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| {{#Wiki_filter:ACCELERATE UTION DEMONSATION SYSIEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)ACCESSION NBR:9004130181 DOC DATE: 90/03/28 NOTARIZED: | | {{#Wiki_filter:ACCELERATE UTION DEMONSATION SYSIEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS) |
| NO FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester G AUTH.NAME AUTHOR AFFILIATION CAVANAUGH,M.E. | | ACCESSION NBR:9004130181 DOC DATE: 90/03/28 NOTARIZED: NO DOCKET FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester G 05000244 AUTH. NAME AUTHOR AFFILIATION CAVANAUGH,M.E. Rochester Gas & Electric Corp. |
| Rochester Gas&Electric Corp.MECREDY,R.C. | | MECREDY,R.C. Rochester Gas & Electric Corp. |
| Rochester Gas&Electric Corp.RECIP.NAME RECIPIENT AFFILIATION DOCKET 05000244 | | RECIP.NAME RECIPIENT AFFILIATION |
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| ==SUBJECT:== | | ==SUBJECT:== |
| LER 90-002-00:on 900226,fire watch patrol hourly patrol performed in wrong areas due to'personnel error.W/9 DISTRIBUTION CODE: IE22T COPIES RECEIVED LTR ENCL SIZE: TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72). | | LER 90-002-00:on 900226,fire watch patrol hourly patrol performed in wrong areas due to'personnel error. |
| /05000244 RECIPIENT ID CODE/NAME PD1-3 LA JOHNSON,A INTERNAL: ACNW AEOD/DSP/TPAB DEDRO NRR/DET/EMEB9H3 NRR/DLPQ/LHFB11 NRR/DOEA/OEAB11 NRR/DST/SELB 8D D LB8D1 EG 02 RGN1 FILE 01 EXTERNAL: EG&G STUART, V.A LPDR NSIC MAYS,G NUDOCS FULL TXT COPIES LTTR ENCL 1 1 1 1 2 2 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 , 4 4 1 1 1 1 1 1 RECIPIENT ID CODE/NAME PD1-3 PD AEOD/DOA AEOD/ROAB/-DS P NRR/DET/ECMB 9H NRR/DET/ESGB 8D NRR/DLPQ/LPEB10 NRR/DREP/PRPB11 NRR/DST/SICB 7E NRR/DST/SRXB 8E RES/DSIR/EIB L ST LOBBY WARD NRC PDR NSIC MURPHY,G.A COPIES LTTR ENCL 1 1 1 1 2 2 1 1 1 1 1 1 2 2 1 1 1 1 1 1 1 1 1 1 1 1 D R D P>Vc Ps 72o>NOTE TO ALL"RIDS" RECIPIENTS'LEASE HELP US TO REDUCE WASTEl CONTACT~DOCUMENT CONSOL DESK, ROOM Pl-37 (EXT.20079)'IO ELIMINATE YOUR NAME FROM DISHUBVIION D D FULL TEXT, CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 35 ENCL 35 loam C, STATK ROCHESTER GAS AND ELECTRIC CORPORATION
| | W/9 DISTRIBUTION CODE: IE22T COPIES RECEIVED LTR ENCL SIZE: |
| ~89 EAST AVENUE, ROCHESTER, N.K 14649-0001 March 23, 1990 TEI.C>~ONf. | | TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc. / |
| Aec*cooa vie 546 2700 U.S.Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 | | NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72). 05000244 RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD1-3 LA 1 1 PD1-3 PD 1 1 D JOHNSON,A 1 1 INTERNAL: ACNW 2 2 AEOD/DOA 1 1 AEOD/DSP/TPAB 1 1 AEOD/ROAB/-DS P 2 2 DEDRO 1 1 NRR/DET/ECMB 9H 1 1 NRR/DET/EMEB9H3 1 1 NRR/DET/ESGB 8D 1 1 NRR/DLPQ/LHFB11 1 1 NRR/DLPQ/LPEB10 1 1 NRR/DOEA/OEAB11 1 1 NRR/DREP/PRPB11 2 2 NRR/DST/SELB 8D 1 1 NRR/DST/SICB 7E 1 1 D LB8D1 1 1 NRR/DST/SRXB 8E 1 1 EG 02 1 1 RES/DSIR/EIB 1 1 RGN1 FILE 01 1 1 EXTERNAL: EG&G STUART, V.A , 4 4 L ST LOBBY WARD 1 1 LPDR 1 1 NRC PDR 1 1 R NSIC MAYS,G 1 1 NSIC MURPHY,G.A 1 1 NUDOCS FULL TXT 1 1 D |
| | P>Vc Ps 72o > |
| | D D |
| | NOTE TO ALL "RIDS" RECIPIENTS'LEASE HELP US TO REDUCE WASTEl CONTACT ~ DOCUMENT CONSOL DESK, ROOM Pl-37 (EXT. 20079) 'IO ELIMINATEYOUR NAME FROM DISHUBVIION FULL TEXT, CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 35 ENCL 35 |
| | |
| | loam C, |
| | STATK ROCHESTER GAS AND ELECTRIC CORPORATION ~ 89 EAST AVENUE, ROCHESTER, N.K 14649-0001 TEI.C>~ONf. |
| | Aec* cooa vie 546 2700 March 23, 1990 U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 |
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| ==Subject:== | | ==Subject:== |
| LER 90-002, Fire Watch Patrol Performed Technical Specification Hourly Patrol in the Wrong Areas Due to Personnel Error.R.E.Ginna Nuclear Power Plant Docket: No.50-244 In accordance with 10CFR50.73, Licensee Event Report System, Item (a)(2)(i)(B), which requires reporting of<<Any Operation Or Condition Prohibited by the Plant's Technical Specifications", the attached Licensee Event Report LER 90-002 is being submitted. | | LER 90-002, Fire Watch Patrol Performed Technical Specification Hourly Patrol in the Wrong Areas Due to Personnel Error. |
| This LER is being submitted because an Hourly Fire Watch Patrol patrolled the wrong area and did not meet the Ginna Technical Specification 3.14 requirements for hourly patrol for two (2)Technical Specifications systems.This event in no way affected the public health and safety.Very truly yours, Robert C.Mec dy Division Manager Nuclear Production xc: U.S.Nuclear Regulatory Commission Region I 475 Allendale Road King of Prussia, PA 19406 Ginna USNRC Senior Resident Inspector 9004l30i8i 90032''PDR ADOCK 05000244 S PDC p4.0~ | | R. E. Ginna Nuclear Power Plant Docket: No. 50-244 In accordance with 10CFR50.73, Licensee Event Report System, Item (a)(2)(i)(B), which requires reporting of Specifications", |
