rochester G05000244AUTH.NAPEAUTHORAFFILIA.ION ST.HARTIN,J.T.

Rochester Gas&ElectricCorp.MECREDY,R,C.

Rochester Gas&ElectricCorp.RECIP.NAME RECIPIENT AFFILIATION VISSING,G.

SUBJECT:

LER97-002-00:on 970720,34.5 KVoffsite.powercircuit751waslost.Causedbyautoma;icactua"ionof"B"emergency DGduerounder;oitage onsafeguards buses16&17.0ffsir.e powerrestoredtosafeguards buses16&17.W/970819 ltr.DISTRIBUTION CODE:IE22TCOPIESRECEIVED:ITR JENCILSIZE:TITLE:50.73/50.9 LicenseeEventReport(LER),IncidentRpt,etc.NOTES:License Expdateinaccordance with10CFR2,2.109(9/19/72).

c'50002446INTERNAL:

RECIPIENT IDCODE/NAME PD1-1PDILECENTENRR/DRCH/HHFB NRR/DRCH/HOLB NRR/DRPM/PECB NRR/DSSA/SRXB RGN1FILE01COPIESLTTRENCL112211111111111111RECIPIENT IDCODE/NAME VISSING,G.

AEOD/SPD/RRAB NRR/DE/ECGB NRR/DE/EMEB NRR/DRCH/HICB NRR/DRCH/HQMB NRR/DSSA/SPLB RES/DET/EIB COPIESLTTRENCL1111111111111111RDEXTERNAL:

LSTLOBBYWARDNOACPOORE,W.NRCPDR111111LITCOBRYCE,JHNOACQUEENER,DS NUDOCSFULLTXT111111CUNNOTETOALL"RIDS"RECIPIENTS:

PLEASEHELPUSTOREDUCEWASTE.TOHAVEYOURNAMEORORGANIZATION REMOVEDFROMDISTRIBUTION LISTSORREDUCETHENUMBEROFCOPIESRECEIVEDBYYOUORYOURORGANIZATION, CONTACTTHEDOCUMENTCONTROLDESK(DCD)ONEXTENSION 415-2083FULLTEXTCONVERSION REQUIREDTOTALNUMBEROFCOPIESREQUIRED:

LTTR24ENCL24

ANDo~("iv.igqgclap('rip+~/~i~<<l:"~~wv~hp'g~co'E)r~<

v(+ofCQc<of01;sAugust19,1997U.S.NuclearRegulatory Commission DocumentControlDeskAttn:GuyS.VissingProjectDirectorate I-1Washington, D.C.20555

Subject:

LER97-002,Lossof34.5KVOffsitePowerCircuit751,DuetoExternalCause,ResultsinAutomatic Startof"B"Emergency DieselGenerator R.E.GinnaNuclearPowerPlantDocketNo.50-244

DearMr.Vissing:

Inaccordance with10CFR50.73,LicenseeEventReportSystem,item(a)(2)(iv),whichrequiresareportof,"Anyeventorcondition thatresultedinamanualorautomatic actuation ofanyengineered safetyfeature(ESF),including thereactorprotection system(RPS)",theattachedLicenseeEventReportLER97-002isherebysubmitted.

Thiseventhasinnowayaffectedthepublic'shealthandsafety.Verytrulyyours,RobertC.Mecredyxc:Mr.GuyS.Vissing(MailStop14B2)PWRProjectDirectorate I-1Washington, D.C.20555U.S.NuclearRegulatory Commission RegionI475Allendale RoadKingofPrussia,PA19406GinnaSeniorResidentInspector 97082700i5 9708i9PDRADQCK05000244SPDRlllllllllilllilllllllllllllillllllll

~l NRCFORM366(4.95)U.S.NUCLEARREGULATORY COMMISSIO LICENSEEEVENTREPORT(LER)(Seereverseforrequirednumberofdigits/characters foreachblock)APPROVEDBYOMBNo.3150-0104 EXPIRES04/30/96ESTIMATED BURDENPERRESPONSEToCOMPLYWITHTHISMANDATORY INFORMATION COLLECTION REQUEST:50.0HRS.REPORTEDLESSONSLEARNEDAREINCORPORATED INTOTHELICENSING PROCESSANDFEDBACKToINDUSTRY.

