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| {{#Wiki_filter:~0- f 9 Acre UNITED STATES NUCLEAR REGULATORY | | {{#Wiki_filter:Acre |
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| COMMISSION
| | ~0- f9 UNITED STATES |
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| ===OFFICE OF NUCLEAR REACTOR REGULATION===
| | NUCLEAR REGULATORY COMMISSION |
| WASHINGTON, D.C. 20555-0001 September
| |
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| 18, 1998 NRC INFORMATION
| | OFFICE OF NUCLEAR REACTOR REGULATION |
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| NOTICE 98-36: INADEQUATE | | WASHINGTON, D.C. 20555-0001 September 18, 1998 NRC INFORMATION NOTICE 98-36: INADEQUATE OR POORLY CONTROLLED, NON- |
| | SAFETY-RELATED MAINTENANCE ACTIVITIES |
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| |
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| OR POORLY CONTROLLED, NON-SAFETY-RELATED
| | UNNECESSARILY CHALLENGED SAFETY SYSTEMS |
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| MAINTENANCE
| | Addressee |
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| |
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| ACTIVITIES
| | All holders of operating licenses for nuclear power reactors. |
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| |
|
| UNNECESSARILY
| | purpose |
|
| |
|
| CHALLENGED
| | The U.S. Nuclear Regulatory Commission (NRC) is issuing this information notice (IN) to alert |
|
| |
|
| SAFETY SYSTEMS Addressee All holders of operating
| | addressees to several recent events in which inadequate or poorly controlled, non-safety- related maintenance activities resulted in unnecessary challenges to safety systems. It is |
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| |
|
| licenses for nuclear power reactors.purpose The U.S. Nuclear Regulatory
| | expected that recipients will review the information for applicability to their facilities and consider |
|
| |
|
| Commission (NRC) is issuing this information
| | action, as appropriate to avoid similar problems. However, suggestions contained in this |
|
| |
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| notice (IN) to alert addressees | | information notice are not NRC requirements; therefore, no specific action or written response |
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| |
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| to several recent events in which inadequate
| | is required. |
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| |
|
| or poorly controlled, non-safety- related maintenance
| | ==Description of Circumstances== |
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| |
|
| activities
| | ===BRAIDWOOD UNIT 2=== |
| | On January 18, 1996, with Braidwood Unit 2 operating at full power, .offsite power was lost. |
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| |
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| resulted in unnecessary
| | Inadequately secured roofing repair materials located on the roof of the adjacent service |
|
| |
|
| challenges
| | building were blown off the roof during a rain storm, causing a phase-to-ground arc on one of |
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| |
|
| to safety systems. It is expected that recipients
| | two station auxiliary transformers (SATs). As designed, the second SAT tripped when the first |
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| |
|
| will review the information
| | SAT failed. Both emergency diesel generators (EDGs) automatically started and all safe- shutdown loads automatically sequenced on to the engineered safety feature (ESF) buses. All |
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| |
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| for applicability
| | automatic bus transfers occurred as designed, maintaining power to non-ESF buses from the |
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| |
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| to their facilities
| | unit auxiliary transformers (UATs). The reactor remained stable at full power throughout the |
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| |
|
| and consider action, as appropriate
| | event. To restore offsite power to Unit 2, the licensee cross-tied both Unit 2 ESF buses to the |
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| |
|
| to avoid similar problems.
| | respective ESF buses of Unit 1, which also remained at full power throughout the event. |
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| |
|
| However, suggestions
| | Inspection of the faulted SAT revealed damage to (1) the Phase B and C bushings and (2) a |
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| |
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| contained
| | gas detector relay on top of the transformer where heavy arcing occurred. The licensee |
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| |
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| in this information
| | determined that the Initiating event was a Phase C arc-to-ground, followed by a Phase B to |
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| |
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| notice are not NRC requirements;
| | vNOrT g NO -98T- goz 98 0e 8 |
| therefore, no specific action or written response is required.Description
| | <9809 td n |
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| |
|
| of Circumstances
| | f IN 98-36 September 18, 1998 Phase C arc. A 345-kilovolt switchyard breaker, Which connected the SAT to the switchyard |
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| |
|
| BRAIDWOOD
| | ring bus, was also damaged. Approximately one square foot of the Phase B bushing was |
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| |
|
| UNIT 2 On January 18, 1996, with Braidwood
| | blown out. |
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| |
|
| Unit 2 operating | | ===BYRON UNIT I=== |
| | On May 23, 1996, with the Unit 1 reactor shut down In excess of a month for a refueling outage, offsite power was lost when one of the two Unit I SATs Isolated because of a Phase A to |
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| |
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| at full power, .offsite power was lost.Inadequately
| | Phase B current differential relay operation. The second SAT tripped as designed when the |
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| |
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| secured roofing repair materials
| | first SAT failed. Both EDGs automatically started and all safe-shutdown loads automatically |
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| |
|
| located on the roof of the adjacent service building were blown off the roof during a rain storm, causing a phase-to-ground
| | sequenced on to the ESF buses. Because the reactor was shut down, power to non-ESF |
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| |
|
| arc on one of two station auxiliary
| | buses was lost and two service water pumps and a station air compressor common to both |
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| |
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| transformers (SATs). As designed, the second SAT tripped when the first SAT failed. Both emergency
| | Byron units tripped. Without the service water pumps, Unit 2, which was operating at full |
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| |
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| diesel generators (EDGs) automatically
| | power, had no cooling water to many loads, including the main generator auxiliaries, station air |
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| |
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| started and all safe-shutdown loads automatically
| | compressors, condensate pumps, and condensate booster pumps. Subsequently, Unit 2 was |
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| |
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| sequenced
| | manually tripped. |
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| |
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| on to the engineered | | The licensee determined that the SAT that initially tripped underwent a phase-to-ground fault on |
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| |
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| safety feature (ESF) buses. All automatic
| | a Phase B insulator. The failed insulator was located outdoors, about halfway between the SAT |
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| |
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| bus transfers | | and the auxiliary building. After Initiating, the arc continued down the bus bar, Increasing in |
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| |
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| occurred as designed, maintaining
| | width until It involved the other two phases. Air and water present in the bus bar duct was |
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| |
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| power to non-ESF buses from the unit auxiliary
| | heated by the arc and resulted in pressurization of the duct. |
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| |
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| transformers (UATs). The reactor remained stable at full power throughout
| | Chronic water leakage through inadequately caulked Insulator mounting holes and through an |
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| |
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| the event. To restore offsite power to Unit 2, the licensee cross-tied | | improperly compressed gasket caused degradation of the insulator metal inserts and Insulator |
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| |
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| both Unit 2 ESF buses to the respective
| | material between these inserts. Eventually, the bus flashed to ground through the degraded |
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| |
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| ESF buses of Unit 1, which also remained at full power throughout
| | insulator and initiated the transient. |
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| |
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| the event.Inspection
| | PERRY |
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| |
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| of the faulted SAT revealed damage to (1) the Phase B and C bushings and (2) a gas detector relay on top of the transformer
| | On June 5, 1997, Perry was operating at full power when an automatic reactor scram occurred |
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| |
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| where heavy arcing occurred.