| <<AC P>>>>S00>00II LICENSEE EVENT REPORT{LER)VS, NUCLSAA 1IOULATOAY COMMIHION APPAOVIO OMS HO.SI00 0IOV SXPIASS~0/Sll~S PACILITY HAMS III R.E.Ginna Nuclear Power Plant OOCXIT NVMSS1 QI 0 6 0 0 0 2 4 1OF 0 in the Wron Area D e r onnel Fire Watch Patrol Performed Technical Specification Hourly Patrol SYIHT OATS III LS1 HVM001 IM ASPOAT OATS III OTHIA PACILITISS INYOLYIO NI UO<<T<<O*Y YTAA YTA1~IOVI<<TIAL<<v<<PPA MVS~Mo<<I<<<<valPPA OAY YSAA~ACILITT<<AMLS OOCKIT HUMSSHISI 0 6 0 0 0 0 2 2 6 9 9 0 0 0 p pp 3 2 8 9 0 0 6 0 0 0 Ot I A AT I<<0 MOOS PPI PONS A LSVSL I I 0 I SOAOlltl S0.A00 li I I I I I I S0.4CO 4 I I I I I I I SOA004III IIMI So A00 4 I I I I l<<l S0.400 4 I II I lil IO.MHIil~0 004I III lOMIM Ql X 00.TS4IQIIU SO.TS4IQII | | <<Any Operation Or Condition Prohibited by the Plant's Technical the attached Licensee Event Report LER 90-002 is being submitted. |
| ~I l0.7 S 4 I Q I I M I LICSHSSI CONTACT toll TIIQ LS1 IISI~0, 1 S4)Q I I<<I~0.TSV IQIIPI 00.TS4IQllwl SOS S4 I QI I<<X IIAI l0.PS 4 I IS II>WII~I~0.T S41 Q lltl 0 Till AIOVI ASMIHTT Ot 14 Ct 1$i IO>>>t>><<>>>>>>P PP t>P Pttt<<>>ti Ill Tlllt ASPOAT IS IVAMITTSO WAPVA<<T T TLTIQI TS.)I10I OTHS1 ISttt<<P r A>>Y>>I~>>P<<P<<0 M PttL N1C I>>><<BASSA/"*"'ark E.Cavanaugh Fire Protection Engineer ANSA COOS TILSPHOHI HVLQl1 1 5 5 2 4 4 4 4 COMPLSTS ONS LINT POA SAC>i COMPO<<THY PAll V1S OIPCAISSO IH THQ 1IPO1T IISI CAUS S SYSTIM COMPOHINT MAHUPAC TVIIS1 IPONTASLS To HP1OS SYSTIM COMPO<<SHY MAHVP*O TU101 SPOHTASL TO HPOOS SjKa$~4>,&gg>>+'<<I
| | This LER is being submitted because an Hourly Fire Watch Patrol patrolled the wrong area and did not meet the Ginna Technical Specification 3.14 requirements for hourly patrol for two (2) |
| 'pe~>SQ4(:
| | Technical Specifications systems. |
| SVPPLIMLHTAL 1SPOAT SXPTCTlo II4I YSS III P>>.P>><<t<<N CXPSCTSO SVPVISSION OATSI<<0 ASSTAACT IIJ<<>H>>lt00 MW>>, I~., ttt>>i>>V>>it Nt>>t<<el~i~t Itre~<<>>A A~>>I ll~I SXPICTSO LVSMISSIOH OATS II II Rgb)"T>>.-." MONT<<CAY YCA1 On February 26, 1990, at approximately 1544 EST with the Reactor at approximately 98%, it was determined that the roving Fire Watch that was assigned to perform the hourly tours of the"A" and"B" Battery Rooms mistakenly performed the tours of the"A" and"B" Diesel Generator Rooms.The error was identified by the responsible Fire Watch during an afternoon pre-turnover meeting.Immediate action was to ensure an hourly patrol covered the"A" and"B" Battery Rooms.The cause of the event was determined to be personnel error by the assigned Fire Watch.Corrective action has been taken by the Fire Protection section by issuing a card to each individual performing a Technical Specifi-cation Fire Watch commitment, which identifies the area of their responsibility.
| | This event in no way affected the public health and safety. |
| N<<AC Pv>>S00 I}0SI
| | Very truly yours, Robert C. Mec dy Division Manager Nuclear Production xc: U. S. Nuclear Regulatory Commission Region I 475 Allendale Road King of Prussia, PA 19406 Ginna USNRC Senior Resident Inspector 9004l30i8i 90032'' |
| , I NRC Rerm 344A I444I LICENSEE EVENT REPORT{LER)TEXT CONTINUATION V.E.NUCLEAR REOULATORY COMMIEEION ARAROVEO OM4 40 5I50&IOI EXlrIRES EflII45 RACILITY NAME III OOCKET NVMEE R ITI LER NUMEER IEI SEOUE4TIAL i rlEYIEIO4 4@M ER 4IIM EA~AOE IEI R.E.Ginna Nuclear Power Plant TEXT Ih'rrrr roect R rRRrrnd.rrer aamonel HlK'rxrrr 444A'I I I IT)o so oo 244-0 0 2-0 0 02o~0 5 I.I IA PLA 0 T ON The plant was at approximately 98%steady state full power with no major activities in progress.II.DESCRIPTION 0 EVENT A.DATES AND APPROXIMATE TIMES FOR MAJOR OCCURRENCES: | | PDR S |
| February 26, 1990, 1544 EST: Discovery date and time.February 26, 1990, 1551 EST: Fire Watch correctly performed hourly patrol of"A" and"B" Battery Rooms, in compliance'ith Technical Specif ications.February 26, 1990, 1744 EST: Fire Detection System which was inoperable due to construction activities was restored to service, B.EVENT: C.On February 26, 1990, at approximately 1544 EST with the Reactor at approximately 98%full power, it was determined.by the Fire Watch Patrol that she was touring the"A" and"B" Diesel Generator Rooms instead of the"A" and"B" Battery Rooms, On February 26, 1990, at approximately 1551 EST, a Fire Watch was sent to the"A" and"B" Battery Rooms to perform the hourly tour.INOPERABLE STRUCTURES,.