FORWARDCOMMENTSREGARDING BURDENESTIMATEToTHEINFORMATION ANDRECORDSMANAGEMENT BRANCHIT-6F33).U.S.NUCLEARREGULATORY COMMISSION, WASHINGTON, DC20555-000t, ANDToTHEPAPERWORK REDUCTION PROJECTFACILITYNAMEIIIR.E.GinnaNuclearPowerPlantOOCKEfNUMBERI2)05000244PAGEI3)1OF8TITLEI4ILossof34.5KVOffsitePowerCircuit751,DuetoExternalCause,ResultsinAutomatic Startof"B"Emergency DieselGenerator EVENTDATE(5)LERNUMBER(61REPORTDATE(7lOTHERFACILITIES INVOLVED(BlDOCKETNUMBERMONTHDAY0720YEAR97SEQUENTIAL REVISIONNUMBERNUMBER97-002-00MONTH08DAY19YEAR97FACILITYNAMEFACILITYNAMEDOCKETNUMBEIIOPERATING MODE(9)POWERLEVEL(10)100THISREPORTISSUBMITTED PUR20.2201(b) 20.2203(al(1) 20.2203(al(2)(i) 20.2203(a)(2)(iil 20.2203(a)

(2)(iii)SUANTTOTHEREQUIREMENTS OF10CFRE:(Checkoneormore)(11)20.2203(a)(2)(v) 50.73(a)(2)(viii)50.73(a)(2)(i) 50.73(a)(2)(x) 50.73(a)(2)(ii) 20.2203(a)

(3)(i)73.7150.73(a)(2)(iii)20.2203(a)(3)(ii)

OTHERX50.73(al(2)(iv) 50.73(a)(2)(v)20.2203(a)(4) 50.36(c)(1)

SpecityinAbstractbeloworinNRCFoim366A20.2203(a)

(2)(iv)50.36(c)(2)

LICENSEECONTACTFORTHISLER(12)50.73(a)(2)(vii)

NAMETELEPHONE NUMBER(IneiudeAresCodeiJohnT.St.Martin-Technical Assistant (716)771-3641COMPLETEONELINEFOREACHCOMPONENT FAILUREDESCRIBED INTH(SREPORT(13lCAUSESYSTEMCOMPONENT MANUFACTURER ToNPRDSCAUSESYSTEMCOMPONENT MANUFACTURER REPORTABLE ToNPRDSEACBL5XOOONSUPPLEMENTAL REPORTEXPECTED(14)YES(Ityes,completeEXPECTEDSUBMISSION DATE).XNoEXPECTEDSUBMISSION DATE(15)MONTHDAYYEARABSTRACT(Limitto1400spaces,i.e.,approximatelY 15single.spacedtypewritten lines)(16)OnJuly20,1997,atapproximately 0043EDST,theplantwasinMode1atapproximately 100%steadystatepower.PowerfromCircuit751(34.5KVoffsitepowersource)waslost.Thisresultedindeenergization of4160Voltbus12Band"B"train480Voltsafeguards buses16and17.The"B"Emergency DieselGenerator (D/G)automatically startedandreenergized buses16and17asperdesign.Therewasnochangeinreactorpowerorturbineload.Immediate corrective actionwastoperformtheappropriate actionsofAbnormalProcedure AP-ELEC.1 (Lossof12AAnd/Or12BBuses)tostabilize theplantandtoverifythatthe"B"Emergency D/Ghadstartedandreenergized buses16and17.ThecauseofthelossofpowerfromCircuit751wasdetermined tobeaphase-to-phase faultcausedbyaraccoon.Thisfaultcausedtheinsulators onanoffsitepoleforCircuit75'ltofail.ThiseventisNUREG-1022 CauseCode(C).Corrective actiontopreventrecurrence isoutlinedinSectionV.B.NRCFORM366(4.95)

NRCFORM366A(4-95)LICENSEEEVENTREPORT(LER)TEXTCONTINUATION U.S.NUCLEARREGULATORY COMMISSION FACILITYNAMEI1)R.E.GinnaNuclearPowerPlantDOCKET05000244LERNUMBERI6)YEARSEQUENTIAL REVISIONNUMBERNUMBER97-,002-00PAGEI3)2OF8TEXTllfmorespaceisrequired, useadditional copiesofNRCForm366A/I17)PRE-EVENT PLANTCONDITIONS OnJuly20,1997,atapproximateiy 0043EDST,theplantwasinMode1atapproximately 100%steadystatereactorpower.Therewerenosignificant activities inprogress.