| | following a three-phase fault in one of two high-voltage secondary winding termination |
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| |
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| The licensee determined | | compartments of the UAT. The fault resulted in the actuation of the auxiliary transformer phase |
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| |
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| that the Initiating
| | differential relay, a main generator lockout, a main turbine trip, and fast closure of the turbine |
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| |
|
| event was a Phase C arc-to-ground, followed by a Phase B to vNOrT g NO -98T- goz 98 0e 8<9809 td n
| | control valves. |
|
| |
|
| f IN 98-36 September
| | At the time of the transient, safety-related electrical loads were being supplied by the in-service |
|
| |
|
| 18, 1998 Phase C arc. A 345-kilovolt
| | startup transformer. The non-safety-related electrical loads supplied by the transformer |
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| |
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| switchyard
| | automatically transferred to the startup transformer except for the bus that was faulted. |
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| |
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| breaker, Which connected
| | Operators stabilized the plant without major complication. |
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| |
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| the SAT to the switchyard | | The licensee determined that the fault had developed as a result of an accumulation of moisture |
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| |
|
| ring bus, was also damaged. Approximately
| | and dust that had entered the termination compartment housing where a 2-Inch-long piece of |
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| |
|
| one square foot of the Phase B bushing was blown out.BYRON UNIT I On May 23, 1996, with the Unit 1 reactor shut down In excess of a month for a refueling
| | gasket material was missing from the compartment housing-to-transformer sealing surface. |
|
| |
|
| outage, offsite power was lost when one of the two Unit I SATs Isolated because of a Phase A to Phase B current differential
| | The missing piece of gasket material may have been lost during work performed when |
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| |
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| relay operation.
| | K>1 IN 98-36 September 18, 1998 replacing the auxiliary transformer following failure of the transformer on May 30, 1996. The |
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| |
|
| The second SAT tripped as designed when the first SAT failed. Both EDGs automatically
| | cause of that failure was attributed to Inadequate original design or poor assembly practices or |
|
| |
|
| started and all safe-shutdown
| | both. |
|
| |
|
| loads automatically
| | ===POINT BEACH UNIT I=== |
| | During a severe storm on January 8, 1998, a ground In the low-voltage-side bus duct caused |
|
| |
|
| sequenced
| | the failure of the Unit I SAT. This failure and a failure of the 13.8-kilovolt automatic bus transfer |
|
| |
|
| on to the ESF buses. Because the reactor was shut down, power to non-ESF buses was lost and two service water pumps and a station air compressor
| | to the Unit 2 SAT resulted in the loss of normal power to the Unit I safeguards buses. The |
|
| |
|
| common to both Byron units tripped. Without the service water pumps, Unit 2, which was operating
| | EDGs subsequently started and restored power to the buses. Unit I remained at 98 percent |
|
| |
|
| at full power, had no cooling water to many loads, including
| | power throughout the transient. Unit 2 was in cold shutdown. |
|
| |
|
| the main generator | | The licensee attributed the failure of the transformer to the buildup of condensation internal to |
|
| |
|
| auxiliaries, station air compressors, condensate
| | the buses and long-term insulation degradation In the bus duct on the low-voltage side of the |
|
| |
|
| pumps, and condensate
| | transformer. Before the transformer failed, the circuit breaker for a heater designed to keep the |
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| |
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| booster pumps. Subsequently, Unit 2 was manually tripped.The licensee determined
| | bus duct dry would not remain closed. Consequently, in August 1996, the licensee left the |
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| |
|
| that the SAT that initially
| | circuit breaker open and wrote a work order for its repair. However, work schedulers did not |
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| |
|
| tripped underwent
| | recognize that the bus duct heater was inoperable with the circuit breaker open, and the work |
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| |
|
| a phase-to-ground
| | order was erroneously classified as "minor maintenance" and given low priority. At the time the |
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| |
|
| fault on a Phase B insulator.
| | transformer failed, the work order was in the "backlog' of maintenance Items. In addition to the |
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| |
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| The failed insulator
| | inoperable heater, the:licensee determined that the lack of a routine inspection program for the |
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| |
|
| was located outdoors, about halfway between the SAT and the auxiliary
| | bus ducts may have contributed to the event. Inspection of the bus ducts after the transformer |
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| |
|
| building.
| | failed revealed insulation breakdown that would likely have been Identified through a periodic |
|
| |
|
| After Initiating, the arc continued
| | Inspection program. |
|
| |
|
| down the bus bar, Increasing
| | Discussion |
|
| |
|
| in width until It involved the other two phases. Air and water present in the bus bar duct was heated by the arc and resulted in pressurization
| | These events illustrate the potentially significant consequences of inadequate or poorly |
|
| |
|
| of the duct.Chronic water leakage through inadequately
| | performed maintenance activities on non-safety-related plant components. Unnecessary |
|
| |
|
| caulked Insulator
| | challenges to plant safety systems or control room operators or both could result from |
|
| |
|
| mounting holes and through an improperly
| | inadequate control or inattention to detail during non-safety-related maintenance activities. The |
|
| |
|
| compressed
| | potential impact on safety systems of such activities as the re-roofing of nuclear power plant |
|
| |
|
| gasket caused degradation
| | support buildings, the Installation of gaskets, or the caulking of outdoor components, could |
|
| |
|
| of the insulator | | easily be overlooked. In addition, several of the events discussed here highlight the need for |
|
| |
|
| metal inserts and Insulator material between these inserts. Eventually, the bus flashed to ground through the degraded insulator
| | licensees to have better control over the maintenance activities of contractor and non-station |
|
| |
|
| and initiated | | utility employees, and the need for thorough periodic walkdowns or preventive maintenance on |
|
| |
|
| the transient. | | auxiliary transformers and the associated outdoor bus ducts. |
|
| |
|
| PERRY On June 5, 1997, Perry was operating
| | IN 98-36 September 18, 1998 This information notice requires no specific action or written response. However, recipients are |
|
| |
|
| at full power when an automatic
| | reminded that they are required to consider Industry-wide operating experience (including NRC |
|
| |
|
| reactor scram occurred following
| | INs) where practical, when setting goals and performing periodic evaluations under Section |
|
| |
|
| a three-phase
| | 50.65, "Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power |
|
| |
|
| fault in one of two high-voltage
| | Plants," of Part 50 of Title 10 of the Code of Federal Regulations. If you have any questions |
|
| |
|
| secondary
| | about the information Inthis notice, please contact one of the technical contacts listed below or |
|
| |
|
| winding termination
| | the appropriate Office of Nuclear Reactor Regulation (NRR) project manager. |
|
| |
|
| compartments
| | , Acting Director |
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| |
|
| of the UAT. The fault resulted in the actuation
| | eJack |
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| |
|
| of the auxiliary | | Division of Reactor Program Management |
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| |
|
| transformer
| | Office of Nuclear Reactor Regulation |
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| |
|
| phase differential
| | Technical contacts: Mike Kunowski, Region IlIl John Neisler, Region IlIl |
|
| |
|
| relay, a main generator
| | 630-829-9816 630429-9718 E-mail: mak3@nrc.gov E-mail: jhn@nrc.gov |
|
| |
|
| lockout, a main turbine trip, and fast closure of the turbine control valves.At the time of the transient, safety-related
| | Attachment: List of Recently Issued NRC Information Notices |
|
| |
|
| electrical
| | A,(ttachment 1 IN 98-36 September 18, 1998 LIST OF RECENTLY ISSUED |
|
| |
|
| loads were being supplied by the in-service
| | NRC INFORMATION NOTICES |
|
| |
|
| startup transformer.