| | ADOCK 05000244 PDC p4.0~ |
| COMPONENTS OR SYSTEM THAT CONTRIBUTED TO THE EVENT: Inoperable Fire Detection System-Pyrotronics VRC AORM 544A I443I NRC So<~944A I945I LICENSEE EVENT REPORT (LERI TEXT CONTINUATION V.S.NUCLEAR REOULATORY COMMISSION AFSROVEO OM4 NO 5150&IOC EXPIRES 4/SI/45 FACILITY NAME I11 OOCKET NVM'4ER IEI YEAR LER NIJM4ER IEI SSQV IN>>AL" REVISION~4VM CR-VVV CA~AOE ISI R.E.Ginna Nuclear Power Plant TEXT 0Smcvc NMCC N CCtvnd.vcc ccRF4+w'HRC Ann PSA'cc lltl o s o o o 4 4 9 0 0 0 2-0 0 03 OF D.OTHER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED: None E.'ETHOD OF DISCOVERY:
| | |
| This event was discovered by the responsible Fire Watch during an afternoon turn-over meeting.F.OPERATOR ACTION: The control'oom operators were notified by the Safety Coordinator at which time they performed the following:
| | <<AC P>>>> S00 VS, NUCLSAA 1IOULATOAYCOMMIHION |
| Initiated an A-25.1'Stat't e o t Notified Duty Engineer Notified Shift Technical Advisor (STA)Notified Plant Superintendent Notified Nuclear Regulatory Commission Resident Inspector G.SAFETY SYSTEM RESPONSES:
| | >00II APPAOVIO OMS HO. SI00 0IOV LICENSEE EVENT REPORT {LER) SXPIASS ~ 0/Sll ~ S PACILITY HAMS III OOCXIT NVMSS1 QI R. E. Ginna Nuclear Power Plant 0 6 0 0 0 2 4 1OF 0 Fire Watch Patrol Performed Technical Specification Hourly Patrol in the IIIWron Area D e SYIHT OATS LS1 HVM001 IM r onnelIII ASPOAT OATS OTHIA PACILITISS INYOLYIO NI IOVI<<TIAL MVS~ ACILITT<<AMLS OOCKIT HUMSSHISI |
| None III.CAUSE OF EVENT A.IMMEDIATE CAUSE: Technical Specifications fire detection system was not Fire Watch toured hourly.B.ROOT CAUSE: The root cause was determined to be unintentional human error.IV.ALYSIS OF EVENT Hourly Fire Watch tours of two (2)Technical Specifications areas with inoperable fire detection systems were not conducted so Technical Specifications 3.14.1 and 3.14.1.1 were not met.This event is reportable in accordance with 10CFR50.73, Licensee Event Report System, Item (a)(2)(i)(B), which requires reporting of,"Any Operation Or Condition Prohibited by the Plant's Technical Specifications".
| | <<valPPA Mo<< I<< |
| NRC FORM 544A l94SI HAC SM~444A i44)I LICENSEE E ENT'REPORT ILER)TEXT CONTINUA N V 4.HVC44*II IIIOVlATOIIY COMMI44IOH ATMOV40 OM4 HO 4I40&IOl 4XAH44.4QI44 SACIllTY HAM4 III COCK T 7 HVM44A ITI I,4A HVM44H I4I~44OVIHTtkl, 1 AIVISIO<1~AOI I4I R.E.Ginna Nuclear Power Plant TEXT W mOn HMTT H nouns YM~HAC~JNA'II I IT I oIs o o o 44 9 0-0 0 2-0 0 0 40F An assessment was performed considering the safety of this event with the following results and conclusions:
| | ~ |
| There were no operational or, safety consequences or implica-tions attributed to the inoperable fire detection system because: Inoperable Fire Detection System>>A>>Battery Room: The fire area for the TTA>>Battery Room has a maximum permissible fire load of 160,000 BTU's/Sq.Ft.with an actual fire load of 44,021 BTU's/Sq.Ft.
| | UO<<T<<O*Y YTAA YTA1 ~ |
| The actual fire load of 44,021 BTU's/Sq.Ft. | | <<v<<PPA OAY YSAA 0 6 0 0 0 0 2 2 6 9 9 0 0 0 p pp 3 2 8 9 0 0 6 0 0 0 Tlllt ASPOAT IS IVAMITTSO WAPVA<<T T 0 Till AIOVIASMIHTT Ot 14 Ct 1 $ i IO>>>t >><<>>>>>>P PP t>P Pttt<<>>ti Ill Ot I AATI <<0 MOOS PPI SOAOlltl IO.MHIil ~ 0, 1 S4)Q I I<<I TLTIQI PONS A S0. A00 liII I II I ~ 0 004I III ~ 0.TSV IQIIPI TS.)I10I LSVSL OTHS1 ISttt<<P r A>>Y>>I II0 I S0.4CO 4 II I I I II lOMIMQl 00.TS4IQllwl |
| is considered low (<80,000 BTU's/Sq.Ft.). | | ~ >>P<<P<<0 M PttL N1C I>>><< |
| The wall separating the>>A>>Battery Room from the Turbine Building is a2 hour rated wall.The wall , separating the>>A>>Battery.Room from the>>B>>Battery Room is a 2 hour rated wall.The wall separating the>>A>>Battery Room from the Air.Handling Room is a 2 hour rated wall.Inoperable Fire Detection System>>B>>Battery Room: The fire area for the>>B>>Battery Room has a maximum permissible fire load of 160,000 BTU's/Sq.Ft. | | SOA004III IIMI X 00.TS4IQIIU SOS S4 I QI I<<XIIAI BASSA/ |
| with an actual fire load of 52,656 BTU's/Sq.Ft.
| | So A00 4 II I I l<<l SO.TS4IQII ~ I l0.PS 4 I IS II>WII~ I S0.400 4 I II I lil l0.7 S 4 I Q II M I ~ 0.T S41 Q lltl LICSHSSI CONTACT toll TIIQ LS1 IISI |
| The actual fire load of 52,656 BTU's/Sq.Ft.
