ML19309H661: Difference between revisions

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Latest revision as of 20:55, 21 February 2020

LER 80-035/01T-0:on 800421,during Pipe Hanger Insp, Discovered That Pipe Hanger from Previous Design Revision Had Not Been Removed from Auxiliary Feedwater Sys Pipe. Caused by Personnel Error.Pipe Hanger Removed
ML19309H661
Person / Time
Site: Sequoyah Tennessee Valley Authority icon.png
Issue date: 05/02/1980
From: Ken Wilson
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19309H655 List:
References
LER-80-035-01T, LER-80-35-1T, NUDOCS 8005130628
Download: ML19309H661 (2)


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"- 8005130 bM U.S. NUCLEAR REGULATORY COMMIS$f0N 1; NRC FORitt 366 tr.s n EXHtBIT A i.; LICENSEE EVENT REPORT

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i LoJ 2J l During a pipe hanger inscection, a pipe hanaer from a previous design /

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. - . . . . . - - - - f5 TT1 I revision-had r[oI ~been Nmove'd frct$ an cabxiliarv feedwater system oice.

got.it This configuration had not been seismically analyzed. This configuration I iTTil I could introduce unknown forces and stress uoon the lina and thereby I lo M i t endanger the safety of a safety-related system. I I

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5 3 a0 ei 43 44 4, CAUSE O!$CRIPTICN AND CCRREC(IVE ACTICNS IiIal1One variable scring hanger assembly MK Mo. 1-AFDH-375 was installed rer I i

Another variable sorina hancer asso-My '. ras I i i i Drawing H3-431, Rev. 3.

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l *ennessee Valley Authority Sequoyah Nuclear Plant LER SUPPLEMENTAL IhTORMATICN SQRO-50-327/8035 Technical Specification Involved: 6.9.1.12.1 Reported Under Technical Specification 6.9.1.12.1 Date of Occurrence: 4/21/80 Time of Occurrence: 0900 CST Unit 1 i,

i Identification and Description of Occurrence During a recent pipe hanger inspection, it was discovered that a pipe hanger from a previous design revisien had not been removed from an auxiliary feedwater system pipe. This constituted a hanger configuration which had not been seismically analyzed.

Conditions Prior to Occurrence Mode 5 and filling and venting RCS.

Action Specified in the Technical Specification Surveillance Requirements Met Due to Inoperable Eauipment N/A Apparent Cause of Occurrence Personnel error. Pipe hanger should have been removed.

. Analysis of Occurrence N/A Corrective Action The pipe hanger installed from the previous design revision was removed; therefore, the system should operate with no adverse effects as designed.

Failure Date

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