| | Information Date of |
|
| |
|
| The non-safety-related
| | Notice No. Subject Issuance Issued to |
|
| |
|
| electrical
| | 98-35 Threat Assessments and 914/98 All U.S. NRC fuel cycle facilities |
|
| |
|
| loads supplied by the transformer
| | Consideration of Heightened power and non-power reactor |
|
| |
|
| automatically
| | Physical Protection Measures licensees (Safeguard issues, not |
|
| |
|
| transferred
| | for public disclosure.) |
| | 98-34 NRC Configuration Control 8/28/98 All holders of Operating licenses |
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| |
|
| to the startup transformer
| | Errors for nuclear power reactors, except |
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| |
|
| except for the bus that was faulted.Operators
| | for those who have ceased |
|
| |
|
| stabilized
| | operations and have certified that |
|
| |
|
| the plant without major complication.
| | fuel has been permanently |
|
| |
|
| The licensee determined
| | removed from the reactor vessel |
|
| |
|
| that the fault had developed
| | 98-33 NRC Regulations Prohibit 8128198 All holders of a U.S. Nuclear |
|
| |
|
| as a result of an accumulation
| | Agreements that restrict or Regulatory Commission (NRC) |
| | Discourage an Employee from license. |
|
| |
|
| of moisture and dust that had entered the termination
| | Participating In Protected Activities |
|
| |
|
| compartment
| | 98-32 Problems Associated with Post- 8126198 All holders of operating licenses |
|
| |
|
| housing where a 2-Inch-long
| | Fire Safe-Shutdown Circuit for nuclear power reactors, except |
|
| |
|
| piece of gasket material was missing from the compartment
| | Analyses those who have permanently |
|
| |
|
| housing-to-transformer
| | ceased operations and have |
|
| |
|
| sealing surface.The missing piece of gasket material may have been lost during work performed
| | certified that fuel has been |
|
| |
|
| when
| | permanently removed form the |
|
| |
|
| K>1 IN 98-36 September
| | reactor |
|
| |
|
| 18, 1998 replacing
| | 98-31 Fire Protection System Design 8/26/98 All holders of operating licences |
|
| |
|
| the auxiliary
| | Deficiencies and Common-Mode for nuclear power reactors, except |
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| |
|
| transformer
| | Flooding of Emergency Core Cooling those licensees that have |
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| |
|
| following
| | System Rooms at Washington Nuclear permanently ceased operations |
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| |
|
| failure of the transformer
| | Project Unit 2 and have certified that fuel has |
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| |
|
| on May 30, 1996. The cause of that failure was attributed
| | been permanently removed from |
|
| |
|
| to Inadequate
| | the reactor vessel. |
|
| |
|
| original design or poor assembly practices
| | OL = Operating License |
|
| |
|
| or both.POINT BEACH UNIT I During a severe storm on January 8, 1998, a ground In the low-voltage-side
| | CP = Construction Permit |
|
| |
|
| bus duct caused the failure of the Unit I SAT. This failure and a failure of the 13.8-kilovolt
| | - IN 98-36 September 18, 1998 This information notice requires no specific action or written response. However, recipients are |
|
| |
|
| automatic
| | reminded that they are required to consider industry-wide operating experience (including NRC |
|
| |
|
| bus transfer to the Unit 2 SAT resulted in the loss of normal power to the Unit I safeguards
| | INs) where practical, when setting goals and performing periodic evaluations under Section |
|
| |
|
| buses. The EDGs subsequently
| | 50.65, "Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power |
|
| |
|
| started and restored power to the buses. Unit I remained at 98 percent power throughout
| | Plants," of Part 50 of Title 10 of the Code of Federal Regulations. If you have any questions |
|
| |
|
| the transient. | | about the information in this notice, please contact one of the technical contacts listed below or |
|
| |
|
| Unit 2 was in cold shutdown.The licensee attributed
| | the appropriate Office of Nuclear Reactor Regulation (NRR) project manager. |
|
| |
|
| the failure of the transformer
| | Jack W. Roe, Acting Director |
|
| |
|
| to the buildup of condensation
| | Division of Reactor Program Management |
|
| |
|
| internal to the buses and long-term
| | Office of Nuclear Reactor Regulation |
|
| |
|
| insulation
| | Technical contacts: Mike Kunowski, Region IlIl John Neisler, Region IlIl |
|
| |
|
| degradation
| | 630-829-9816 630-829-9718 E-mail: mak3@nrc.gov E-mail: jhn@nrc.gov |
|
| |
|
| In the bus duct on the low-voltage
| | Attachment: List of Recently Issued NRC Information Notices |
|
| |
|
| side of the transformer.
| | *See previous concurrence & e. |
|
| |
|
| Before the transformer
| | C,,tt |
|
| |
|
| failed, the circuit breaker for a heater designed to keep the bus duct dry would not remain closed. Consequently, in August 1996, the licensee left the circuit breaker open and wrote a work order for its repair. However, work schedulers
| | **E-mail concurrence c<f() |
| | DOCUMENT NAME: G:\NICK\REGION.IN |
|
| |
|
| did not recognize
| | To receive a copy of this document, indicate in the box C=Copy wlo attachment/enclosure E=Copy with attachmentlenclosure N = No copy |
|
| |
|
| that the bus duct heater was inoperable
| | OFFICE PECB I Tech EdI Reg III [ Regil I PECB I C:PECB l_ji D M |
|
| |
|
| with the circuit breaker open, and the work order was erroneously
| | NAME NFields* RSanders* MKunowski** JNeisler** RDennig* JStolz* JRo |
|
| |
|
| classified
| | DATE 09/03/98 08/26/98 09/03/98 Ii09/03/98 09/14/98 J09/14/98 \/98 OFFICIAL RECORD COPY |
|
| |
|
| as "minor maintenance" and given low priority.