Theoffsitepowerconfiguration totheplantwasinthealternate "50%/50%"offsitepowerlineup:Circuit751(34.5KVoffsitepowersource)wassupplying powertothe"B"train480Voltsafeguards buses16and17through34.5KVto4160Volttransformer 12A(12Atransformer),

viacircuitbreaker52/12AX,to4160Voltbus12B,andthroughthesafeguards bus4160Voltto480Volttransformers 16and17.Circuit767(34.5KVoffsitepowersource)wassupplying powertothe"A"train480Voltsafeguards buses14and18through34.5KVto4160Volttransformer 12B(12Btransformer),

viacircuitbreaker52/12BY,to4160Voltbus12A,andthroughthesafeguards bus4160Voltto480Volttransformers 14and18.Seetheattachedsketchoftheoffsitepowerdistribution system.II.DESCRIPTION OFEVENTA.DATESANDAPPROXIMATE TIMESOFMAJOROCCURRENCES:

July20,1997,0043EDST:Eventdateandtime.July20,1997,0043EDST:Discovery dateandtime.July20,1997,0044EDST:ControlRoomoperators verifythe"B"Emergency DieselGenerator (D/G)operation andthatsafeguards buses16and17areenergized.

July20,1997,0114EDST:Safeguards buses16and17weretransferred toCircuit767fromthe"B"Emergency D/G.July20,1997,0124EDST:The"B"Emergency D/Gwasstoppedandrealigned forautostandby.July20,1997,1228EDST:Circuit751wasdeclaredoperable.

July20,1997,1232EDST:Offsitepowerconfiguration wasrestoredtothealternate "50%/50%"lineup.NRCFORM366AI4.95)

NRCFORM366AI4-95)LICENSEEEVENTREPORT(LER)TEXTCONTINUATION U.S.NUCLEARREGULATORY COMMISSION

~FACILITYNAMEI1)R.E.GinnaNuclearPowerPlantDOCKET05000244LERNUMBERIB)PAGEI3)YEARSEQUENTIAL REVISIONNUMBERNUMBER3OF897-002-00TEXTIlfmorespaceisrequired, useadditional copiesofNRCForm366AII17)EVENT:OnJuly20,1997,atapproximately 0043EDST,theplantwasinMode1atapproximately 100%steadystatefullpower.TheControlRoomoperators receivednumerousMainControlBoardannunciator alarms.AmongthesealarmswereL-20(12AXFMROR12ABUSTROUBLE),

J-5(¹11OR¹12TRANSFORMER OUTOFSYNCH),J-7(480VMAINORTIEBREAKERTRIP),J-9(SAFEGUARD BREAKERTRIP),andJ-32(EMERGENCY DIESELGEN1BPANEL).TheControlRoomoperators determined thatthefollowing eventshadoccurred:

Circuit751(34.5KVoffsitepowersource)wasdeenergized "B"train480Voltsafeguards buses16and17hadlosttheirpowersupplyfrom4160Voltbus12B(buses16and17hadbeenmomentarily deenergized)

The"B"Emergency D/Ghadautomatically startedandwastiedtosafeguards buses16and17TheControlRoomoperators verifiedthatreactorcoolantsystemtemperature andpressurewerestable,andthattherewasnochangeinreactorpowerorturbineload.Theyperformed theappropriate actionsofAbnormalProcedure AP-ELEC.1 (Lossof12AAnd/Or12BBuses)tostabilize theplant.Theyverifiedthatthe"B"Emergency D/Gwasoperating andthatsafeguards buses16and17wereenergized.

TheControlRoomoperators observedthatCircuit751andbus128displayed zero(0)voltage.ThelossofpowerfromCircuit751resultedinundervoltage onsafeguards buses16and17,andthe"B"Emergency D/Gautomatically startedasperdesignandreenergized thesebuses.EnergyOperations personnel alsoidentified thelossofpowerfromCircuit751,andpromptlynotifiedGinnaControlRoomoperators ofthelossofpowerfromCircuit751.TheControlRoomoperators referredtoEquipment Restoration procedure ER-ELEC.1 (Restoration ofOffsitePower)torestoreoffsitepowerto4160Voltbus12Band480Voltsafeguards buses16and17.TheControlRoomoperators closed4160Voltcircuitbreaker52/12BXtoenergizebus12BfromCircuit767,viathe12Btransformer, atapproximately 0053EDST.Atapproximately 0114EDST,safeguards buses16and17weretransferred toCircuit767fromthe"B"Emergency D/G.(Circuit767hadremainedinoperation, supplying "A"train480Voltsafeguards buses14and18,throughout theevent.)Atapproximately 0124EDSTonJuly20,the"B"Emergency D/Gwasstoppedandrealigned forautostandby.EnergyOperations subsequently contacted theControlRoomoperators andconfirmed thatthelossofpowerfromCircuit751occurredwhenaraccoonclimbedanoffsitepoleforCircuit751andcausedaphase-to-phase fault.Thefaultcausedinsulators onthepoletofail.(Theraccoonperished.)