| | "*"'ark E. Cavanaugh ANSA COOS TILSPHOHI HVLQl1 Fire Protection Engineer 1 5 5 2 4 4 4 4 COMPLSTS ONS LINT POA SAC>i COMPO<<THY PAll V1S OIPCAISSO IH THQ 1IPO1T IISI IPONTASLS MAHVP*O SPOHTASL SjKa$ ~4>,&gg>>+'<<I MAHUPAC SYSTIM COMPO<<SHY CAUS S SYSTIM COMPOHINT TVIIS1 To HP1OS TU101 TO HPOOS 'pe~>SQ4(: |
| is considered low(<80,000 BTU's/Sq.Ft.).
| | Rgb)"T>>. -." |
| The wall separating the>>B>>Battery Room from the Turbine Building is a 2 hour rated wall.The wall separating the>>B>>Battery Room from the>>A>>Battery Room is a 2 hour rated wall.These two fire areas/zones (BR1A-1 and BR1B-1)have fire extinguishing equipment within the area and there are hose stations adjacent to them.The fire detection system for the area adjacent to the>>A>>and"B>>Battery Room in the Turbine Building basement,was operable.The fire suppression system for the area adjacent to the>>A>>Battery Room in the Air Handling Room was operable.
| | SVPPLIMLHTAL 1SPOAT SXPTCTlo II4I MONT<<CAY YCA1 SXPICTSO LVSMISSIOH OATS II II YSS IIIP>>. P>><<t<<N CXPSCTSO SVPVISSION OATSI <<0 ASSTAACT IIJ<<>H>> lt00 MW>>, I ~ ., ttt>>i>>V>>it Nt>>t<< el~i~t Itre~<<>>A A~>>I ll~ I On February 26, 1990, at approximately 1544 EST with the Reactor at approximately 98%, |
| V NRC fWm 99EA (949 I LICENSEE EVENT REPORT (LER)TEXT CONTINUATION U.E.NUCLEAR RlOULATORY COMM)El)ON AttROVEO OM9 NO 5)50&)0e EXtlRES<9/5)/95 tACI(.I'TY NAME (1)OOCXET NUMEER CI)LER NUMEER (9)eeQI/ENTIAL M R.N.~REVISION Ie>>~AOE (9)R.E.Ginna Nuclear Power Plant 0 s 0 0 o 4 4 TExT///mme etece N nqvwaf.tee e)99(eN/HRC te/m~'I/(IT)9 0 0 0 2 0 0 05oF0 No work was performed in either of the<<A<<or<<B<<Battery Rooms.Based on the above, it can be c'oncluded that the public's health and safety was assured at all times.i V., CORRECTIVE ACTION A.ACTION TAKEN TO RETURN INOPERABLE FIRE DETECTION SYSTEM TO OPERABLE STATUS: Fire System reconnect was performed under plant procedure SC-3.16.2.4
| | Watch that was assigned to perform the hourly tours of the "A" it was determined that the roving Fire and "B" Battery Rooms mistakenly performed the tours of the "A" and "B" Diesel Generator Rooms. The error was identified by the responsible Fire Watch during an afternoon pre-turnover meeting. |
| 're S'S s e Co-o t isco ct'o-o e System declared operable on February 26, 1990 at 1744 EST.B.-ACTION TAKEN OR PLANNED TO PREVENT RECURRENCE:
| | Immediate action was to ensure an hourly patrol covered the "A" and "B" Battery Rooms. |
| As the root cause was determined to be a personnel error, the Fire Watch Supervisor has been instructed to follow-up the assignments given to fire watches to ensure they are going to the right area.Index cards have also been issued to the Fire Watch to ensure they have written instructions on where their patrols are to be conducted.
| | The cause of the event was determined to be personnel error by the assigned Fire Watch. |
| VI.ADDITIONAL INFORMATION A.B.FAILED COMPONENTS:
| | Corrective action has been taken by the Fire Protection section by issuing a card to each individual performing a Technical Specifi-cation Fire Watch commitment, which identifies the area of their responsibility. N |
| None PREVIOUS LER'S ON SIMILAR EVENTS: A similar LER event historical search was conducted with the following results;No documentation of similar LER events with the same root cause at Ginna Station could be identified.
| | <<AC Pv>> S00 I}0SI |
| C.SPECIAL COMMENTS: During the five (5)hours in which the assigned Fire Watch inspected the incorrect area, Security entered the area of concern ten (10)times.NRC tORM 99EA)9451}}
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| | , |
| | I NRC Rerm 344A V.E. NUCLEAR REOULATORY COMMIEEION I444I LICENSEE EVENT REPORT {LER) TEXT CONTINUATION ARAROVEO OM4 40 5I50&IOI EXlrIRES EflII45 RACILITY NAME III OOCKET NVMEE R ITI LER NUMEER IEI ~ AOE IEI SEOUE4TIAL i rlEYIEIO4 4@M ER 4IIM EA R. E. Ginna Nuclear Power Plant o so TEXT Ih'rrrr roect R rRRrrnd. rrer aamonel HlK'rxrrr444A'I I I IT) oo 244 0 0 2 0 0 02o~ 0 5 I. I IA PLA 0 T ON The plant was at approximately 98% steady state full power with no major activities in progress. |
| | II. DESCRIPTION 0 EVENT A. DATES AND APPROXIMATE TIMES FOR MAJOR OCCURRENCES: |
| | February 26, 1990, 1544 EST: Discovery date and time. |
| | February 26, 1990, 1551 EST: Fire Watch correctly performed hourly patrol of "A" and "B" Battery Rooms, in compliance'ith Technical Specif ications. |
| | February 26, 1990, 1744 EST: Fire Detection System which was inoperable due to construction activities was restored to service, B. EVENT: |
| | On February 26, 1990, at approximately 1544 EST with the Reactor at approximately 98% full power, it was determined .by the Fire Watch Patrol that she was touring the "A" and "B" Diesel Generator Rooms instead of the "A" and "B" Battery Rooms, On February 26, 1990, at approximately 1551 EST, a Fire Watch was sent to the "A" and "B" Battery Rooms to perform the hourly tour. |
| | C. INOPERABLE STRUCTURES,. COMPONENTS OR SYSTEM THAT CONTRIBUTED TO THE EVENT: |
| | Inoperable Fire Detection System - Pyrotronics VRC AORM 544A I443I |
| | |
| | NRC So<~ 944A V.S. NUCLEAR REOULATORY COMMISSION I945I LICENSEE EVENT REPORT (LERI TEXT CONTINUATION AFSROVEO OM4 NO 5150&IOC EXPIRES 4/SI/45 FACILITY NAME I11 OOCKET NVM'4ER IEI ~ AOE LER NIJM4ER IEI ISI YEAR SSQV IN>>AL " REVISION |
| | ~ 4VM CR - VVV CA R. E. Ginna Nuclear Power Plant o s o o o 4 4 9 0 0 0 2 0 0 03 OF TEXT 0Smcvc NMCC N CCtvnd. vcc ccRF4+w'HRC Ann PSA'cc lltl D. OTHER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED: |