| | IN 98-xx |
|
| |
|
| At the time the transformer
| | September xx, 1998 This information notice requires no specific action or written response. However, recipie are |
|
| |
|
| failed, the work order was in the "backlog'
| | reminded that they are required to consider industry-wide operating experience (includ g NRC |
| of maintenance
| |
|
| |
|
| Items. In addition to the inoperable
| | INs) where practical, when setting goals and performing periodic evaluations under ection |
|
| |
|
| heater, the:licensee
| | 50.65, "Requirements for Monitoring the Effectiveness of Maintenance at Nuclea ower |
|
| |
|
| determined
| | Plants," of Part 50 of Title 10 of the Code of Federal Regulations. If you have ny questions |
|
| |
|
| that the lack of a routine inspection
| | about the information in this notice, please contact one of the technical con cts listed below or |
|
| |
|
| program for the bus ducts may have contributed
| | the appropriate Office of Nuclear Reactor Regulation (NRR) project man er. |
|
| |
|
| to the event. Inspection
| | Jack W. Roe, Acting irector |
|
| |
|
| of the bus ducts after the transformer | | Division of Reactor rogram Management |
|
| |
|
| failed revealed insulation
| | Office of Nuclea eactor Regulation |
|
| |
|
| breakdown
| | Technical contacts: Mike Kunowski, Region IlIl Joh eisler, Region IlIl |
|
| |
|
| that would likely have been Identified
| | 630-829-9816 63 -829-9718 E-mail: mak3@nrc.gov -mail: jhn@nrc.gov |
|
| |
|
| through a periodic Inspection
| | Attachment: List of Recently Issued NRC Info tion Notices |
|
| |
|
| program.Discussion
| | DOCUMENT NAME: G:\NICK\REGION.IN |
|
| |
|
| These events illustrate
| | To receive a copy of this document, Indicate in the box C=Copy wlo attachmentenclosure E=Copy with attachmentlenclosure N = No copy |
|
| |
|
| the potentially
| | OFFICE PECB. I _ Tech Ed I _ Reg I lI _I Reg 11 l 1/E "ECB (A)D:DRPM l |
|
| |
|
| significant
| | NAME NFiells' { RSanders MKu owsk Jeisler ennig l l JRoe |
|
| |
|
| consequences
| | l DATE /3/98 1SW98 17/3/98 15/3198 lH/ 48 q/l98 l I /98 OFFICIAL RECORD COPY I}} |
| | |
| of inadequate
| |
| | |
| or poorly performed
| |
| | |
| maintenance
| |
| | |
| activities
| |
| | |
| on non-safety-related
| |
| | |
| plant components.
| |
| | |
| Unnecessary
| |
| | |
| challenges
| |
| | |
| to plant safety systems or control room operators
| |
| | |
| or both could result from inadequate
| |
| | |
| control or inattention
| |
| | |
| to detail during non-safety-related
| |
| | |
| maintenance
| |
| | |
| activities.
| |
| | |
| The potential
| |
| | |
| impact on safety systems of such activities
| |
| | |
| as the re-roofing
| |
| | |
| of nuclear power plant support buildings, the Installation
| |
| | |
| of gaskets, or the caulking of outdoor components, could easily be overlooked.
| |
| | |
| In addition, several of the events discussed
| |
| | |
| here highlight
| |
| | |
| the need for licensees
| |
| | |
| to have better control over the maintenance
| |
| | |
| activities
| |
| | |
| of contractor
| |
| | |
| and non-station
| |
| | |
| utility employees, and the need for thorough periodic walkdowns
| |
| | |
| or preventive
| |
| | |
| maintenance
| |
| | |
| on auxiliary
| |
| | |
| transformers
| |
| | |
| and the associated
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| | |
| outdoor bus ducts.
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| | |
| IN 98-36 September
| |
| | |
| 18, 1998 This information
| |
| | |
| notice requires no specific action or written response.
| |
| | |
| However, recipients
| |
| | |
| are reminded that they are required to consider Industry-wide
| |
| | |
| operating
| |
| | |
| experience (including
| |
| | |
| NRC INs) where practical, when setting goals and performing
| |
| | |
| periodic evaluations
| |
| | |
| under Section 50.65, "Requirements
| |
| | |
| for Monitoring
| |
| | |
| the Effectiveness
| |
| | |
| of Maintenance
| |
| | |
| at Nuclear Power Plants," of Part 50 of Title 10 of the Code of Federal Regulations.
| |
| | |
| If you have any questions about the information
| |
| | |
| In this notice, please contact one of the technical
| |
| | |
| contacts listed below or the appropriate
| |
| | |
| Office of Nuclear Reactor Regulation (NRR) project manager.eJack , Acting Director Division of Reactor Program Management
| |
| | |
| ===Office of Nuclear Reactor Regulation===
| |
| Technical
| |
| | |
| contacts:
| |
| Mike Kunowski, Region IlIl John Neisler, Region IlIl 630-829-9816
| |
| 630429-9718 E-mail: mak3@nrc.gov
| |
| | |
| E-mail: jhn@nrc.gov
| |
| | |
| Attachment:
| |
| List of Recently Issued NRC Information
| |
| | |
| Notices
| |
| | |
| A,(ttachment
| |
| | |
| 1 IN 98-36 September
| |
| | |
| 18, 1998 LIST OF RECENTLY ISSUED NRC INFORMATION
| |
| | |
| ===NOTICES Information===
| |
| Notice No.Date of Issuance Subject 98-35 Threat Assessments
| |
| | |
| and Consideration
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| | |
| of Heightened
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| | |
| Physical Protection
| |
| | |
| Measures 914/98 Issued to All U.S. NRC fuel cycle facilities
| |
| | |
| power and non-power
| |
| | |
| reactor licensees (Safeguard
| |
| | |
| issues, not for public disclosure.)