NRCFORM366AI4.95)

NRCFORM366A(4.95)LICENSEEEVENTREPORT(LER)TEXTCONTINUATION U.S.NUCLEARREGULATORY COMMISSION FACILITYNAMEI1)DOCKETLERNUMBERIB)PAGEI3)R.E.GinnaNuclearPowerPlant05000244YEARSEQUENTIAL REVISIONNUMBERNUMBER4OF897-002-00TEXT(Ifmorespaceisreqtrired, tjseadditional copiesofNRCForm366AII17)Circuit751wasreenergized anddeclaredoperableatapproximately 1228EDSTonJuly20.Circuit751waslineduptosupplyplantloads,andtheoffsitepowerconfiguration wasrestoredtothealternate "50%/50%"offsitepowerlineupatapproximately 1232EDST.C.INOPERABLE STRUCTURES, COMPONENTS, ORSYSTEMSTHATCONTRIBUTED TOTHEEVENT:NoneD.OTHERSYSTEMSORSECONDARY FUNCTIONS AFFECTED:

NoneE.METHODOFDISCOVERY'his eventwasimmediately apparentduetonumerousMainControlBoardalarmsandotherindications intheControlRoomwhenpowerfromCircuit751waslost.F.OPERATORACTION:Following theundervoltage condition onbuses16and17,the"B"Emergency D/Gautomatically startedandreenergized thesebuses.TheControlRoomoperators performed theappropriate actionstoverifythatthe"B"Emergency D/Gwasoperating andsafeguards buses16and17wereenergized.

TheControlRoomoperators manuallyrestarted the"B"and"C"containment recirculation fans,whichhadtrippedduetothelossofbus16.Themomentary lossofpowertobuses16and17causedthetripofthecommonsamplepumpformonitoring ofthecontainment (CNMT)atmosphere bychannelsR-10A(iodine),

R-11(particulate) andR-12(noblegas).TheControlRoomoperatormanuallyrestarted thecommonsamplepumpatapproximately 0100EDST.TheControlRoomoperators restoredoffsitepower(fromCircuit767)tobuses16and17,stoppedthe"B"Emergency D/G,andrealigned itforautostandby.TheShiftSupervisor notifiedhighetsupervision andtheNRCResidentInspector ofthelossofoffsiteCircuit751.Subsequently, theShiftSupervisor notifiedtheNRCper10CFR50.72(b)(2)(ii),non-emergency fourhournotification, atapproximately 0317EDSTonJuly20,1997.NACFOAM366AI495)

NRCFORM366AI4.95)LICENSEEEVENTREPORT(LER)TEXTCONTINUATION U.S.NUCLEARREGULATORY COMMISSION FACILITYNAMEI1)R.E.GinnaNuclearPowerPlantDOCKET05000244LERNUMBERI6)YEARSEQUENTIAL REVISIONNUMBERNUMBER97-002-00PAGE(3)5OF8TEXTilfmorespeceisrequired, useadditionelcopiesofNRCForm368A/I17)G.SAFETYSYSTEMRESPONSES:

AIIsafeguards equipment functioned properly.

The"B"Emergency D/Gautomatically startedduetotheundervoltage condition onbuses16and17,displayed propervoltageandfrequency, andreenergized safeguards buses16and17tosupplyemergency power.Runningcontainment recirculation fansonbus16trippedasdesignedandweremanuallyrestarted asneededtorestorenormalcoolingtotheContainment.

Runningservicewaterpumpsonbus17trippedasdesignedandthepumpselectedforautostart startedwhenpowerwasrestoredtobus17.III.CAUSEOFEVENTA.IMMEDIATE CAUSE:Theautomatic actuation ofthe"B"Emergency D/Gwasduetoundervoltage onsafeguards buses16and17.IB.INTERMEDIATE CAUSE:The(jndervoltage onsafeguards buses16and17wasduetothelossofpowerfromCircuit751.C.ROOTCAUSE:Theunderlying causeofthelossofpowerfromCircuit751wasaphase-to-phase faultonCircuit751.ThisfaultoccurredwhenaraccoonclimbedanoffsitepoleforCircuit751.Thefaultcausedtheinsulators tofail.Theinsulator failureaffectedcircuitsatoffsiteStation204andtrippedrelaysforCircuit751,deenergizing Circuit751.ThiseventisNUREG-1022 CauseCode(C),"External Cause".Thislossofpowerandsubsequent startofanEmergency D/GdoesnotmeettheNUMARC93-01,"Industry Guideline forMonitoring theEffectiveness ofMaintenance atNuclearPowerPlants",definition ofa"Maintenance Preventable Functional Failure".

