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| {{#Wiki_filter:ACCELERATED DILUTIONDEMONS~TION SYSTEMiPREGULATORY INFORMATION DISTRIBUTION SYSTEM(RIDS)ACCESSION NBR:9105210249 DOC.DATE: | | {{#Wiki_filter:ACCELERATED DILUTION DEMONS~TION SYSTEM iP REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)ACCESSION NBR:9105210249 DOC.DATE: 91/05/13 NOTARIZED: |
| 91/05/13NOTARIZED: | | NO FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester G AUTH.NAME.AUTHOR AFFILIATION GORSKI,P.Rochester Gas&Electric Corp.MECREDY,R.C. |
| NOFACIL:50-244 RobertEmmetGinnaNuclearPlant,Unit1,Rochester GAUTH.NAME.AUTHORAFFILIATION GORSKI,P.
| | Rochester Gas&Electric Corp.RECIP.NAME |
| Rochester Gas&ElectricCorp.MECREDY,R.C. | | 'ECIPIENT AFFILIATION DOCKET g 05000244 R |
| Rochester Gas&ElectricCorp.RECIP.NAME | |
| 'ECIPIENT AFFILIATION DOCKETg05000244R | |
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| ==SUBJECT:== | | ==SUBJECT:== |
| LER91-005-00:on 910414,steam generator tubedegradation.
| | LER 91-005-00:on 910414,steam generator tube degradation. |
| Causedby"A"&"B"S/GStubedegradation inexcessofGinnaQAMreportability limits.TubesrepairedusingCombustion Engineering weldedsleeve.W/910513 ltr.DISTRIBUTION CODE:IE22TCOPIESRECEIVED:LTR ENCLSIZE:TITLE:50.73/50.9 LicenseeEvent,Report(LER),IncidentRpt,etc..SNOTES:License Expdateinaccordance with10CFR2,2.109(9/19/72).
| | Caused by"A"&"B" S/GS tube degradation in excess of Ginna QAM reportability limits.Tubes repaired using Combustion Engineering welded sleeve.W/910513 ltr.DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE: TITLE: 50.73/50.9 Licensee Event, Report (LER), Incident Rpt, etc..S NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72). |
| 05000244RECIPIENT IDCODE/NAME PD1-3LAJOHNSON,A INTERNAL:
| | 05000244 RECIPIENT ID CODE/NAME PD1-3 LA JOHNSON,A INTERNAL: ACNW AEOD/DS P/TPAB NRR/DET/ECMB 9H NRR/DLPQ/LHFB11 NRR/DOEA/OEAB NRR/DST/SELB SD Nj%/BS~LBSD1 RE~IL~02 FILE 01 EXTERNAL: EG&G BRYCE, J.H NRC PDR NSIC POORE,W.COPIES LTTR ENCL 1 1 1 1 2 2 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 3 3 1 1 1 1 RECIPIENT ID CODE/NAME PD1-3 PD AEOD/DOA AEOD/ROAB/DSP NRR/DET/EMEB 7E NRR/DLPQ/LPEB10 NRR/DREP/PRPB11 NRR/DST/SICB 7E NRR/DST/SRXB SE RES/DSIR/EIB L ST LOBBY WARD NSIC MURPHY,G.A NUDOCS FULL TXT COPIES LTTR ENCL 1 1 1 1 2 2 1'1 1 2 2 1 1 1 1 1 1 1 1 1 1 1 1 D NOTE TO ALL"RIDS" RECIPIENTS: |
| ACNWAEOD/DSP/TPABNRR/DET/ECMB 9HNRR/DLPQ/LHFB11 NRR/DOEA/OEAB NRR/DST/SELB SDNj%/BS~LBSD1 RE~IL~02FILE01EXTERNAL:
| | PLEASE HELP US TO REDUCE iVASTE!CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT.20079)TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!D D FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED'TTR 31 ENCL 31 |
| EG&GBRYCE,J.HNRCPDRNSICPOORE,W.COPIESLTTRENCL1111221111111111111111331111RECIPIENT IDCODE/NAME PD1-3PDAEOD/DOAAEOD/ROAB/DSP NRR/DET/EMEB 7ENRR/DLPQ/LPEB10 NRR/DREP/PRPB11 NRR/DST/SICB 7ENRR/DST/SRXB SERES/DSIR/EIB LSTLOBBYWARDNSICMURPHY,G.A NUDOCSFULLTXTCOPIESLTTRENCL1111221'1122111111111111DNOTETOALL"RIDS"RECIPIENTS: | |
| PLEASEHELPUSTOREDUCEiVASTE!CONTACTTHEDOCUMENTCONTROLDESK,ROOMPl-37(EXT.20079)TOELIMINATE YOURNAMEFROMDISTRIBUTION LISTSFORDOCUMENTS YOUDON'TNEED!DDFULLTEXTCONVERSION REQUIREDTOTALNUMBEROFCOPIESREQUIRED'TTR 31ENCL31
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| ROCHESTER GASANDELECTRICCORPORATION o89EASTAVENUE,ROCHESTER N.Y.14649-0001+, | | ROCHESTER GAS AND ELECTRIC CORPORATION o 89 EAST AVENUE, ROCHESTER N.Y.14649-0001+, ROBERT C.MECREDY Vice President Cinna Nuclear Production TELEPHONE AREA CODE 716 546 2700 May 13, 1991 U.S.Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 |
| ROBERTC.MECREDYVicePresident CinnaNuclearProduction TELEPHONE AREACODE7165462700May13,1991U.S.NuclearRegulatory Commission DocumentControlDeskWashington, DC20555
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| ==Subject:== | | ==Subject:== |
| LER91-005,SteamGenerator TubeDegradation DuetoIGA/SCCCausesQ.A.ManualReportable LimitstobeReachedR.E.GinnaNuclearPowerPlantDocketNo.50-244Inaccordance with10CFR50.73,LicenseeEventReportSystem,item(Other),andtheGinnaStationQualityAssurance ManualAppendixB,whichrequiresthat,"Ifthenumberoftubesinagenerator fallingintocategories aorbbelowexceedsthecriteria, thenresultsoftheinspection shallbeconsidered aReportable Eventpursuantto10CFR50.73,"theattachedLicenseeEventReportLER91-005isherebysubmitted.