| |
| 98-34 98-33 98-32 98-31 NRC Configuration
| |
| | |
| Control Errors NRC Regulations
| |
| | |
| Prohibit Agreements
| |
| | |
| that restrict or Discourage
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| | |
| an Employee from Participating
| |
| | |
| In Protected
| |
| | |
| Activities
| |
| | |
| Problems Associated
| |
| | |
| with Post-Fire Safe-Shutdown
| |
| | |
| Circuit Analyses 8/28/98 8128198 8126198 All holders of Operating
| |
| | |
| licenses for nuclear power reactors, except for those who have ceased operations
| |
| | |
| and have certified
| |
| | |
| that fuel has been permanently
| |
| | |
| removed from the reactor vessel All holders of a U.S. Nuclear Regulatory
| |
| | |
| Commission (NRC)license.All holders of operating
| |
| | |
| licenses for nuclear power reactors, except those who have permanently
| |
| | |
| ceased operations
| |
| | |
| and have certified
| |
| | |
| that fuel has been permanently
| |
| | |
| removed form the reactor All holders of operating
| |
| | |
| licences for nuclear power reactors, except those licensees
| |
| | |
| that have permanently
| |
| | |
| ceased operations
| |
| | |
| and have certified
| |
| | |
| that fuel has been permanently
| |
| | |
| removed from the reactor vessel.Fire Protection
| |
| | |
| System Design 8/26/98 Deficiencies
| |
| | |
| and Common-Mode
| |
| | |
| Flooding of Emergency
| |
| | |
| Core Cooling System Rooms at Washington
| |
| | |
| Nuclear Project Unit 2 OL = Operating
| |
| | |
| License CP = Construction
| |
| | |
| Permit
| |
| | |
| -IN 98-36 September
| |
| | |
| 18, 1998 This information
| |
| | |
| notice requires no specific action or written response.
| |
| | |
| However, recipients
| |
| | |
| are reminded that they are required to consider industry-wide
| |
| | |
| operating
| |
| | |
| experience (including
| |
| | |
| NRC INs) where practical, when setting goals and performing
| |
| | |
| periodic evaluations
| |
| | |
| under Section 50.65, "Requirements
| |
| | |
| for Monitoring
| |
| | |
| the Effectiveness
| |
| | |
| of Maintenance
| |
| | |
| at Nuclear Power Plants," of Part 50 of Title 10 of the Code of Federal Regulations.
| |
| | |
| If you have any questions about the information
| |
| | |
| in this notice, please contact one of the technical
| |
| | |
| contacts listed below or the appropriate
| |
| | |
| Office of Nuclear Reactor Regulation (NRR) project manager.Jack W. Roe, Acting Director Division of Reactor Program Management
| |
| | |
| ===Office of Nuclear Reactor Regulation===
| |
| Technical
| |
| | |
| contacts:
| |
| Mike Kunowski, Region IlIl 630-829-9816 E-mail: mak3@nrc.gov
| |
| | |
| John Neisler, Region IlIl 630-829-9718 E-mail: jhn@nrc.gov
| |
| | |
| Attachment:
| |
| List of Recently Issued NRC Information
| |
| | |
| Notices*See previous concurrence
| |
| | |
| C,,tt & e.**E-mail concurrence
| |
| | |
| c<f()DOCUMENT NAME: G:\NICK\REGION.IN
| |
| | |
| To receive a copy of this document, indicate in the box C=Copy wlo attachment/enclosure
| |
| | |
| E=Copy with attachmentlenclosure
| |
| | |
| N = No copy OFFICE PECB I Tech Ed I Reg III Reg [ il I PECB I C:PECB l_ji D M NAME NFields* RSanders*
| |
| MKunowski**
| |
| JNeisler**
| |
| RDennig* JStolz* JRo DATE 09/03/98 08/26/98 09/03/98 Ii09/03/98
| |
| 09/14/98 J 09/14/98 \/98 OFFICIAL RECORD COPY
| |
| | |
| IN 98-xx September
| |
| | |
| xx, 1998 This information
| |
| | |
| notice requires no specific action or written response.
| |
| | |
| However, recipie are reminded that they are required to consider industry-wide
| |
| | |
| operating
| |
| | |
| experience (includ g NRC INs) where practical, when setting goals and performing
| |
| | |
| periodic evaluations
| |
| | |
| under ection 50.65, "Requirements
| |
| | |
| for Monitoring
| |
| | |
| the Effectiveness
| |
| | |
| of Maintenance
| |
| | |
| at Nuclea ower Plants," of Part 50 of Title 10 of the Code of Federal Regulations.
| |
| | |
| If you have ny questions about the information
| |
| | |
| in this notice, please contact one of the technical
| |
| | |
| con cts listed below or the appropriate
| |
| | |
| Office of Nuclear Reactor Regulation (NRR) project man er.Jack W. Roe, Acting irector Division of Reactor rogram Management
| |
| | |
| ===Office of Nuclea eactor Regulation===
| |
| Technical
| |
| | |
| contacts:
| |
| Mike Kunowski, Region IlIl Joh eisler, Region IlIl 630-829-9816
| |
| 63 -829-9718 E-mail: mak3@nrc.gov -mail: jhn@nrc.gov
| |
| | |
| Attachment:
| |
| List of Recently Issued NRC Info tion Notices DOCUMENT NAME: G:\NICK\REGION.IN
| |
| | |
| To receive a copy of this document, Indicate in the box C=Copy wlo attachmentenclosure
| |
| | |
| E=Copy with attachmentlenclosure
| |
| | |
| N = No copy OFFICE PECB. I _ Tech Ed I _ Reg I _I lI Reg 11 l 1/E "ECB (A)D:DRPM
| |
| | |
| lNAME NFiells' { RSanders MKu owsk Jeisler ennig l l JRoel DATE /3/98 1SW98 17/3/98 15/3198 lH/ 48 q/l98 l I /98 OFFICIAL RECORD COPY I}}
| |
|
| |
|
| {{Information notice-Nav}} | | {{Information notice-Nav}} |
Inadequate or Poorly Controlled, Non-Safety-Related Maintenance Activities Unnecessarily Challenged Safety SystemsML031040558 |
Person / Time |
---|
Site: |
Beaver Valley, Millstone, Hatch, Monticello, Calvert Cliffs, Dresden, Davis Besse, Peach Bottom, Browns Ferry, Salem, Oconee, Mcguire, Nine Mile Point, Palisades, Palo Verde, Perry, Indian Point, Fermi, Kewaunee, Catawba, Harris, Wolf Creek, Saint Lucie, Point Beach, Oyster Creek, Watts Bar, Hope Creek, Grand Gulf, Cooper, Sequoyah, Byron, Pilgrim, Arkansas Nuclear, Three Mile Island, Braidwood, Susquehanna, Summer, Prairie Island, Columbia, Seabrook, Brunswick, Surry, Limerick, North Anna, Turkey Point, River Bend, Vermont Yankee, Crystal River, Haddam Neck, Ginna, Diablo Canyon, Callaway, Vogtle, Waterford, Duane Arnold, Farley, Robinson, Clinton, South Texas, San Onofre, Cook, Comanche Peak, Yankee Rowe, Maine Yankee, Quad Cities, Humboldt Bay, La Crosse, Big Rock Point, Rancho Seco, Zion, Midland, Bellefonte, Fort Calhoun, FitzPatrick, McGuire, LaSalle, Fort Saint Vrain, Shoreham, Satsop, Trojan, Atlantic Nuclear Power Plant ![Entergy icon.png](/w/images/7/79/Entergy_icon.png) |