| | None E. 'ETHOD OF DISCOVERY: |
| | This event was discovered by the responsible Fire Watch during an afternoon turn-over meeting. |
| | F. OPERATOR ACTION: |
| | The control'oom operators were notified by the Safety Coordinator at which time they performed the following: |
| | Initiated an A-25.1 ' |
| | Notified Duty Engineer Stat' t e o t Notified Shift Technical Advisor (STA) |
| | Notified Plant Superintendent Notified Nuclear Regulatory Commission Resident Inspector G. SAFETY SYSTEM RESPONSES: |
| | None III. CAUSE OF EVENT A. IMMEDIATE CAUSE: |
| | Technical Specifications fire detection system was not Fire Watch toured hourly. |
| | B. ROOT CAUSE: |
| | The root cause was determined to be unintentional human error. |
| | IV. ALYSIS OF EVENT Hourly Fire Watch tours of two (2) Technical Specifications areas with inoperable fire detection systems were not conducted so Technical Specifications 3.14.1 and 3.14.1.1 were not met. This event is reportable in accordance with 10CFR50.73, Licensee Event Report System, Item (a)(2)(i)(B), |
| | which requires reporting of, "Any Operation Or Condition Prohibited by the Plant's Technical Specifications". |
| | NRC FORM 544A l94SI |
| | |
| | HAC SM~ 444A V 4. HVC44*II IIIOVlATOIIYCOMMI44IOH i44) I LICENSEE E ENT'REPORT ILER) TEXT CONTINUA N ATMOV40 OM4 HO 4I40&IOl 4XAH44. 4QI44 SACIllTY HAM4 III COCK T 7 HVM44A ITI I,4A HVM44H I4I ~ AOI I4I |
| | ~ 44OVIHTtkl, AIVISIO< |
| | 1 1 R. E. Ginna TEXT W mOn HMTT H nouns YM ~ |
| | Nuclear Power Plant oIs HAC ~ JNA'II I IT I o o o 44 9 0 0 0 20 0 0 40F An assessment was performed considering the safety of this event with the following results and conclusions: |
| | There were no operational or, safety consequences or implica-tions attributed to the inoperable fire detection system because: |
| | Inoperable Fire Detection System >>A>> Battery Room: |
| | The fire area for the TTA>> Battery Room has a maximum permissible fire load of 160,000 BTU's/Sq. |
| | Ft. with an actual fire load of 44,021 BTU's/Sq.Ft. |
| | The actual fire load of 44,021 BTU's/Sq.Ft. is considered low (<80,000 BTU's/Sq.Ft.). The wall separating the >>A>> Battery Room from the Turbine Building is a 2 hour rated wall. The wall separating the >>A>> Battery .Room from the >>B>> |
| | is wall. |
| | , |
| | Battery Room a 2 hour rated The wall separating the >>A>> Battery Room from the Air |
| | . Handling Room is a 2 hour rated wall. |
| | Inoperable Fire Detection System >>B>> Battery Room: |
| | The fire area for the >>B>> Battery Room has a maximum permissible fire load of 160,000 BTU's/Sq.Ft. with an actual fire load of 52,656 BTU's/Sq.Ft. The actual fire load of 52,656 BTU's/Sq.Ft. is considered low(<80,000 BTU's/Sq.Ft.). The wall separating the >>B>> |
| | Battery Room from the Turbine Building is a 2 hour rated wall. The wall separating the >>B>> Battery Room from the >>A>> Battery Room is a 2 hour rated wall. |
| | These two fire areas/zones (BR1A-1 and BR1B-1) have fire extinguishing equipment within the area and there are hose stations adjacent to them. |
| | The fire detection system for the area adjacent to the >>A>> and "B>> Battery Room in the Turbine Building basement,was operable. |
| | The fire>>A>>suppression system for the area adjacent to the Battery Room in the Air Handling Room was operable. |
| | |
| | V NRC fWm 99EA U.E. NUCLEAR RlOULATORY COMM)El)ON (949 I LICENSEE EVENT REPORT (LER) TEXT CONTINUATION AttROVEO OM9 NO 5)50&)0e EXtlRES< 9/5) /95 tACI(.I'TY NAME (1) OOCXET NUMEER CI) LER NUMEER (9) ~ AOE (9) eeQI/ENTIAL .N.~ REVISION M R Ie>> |
| | R. E. Ginna Nuclear Power Plant 0 s 0 0 o 4 4 9 0 0 0 2 0 0 05oF0 TExT /// mme etece N nqvwaf. tee e)99(eN/ HRC te/m ~'I/ (IT) |
| | No work was performed in either of the <<A<< or <<B<< |
| | Battery Rooms. |
| | Based on the above, it health and safety was assured at all times. |
| | can be c'oncluded that the public's i |
| | V. , CORRECTIVE ACTION A. ACTION TAKEN TO RETURN INOPERABLE FIRE DETECTION SYSTEM TO OPERABLE STATUS: |
| | Fire System reconnect was performed under plant procedure SC-3.16.2.4 're S' S s e Co-o t isco ct'o o e System declared operable on February 26, 1990 at 1744 EST. |
| | B. - ACTION TAKEN OR PLANNED TO PREVENT RECURRENCE: |
| | As the root cause was determined to be a personnel error, the Fire Watch Supervisor has been instructed to follow-up the assignments given to fire watches to ensure they are going to the right area. Index cards have also been issued to the Fire Watch to ensure they have written instructions on where their patrols are to be conducted. |
| | VI. ADDITIONAL INFORMATION A. FAILED COMPONENTS: |
| | None B. PREVIOUS LER'S ON SIMILAR EVENTS: |
| | A similar LER event historical search was conducted with the following results; No documentation of similar LER events with the same root cause at Ginna Station could be identified. |
| | C. SPECIAL COMMENTS: |
| | During the five (5) hours in which the assigned Fire Watch inspected the incorrect area, Security entered the area of concern ten (10) times. |
| | NRC tORM 99EA |
| | )9451}} |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:RO)