| | LER 91-005, Steam Generator Tube Degradation Due to IGA/SCC Causes Q.A.Manual Reportable Limits to be Reached R.E.Ginna Nuclear Power Plant Docket No.50-244 In accordance with 10 CFR 50.73, Licensee Event Report System, item (Other), and the Ginna Station Quality Assurance Manual Appendix B, which requires that,"If the number of tubes in a generator falling into categories a or b below exceeds the criteria, then results of the inspection shall be considered a Reportable Event pursuant to 10 CFR 50.73," the attached Licensee Event Report LER 91-005 is hereby submitted. |
| Thiseventhasinnowayaffectedthepublic'shealthandsafety.Vertrulyyours,XC:RobertC.MeredyU.S.NuclearRegulatory Commission RegionI475Allendale RoadKingofPrussia,PA19406GinnaUSNRCSeniorResidentInspector 9105210249 9i05i3PDFlADQCK0000244sFDRWG&a~II I
| | This event has in no way affected the public's health and safety.Ver truly yours, XC: Robert C.Me redy U.S.Nuclear Regulatory Commission Region I 475 Allendale Road King of Prussia, PA 19406 Ginna USNRC Senior Resident Inspector 9105210249 9i05i3 PDFl ADQCK 0 000244 s FDR WG&a~II I |
| rACSeeaIIOIOAIIUCENSEEEVENTREPORTLER)U*IACLIAIAIOULATON>
| | rAC Seea IIO IOAII UCENSEE EVENT REPORT LER)U*IACLIAI A IOULATON>COANI~Ase1ovto OUI INL IIII Olov CISINCI IIII/II OOCltT NUIIOCN Ql o6oo0244>ot SACILITY NAIIC I'l R.E.Ginna Nuclear Power Plant TLI lel Steam Generator Tube Degradation Due to IGA/SCC Causes Q.A.Manual Reportable Limits to be Reached CVINT OATI Itl LC1 NVIIOCA IN 1CSOA'1 OATI Ih OTNI1 SACILITIC~INVOLVto Nl eeoeeTN OAY YCAN ey IIOVINTIAL I.Nvee~11 AI Veeeee~evWIA NOee TN OAY YCA1 SACILITY NAeele oocCIT NUIIIIAQI 0 6 0 0 0 0 414 9 1 1 005 0 0 0 5 1 391 0 6 0 0 0 OSCAATINO~eOOI Oll~OIVIA CIVIL P P P'101 TNII 1tSONT Q WINITTCO SVIQVANT T~OOI4l Ql I Iel N.T 041 Q II el II.T$4I QI I eel~IOI41QIINIIW |
| COANI~Ase1ovtoOUIINLIIIIOlovCISINCIIIII/IIOOCltTNUIIOCNQlo6oo0244>ot SACILITYNAIICI'lR.E.GinnaNuclearPowerPlantTLIlelSteamGenerator TubeDegradation DuetoIGA/SCCCausesQ.A.ManualReportable LimitstobeReachedCVINTOATIItlLC1NVIIOCAIN1CSOA'1OATIIhOTNI1SACILITIC | | ~O.T Ilel QI IVNI Ql~O.TSNIQIIII Io.cot l~I IO.IOllel IOOIlellll IOM W Itl IO.AOI 4111110 I0%4411I I I II CO.III 4)l1IINI~O.T 04 I QI ll~O.T I 4 1 Q I I II COAS4 I II I Oel!O.III III II llel IO J III IQI INI LICtNtll CONTACT SON TIIQ LI1 Iltl 0 Teel 1lovlAILIINTI os 10cs1 j;Iceeee eee ey eeae el SN eeeeeeel 111 1%71 OI TXTIW oTIIC1 lteeexy le Aeeeeet~eeet eee ee TeeL NIC Sow JIIAI NAVC Paul Gorski Mechanical Maintenance Mana er TILCSeeONC NVNII1 ANIA COOC 3155 COUSLCT 8 ONI LINt SON CACII COIISON CNT SAILUIC OCICIII to NI TNII 1CSOIT Iltl CAUtl IYITIII X CONSONINT T B NANUSAO TUN III H 3 4 TO NS I OI AIjl+M(lh w 7 CAUII IYCTCII coeesoNINT |
| ~INVOLVtoNleeoeeTNOAYYCANeyIIOVINTIAL I.Nvee~11AIVeeeee~evWIANOeeTNOAYYCA1SACILITYNAeeleoocCITNUIIIIAQI 0600004149110050005139106000OSCAATINO | | ~IANUIAO TUNCN~P0IITU g~(A~t:@%FATS!M%~V: IVSSLCNINTAL IICSOAT CLSCCTCO IIII Ylt Oy y<<.~CXSCCTCO CVINIC>>ON OAT>>NO AICTAACT ILJevc 0 I Axl eeeee.IA, eeeyeeeeeMy NINee eeeseeeeeee Iyftsrlllee |
| ~eOOIOll~OIVIACIVILPPP'101TNII1tSONTQWINITTCOSVIQVANTT~OOI4lQlIIelN.T041QIIelII.T$4IQIIeel~IOI41QIINIIW | | <<eeeI IW IIONTII CAY YCA1 CISCCTCO WIIN CC ION OATI 11~I During the 1991 Annual Refueling and Maintenance Outage subsequent to the eddy current examination performed on both the"A" and"B" Westinghouse series 44 Steam Generator (S/G), 116 tubes in the"A" S/G and 117 tubes in the"B" S/G required corrective action due to tube degradation. |
| ~O.TIlelQIIVNIQl~O.TSNIQIIII Io.cotl~IIO.IOllel IOOIlellll IOMWItlIO.AOI4111110I0%4411IIIIICO.III4)l1IINI~O.T04IQIll~O.TI41QIIIICOAS4IIIIOel!O.IIIIIIIIllelIOJIIIIQIINILICtNtllCONTACTSONTIIQLI1Iltl0Teel1lovlAILIINTI os10cs1j;IceeeeeeeeyeeaeelSNeeeeeeel1111%71OITXTIWoTIIC1lteeexyleAeeeeet~eeeteeeeeTeeLNICSowJIIAINAVCPaulGorskiMechanical Maintenance ManaerTILCSeeONC NVNII1ANIACOOC3155COUSLCT8ONILINtSONCACIICOIISONCNTSAILUICOCICIIItoNITNII1CSOITIltlCAUtlIYITIIIXCONSONINT TBNANUSAOTUNIIIH34TONSIOIAIjl+M(lh w7CAUIIIYCTCIIcoeesoNINT | | The immediate cause of the event was that the"A" and"B" S/Gs tube degradation was in excess of the Ginna Quality Assurance Manual reportability limits.The underlying cause of the tube degradation is a common S/G problem of a partially rolled tube sheet crevice with recurring Intergranular Attack/Stress Corrosion Cracking (ZGA/SCC)and Primary Water Stress Corrosion Cracking (PWSCC)attack on S/G tubing.Corrective action taken was to ei.ther sleeve or plug the affected tubes with accepted industry repair methods.NAC Seee IOI I&All |
| ~IANUIAOTUNCN~P0IITUg~(A~t:@%FATS!M%~V:IVSSLCNINTAL IICSOATCLSCCTCOIIIIYltOyy<<.~CXSCCTCOCVINIC>>ON OAT>>NOAICTAACTILJevc0IAxleeeee.IA,eeeyeeeeeMy NINeeeeeseeeeeee Iyftsrlllee | |
| <<eeeIIWIIONTIICAYYCA1CISCCTCOWIINCCIONOATI11~IDuringthe1991AnnualRefueling andMaintenance Outagesubsequent totheeddycurrentexamination performed onboththe"A"and"B"Westinghouse series44SteamGenerator (S/G),116tubesinthe"A"S/Gand117tubesinthe"B"S/Grequiredcorrective actionduetotubedegradation. | |
| Theimmediate causeoftheeventwasthatthe"A"and"B"S/Gstubedegradation wasinexcessoftheGinnaQualityAssurance Manualreportability limits.Theunderlying causeofthetubedegradation isacommonS/Gproblemofapartially rolledtubesheetcrevicewithrecurring Intergranular Attack/Stress Corrosion Cracking(ZGA/SCC) andPrimaryWaterStressCorrosion Cracking(PWSCC)attackonS/Gtubing.Corrective actiontakenwastoei.thersleeveorplugtheaffectedtubeswithacceptedindustryrepairmethods.NACSeeeIOII&All
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| 1114terU~10451LICENSEEEVENTREPORTILERITEXTCONTINUATION II.5.IIIICLtA1 154MLATOAY COQMINIISI rAftAOvtOOUOHO5ltOWIOtt)CPIII55 t/TIESFACILITYIIAAIt111OOCKtTIIIIlttt1 IllL51IluatttaIa~54VtleTIAL UVISIONUA~AOtItlR.E.GinnaNuclearPowerPlantTtXTIIT~~1~.~~I@AC/4PIII~tlIITIosooo24491-005-0002OFPRE-%TENT PLANT'ONDITIONS TheunitwasintheCold/Refueling Shutdowncondition for~theAnnualRefueling andMaintenance Outage.ReactorCoolantSystem(RCS)pressurewaszero(0)psigandRCStemperature wasapproximately 68F.SteamGenerator eddycurrentinspection wasinprogress.
| | 1114 terU~10451 LICENSEE EVENT REPORT ILERI TEXT CONTINUATION II.5.IIIICLtA1 154MLATOAY COQMINIISI r AftAOvtO OUO HO 5ltOWIOt t)CPIII55 t/TIES FACILITY IIAAIt 111 OOCKtT IIIIlttt1 Ill L51 Iluattta Ia~54VtleTIAL U VISION U A~AOt Itl R.E.Ginna Nuclear Power Plant TtXT IIT~~1~.~~I@AC/4PIII~tl IITI o s o o o 24 491-005-00 02 OF PRE-%TENT PLANT'ONDITIONS The unit was in the Cold/Refueling Shutdown condition for~the Annual Refueling and Maintenance Outage.Reactor Coolant System (RCS)pressure was zero (0)psig and RCS temperature was approximately 68 F.Steam Generator eddy current inspection was in progress.DESCRIPTION OP~9FZ A.DATES AND APPROXIMATE TIMES OP MAZOR OCCtJREUBTCES: |
| DESCRIPTION OP~9FZA.DATESANDAPPROXIMATE TIMESOPMAZOROCCtJREUBTCES: | | o April 14, 1991, 1600 EDST: Event date and time.o April 14, 1991, 1600 EDST: Discovery date and time.o April 16, 1991, 1430 EDST: Oral notification made to the NRC office of Nuclear Reactor Regulation (NRR).o April 22, 1991, 0400 EDST: Steam Generator repairs completed. |
| oApril14,1991,1600EDST:Eventdateandtime.oApril14,1991,1600EDST:Discovery dateandtime.oApril16,1991,1430EDST:Oralnotification madetotheNRCofficeofNuclearReactorRegulation (NRR).oApril22,1991,0400EDST:SteamGenerator repairscompleted.