---|
Issue date: |
09/18/1998 |
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From: |
Roe J Office of Nuclear Reactor Regulation |
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To: |
|
---|
References |
---|
IN-98-036, NUDOCS 9809210079 |
Download: ML031040558 (7) |
|
Similar Documents at Beaver Valley, Millstone, Hatch, Monticello, Calvert Cliffs, Dresden, Davis Besse, Peach Bottom, Browns Ferry, Salem, Oconee, Mcguire, Nine Mile Point, Palisades, Palo Verde, Perry, Indian Point, Fermi, Kewaunee, Catawba, Harris, Wolf Creek, Saint Lucie, Point Beach, Oyster Creek, Watts Bar, Hope Creek, Grand Gulf, Cooper, Sequoyah, Byron, Pilgrim, Arkansas Nuclear, Three Mile Island, Braidwood, Susquehanna, Summer, Prairie Island, Columbia, Seabrook, Brunswick, Surry, Limerick, North Anna, Turkey Point, River Bend, Vermont Yankee, Crystal River, Haddam Neck, Ginna, Diablo Canyon, Callaway, Vogtle, Waterford, Duane Arnold, Farley, Robinson, Clinton, South Texas, San Onofre, Cook, Comanche Peak, Yankee Rowe, Maine Yankee, Quad Cities, Humboldt Bay, La Crosse, Big Rock Point, Rancho Seco, Zion, Midland, Bellefonte, Fort Calhoun, FitzPatrick, McGuire, LaSalle, Fort Saint Vrain, Shoreham, Satsop, Trojan, Atlantic Nuclear Power Plant |
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Category:NRC Information Notice
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Appendix VI: NRC FOIA Responses (B-51 Through B-53); Turkey Point Event Report; NRC Information Notice 2010-12: Containment Liner Cor Information Notice 2010-12, Intervenors' Fifth Motion to Amend And/Or Supplement Proposed Contention No. 5 (Shield Building Cracking). Appendix VI: NRC FOIA Responses (B-51 Through B-53); Turkey Point Event Report; NRC Information Notic2012-08-17017 August 2012 Intervenors' Fifth Motion to Amend And/Or Supplement Proposed Contention No. 5 (Shield Building Cracking). Appendix VI: NRC FOIA Responses (B-51 Through B-53); Turkey Point Event Report; NRC Information Notice 2010-12: Containment Liner Cor Information Notice 2012-13, Boraflex Degradation Surveillance Programs and Corrective Actions in the Spent Fuel Pool2012-08-10010 August 2012 Boraflex Degradation Surveillance Programs and Corrective Actions in the Spent Fuel Pool Information Notice 2012-13, Boraflex Degradation Surveillance Programs And Corrective Actions In The Spent Fuel Pool2012-08-10010 August 2012 Boraflex Degradation Surveillance Programs And Corrective Actions In The Spent Fuel Pool Information Notice 2012-11, Age Related Capacitor Degradation2012-07-23023 July 2012 Age Related Capacitor Degradation ML12031A0132012-02-0606 February 2012 U.S. Nuclear Regulatory Commission Investigation Report No. 2-2010-058, Cpn International, Inc Information Notice 2011-19, Licensee Event Reports Containing Information Pertaining to Defects to Basic Components2011-09-26026 September 2011 Licensee Event Reports Containing Information Pertaining to Defects to Basic Components Information Notice 2011-15, Steel Containment Degradation and Associated License Renewal Aging Management Issues2011-08-0101 August 2011 Steel Containment Degradation and Associated License Renewal Aging Management Issues Information Notice 2011-17, Calculation Methodologies for Operability Determinations of Gas Voids in Nuclear Power Plant Piping2011-07-26026 July 2011 Calculation Methodologies for Operability Determinations of Gas Voids in Nuclear Power Plant Piping Information Notice 2011-13, Official Exhibit - 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Mclaughlin on NRC, Regarding NRC Information Notice 2006-13: Groundwater Contamination2006-07-13013 July 2006 E-mail from M. Mclaughlin on NRC, Regarding NRC Information Notice 2006-13: Groundwater Contamination 2020-09-03 The following query condition could not be considered due to this wiki's restrictions on query size or depth: <code> [[:Beaver Valley]] OR [[:Millstone]] OR [[:Hatch]] OR [[:Monticello]] OR [[:Calvert Cliffs]] OR [[:Dresden]] OR [[:Davis Besse]] OR [[:Peach Bottom]] OR [[:Browns Ferry]] OR [[:Salem]] OR [[:Oconee]] OR [[:Mcguire]] OR [[:Nine Mile Point]] OR [[:Palisades]] OR [[:Palo Verde]] OR [[:Perry]] OR [[:Indian Point]] OR [[:Fermi]] OR [[:Kewaunee]] OR [[:Catawba]] OR [[:Harris]] OR [[:Wolf Creek]] OR [[:Saint Lucie]] OR [[:Point Beach]] OR [[:Oyster Creek]] OR [[:Watts Bar]] OR [[:Hope Creek]] OR [[:Grand Gulf]] OR [[:Cooper]] OR [[:Sequoyah]] OR [[:Byron]] OR [[:Pilgrim]] OR [[:Arkansas Nuclear]] OR [[:Three Mile Island]] OR [[:Braidwood]] OR [[:Susquehanna]] OR [[:Summer]] OR [[:Prairie Island]] OR [[:Columbia]] OR [[:Seabrook]] OR [[:Brunswick]] OR [[:Surry]] OR [[:Limerick]] OR [[:North Anna]] OR [[:Turkey Point]] OR [[:River Bend]] OR [[:Vermont Yankee]] OR [[:Crystal River]] OR [[:Haddam Neck]] OR [[:Ginna]] OR [[:Diablo Canyon]] OR [[:Callaway]] OR [[:Vogtle]] OR [[:Waterford]] OR [[:Duane Arnold]] OR [[:Farley]] OR [[:Robinson]] OR [[:Clinton]] OR [[:South Texas]] OR [[:San Onofre]] OR [[:Cook]] OR [[:Comanche Peak]] OR [[:Yankee Rowe]] OR [[:Maine Yankee]] OR [[:Quad Cities]] OR [[:Humboldt Bay]] OR [[:La Crosse]] OR [[:Big Rock Point]] OR [[:Rancho Seco]] OR [[:Zion]] OR [[:Midland]] OR [[:Bellefonte]] OR [[:Fort Calhoun]] OR [[:FitzPatrick]] OR [[:McGuire]] OR [[:LaSalle]] OR [[:Fort Saint Vrain]] OR [[:Shoreham]] OR [[:Satsop]] OR [[:Trojan]] OR [[:Atlantic Nuclear Power Plant]] </code>.