MONTHYEARML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17265A7601999-10-0505 October 1999 Part 21 Rept Re W2 Switch Supplied by W Drawn from Stock, Did Not Operate Properly After Being Installed on 990409. Switch Returned to W on 990514 for Evaluation & Root Cause Analysis ML17265A7621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Re Ginna Npp.With 991008 Ltr ML17265A7531999-09-23023 September 1999 Part 21 Rept Re Corrective Action & Closeout of 10CFR21 Rept of Noncompliance Re Unacceptable Part for 30-4 Connector. Unacceptable Parts Removed from Stock & Scrapped ML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7471999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Re Ginna Npp.With 990909 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7341999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Re Ginna Npp.With 990806 Ltr ML17265A7291999-07-29029 July 1999 Interim Part 21 Rept Re safety-related DB-25 Breaker Mechanism Procured from W Did Not Pas Degradatin Checks When Drawn from Stock to Be Installed Into BUS15/03A.Holes Did Not line-up & Tripper Pan Bent ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7131999-07-22022 July 1999 Special Rept:On 990407,radiation Monitor RM-14A Was Declared Inoperable.Caused by Failed Communication Link from TSC to Plant Process Computer Sys.Communication Link Was re-established & RM-14A Was Declaed Operable on 990521 ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7211999-07-19019 July 1999 ISI Rept for Third Interval (1990-1999) Third Period, Second Outage (1999) at Re Ginna Npp. ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A7661999-06-30030 June 1999 1999 Rept of Facility Changes,Tests & Experiments Conducted Without Prior NRC Approval for Jan 1998 Through June 1999, Per 10CFR50.59.With 991020 Ltr ML17265A7011999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Re Ginna Npp.With 990712 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6761999-06-16016 June 1999 Part 21 Rept Re Defects & noncompliances,10CFR21(d)(3)(ii), Which Requires Written Notification to NRC on Identification of Defect or Failure to Comply. Relays Were Returned to Eaton for Evaluation & Root Cause Analysis ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17265A6681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Re Ginna Nuclear Power Plant.With 990608 Ltr ML17265A6651999-05-27027 May 1999 Interim Rept Re W2 Control Switch,Procured from W,Did Not Operate Satisfactorily When Drawn from Stock to Be Installed in Main Control Board for 1C2 Safety Injection Pump. Estimated That Evaluation Will Be Completed by 991001 ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6591999-05-17017 May 1999 Part 21 Rept Re Relay Deficiency Detected During pre-installation Testing.Caused by Incorrectly Wired Relay Coil.Relays Were Returned to Eaton Corp for Investigation. Relays Were Repaired & Retested ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6381999-05-0707 May 1999 Part 21 Rept Re Replacement Turbocharger Exhaust Turbine Side Drain Port Not Functioning as Design Intended.Caused by Manufacturing Deficiency.Turbocharger Was Reaasembled & Reinstalled on B EDG ML17265A6391999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Re Ginna Nuclear Power Plant.With 990510 Ltr ML17265A6361999-04-23023 April 1999 Part 21 Rept Re Power Supply That Did Not Work Properly When Drawn from Stock & Installed in -25 Vdc Slot.Power Supply Will Be Sent to Vendor to Perform Failure Mode Assessment.Evaluation Will Be Completed by 991001 ML17265A6301999-04-18018 April 1999 Rev 1 to Cycle 28 COLR for Re Ginna Npp. ML17265A6251999-04-15015 April 1999 Special Rept:On 990309,halon Systems Were Removed from Svc & Fire Door F502 Was Blocked Open.Caused by Mods Being Made to CR Emergency Air Treatment Sys.Continuous Fire Watch Was Established with Backup Fire Suppression Equipment ML17265A6551999-04-0909 April 1999 Initial Part 21 Rept Re Mfg Deficiency in Replacement Turbocharger for B EDG Supplied by Coltec Industries. Deficiency Consisted of Missing Drain Port in Intermediate Casing.Required Oil Drain Port Machined Open ML17265A6291999-03-31031 March 1999 Rev 0 to Cycle 28 COLR for Re Ginna Npp. ML17265A6241999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Ginna Station.With 990409 Ltr ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A5661999-03-0101 March 1999 Rev 26 to QA Program for Station Operation. ML17265A5961999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Ginna Nuclear Power Plant.With 990310 Ltr ML17265A5371999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Re Ginna Nuclear Power Plant.With 990205 Ltr ML17265A5951998-12-31031 December 1998 Rg&E 1998 Annual Rept. ML17265A5001998-12-21021 December 1998 Rev 26 to QA Program for Station Operation. ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4761998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Re Ginna Nuclear Power Plant.With 981210 Ltr ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4531998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Re Ginna Nuclear Power Plant.With 981110 Ltr ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A4291998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Re Ginna Nuclear Power Plant.With 981009 Ltr 1999-09-30
[Table view] |
Text
ACCELERATE UTION DEMONSATION SYSIEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:9004130181 DOC DATE: 90/03/28 NOTARIZED: NO DOCKET FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester G 05000244 AUTH. NAME AUTHOR AFFILIATION CAVANAUGH,M.E. Rochester Gas & Electric Corp.
MECREDY,R.C. Rochester Gas & Electric Corp.
RECIP.NAME RECIPIENT AFFILIATION
SUBJECT:
LER 90-002-00:on 900226,fire watch patrol hourly patrol performed in wrong areas due to'personnel error.