| | o April 26, 1991, Follow-up written report sent to NRC Office of NRR.r B.&TENT: During the 1991 Annual Refueling and Maintenance Outage, an eddy current examination.was performed in both the"A" and"B" Westinghouse miseries 44 iDesign recirculating steam generators. |
| oApril26,1991,Follow-up writtenreportsenttoNRCOfficeofNRR.rB.&TENT:Duringthe1991AnnualRefueling andMaintenance Outage,aneddycurrentexamination
| | The purpose of the eddy current examination was to assess any corrosion or mechanical damage that may have occurred during the cycle since the 1990 examin-ation.vAC 14111 tttA r~ |
| .wasperformed inboththe"A"and"B"Westinghouse miseries44iDesignrecirculating steamgenerators. | | I NAC term ESSA I~I LICENSEE EVENT REPORT ILERI TEXT CONTINUATION U.S.NUCEtAN AtoULATOAV COMMISOON/Aee1OVEO OMS NO SISO&IOe EXPIIIES.SIS14S DOCKET NUMStll Itl EEII NUMOSN Itl stoUENnAI. |
| Thepurposeoftheeddycurrentexamination wastoassessanycorrosion ormechanical damagethatmayhaveoccurredduringthecyclesincethe1990examin-ation.vAC14111tttAr~
| | " etv4ON N M 1 M A~AOE ISI R.E.Ginna Nuclear~Plant TExT/1I'vee NMee e~.eee eeeaonM ITIIC~JKI'el I ITI o s o o o 244 91-005-00 030F 0 8 The examination was performed by personnel from Rochester Gas and Electric (RG&E)and Allen Nuclear.Associates, Inc.(ANA)..All p'ersonnel were trained and qualified in the eddy current examination method and had been certified to a minimum af Level I for data acquisition and Level II for data analysis.The eddy current examination of the"A" and"B" steam generators was performed utilizing the Zetec Miz-18 Digital Data Acquisition system.The frequencies selected were 400, 200, 100 and 25 KHZ.The inlet or hot leg examination program plan included the examination of 100%of each open unsleeved steam generator tube from the tube end to the first tube support.20%of the hotleg tubes were selected for examination for their full length (20%random sample as recommended in the Electric Power Research Institute (EPRI)guidelines.) |
| I NACtermESSAI~ILICENSEEEVENTREPORTILERITEXTCONTINUATION U.S.NUCEtANAtoULATOAV COMMISOON | | In addition, 20%of each type of sleeve was examined and the remaining tube examined full length.All previous tubes with indications greater than 20%through wall (TW)depth were examined, as a minimum, to the location of their degradation. |
| /Aee1OVEOOMSNOSISO&IOeEXPIIIES. | | All Row 1 and Row 2 U-Bend regions selected as part of the 20%random sample were examined with the Motorized Rotating Pancake Coil (MRPC)between the g6 Tube Support Plate Hot (TSPH)and the g6 Tube Support Plate Cold (TSPC)from the cold leg side.Results of the above inspections indicated that 116 tubes in the"A" steam generator (i.e.91 new repairs--plus 1 pulled tube plus 24 previously plugged tubes)and 117 tubes in the"B" steam generator (i.e.98 new-mepairs plus 1 obstructed sleeved tube plus 16 previously plugged tubes plus 2 plugs exhibiting PWSCC)required corrective action.NAC eOAM SNA (eg]I |
| SIS14SDOCKETNUMStllItlEEIINUMOSNItlstoUENnAI.
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| "etv4ONNM1MA~AOEISIR.E.GinnaNuclear~PlantTExT/1I'veeNMeee~.eeeeeeaonMITIIC~JKI'elIITIosooo24491-005-00030F08Theexamination wasperformed bypersonnel fromRochester GasandElectric(RG&E)andAllenNuclear.Associates, Inc.(ANA)..Allp'ersonnel weretrainedandqualified intheeddycurrentexamination methodandhadbeencertified toaminimumafLevelIfordataacquisition andLevelIIfordataanalysis. | |
| Theeddycurrentexamination ofthe"A"and"B"steamgenerators wasperformed utilizing theZetecMiz-18DigitalDataAcquisition system.Thefrequencies selectedwere400,200,100and25KHZ.Theinletorhotlegexamination programplanincludedtheexamination of100%ofeachopenunsleeved steamgenerator tubefromthetubeendtothefirsttubesupport.20%ofthehotlegtubeswereselectedforexamination fortheirfulllength(20%randomsampleasrecommended intheElectricPowerResearchInstitute (EPRI)guidelines.)
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| Inaddition, 20%ofeachtypeofsleevewasexaminedandtheremaining tubeexaminedfulllength.Allprevioustubeswithindications greaterthan20%throughwall(TW)depthwereexamined, asaminimum,tothelocationoftheirdegradation.
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| AllRow1andRow2U-Bendregionsselectedaspartofthe20%randomsamplewereexaminedwiththeMotorized RotatingPancakeCoil(MRPC)betweentheg6TubeSupportPlateHot(TSPH)andtheg6TubeSupportPlateCold(TSPC)fromthecoldlegside.Resultsoftheaboveinspections indicated that116tubesinthe"A"steamgenerator (i.e.91newrepairs--plus1pulledtubeplus24previously pluggedtubes)and117tubesinthe"B"steamgenerator (i.e.98new-mepairsplus1obstructed sleevedtubeplus16previously pluggedtubesplus2plugsexhibiting PWSCC)requiredcorrective action.NACeOAMSNA(eg]I
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| IIACtens~(t43ILICENSEEEVENTAEPOATILEA)TEXTCONTINUATION U~IIUCl,fAll1SOUlATOAT COMMt%IOSI AttAOVEOOUSSIO31SO&IOSIIItkAl5SI3lkTStACILITTISASISIIIOOCIISTIIUMISIIQlLlllIIIASCIRISISSQVSATkAL
| | IIAC tens~(t43I LICENSEE EVENT AEPOAT ILEA)TEXT CONTINUATION U~IIUCl,f All 1SOUlATOAT COMMt%IOSI AttAOVEO OUS SIO 31SO&IOS IIItkAl5 SI3lkTS tACILITT ISASIS I I I OOCIIST IIUMISII Ql Llll IIIASCIR ISI SSQVSATkAL |
| ~kU1gkSkQkk1tAOEISIR.E.GinnaNuclearPowerPlantTEXTlS'tktt~etWVsrC~~tIIICIktttk~'SlIITI2449l-005-0004Oi08OnApril14,1991atapproximately 1600EDST,thereactorwasintheCold/Refueling Shutdowncondition withRCSTemperature andpressureatapproximately 68Fandzero(0)psigrespectively. | | ~k U 1 g kS kQ kk 1 tAOE ISI R.E.Ginna Nuclear Power Plant TEXT lS'tktt~e tWVsrC~~tIIIC Iktttk~'Sl IITI 2 449 l-0 05-00 04 Oi0 8 On April 14, 1991 at approximately 1600 EDST, the reactor was in the Cold/Refueling Shutdown condition with RCS Temperature and pressure at approximately 68 F and zero (0)psig respectively. |
| Atthistimeafinalreviewoftheeddycurrentdatawascompleted andresultsindicated thatmorethan1percentofthetotaltubesinspected weredegraded(i.e.imperfections greaterthantherepairlimit).Becauseoftheabove,theresultsoftheinspection areconsidered areportable eventpursuantto10CFR50.73perAppendixBoftheGinnaStationQualityAssurance Manual.OnApril16,1991atapproximately 1430EDSTOralNotification wasmadetotheNRC'officeofNRRpursuanttoAppendixBoftheGinnaStationQualityAssurance Manual.OnApril26,1991,afollow-up writtenreportofthesteamgenerators inspection andrepairswassenttotheNRCOfficeofNRRpursuanttoAppendixBoftheGinnaStationQualityAssurance Manual:CINOPERABLE STRUCTURESt COMPONENTSt ORSYSTEMSTHATCONTRIBUTED TOTHEEVENT:None.D.OTHERSYSTEMSORSECONDARY FUNCTIONS AFFECTED-kNone.E.METHODOFDISCOVERY:
| | At this time a final review of the eddy current data was completed and results indicated that more than 1 percent of the total tubes inspected were degraded (i.e.imperfections greater than the repair limit).Because of the above, the results of the inspection are considered a reportable event pursuant to 10 CFR 50.73 per Appendix B of the Ginna Station Quality Assurance Manual.On April 16, 1991 at approximately 1430 EDST Oral Notification was made to the NRC'office of NRR pursuant to Appendix B of the Ginna Station Quality Assurance Manual.On April 26, 1991, a follow-up written report of the steam generators inspection and repairs was sent to the NRC Office of NRR pursuant to Appendix B of the Ginna Station Quality Assurance Manual: C INOPERABLE STRUCTURESt COMPONENTSt OR SYSTEMS THAT CONTRIBUTED TO THE EVENT: None.D.OTHER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED-k None.E.METHOD OF DISCOVERY: |