[Table view]The following query condition could not be considered due to this wiki's restrictions on query size or depth: <code> [[:Beaver Valley]] OR [[:Millstone]] OR [[:Hatch]] OR [[:Monticello]] OR [[:Calvert Cliffs]] OR [[:Dresden]] OR [[:Davis Besse]] OR [[:Peach Bottom]] OR [[:Browns Ferry]] OR [[:Salem]] OR [[:Oconee]] OR [[:Mcguire]] OR [[:Nine Mile Point]] OR [[:Palisades]] OR [[:Palo Verde]] OR [[:Perry]] OR [[:Indian Point]] OR [[:Fermi]] OR [[:Kewaunee]] OR [[:Catawba]] OR [[:Harris]] OR [[:Wolf Creek]] OR [[:Saint Lucie]] OR [[:Point Beach]] OR [[:Oyster Creek]] OR [[:Watts Bar]] OR [[:Hope Creek]] OR [[:Grand Gulf]] OR [[:Cooper]] OR [[:Sequoyah]] OR [[:Byron]] OR [[:Pilgrim]] OR [[:Arkansas Nuclear]] OR [[:Three Mile Island]] OR [[:Braidwood]] OR [[:Susquehanna]] OR [[:Summer]] OR [[:Prairie Island]] OR [[:Columbia]] OR [[:Seabrook]] OR [[:Brunswick]] OR [[:Surry]] OR [[:Limerick]] OR [[:North Anna]] OR [[:Turkey Point]] OR [[:River Bend]] OR [[:Vermont Yankee]] OR [[:Crystal River]] OR [[:Haddam Neck]] OR [[:Ginna]] OR [[:Diablo Canyon]] OR [[:Callaway]] OR [[:Vogtle]] OR [[:Waterford]] OR [[:Duane Arnold]] OR [[:Farley]] OR [[:Robinson]] OR [[:Clinton]] OR [[:South Texas]] OR [[:San Onofre]] OR [[:Cook]] OR [[:Comanche Peak]] OR [[:Yankee Rowe]] OR [[:Maine Yankee]] OR [[:Quad Cities]] OR [[:Humboldt Bay]] OR [[:La Crosse]] OR [[:Big Rock Point]] OR [[:Rancho Seco]] OR [[:Zion]] OR [[:Midland]] OR [[:Bellefonte]] OR [[:Fort Calhoun]] OR [[:FitzPatrick]] OR [[:McGuire]] OR [[:LaSalle]] OR [[:Fort Saint Vrain]] OR [[:Shoreham]] OR [[:Satsop]] OR [[:Trojan]] OR [[:Atlantic Nuclear Power Plant]] </code>. |
Acre
~0- f9 UNITED STATES
NUCLEAR REGULATORY COMMISSION
OFFICE OF NUCLEAR REACTOR REGULATION
WASHINGTON, D.C. 20555-0001 September 18, 1998 NRC INFORMATION NOTICE 98-36: INADEQUATE OR POORLY CONTROLLED, NON-
SAFETY-RELATED MAINTENANCE ACTIVITIES
UNNECESSARILY CHALLENGED SAFETY SYSTEMS
Addressee
All holders of operating licenses for nuclear power reactors.
purpose
The U.S. Nuclear Regulatory Commission (NRC) is issuing this information notice (IN) to alert
addressees to several recent events in which inadequate or poorly controlled, non-safety- related maintenance activities resulted in unnecessary challenges to safety systems. It is
expected that recipients will review the information for applicability to their facilities and consider
action, as appropriate to avoid similar problems. However, suggestions contained in this
information notice are not NRC requirements; therefore, no specific action or written response
is required.
Description of Circumstances
BRAIDWOOD UNIT 2
On January 18, 1996, with Braidwood Unit 2 operating at full power, .offsite power was lost.
Inadequately secured roofing repair materials located on the roof of the adjacent service
building were blown off the roof during a rain storm, causing a phase-to-ground arc on one of
two station auxiliary transformers (SATs). As designed, the second SAT tripped when the first
SAT failed. Both emergency diesel generators (EDGs) automatically started and all safe- shutdown loads automatically sequenced on to the engineered safety feature (ESF) buses. All
automatic bus transfers occurred as designed, maintaining power to non-ESF buses from the
unit auxiliary transformers (UATs). The reactor remained stable at full power throughout the
event. To restore offsite power to Unit 2, the licensee cross-tied both Unit 2 ESF buses to the
respective ESF buses of Unit 1, which also remained at full power throughout the event.
Inspection of the faulted SAT revealed damage to (1) the Phase B and C bushings and (2) a
gas detector relay on top of the transformer where heavy arcing occurred. The licensee
determined that the Initiating event was a Phase C arc-to-ground, followed by a Phase B to
vNOrT g NO -98T- goz 98 0e 8
<9809 td n
f IN 98-36 September 18, 1998 Phase C arc. A 345-kilovolt switchyard breaker, Which connected the SAT to the switchyard
ring bus, was also damaged. Approximately one square foot of the Phase B bushing was
blown out.
BYRON UNIT I
On May 23, 1996, with the Unit 1 reactor shut down In excess of a month for a refueling outage, offsite power was lost when one of the two Unit I SATs Isolated because of a Phase A to
Phase B current differential relay operation. The second SAT tripped as designed when the
first SAT failed. Both EDGs automatically started and all safe-shutdown loads automatically
sequenced on to the ESF buses. Because the reactor was shut down, power to non-ESF
buses was lost and two service water pumps and a station air compressor common to both
Byron units tripped. Without the service water pumps, Unit 2, which was operating at full
power, had no cooling water to many loads, including the main generator auxiliaries, station air
compressors, condensate pumps, and condensate booster pumps. Subsequently, Unit 2 was
manually tripped.
The licensee determined that the SAT that initially tripped underwent a phase-to-ground fault on
a Phase B insulator. The failed insulator was located outdoors, about halfway between the SAT
and the auxiliary building. After Initiating, the arc continued down the bus bar, Increasing in
width until It involved the other two phases. Air and water present in the bus bar duct was
heated by the arc and resulted in pressurization of the duct.
Chronic water leakage through inadequately caulked Insulator mounting holes and through an
improperly compressed gasket caused degradation of the insulator metal inserts and Insulator
material between these inserts. Eventually, the bus flashed to ground through the degraded
insulator and initiated the transient.
