ML19322E871: Difference between revisions
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IF 779 | IF 779 LICENSEC EVENT HEPOTIT EXHlUIT A cosi..., eu. | ||
LICENSEC EVENT HEPOTIT EXHlUIT A cosi..., eu. | |||
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(_ The contents of the task decontamination collector tank was discharged 4 Lo.l.:.J I via the liquid redwaste effluent line to the cooling tower blowdown with , | (_ The contents of the task decontamination collector tank was discharged 4 Lo.l.:.J I via the liquid redwaste effluent line to the cooling tower blowdown with , | ||
ETB L_._the { low elements in both lines inoperable without flow estimates being _j | ETB L_._the { low elements in both lines inoperable without flow estimates being _j | ||
[JTR L_. performed. The event occurred at 0345 CST (TS LCO 3.3.3.9). There was i | [JTR L_. performed. The event occurred at 0345 CST (TS LCO 3.3.3.9). There was i | ||
[H] L no d_an_3_er_to,the health and safegof the public. Previous occurrences ; | [H] L no d_an_3_er_to,the health and safegof the public. Previous occurrences ; | ||
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gi Plant personnel instructed in need to comply with technical specificationg | gi Plant personnel instructed in need to comply with technical specificationg | ||
.agardless of lack of radioactivity. | .agardless of lack of radioactivity. | ||
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Line 158: | Line 91: | ||
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o Tennessee Valley Authority - | |||
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Sequoyah Nuclear Plant - | Sequoyah Nuclear Plant - | ||
LER SUPPLEMENTAL INFORMATION BQRO-50-327/8002 Technical Specification Involved 3.3.3.9 Reported Under Technical Specification 6.9.1.12.b Date of Occurrence: 3/6/80 Time of occurrence: 1000 CST Unit 1 Identification and Description of Occurrence: | |||
LER SUPPLEMENTAL INFORMATION | |||
BQRO-50-327/8002 Technical Specification Involved 3.3.3.9 Reported Under Technical Specification 6.9.1.12.b Date of Occurrence: 3/6/80 Time of occurrence: 1000 CST Unit 1 Identification and Description of Occurrence: | |||
Engineering personnel in reviewing surveillance instructions noted that the contents of the task decontamination collector tank was discharged via the liquid radwaste effluent line to the cooling tower blowdown with the flow elements in both lines inoperable without flow estimates being performed. This is in violation of Action 30 of Table 3.3-12 of LCO 3.3.3.9. | Engineering personnel in reviewing surveillance instructions noted that the contents of the task decontamination collector tank was discharged via the liquid radwaste effluent line to the cooling tower blowdown with the flow elements in both lines inoperable without flow estimates being performed. This is in violation of Action 30 of Table 3.3-12 of LCO 3.3.3.9. | ||
Conditions Prior to Occurrence: | Conditions Prior to Occurrence: | ||
Line 183: | Line 105: | ||
There was no hazard to the public health or safety. SI-400, Release Permit, was performed and verified no activity in the tank. | There was no hazard to the public health or safety. SI-400, Release Permit, was performed and verified no activity in the tank. | ||
Corrective Action: | Corrective Action: | ||
Personnel instructed to observe requirements for inoperable monitor. | Personnel instructed to observe requirements for inoperable monitor. | ||
Failure Data: | Failure Data: | ||
N/A | N/A | ||
~_n - | ~_n - | ||
e ,_}} | e ,_}} |
Revision as of 02:45, 1 February 2020
ML19322E871 | |
Person / Time | |
---|---|
Site: | Sequoyah |
Issue date: | 03/19/1980 |
From: | Kinsey W TENNESSEE VALLEY AUTHORITY |
To: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
Shared Package | |
ML19322E866 | List: |
References | |
LER-80-002-01T, LER-80-2-1T, NUDOCS 8004020371 | |
Download: ML19322E871 (2) | |
Text
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~
. 1. -
.o
~ ,,,.c ,o m. u u/ 'veu,,i nna,i nou co .w,o,.
IF 779 LICENSEC EVENT HEPOTIT EXHlUIT A cosi..., eu.
t, _ L ! . I , J .. L_j. G i,u .se....c o w rtau nrow..to.. n....,.rc . . ,
o e
. . I TI tr.S.J..
, ,... .N! P 1. L..tCL.a.I 01_.l. 0 f 0 ! OJ 010a.I -1i.s
. . . . . . . 01.0.J.Gl
... ... u 4 I s'.
l'I t'i !Q1!! 10 CL.%'t
. '. c1. L. .L@L. 0.L5.J.0L,,oj.0_g i 2 .
i 7 *GL.Oj_3r 016 t 8101@t Oi a 1!9 !_al O!@
i i i . ,. . n ,. ,- . . . ,. . . ., c i .,
t v t N1 ::n,;n *: N ac es. u s' .1 L..v..t ,,s ".ct l yo)
(_ The contents of the task decontamination collector tank was discharged 4 Lo.l.:.J I via the liquid redwaste effluent line to the cooling tower blowdown with ,
ETB L_._the { low elements in both lines inoperable without flow estimates being _j
[JTR L_. performed. The event occurred at 0345 CST (TS LCO 3.3.3.9). There was i
[H] L no d_an_3_er_to,the health and safegof the public. Previous occurrences ;
E, .1_J.2L.... . . . . . . . . _ .._. _ _ . . _ _ . . . .. _ _ _ _ - I
- 1.
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C o' * * .a .g
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gi Misunderstanding of technic 1 specifications. Operations personnel did j I rTG L not understand need for flow monitoring if no radioactivity was present. , , , _
gi Plant personnel instructed in need to comply with technical specificationg
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I o
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- T ii) o yy9 80040203H
\' s.s N s.R .
Xlh n .
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o Tennessee Valley Authority -
Sequoyah Nuclear Plant -
LER SUPPLEMENTAL INFORMATION BQRO-50-327/8002 Technical Specification Involved 3.3.3.9 Reported Under Technical Specification 6.9.1.12.b Date of Occurrence: 3/6/80 Time of occurrence: 1000 CST Unit 1 Identification and Description of Occurrence:
Engineering personnel in reviewing surveillance instructions noted that the contents of the task decontamination collector tank was discharged via the liquid radwaste effluent line to the cooling tower blowdown with the flow elements in both lines inoperable without flow estimates being performed. This is in violation of Action 30 of Table 3.3-12 of LCO 3.3.3.9.
Conditions Prior to Occurrence:
Unit 1 in mode 6 loading fuel for first core load.
Action specified in the Technical Specification Surveillance Requirements met due to inoperable equipment. Describe.
~
N/A Apparent Cause of Occurrence:
Misunderstanding of Technical Specification requirements.
Analysis of occurrence:
There was no hazard to the public health or safety. SI-400, Release Permit, was performed and verified no activity in the tank.
Corrective Action:
Personnel instructed to observe requirements for inoperable monitor.
Failure Data:
N/A
~_n -
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