| Theeventwasapparentafterthereviewofthe"A"and"B"SteamGenerators eddycurrentexamination results.F.OPERATORACTION:None.VACtOAISSQSAkt4$I
| | The event was apparent after the review of the"A" and"B" Steam Generators eddy current examination results.F.OPERATOR ACTION: None.VAC tOAIS SQSA kt4$I |
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| 11CSons5$5AI$45ILICENSEEEVENTREPORT(LERITEXTCONTINUATION VS.IIVCL5AA150VLATOAT COI<<It&IOII ASSAOV50O<<5HO5I$4&IOI5)ISI1555ITI4$SACILITTIIA<<5IIIOOCKSTIIV<<llllITILl114<<ll1IN$$4yonnsLM1ylglosvSA4lI5IR.E.GinnaNuclearPowerPlantTTXTIIS~<<eee1<<O<<OO,y<<OOSS<<nOS ITACSOno~$IIITIosooo244910050005OFG.SAFETYSYSTEMRESPONSES:
| | 11C Sons 5$5A I$45 I LICENSEE EVENT REPORT (LERI TEXT CONTINUATION VS.IIVCL5AA 150VLATOAT COI<<It&IOII ASSAOV50 O<<5 HO 5I$4&IOI 5)ISI155 5ITI4$SACILITT IIA<<5 III OOCKST IIV<<llll ITI Ll1 14<<ll1 IN$$4yonnsL M 1 ylg los v SA4l I5I R.E.Ginna Nuclear Power Plant TTXT IIS~<<eee 1<<O<<OO, y<<OOSS<<nOS IT AC SOno~$I I I TI o s o o o 24 4 91 005 00 0 5 OF G.SAFETY SYSTEM RESPONSES: |
| None.III.CAUSEOPEVE2FZA.IMMEDIATE CAUSE:TheImmediate Causeoftheeventwasthatthe"A"and~"B"steamgenerator tubedegradation wasinexcessoftheGinnaStationQualityAssurance ManualReportable limits.B.ROOTCAUSE:Theresultsoftheexamination indicatethatIGAandIGSCCcontinuetobeactivewithinthetubesheet creviceregionontheinletsideofeachsteamgenerator. | | None.III.CAUSE OP EVE2FZ A.IMMEDIATE CAUSE: The Immediate Cause of the event was that the"A" and~"B" steam generator tube degradation was in excess of the Ginna Station Quality Assurance Manual Reportable limits.B.ROOT CAUSE: The results of the examination indicate that IGA and IGSCC continue to be active within the tubesheet crevice region on the inlet side of each steam generator. |
| Asinthepast,IGA/SCCismuchmoreprevalent inthe"B"steamgenerator with42newIGAindication and37newIGSCCindications reported.
| | As in the past, IGA/SCC is much more prevalent in the"B" steam generator with 42 new IGA indication and 37 new IGSCC indications reported.In the"A" steam generator, 14 new IGA indications and 16 new IGSCC indications were reported.The majority of the inlet tubesheet crevice corrosion.indications are IGA/SCC of the Mil-annealed Inconel 600 Tube Material.This form of corrosion is believed to be the result of the tubesheet crevices forming an alkaline environment. |
| Inthe"A"steamgenerator, 14newIGAindications and16newIGSCCindications werereported.
| | This environment has developed over the years as deposits and active species like sodium and phosphates, have reacted, changing a neutral or inhibited crevice into the aggressive environment that presently exists.Along with IGA/SCC in the crevice, PWSCC at the roll transition appears to have a slight increase in growth during the last operating cycle.This mechanism was first addressed in 1989 and this year there were 19 PWSCC indications in"B" Steam Generator and 59 PWSCC indications in"A" Steam Generator. |
| Themajorityoftheinlettubesheet crevicecorrosion
| | ssC s41<<$4AA |
| .indications areIGA/SCCoftheMil-annealed Inconel600TubeMaterial. | |
| Thisformofcorrosion isbelievedtobetheresultofthetubesheet crevicesforminganalkalineenvironment.
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| Thisenvironment hasdeveloped overtheyearsasdepositsandactivespecieslikesodiumandphosphates, havereacted,changinganeutralorinhibited creviceintotheaggressive environment thatpresently exists.AlongwithIGA/SCCinthecrevice,PWSCCattherolltransition appearstohaveaslightincreaseingrowthduringthelastoperating cycle.Thismechanism wasfirstaddressed in1989andthisyeartherewere19PWSCCindications in"B"SteamGenerator and59PWSCCindications in"A"SteamGenerator.
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| ssCs41<<$4AA
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| IIACtvvMI~lLICENSEEEVENTREPORTILERITEXTCONTINUATION II%NVCLfAAAfOIJLATOAT CCNQN&IOII' AttAOVfOOllfrOfISO&10if)Irlllf5~ITIS'ACILITTHAIrfIIIOOCCfTIILAWfAlflLfllIIUMMR(flyfAAWOMLNTIAL
| | IIAC tvv M I~l LICENSEE EVENT REPORT ILERI TEXT CONTINUATION II%NVCLfAA AfOIJLATOAT CCNQN&IOII' AttAOVfO Ollf rO fISO&10i f)Irlllf 5~ITIS'ACILITT HAIrf III OOCCfT IILAWfA lfl Lfll IIUMMR (fl yf AA WOMLNTIAL'4IOH r 1~Aof Ifl R.E.Ginna Nuclear Power Plant TEXT Ill'Vrv r teWeer.yv ereecveV r'IIC~~'al I ITI o s o o o 2 4 4 91-00 5 0 006 0FO 8 ANALYSIS OF EVENT The event is reportable in accordance with 10 CFR 50.73, Licensee Event Report item (Other)and the Ginna Station Quality Assurance Manual Appendix B which requires that,"If the number of tubes in a generator falling into categories a or b exceeds the criteria, then results of the inspection shall be considered a Reportable Event pursuant to 10 CFR 50.73." The, tube degradation in the"A" and"B" steam generators exceeded the criterion of (b)which states,"more than 1%of total tubes inspected are degraded, (imperfections greater than the repair limit)." This repair limit is defined as,"steam generator tubes that have imperfections greater than 404 through wall, as indicated by eddy current, shall be repaired by plugging or sleeving." An assessment was performed considering the safety con-sequences and implications of this event with the following results and conclusions: |
| '4IOHr1~AofIflR.E.GinnaNuclearPowerPlantTEXTIll'VrvrteWeer.yvereecveVr'IIC~~'alIITIosooo24491-00500060FO8ANALYSISOFEVENTTheeventisreportable inaccordance with10CFR50.73,LicenseeEventReportitem(Other)andtheGinnaStationQualityAssurance ManualAppendixBwhichrequiresthat,"Ifthenumberoftubesinagenerator fallingintocategories aorbexceedsthecriteria, thenresultsoftheinspection shallbeconsidered aReportable Eventpursuantto10CFR50.73."The,tubedegradation inthe"A"and"B"steamgenerators exceededthecriterion of(b)whichstates,"morethan1%oftotaltubesinspected aredegraded, (imperfections greaterthantherepairlimit)."Thisrepairlimitisdefinedas,"steamgenerator tubesthathaveimperfections greaterthan404throughwall,asindicated byeddycurrent,shallberepairedbypluggingorsleeving." | | There were no operational or safety consequences or safety implications resulting from the steam generator tube degradation in excess of the Quality Assurance Manual reportable'imits because: o The degraded tubes were identified and repaired prior to any significant leakage or steam generator tube rupture occurring. |
| Anassessment wasperformed considering thesafetycon-sequences andimplications ofthiseventwiththefollowing resultsandconclusions:
| | o Even assuming a complete severance of a steam generator tube at full power, as stated in the R.E.Ginna Nuclear Power Plant updated Final ,Safety Analysis Report (Ginna/UFSAR) section 15.6.3, (Steam Generator Tube Rupture)the sequence of recovery actions ensures early'ermination of primary to secondary leakage with or without offsite power available thus limiting offsite radiation doses to within the guidelines of 10 CFR 100.Based on the above, it can be concluded that the public's health and safety were assured at all times.rAC NOAH~ |
| Therewerenooperational orsafetyconsequences orsafetyimplications resulting fromthesteamgenerator tubedegradation inexcessoftheQualityAssurance Manualreportable'imits because:oThedegradedtubeswereidentified andrepairedpriortoanysignificant leakageorsteamgenerator tuberuptureoccurring.