IV.ANALYSISOFEVENT:Thiseventisreportable inaccordance with10CFR50.73,LicenseeEventReportSystem,item(a)(2)(iv),whichrequiresareportof,"Anyeventorcondition thatresultedinamanualorautomatic actuation ofanyengineered safetyfeature(ESF),including thereactorprotection system(RPS)",inthatthestartingofthe"B"Emergency D/Gwasanautomatic actuation ofanESFsystem.NRCFORM366A(495)

,~

ONRCFORM366AI4-95)LICENSEEEVENTREPORT(LER)TEXTCONTINUATION U.s.NUCLEARREGULATORY COMMISSION FACILITYNAMEI1)R.E.GinnaNuclearPowerPlantDOCKET05000244LERNUMBERI6)YEARSEQUENTIAL REVISIONNUMBERNUMBER97-002-00PAGEI3)6OF8TEXTllfmorespaceisrequired, useadditional copiesofNRCForm366AlI17)Anassessment wasperformed considering boththesafetyconsequences andimplications ofthiseventwiththefollowing resultsandconclusions:

Therewerenooperational orsafetyconsequences orimplications attributed tothelossofCircuit751andstartoftheEmergency D/Gbecause:oAllreactorcontrolandprotection systemsperformed asdesigned.

oThe"B"Emergency D/Gwasavailable foroperation andfunctioned asdesignedtoreenergize "B"trainsafeguards buses16and17.oWhileinthiscondition, theplantelectrical powersystems(offsitepowersourcesandtheEmergency D/Gs)remainedwithintherequirements oftheGinnaStationImprovedTechnical Specifications (ITS)LimitingCondition forOperation (LCO)RequiredAction3.8.1.A.oCircuit767remainedinoperation supplying powertothe"A"trainsafeguards buses;subsequently, Circuit767waslineduptosupplypowertothe"B"trainsafeguards busesalso.oRadiation monitorchannelsR-10A,R-11,andR-12weretemporarily lost.Thecommonsamplepumpwasmanuallyrestarted withinafewminutes.Thisresponsecompliedwiththerequirements ofITSLCORequiredAction3.3.5.B.1.

Basedontheabove,itcanbeconcluded thattheplantoperatedasdesigned, andthatthepublic'shealthandsafetywasassuredatalltimes.V.CORRECTIVE ACTIONA..ACTIONTAKENTORETURNAFFECTEDSYSTEMSTOPRE-EVENT NORMALSTATUSoOffsitepowerwasrestoredtosafeguards buses16and17fromCircuit767,andthe"B"Emergency D/Gwasstoppedandrealigned forautostandby.oCircuit751wasclearedforusebyEnergyOperations, protective relaysforCircuit751(atStation204)wereresetbyEnergyOperations, andCircuit751wasreenergized andrestoredtooperablestatus.ACTIONTAKENORPLANNEDTOPREVENTRECURRENCE:

Sincethiswasanisolatedoccurrence, nocorrective actionisplanned.NRcFORM366AI4.95)

NRCFORM366A<4-95)LICENSEEEVENTREPORT(LER)TEXTCONTINUATION U.S.NUCLEARREGULATORY COMMISSION FACILITYNAME(1)R.E.GinnaNuclearPowerPlantDOCKET05000244LERNUMBER(6)YEARSEQUENTIAL REVISIONNUMBERNUMBER97-002-00PAGE(3)TEXTllfmorespaceisrequired, useadditional copiesofNRCForm866A/(17)VI.ADDITIONAL INFORMATION A.FAILEDCOMPONENTS:

None8.PREVIOUSLERsONSIMILAREVENTS:AsimilarLEReventhistorical searchwasconducted withthefollowing results:LERs91-002,92-007,94-012,95-006,and95-007weresimilareventswithsimilarrootcauses(startofanEmergency D/Gduetolossofoffsitepowerfromexternalcauses).However,noneoftheexternalcausesfortheseLERswasduetoananimal.C.SPECIALCOMMENTS:

NoneNRCFORM366A<4-95)

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