W/9 DISTRIBUTION CODE: IE22T COPIES RECEIVED LTR ENCL SIZE:
TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc. /
NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72). 05000244 RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD1-3 LA 1 1 PD1-3 PD 1 1 D JOHNSON,A 1 1 INTERNAL: ACNW 2 2 AEOD/DOA 1 1 AEOD/DSP/TPAB 1 1 AEOD/ROAB/-DS P 2 2 DEDRO 1 1 NRR/DET/ECMB 9H 1 1 NRR/DET/EMEB9H3 1 1 NRR/DET/ESGB 8D 1 1 NRR/DLPQ/LHFB11 1 1 NRR/DLPQ/LPEB10 1 1 NRR/DOEA/OEAB11 1 1 NRR/DREP/PRPB11 2 2 NRR/DST/SELB 8D 1 1 NRR/DST/SICB 7E 1 1 D LB8D1 1 1 NRR/DST/SRXB 8E 1 1 EG 02 1 1 RES/DSIR/EIB 1 1 RGN1 FILE 01 1 1 EXTERNAL: EG&G STUART, V.A , 4 4 L ST LOBBY WARD 1 1 LPDR 1 1 NRC PDR 1 1 R NSIC MAYS,G 1 1 NSIC MURPHY,G.A 1 1 NUDOCS FULL TXT 1 1 D
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NOTE TO ALL "RIDS" RECIPIENTS'LEASE HELP US TO REDUCE WASTEl CONTACT ~ DOCUMENT CONSOL DESK, ROOM Pl-37 (EXT. 20079) 'IO ELIMINATEYOUR NAME FROM DISHUBVIION FULL TEXT, CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 35 ENCL 35
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STATK ROCHESTER GAS AND ELECTRIC CORPORATION ~ 89 EAST AVENUE, ROCHESTER, N.K 14649-0001 TEI.C>~ONf.
Aec* cooa vie 546 2700 March 23, 1990 U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555
Subject:
LER 90-002, Fire Watch Patrol Performed Technical Specification Hourly Patrol in the Wrong Areas Due to Personnel Error.
R. E. Ginna Nuclear Power Plant Docket: No. 50-244 In accordance with 10CFR50.73, Licensee Event Report System, Item (a)(2)(i)(B), which requires reporting of Specifications",
<<Any Operation Or Condition Prohibited by the Plant's Technical the attached Licensee Event Report LER 90-002 is being submitted.
This LER is being submitted because an Hourly Fire Watch Patrol patrolled the wrong area and did not meet the Ginna Technical Specification 3.14 requirements for hourly patrol for two (2)
Technical Specifications systems.
This event in no way affected the public health and safety.
Very truly yours, Robert C. Mec dy Division Manager Nuclear Production xc: U. S. Nuclear Regulatory Commission Region I 475 Allendale Road King of Prussia, PA 19406 Ginna USNRC Senior Resident Inspector 9004l30i8i 90032
PDR S
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"*"'ark E. Cavanaugh ANSA COOS TILSPHOHI HVLQl1 Fire Protection Engineer 1 5 5 2 4 4 4 4 COMPLSTS ONS LINT POA SAC>i COMPO<<THY PAll V1S OIPCAISSO IH THQ 1IPO1T IISI IPONTASLS MAHVP*O SPOHTASL SjKa$ ~4>,&gg>>+'<<I MAHUPAC SYSTIM COMPO<<SHY CAUS S SYSTIM COMPOHINT TVIIS1 To HP1OS TU101 TO HPOOS 'pe~>SQ4(:
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SVPPLIMLHTAL 1SPOAT SXPTCTlo II4I MONT<<CAY YCA1 SXPICTSO LVSMISSIOH OATS II II YSS IIIP>>. P>><<t<<N CXPSCTSO SVPVISSION OATSI <<0 ASSTAACT IIJ<<>H>> lt00 MW>>, I ~ ., ttt>>i>>V>>it Nt>>t<< el~i~t Itre~<<>>A A~>>I ll~ I On February 26, 1990, at approximately 1544 EST with the Reactor at approximately 98%,
Watch that was assigned to perform the hourly tours of the "A" it was determined that the roving Fire and "B" Battery Rooms mistakenly performed the tours of the "A" and "B" Diesel Generator Rooms. The error was identified by the responsible Fire Watch during an afternoon pre-turnover meeting.
Immediate action was to ensure an hourly patrol covered the "A" and "B" Battery Rooms.
The cause of the event was determined to be personnel error by the assigned Fire Watch.
Corrective action has been taken by the Fire Protection section by issuing a card to each individual performing a Technical Specifi-cation Fire Watch commitment, which identifies the area of their responsibility. N
<<AC Pv>> S00 I}0SI
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I NRC Rerm 344A V.E. NUCLEAR REOULATORY COMMIEEION I444I LICENSEE EVENT REPORT {LER) TEXT CONTINUATION ARAROVEO OM4 40 5I50&IOI EXlrIRES EflII45 RACILITY NAME III OOCKET NVMEE R ITI LER NUMEER IEI ~ AOE IEI SEOUE4TIAL i rlEYIEIO4 4@M ER 4IIM EA R. E. Ginna Nuclear Power Plant o so TEXT Ih'rrrr roect R rRRrrnd. rrer aamonel HlK'rxrrr444A'I I I IT) oo 244 0 0 2 0 0 02o~ 0 5 I. I IA PLA 0 T ON The plant was at approximately 98% steady state full power with no major activities in progress.
II. DESCRIPTION 0 EVENT A. DATES AND APPROXIMATE TIMES FOR MAJOR OCCURRENCES:
February 26, 1990, 1544 EST: Discovery date and time.
February 26, 1990, 1551 EST: Fire Watch correctly performed hourly patrol of "A" and "B" Battery Rooms, in compliance'ith Technical Specif ications.
February 26, 1990, 1744 EST: Fire Detection System which was inoperable due to construction activities was restored to service, B. EVENT:
On February 26, 1990, at approximately 1544 EST with the Reactor at approximately 98% full power, it was determined .by the Fire Watch Patrol that she was touring the "A" and "B" Diesel Generator Rooms instead of the "A" and "B" Battery Rooms, On February 26, 1990, at approximately 1551 EST, a Fire Watch was sent to the "A" and "B" Battery Rooms to perform the hourly tour.