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| oEvenassumingacompleteseverance ofasteamgenerator tubeatfullpower,asstatedintheR.E.GinnaNuclearPowerPlantupdatedFinal,SafetyAnalysisReport(Ginna/UFSAR) section15.6.3,(SteamGenerator TubeRupture)thesequenceofrecoveryactionsensuresearly'ermination ofprimarytosecondary leakagewithorwithoutoffsitepoweravailable thuslimitingoffsiteradiation dosestowithintheguidelines of10CFR100.Basedontheabove,itcanbeconcluded thatthepublic'shealthandsafetywereassuredatalltimes.rACNOAH~
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| IIAC>vssstttAI944ILICENSEEEVENTREPORT(LER)TEXTCONTINUATION V.t.ISVCEEAAAEOVLATOIIY COAIMIttIOII IAlrAOYEOOastssO)Ito&IOaEXPIAE$IttIstSlACILITYIIA1ltIIIOOCXETISVIMtllIllEEIIIIIAAtltI~Itt4SStSSTSA4ssYstsOss~stA~AOEItlR.E.GinnaNuclearPowerPlantTExfillsssvYAsAcs0~.ssvAtsssawss sYAcssssssss~TOIITIosooo2449-1-05-0007ov08V.CORRECTIVE ACTIONA.ACTIONTAKENTORETURNAPPECTEDSYSTEMSTOPRE-E%9lT | | IIAC>vsss tttA I944 I LICENSEE EVENT REPORT (LER)TEXT CONTINUATION V.t.ISVCEEAA AEOVLATOIIY COAIMIttIOII I AlrAOYEO Oast ssO)Ito&IOa EXPIAE$IttIstS lACILITY IIA1lt III OOCXET ISVIMtll Ill EEII IIIAAtlt I~I t t 4 SS t SS T S A 4 ss YstsOss~s tA~AOE Itl R.E.Ginna Nuclear Power Plant TExf ill sssvY AsAcs 0~.ssv Atsssawss sYAc ssssssss~TO I I TI o s o o o 2 449-1-05-000 7 ov 08 V.CORRECTIVE ACTION A.ACTION TAKEN TO RETURN APPECTED SYSTEMS TO PRE-E%9lT'ORMAL STATUS: 0 0 Of the 116 degraded tubes in the"A" steam generator, 61 tubes were repaired using a Combustion Engineering'27" welded sleeve in the hot leg plus 41 tubes were repaired using a Combustion Engineering 30" welded sleeve in the hot leg and all of the above tubes will remain in service.The remaining 14 tubes were removed from service by plugging both the hot and cold leg tube ends.A total of 190 tubes in"A"@G are.currently plugged and 324 tubes are sleeved.Of the 117 degraded tubes in the"B" steam generator, 80 tubes were repaired using a Combustion Engineering 27" welded sleeve in the hot leg plus 28 tubes were repaired using a Combustion Engineering 30" welded sleeve in the hot leg and all of the above tubes will remain.in service.The remaining 9 tubes were removed from service by plugging both the hot and cold leg tube ends.A total of 326 tubes in the"B" S/G are currently plugged and 938 tubes are sleeved.B.ACTION TAKEN OR PLANNED TO PE~TENT RECURMQTCE The occurrence/presence of IGA, SCC and PWSCC is a common PWR Steam Generator problem.Utilities with~usceptible tubing and partially rolled crevices must deal with this recurring attack on steam generator--<ubing.R.E.Ginna Station will continue careful monitoring of both primary RCS and secondary side water chemistry parameters. |
| 'ORMALSTATUS:00Ofthe116degradedtubesinthe"A"steamgenerator, 61tubeswererepairedusingaCombustion Engineering'27" weldedsleeveinthehotlegplus41tubeswererepairedusingaCombustion Engineering 30"weldedsleeveinthehotlegandalloftheabovetubeswillremaininservice.Theremaining 14tubeswereremovedfromservicebypluggingboththehotandcoldlegtubeends.Atotalof190tubesin"A"@Gare.currently pluggedand324tubesaresleeved.Ofthe117degradedtubesinthe"B"steamgenerator, 80tubeswererepairedusingaCombustion Engineering 27"weldedsleeveinthehotlegplus28tubeswererepairedusingaCombustion Engineering 30"weldedsleeveinthehotlegandalloftheabovetubeswillremain.inservice.Theremaining 9tubeswereremovedfromservicebypluggingboththehotandcoldlegtubeends.Atotalof326tubesinthe"B"S/Garecurrently pluggedand938tubesaresleeved.B.ACTIONTAKENORPLANNEDTOPE~TENTRECURMQTCE Theoccurrence/presence ofIGA,SCCandPWSCCisacommonPWRSteamGenerator problem.Utilities with~usceptible tubingandpartially rolledcrevicesmustdealwiththisrecurring attackonsteamgenerator | | These water chemistry parameters will be evaluated against accepted industry guidelines in order to minimize harmful and/or secondary side environments. |
| --<ubing.R.E.GinnaStationwillcontinuecarefulmonitoring ofbothprimaryRCSandsecondary sidewaterchemistry parameters. | | asAC lOAsA tttA ha I~as |
| Thesewaterchemistry parameters willbeevaluated againstacceptedindustryguidelines inordertominimizeharmfuland/orsecondary sideenvironments.
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| asAClOAsAtttAhaI~as
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| NIICSeamSNAI04SI1LICENSEEEVENTREPORTILER)TEXTCONTINUATION U.S.NUCLSANAS4ULATOIIY COAIAIISSION ASSAOYSOOMSNOSlSOWI04rs>>sIAsssnInsSACILITYNAIICIllDOC>>STNU~SIIITILSIINI>>AOSIIIIIssQUANT>AL YNIOHSAOSISIR.E.GinnaNuclearPowerPlantTGCTIIIee>>eNNee~teeeecceoeeeeeeeIJV>>CSee>>~'elIITIo5ooo24491-005-0008OFO8DegradedSteamGenerator tubesshallbesleevedorpluggedinaccordance withtheinservice inspection programandacceptedindustryrepairmethods.ADDITIONAL INFORMATION FAILEDCOMPONENTS.
| | NIIC Seam SNA I04SI 1 LICENSEE EVENT REPORT ILER)TEXT CONTINUATION U.S.NUCLSAN AS4ULATOIIY COAIAIISSION ASSAOYSO OMS NO Sl SOWI04 r s>>sIAss snIns SACILITY NAIIC Ill DOC>>ST NU~SII ITI LSII NI>>AOSII III ssQUANT>AL YNIOH SAOS ISI R.E.Ginna Nuclear Power Plant TGCT III ee>>e NNee~teeeec ceo eeeeeeeI JV>>C See>>~'el I ITI o 5 o o o 24 491-00 5-0 0 08 OFO 8 Degraded Steam Generator tubes shall be sleeved or plugged in accordance with the inservice inspection program and accepted industry repair methods.ADDITIONAL INFORMATION FAILED COMPONENTS. |
| Thedegradedcomponents are:InconelGrade600tubeshavinganoutsidediameterof0.875inchesandanominalwallthickness of0.050inches.B.PREVIOUSLERsONSIMILAREVENTS:AsimilarLEReventhistorical searchwasconducted withthefollowing results:Thecreviceindications aresimilartothosereportedinA0-74-02, A0-75-07, R0-75-013, andLERs76-008,77-008,78-003,79-006,79022s80003s81009s82003s82022s83013s89001,and90-004.C.SPECIALCOMMIBFXS:
| | The degraded components are: Inconel Grade 600 tubes having an outside diameter of 0.875 inches and a nominal wall thickness of 0.050 inches.B.PREVIOUS LERs ON SIMILAR EVENTS: A similar LER event historical search was conducted with the following results: The crevice indications are similar to those reported in A0-74-02, A0-75-07, R0-75-013, and LERs 76-008, 77-008, 78-003, 79-006, 79 022s 80 003s 81 009s 82 003s 82 022s 83 013s 89 001, and 90-004.C.SPECIAL COMMIBFXS: |
| Foramoreindepthreport,refertothe,"1991SteamGenerator EddyCurrentExamination SummaryReport"senttotheNRCApril26,1991.~vACSOAKSAAAIeeSTI
| | For a more indepth report, refer to the,"1991 Steam Generator Eddy Current Examination Summary Report" sent to the NRC April 26, 1991.~vAC SOAK SAAA Ie eSTI |
| ~ss~}} | | ~s s~}} |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
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[Table view] Category:RO)
MONTHYEARML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17265A7601999-10-0505 October 1999 Part 21 Rept Re W2 Switch Supplied by W Drawn from Stock, Did Not Operate Properly After Being Installed on 990409. Switch Returned to W on 990514 for Evaluation & Root Cause Analysis ML17265A7621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Re Ginna Npp.With 991008 Ltr ML17265A7531999-09-23023 September 1999 Part 21 Rept Re Corrective Action & Closeout of 10CFR21 Rept of Noncompliance Re Unacceptable Part for 30-4 Connector. Unacceptable Parts Removed from Stock & Scrapped ML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7471999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Re Ginna Npp.With 990909 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7341999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Re Ginna Npp.With 990806 Ltr ML17265A7291999-07-29029 July 1999 Interim Part 21 Rept Re safety-related DB-25 Breaker Mechanism Procured from W Did Not Pas Degradatin Checks When Drawn from Stock to Be Installed Into BUS15/03A.Holes Did Not line-up & Tripper Pan Bent ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7131999-07-22022 July 1999 Special Rept:On 990407,radiation Monitor RM-14A Was Declared Inoperable.Caused by Failed Communication Link from TSC to Plant Process Computer Sys.Communication Link Was re-established & RM-14A Was Declaed Operable on 990521 ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7211999-07-19019 July 1999 ISI Rept for Third Interval (1990-1999) Third Period, Second Outage (1999) at Re Ginna Npp. ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A7661999-06-30030 June 1999 1999 Rept of Facility Changes,Tests & Experiments Conducted Without Prior NRC Approval for Jan 1998 Through June 1999, Per 10CFR50.59.With 991020 Ltr ML17265A7011999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Re Ginna Npp.With 990712 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6761999-06-16016 June 1999 Part 21 Rept Re Defects & noncompliances,10CFR21(d)(3)(ii), Which Requires Written Notification to NRC on Identification of Defect or Failure to Comply. Relays Were Returned to Eaton for Evaluation & Root Cause Analysis ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17265A6681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Re Ginna Nuclear Power Plant.With 990608 Ltr ML17265A6651999-05-27027 May 1999 Interim Rept Re W2 Control Switch,Procured from W,Did Not Operate Satisfactorily When Drawn from Stock to Be Installed in Main Control Board for 1C2 Safety Injection Pump. Estimated That Evaluation Will Be Completed by 991001 ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6591999-05-17017 May 1999 Part 21 Rept Re Relay Deficiency Detected During pre-installation Testing.Caused by Incorrectly Wired Relay Coil.Relays Were Returned to Eaton Corp for Investigation. Relays Were Repaired & Retested ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6381999-05-0707 May 1999 Part 21 Rept Re Replacement Turbocharger Exhaust Turbine Side Drain Port Not Functioning as Design Intended.Caused by Manufacturing Deficiency.Turbocharger Was Reaasembled & Reinstalled on B EDG ML17265A6391999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Re Ginna Nuclear Power Plant.With 990510 Ltr ML17265A6361999-04-23023 April 1999 Part 21 Rept Re Power Supply That Did Not Work Properly When Drawn from Stock & Installed in -25 Vdc Slot.Power Supply Will Be Sent to Vendor to Perform Failure Mode Assessment.Evaluation Will Be Completed by 991001 ML17265A6301999-04-18018 April 1999 Rev 1 to Cycle 28 COLR for Re Ginna Npp. ML17265A6251999-04-15015 April 1999 Special Rept:On 990309,halon Systems Were Removed from Svc & Fire Door F502 Was Blocked Open.Caused by Mods Being Made to CR Emergency Air Treatment Sys.Continuous Fire Watch Was Established with Backup Fire Suppression Equipment ML17265A6551999-04-0909 April 1999 Initial Part 21 Rept Re Mfg Deficiency in Replacement Turbocharger for B EDG Supplied by Coltec Industries. Deficiency Consisted of Missing Drain Port in Intermediate Casing.Required Oil Drain Port Machined Open ML17265A6291999-03-31031 March 1999 Rev 0 to Cycle 28 COLR for Re Ginna Npp. ML17265A6241999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Ginna Station.With 990409 Ltr ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A5661999-03-0101 March 1999 Rev 26 to QA Program for Station Operation. ML17265A5961999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Ginna Nuclear Power Plant.With 990310 Ltr ML17265A5371999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Re Ginna Nuclear Power Plant.With 990205 Ltr ML17265A5951998-12-31031 December 1998 Rg&E 1998 Annual Rept. ML17265A5001998-12-21021 December 1998 Rev 26 to QA Program for Station Operation. ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4761998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Re Ginna Nuclear Power Plant.With 981210 Ltr ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4531998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Re Ginna Nuclear Power Plant.With 981110 Ltr ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A4291998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Re Ginna Nuclear Power Plant.With 981009 Ltr 1999-09-30
[Table view] |
Text
ACCELERATED DILUTION DEMONS~TION SYSTEM iP REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)ACCESSION NBR:9105210249 DOC.DATE: 91/05/13 NOTARIZED:
NO FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester G AUTH.NAME.AUTHOR AFFILIATION GORSKI,P.Rochester Gas&Electric Corp.MECREDY,R.C.
Rochester Gas&Electric Corp.RECIP.NAME
'ECIPIENT AFFILIATION DOCKET g 05000244 R
SUBJECT:
LER 91-005-00:on 910414,steam generator tube degradation.
Caused by"A"&"B" S/GS tube degradation in excess of Ginna QAM reportability limits.Tubes repaired using Combustion Engineering welded sleeve.W/910513 ltr.DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE: TITLE: 50.73/50.9 Licensee Event, Report (LER), Incident Rpt, etc..S NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72).
05000244 RECIPIENT ID CODE/NAME PD1-3 LA JOHNSON,A INTERNAL: ACNW AEOD/DS P/TPAB NRR/DET/ECMB 9H NRR/DLPQ/LHFB11 NRR/DOEA/OEAB NRR/DST/SELB SD Nj%/BS~LBSD1 RE~IL~02 FILE 01 EXTERNAL: EG&G BRYCE, J.H NRC PDR NSIC POORE,W.COPIES LTTR ENCL 1 1 1 1 2 2 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 3 3 1 1 1 1 RECIPIENT ID CODE/NAME PD1-3 PD AEOD/DOA AEOD/ROAB/DSP NRR/DET/EMEB 7E NRR/DLPQ/LPEB10 NRR/DREP/PRPB11 NRR/DST/SICB 7E NRR/DST/SRXB SE RES/DSIR/EIB L ST LOBBY WARD NSIC MURPHY,G.A NUDOCS FULL TXT COPIES LTTR ENCL 1 1 1 1 2 2 1'1 1 2 2 1 1 1 1 1 1 1 1 1 1 1 1 D NOTE TO ALL"RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE iVASTE!CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT.20079)TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!D D FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED'TTR 31 ENCL 31
ROCHESTER GAS AND ELECTRIC CORPORATION o 89 EAST AVENUE, ROCHESTER N.Y.14649-0001+, ROBERT C.MECREDY Vice President Cinna Nuclear Production TELEPHONE AREA CODE 716 546 2700 May 13, 1991 U.S.Nuclear Regulatory Commission Document Control Desk Washington, DC 20555
Subject:
LER 91-005, Steam Generator Tube Degradation Due to IGA/SCC Causes Q.A.Manual Reportable Limits to be Reached R.E.Ginna Nuclear Power Plant Docket No.50-244 In accordance with 10 CFR 50.73, Licensee Event Report System, item (Other), and the Ginna Station Quality Assurance Manual Appendix B, which requires that,"If the number of tubes in a generator falling into categories a or b below exceeds the criteria, then results of the inspection shall be considered a Reportable Event pursuant to 10 CFR 50.73," the attached Licensee Event Report LER 91-005 is hereby submitted.