C. INOPERABLE STRUCTURES,. COMPONENTS OR SYSTEM THAT CONTRIBUTED TO THE EVENT:
Inoperable Fire Detection System - Pyrotronics VRC AORM 544A I443I
NRC So<~ 944A V.S. NUCLEAR REOULATORY COMMISSION I945I LICENSEE EVENT REPORT (LERI TEXT CONTINUATION AFSROVEO OM4 NO 5150&IOC EXPIRES 4/SI/45 FACILITY NAME I11 OOCKET NVM'4ER IEI ~ AOE LER NIJM4ER IEI ISI YEAR SSQV IN>>AL " REVISION
~ 4VM CR - VVV CA R. E. Ginna Nuclear Power Plant o s o o o 4 4 9 0 0 0 2 0 0 03 OF TEXT 0Smcvc NMCC N CCtvnd. vcc ccRF4+w'HRC Ann PSA'cc lltl D. OTHER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED:
None E. 'ETHOD OF DISCOVERY:
This event was discovered by the responsible Fire Watch during an afternoon turn-over meeting.
F. OPERATOR ACTION:
The control'oom operators were notified by the Safety Coordinator at which time they performed the following:
Initiated an A-25.1 '
Notified Duty Engineer Stat' t e o t Notified Shift Technical Advisor (STA)
Notified Plant Superintendent Notified Nuclear Regulatory Commission Resident Inspector G. SAFETY SYSTEM RESPONSES:
None III. CAUSE OF EVENT A. IMMEDIATE CAUSE:
Technical Specifications fire detection system was not Fire Watch toured hourly.
B. ROOT CAUSE:
The root cause was determined to be unintentional human error.
IV. ALYSIS OF EVENT Hourly Fire Watch tours of two (2) Technical Specifications areas with inoperable fire detection systems were not conducted so Technical Specifications 3.14.1 and 3.14.1.1 were not met. This event is reportable in accordance with 10CFR50.73, Licensee Event Report System, Item (a)(2)(i)(B),
which requires reporting of, "Any Operation Or Condition Prohibited by the Plant's Technical Specifications".
NRC FORM 544A l94SI
HAC SM~ 444A V 4. HVC44*II IIIOVlATOIIYCOMMI44IOH i44) I LICENSEE E ENT'REPORT ILER) TEXT CONTINUA N ATMOV40 OM4 HO 4I40&IOl 4XAH44. 4QI44 SACIllTY HAM4 III COCK T 7 HVM44A ITI I,4A HVM44H I4I ~ AOI I4I
~ 44OVIHTtkl, AIVISIO<
1 1 R. E. Ginna TEXT W mOn HMTT H nouns YM ~
Nuclear Power Plant oIs HAC ~ JNA'II I IT I o o o 44 9 0 0 0 20 0 0 40F An assessment was performed considering the safety of this event with the following results and conclusions:
There were no operational or, safety consequences or implica-tions attributed to the inoperable fire detection system because:
Inoperable Fire Detection System >>A>> Battery Room:
The fire area for the TTA>> Battery Room has a maximum permissible fire load of 160,000 BTU's/Sq.
Ft. with an actual fire load of 44,021 BTU's/Sq.Ft.
The actual fire load of 44,021 BTU's/Sq.Ft. is considered low (<80,000 BTU's/Sq.Ft.). The wall separating the >>A>> Battery Room from the Turbine Building is a 2 hour2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> rated wall. The wall separating the >>A>> Battery .Room from the >>B>>
is wall.
,
Battery Room a 2 hour rated The wall separating the >>A>> Battery Room from the Air
. Handling Room is a 2 hour2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> rated wall.
Inoperable Fire Detection System >>B>> Battery Room:
The fire area for the >>B>> Battery Room has a maximum permissible fire load of 160,000 BTU's/Sq.Ft. with an actual fire load of 52,656 BTU's/Sq.Ft. The actual fire load of 52,656 BTU's/Sq.Ft. is considered low(<80,000 BTU's/Sq.Ft.). The wall separating the >>B>>
Battery Room from the Turbine Building is a 2 hour2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> rated wall. The wall separating the >>B>> Battery Room from the >>A>> Battery Room is a 2 hour2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> rated wall.
These two fire areas/zones (BR1A-1 and BR1B-1) have fire extinguishing equipment within the area and there are hose stations adjacent to them.
The fire detection system for the area adjacent to the >>A>> and "B>> Battery Room in the Turbine Building basement,was operable.
The fire>>A>>suppression system for the area adjacent to the Battery Room in the Air Handling Room was operable.
V NRC fWm 99EA U.E. NUCLEAR RlOULATORY COMM)El)ON (949 I LICENSEE EVENT REPORT (LER) TEXT CONTINUATION AttROVEO OM9 NO 5)50&)0e EXtlRES< 9/5) /95 tACI(.I'TY NAME (1) OOCXET NUMEER CI) LER NUMEER (9) ~ AOE (9) eeQI/ENTIAL .N.~ REVISION M R Ie>>
R. E. Ginna Nuclear Power Plant 0 s 0 0 o 4 4 9 0 0 0 2 0 0 05oF0 TExT /// mme etece N nqvwaf. tee e)99(eN/ HRC te/m ~'I/ (IT)
No work was performed in either of the <<A<< or <<B<<
Battery Rooms.
Based on the above, it health and safety was assured at all times.
can be c'oncluded that the public's i
V. , CORRECTIVE ACTION A. ACTION TAKEN TO RETURN INOPERABLE FIRE DETECTION SYSTEM TO OPERABLE STATUS:
Fire System reconnect was performed under plant procedure SC-3.16.2.4 're S' S s e Co-o t isco ct'o o e System declared operable on February 26, 1990 at 1744 EST.
B. - ACTION TAKEN OR PLANNED TO PREVENT RECURRENCE:
As the root cause was determined to be a personnel error, the Fire Watch Supervisor has been instructed to follow-up the assignments given to fire watches to ensure they are going to the right area. Index cards have also been issued to the Fire Watch to ensure they have written instructions on where their patrols are to be conducted.
VI. ADDITIONAL INFORMATION A. FAILED COMPONENTS:
None B. PREVIOUS LER'S ON SIMILAR EVENTS:
A similar LER event historical search was conducted with the following results; No documentation of similar LER events with the same root cause at Ginna Station could be identified.
C. SPECIAL COMMENTS:
During the five (5) hours in which the assigned Fire Watch inspected the incorrect area, Security entered the area of concern ten (10) times.
NRC tORM 99EA
)9451