This event has in no way affected the public's health and safety.Ver truly yours, XC: Robert C.Me redy U.S.Nuclear Regulatory Commission Region I 475 Allendale Road King of Prussia, PA 19406 Ginna USNRC Senior Resident Inspector 9105210249 9i05i3 PDFl ADQCK 0 000244 s FDR WG&a~II I
rAC Seea IIO IOAII UCENSEE EVENT REPORT LER)U*IACLIAI A IOULATON>COANI~Ase1ovto OUI INL IIII Olov CISINCI IIII/II OOCltT NUIIOCN Ql o6oo0244>ot SACILITY NAIIC I'l R.E.Ginna Nuclear Power Plant TLI lel Steam Generator Tube Degradation Due to IGA/SCC Causes Q.A.Manual Reportable Limits to be Reached CVINT OATI Itl LC1 NVIIOCA IN 1CSOA'1 OATI Ih OTNI1 SACILITIC~INVOLVto Nl eeoeeTN OAY YCAN ey IIOVINTIAL I.Nvee~11 AI Veeeee~evWIA NOee TN OAY YCA1 SACILITY NAeele oocCIT NUIIIIAQI 0 6 0 0 0 0 414 9 1 1 005 0 0 0 5 1 391 0 6 0 0 0 OSCAATINO~eOOI Oll~OIVIA CIVIL P P P'101 TNII 1tSONT Q WINITTCO SVIQVANT T~OOI4l Ql I Iel N.T 041 Q II el II.T$4I QI I eel~IOI41QIINIIW
~O.T Ilel QI IVNI Ql~O.TSNIQIIII Io.cot l~I IO.IOllel IOOIlellll IOM W Itl IO.AOI 4111110 I0%4411I I I II CO.III 4)l1IINI~O.T 04 I QI ll~O.T I 4 1 Q I I II COAS4 I II I Oel!O.III III II llel IO J III IQI INI LICtNtll CONTACT SON TIIQ LI1 Iltl 0 Teel 1lovlAILIINTI os 10cs1 j;Iceeee eee ey eeae el SN eeeeeeel 111 1%71 OI TXTIW oTIIC1 lteeexy le Aeeeeet~eeet eee ee TeeL NIC Sow JIIAI NAVC Paul Gorski Mechanical Maintenance Mana er TILCSeeONC NVNII1 ANIA COOC 3155 COUSLCT 8 ONI LINt SON CACII COIISON CNT SAILUIC OCICIII to NI TNII 1CSOIT Iltl CAUtl IYITIII X CONSONINT T B NANUSAO TUN III H 3 4 TO NS I OI AIjl+M(lh w 7 CAUII IYCTCII coeesoNINT
~IANUIAO TUNCN~P0IITU g~(A~t:@%FATS!M%~V: IVSSLCNINTAL IICSOAT CLSCCTCO IIII Ylt Oy y<<.~CXSCCTCO CVINIC>>ON OAT>>NO AICTAACT ILJevc 0 I Axl eeeee.IA, eeeyeeeeeMy NINee eeeseeeeeee Iyftsrlllee
<<eeeI IW IIONTII CAY YCA1 CISCCTCO WIIN CC ION OATI 11~I During the 1991 Annual Refueling and Maintenance Outage subsequent to the eddy current examination performed on both the"A" and"B" Westinghouse series 44 Steam Generator (S/G), 116 tubes in the"A" S/G and 117 tubes in the"B" S/G required corrective action due to tube degradation.
The immediate cause of the event was that the"A" and"B" S/Gs tube degradation was in excess of the Ginna Quality Assurance Manual reportability limits.The underlying cause of the tube degradation is a common S/G problem of a partially rolled tube sheet crevice with recurring Intergranular Attack/Stress Corrosion Cracking (ZGA/SCC)and Primary Water Stress Corrosion Cracking (PWSCC)attack on S/G tubing.Corrective action taken was to ei.ther sleeve or plug the affected tubes with accepted industry repair methods.NAC Seee IOI I&All
1114 terU~10451 LICENSEE EVENT REPORT ILERI TEXT CONTINUATION II.5.IIIICLtA1 154MLATOAY COQMINIISI r AftAOvtO OUO HO 5ltOWIOt t)CPIII55 t/TIES FACILITY IIAAIt 111 OOCKtT IIIIlttt1 Ill L51 Iluattta Ia~54VtleTIAL U VISION U A~AOt Itl R.E.Ginna Nuclear Power Plant TtXT IIT~~1~.~~I@AC/4PIII~tl IITI o s o o o 24 491-005-00 02 OF PRE-%TENT PLANT'ONDITIONS The unit was in the Cold/Refueling Shutdown condition for~the Annual Refueling and Maintenance Outage.Reactor Coolant System (RCS)pressure was zero (0)psig and RCS temperature was approximately 68 F.Steam Generator eddy current inspection was in progress.DESCRIPTION OP~9FZ A.DATES AND APPROXIMATE TIMES OP MAZOR OCCtJREUBTCES:
o April 14, 1991, 1600 EDST: Event date and time.o April 14, 1991, 1600 EDST: Discovery date and time.o April 16, 1991, 1430 EDST: Oral notification made to the NRC office of Nuclear Reactor Regulation (NRR).o April 22, 1991, 0400 EDST: Steam Generator repairs completed.
o April 26, 1991, Follow-up written report sent to NRC Office of NRR.r B.&TENT: During the 1991 Annual Refueling and Maintenance Outage, an eddy current examination.was performed in both the"A" and"B" Westinghouse miseries 44 iDesign recirculating steam generators.
The purpose of the eddy current examination was to assess any corrosion or mechanical damage that may have occurred during the cycle since the 1990 examin-ation.vAC 14111 tttA r~
I NAC term ESSA I~I LICENSEE EVENT REPORT ILERI TEXT CONTINUATION U.S.NUCEtAN AtoULATOAV COMMISOON/Aee1OVEO OMS NO SISO&IOe EXPIIIES.SIS14S DOCKET NUMStll Itl EEII NUMOSN Itl stoUENnAI.
" etv4ON N M 1 M A~AOE ISI R.E.Ginna Nuclear~Plant TExT/1I'vee NMee e~.eee eeeaonM ITIIC~JKI'el I ITI o s o o o 244 91-005-00 030F 0 8 The examination was performed by personnel from Rochester Gas and Electric (RG&E)and Allen Nuclear.Associates, Inc.(ANA)..All p'ersonnel were trained and qualified in the eddy current examination method and had been certified to a minimum af Level I for data acquisition and Level II for data analysis.The eddy current examination of the"A" and"B" steam generators was performed utilizing the Zetec Miz-18 Digital Data Acquisition system.The frequencies selected were 400, 200, 100 and 25 KHZ.The inlet or hot leg examination program plan included the examination of 100%of each open unsleeved steam generator tube from the tube end to the first tube support.20%of the hotleg tubes were selected for examination for their full length (20%random sample as recommended in the Electric Power Research Institute (EPRI)guidelines.)
In addition, 20%of each type of sleeve was examined and the remaining tube examined full length.All previous tubes with indications greater than 20%through wall (TW)depth were examined, as a minimum, to the location of their degradation.
All Row 1 and Row 2 U-Bend regions selected as part of the 20%random sample were examined with the Motorized Rotating Pancake Coil (MRPC)between the g6 Tube Support Plate Hot (TSPH)and the g6 Tube Support Plate Cold (TSPC)from the cold leg side.Results of the above inspections indicated that 116 tubes in the"A" steam generator (i.e.91 new repairs--plus 1 pulled tube plus 24 previously plugged tubes)and 117 tubes in the"B" steam generator (i.e.98 new-mepairs plus 1 obstructed sleeved tube plus 16 previously plugged tubes plus 2 plugs exhibiting PWSCC)required corrective action.NAC eOAM SNA (eg]I
IIAC tens~(t43I LICENSEE EVENT AEPOAT ILEA)TEXT CONTINUATION U~IIUCl,f All 1SOUlATOAT COMMt%IOSI AttAOVEO OUS SIO 31SO&IOS IIItkAl5 SI3lkTS tACILITT ISASIS I I I OOCIIST IIUMISII Ql Llll IIIASCIR ISI SSQVSATkAL
~k U 1 g kS kQ kk 1 tAOE ISI R.E.Ginna Nuclear Power Plant TEXT lS'tktt~e tWVsrC~~tIIIC Iktttk~'Sl IITI 2 449 l-0 05-00 04 Oi0 8 On April 14, 1991 at approximately 1600 EDST, the reactor was in the Cold/Refueling Shutdown condition with RCS Temperature and pressure at approximately 68 F and zero (0)psig respectively.
At this time a final review of the eddy current data was completed and results indicated that more than 1 percent of the total tubes inspected were degraded (i.e.imperfections greater than the repair limit).Because of the above, the results of the inspection are considered a reportable event pursuant to 10 CFR 50.73 per Appendix B of the Ginna Station Quality Assurance Manual.On April 16, 1991 at approximately 1430 EDST Oral Notification was made to the NRC'office of NRR pursuant to Appendix B of the Ginna Station Quality Assurance Manual.On April 26, 1991, a follow-up written report of the steam generators inspection and repairs was sent to the NRC Office of NRR pursuant to Appendix B of the Ginna Station Quality Assurance Manual: C INOPERABLE STRUCTURESt COMPONENTSt OR SYSTEMS THAT CONTRIBUTED TO THE EVENT: None.D.OTHER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED-k None.E.METHOD OF DISCOVERY:
The event was apparent after the review of the"A" and"B" Steam Generators eddy current examination results.F.OPERATOR ACTION: None.VAC tOAIS SQSA kt4$I
11C Sons 5$5A I$45 I LICENSEE EVENT REPORT (LERI TEXT CONTINUATION VS.IIVCL5AA 150VLATOAT COI<<It&IOII ASSAOV50 O<<5 HO 5I$4&IOI 5)ISI155 5ITI4$SACILITT IIA<<5 III OOCKST IIV<<llll ITI Ll1 14<<ll1 IN$$4yonnsL M 1 ylg los v SA4l I5I R.E.Ginna Nuclear Power Plant TTXT IIS~<<eee 1<<O<<OO, y<<OOSS<<nOS IT AC SOno~$I I I TI o s o o o 24 4 91 005 00 0 5 OF G.SAFETY SYSTEM RESPONSES:
None.III.CAUSE OP EVE2FZ A.IMMEDIATE CAUSE: The Immediate Cause of the event was that the"A" and~"B" steam generator tube degradation was in excess of the Ginna Station Quality Assurance Manual Reportable limits.B.ROOT CAUSE: The results of the examination indicate that IGA and IGSCC continue to be active within the tubesheet crevice region on the inlet side of each steam generator.
As in the past, IGA/SCC is much more prevalent in the"B" steam generator with 42 new IGA indication and 37 new IGSCC indications reported.In the"A" steam generator, 14 new IGA indications and 16 new IGSCC indications were reported.The majority of the inlet tubesheet crevice corrosion.indications are IGA/SCC of the Mil-annealed Inconel 600 Tube Material.This form of corrosion is believed to be the result of the tubesheet crevices forming an alkaline environment.
This environment has developed over the years as deposits and active species like sodium and phosphates, have reacted, changing a neutral or inhibited crevice into the aggressive environment that presently exists.Along with IGA/SCC in the crevice, PWSCC at the roll transition appears to have a slight increase in growth during the last operating cycle.This mechanism was first addressed in 1989 and this year there were 19 PWSCC indications in"B" Steam Generator and 59 PWSCC indications in"A" Steam Generator.
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IIAC tvv M I~l LICENSEE EVENT REPORT ILERI TEXT CONTINUATION II%NVCLfAA AfOIJLATOAT CCNQN&IOII' AttAOVfO Ollf rO fISO&10i f)Irlllf 5~ITIS'ACILITT HAIrf III OOCCfT IILAWfA lfl Lfll IIUMMR (fl yf AA WOMLNTIAL'4IOH r 1~Aof Ifl R.E.Ginna Nuclear Power Plant TEXT Ill'Vrv r teWeer.yv ereecveV r'IIC~~'al I ITI o s o o o 2 4 4 91-00 5 0 006 0FO 8 ANALYSIS OF EVENT The event is reportable in accordance with 10 CFR 50.73, Licensee Event Report item (Other)and the Ginna Station Quality Assurance Manual Appendix B which requires that,"If the number of tubes in a generator falling into categories a or b exceeds the criteria, then results of the inspection shall be considered a Reportable Event pursuant to 10 CFR 50.73." The, tube degradation in the"A" and"B" steam generators exceeded the criterion of (b)which states,"more than 1%of total tubes inspected are degraded, (imperfections greater than the repair limit)." This repair limit is defined as,"steam generator tubes that have imperfections greater than 404 through wall, as indicated by eddy current, shall be repaired by plugging or sleeving." An assessment was performed considering the safety con-sequences and implications of this event with the following results and conclusions:
There were no operational or safety consequences or safety implications resulting from the steam generator tube degradation in excess of the Quality Assurance Manual reportable'imits because: o The degraded tubes were identified and repaired prior to any significant leakage or steam generator tube rupture occurring.
o Even assuming a complete severance of a steam generator tube at full power, as stated in the R.E.Ginna Nuclear Power Plant updated Final ,Safety Analysis Report (Ginna/UFSAR) section 15.6.3, (Steam Generator Tube Rupture)the sequence of recovery actions ensures early'ermination of primary to secondary leakage with or without offsite power available thus limiting offsite radiation doses to within the guidelines of 10 CFR 100.Based on the above, it can be concluded that the public's health and safety were assured at all times.rAC NOAH~
IIAC>vsss tttA I944 I LICENSEE EVENT REPORT (LER)TEXT CONTINUATION V.t.ISVCEEAA AEOVLATOIIY COAIMIttIOII I AlrAOYEO Oast ssO)Ito&IOa EXPIAE$IttIstS lACILITY IIA1lt III OOCXET ISVIMtll Ill EEII IIIAAtlt I~I t t 4 SS t SS T S A 4 ss YstsOss~s tA~AOE Itl R.E.Ginna Nuclear Power Plant TExf ill sssvY AsAcs 0~.ssv Atsssawss sYAc ssssssss~TO I I TI o s o o o 2 449-1-05-000 7 ov 08 V.CORRECTIVE ACTION A.ACTION TAKEN TO RETURN APPECTED SYSTEMS TO PRE-E%9lT'ORMAL STATUS: 0 0 Of the 116 degraded tubes in the"A" steam generator, 61 tubes were repaired using a Combustion Engineering'27" welded sleeve in the hot leg plus 41 tubes were repaired using a Combustion Engineering 30" welded sleeve in the hot leg and all of the above tubes will remain in service.The remaining 14 tubes were removed from service by plugging both the hot and cold leg tube ends.A total of 190 tubes in"A"@G are.currently plugged and 324 tubes are sleeved.Of the 117 degraded tubes in the"B" steam generator, 80 tubes were repaired using a Combustion Engineering 27" welded sleeve in the hot leg plus 28 tubes were repaired using a Combustion Engineering 30" welded sleeve in the hot leg and all of the above tubes will remain.in service.The remaining 9 tubes were removed from service by plugging both the hot and cold leg tube ends.A total of 326 tubes in the"B" S/G are currently plugged and 938 tubes are sleeved.B.ACTION TAKEN OR PLANNED TO PE~TENT RECURMQTCE The occurrence/presence of IGA, SCC and PWSCC is a common PWR Steam Generator problem.Utilities with~usceptible tubing and partially rolled crevices must deal with this recurring attack on steam generator--<ubing.R.E.Ginna Station will continue careful monitoring of both primary RCS and secondary side water chemistry parameters.
These water chemistry parameters will be evaluated against accepted industry guidelines in order to minimize harmful and/or secondary side environments.
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NIIC Seam SNA I04SI 1 LICENSEE EVENT REPORT ILER)TEXT CONTINUATION U.S.NUCLSAN AS4ULATOIIY COAIAIISSION ASSAOYSO OMS NO Sl SOWI04 r s>>sIAss snIns SACILITY NAIIC Ill DOC>>ST NU~SII ITI LSII NI>>AOSII III ssQUANT>AL YNIOH SAOS ISI R.E.Ginna Nuclear Power Plant TGCT III ee>>e NNee~teeeec ceo eeeeeeeI JV>>C See>>~'el I ITI o 5 o o o 24 491-00 5-0 0 08 OFO 8 Degraded Steam Generator tubes shall be sleeved or plugged in accordance with the inservice inspection program and accepted industry repair methods.ADDITIONAL INFORMATION FAILED COMPONENTS.
The degraded components are: Inconel Grade 600 tubes having an outside diameter of 0.875 inches and a nominal wall thickness of 0.050 inches.B.PREVIOUS LERs ON SIMILAR EVENTS: A similar LER event historical search was conducted with the following results: The crevice indications are similar to those reported in A0-74-02, A0-75-07, R0-75-013, and LERs76-008, 77-008,78-003, 79-006, 79 022s 80 003s 81 009s 82 003s 82 022s 83 013s 89 001, and 90-004.C.SPECIAL COMMIBFXS:
For a more indepth report, refer to the,"1991 Steam Generator Eddy Current Examination Summary Report" sent to the NRC April 26, 1991.~vAC SOAK SAAA Ie eSTI
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