PERRY
On June 5, 1997, Perry was operating at full power when an automatic reactor scram occurred
following a three-phase fault in one of two high-voltage secondary winding termination
compartments of the UAT. The fault resulted in the actuation of the auxiliary transformer phase
differential relay, a main generator lockout, a main turbine trip, and fast closure of the turbine
control valves.
At the time of the transient, safety-related electrical loads were being supplied by the in-service
startup transformer. The non-safety-related electrical loads supplied by the transformer
automatically transferred to the startup transformer except for the bus that was faulted.
Operators stabilized the plant without major complication.
The licensee determined that the fault had developed as a result of an accumulation of moisture
and dust that had entered the termination compartment housing where a 2-Inch-long piece of
gasket material was missing from the compartment housing-to-transformer sealing surface.
The missing piece of gasket material may have been lost during work performed when
K>1 IN 98-36 September 18, 1998 replacing the auxiliary transformer following failure of the transformer on May 30, 1996. The
cause of that failure was attributed to Inadequate original design or poor assembly practices or
both.
POINT BEACH UNIT I
During a severe storm on January 8, 1998, a ground In the low-voltage-side bus duct caused
the failure of the Unit I SAT. This failure and a failure of the 13.8-kilovolt automatic bus transfer
to the Unit 2 SAT resulted in the loss of normal power to the Unit I safeguards buses. The
EDGs subsequently started and restored power to the buses. Unit I remained at 98 percent
power throughout the transient. Unit 2 was in cold shutdown.
The licensee attributed the failure of the transformer to the buildup of condensation internal to
the buses and long-term insulation degradation In the bus duct on the low-voltage side of the
transformer. Before the transformer failed, the circuit breaker for a heater designed to keep the
bus duct dry would not remain closed. Consequently, in August 1996, the licensee left the
circuit breaker open and wrote a work order for its repair. However, work schedulers did not
recognize that the bus duct heater was inoperable with the circuit breaker open, and the work
order was erroneously classified as "minor maintenance" and given low priority. At the time the
transformer failed, the work order was in the "backlog' of maintenance Items. In addition to the
inoperable heater, the:licensee determined that the lack of a routine inspection program for the
bus ducts may have contributed to the event. Inspection of the bus ducts after the transformer
failed revealed insulation breakdown that would likely have been Identified through a periodic
Inspection program.
Discussion
These events illustrate the potentially significant consequences of inadequate or poorly
performed maintenance activities on non-safety-related plant components. Unnecessary
challenges to plant safety systems or control room operators or both could result from
inadequate control or inattention to detail during non-safety-related maintenance activities. The
potential impact on safety systems of such activities as the re-roofing of nuclear power plant
support buildings, the Installation of gaskets, or the caulking of outdoor components, could
easily be overlooked. In addition, several of the events discussed here highlight the need for
licensees to have better control over the maintenance activities of contractor and non-station
utility employees, and the need for thorough periodic walkdowns or preventive maintenance on
auxiliary transformers and the associated outdoor bus ducts.
IN 98-36 September 18, 1998 This information notice requires no specific action or written response. However, recipients are
reminded that they are required to consider Industry-wide operating experience (including NRC
INs) where practical, when setting goals and performing periodic evaluations under Section
50.65, "Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power
Plants," of Part 50 of Title 10 of the Code of Federal Regulations. If you have any questions
about the information Inthis notice, please contact one of the technical contacts listed below or
the appropriate Office of Nuclear Reactor Regulation (NRR) project manager.
, Acting Director
eJack
Division of Reactor Program Management
Office of Nuclear Reactor Regulation
Technical contacts: Mike Kunowski, Region IlIl John Neisler, Region IlIl
630-829-9816 630429-9718 E-mail: mak3@nrc.gov E-mail: jhn@nrc.gov
Attachment: List of Recently Issued NRC Information Notices
A,(ttachment 1 IN 98-36 September 18, 1998 LIST OF RECENTLY ISSUED
NRC INFORMATION NOTICES
Information Date of
Notice No. Subject Issuance Issued to
98-35 Threat Assessments and 914/98 All U.S. NRC fuel cycle facilities
Consideration of Heightened power and non-power reactor
Physical Protection Measures licensees (Safeguard issues, not
for public disclosure.)
98-34 NRC Configuration Control 8/28/98 All holders of Operating licenses
Errors for nuclear power reactors, except
for those who have ceased
operations and have certified that
fuel has been permanently
removed from the reactor vessel
98-33 NRC Regulations Prohibit 8128198 All holders of a U.S. Nuclear
Agreements that restrict or Regulatory Commission (NRC)
Discourage an Employee from license.
Participating In Protected Activities
98-32 Problems Associated with Post- 8126198 All holders of operating licenses
Fire Safe-Shutdown Circuit for nuclear power reactors, except
Analyses those who have permanently
ceased operations and have
certified that fuel has been
permanently removed form the
reactor
98-31 Fire Protection System Design 8/26/98 All holders of operating licences
Deficiencies and Common-Mode for nuclear power reactors, except
Flooding of Emergency Core Cooling those licensees that have
System Rooms at Washington Nuclear permanently ceased operations
Project Unit 2 and have certified that fuel has
been permanently removed from
the reactor vessel.
OL = Operating License
CP = Construction Permit
- IN 98-36 September 18, 1998 This information notice requires no specific action or written response. However, recipients are
reminded that they are required to consider industry-wide operating experience (including NRC
INs) where practical, when setting goals and performing periodic evaluations under Section
50.65, "Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power
Plants," of Part 50 of Title 10 of the Code of Federal Regulations. If you have any questions
about the information in this notice, please contact one of the technical contacts listed below or
the appropriate Office of Nuclear Reactor Regulation (NRR) project manager.
Jack W. Roe, Acting Director
Division of Reactor Program Management
Office of Nuclear Reactor Regulation
Technical contacts: Mike Kunowski, Region IlIl John Neisler, Region IlIl
630-829-9816 630-829-9718 E-mail: mak3@nrc.gov E-mail: jhn@nrc.gov
Attachment: List of Recently Issued NRC Information Notices
- See previous concurrence & e.
C,,tt
DOCUMENT NAME: G:\NICK\REGION.IN
To receive a copy of this document, indicate in the box C=Copy wlo attachment/enclosure E=Copy with attachmentlenclosure N = No copy
OFFICE PECB I Tech EdI Reg III [ Regil I PECB I C:PECB l_ji D M
NAME NFields* RSanders* MKunowski** JNeisler** RDennig* JStolz* JRo
DATE 09/03/98 08/26/98 09/03/98 Ii09/03/98 09/14/98 J09/14/98 \/98 OFFICIAL RECORD COPY
IN 98-xx
September xx, 1998 This information notice requires no specific action or written response. However, recipie are
reminded that they are required to consider industry-wide operating experience (includ g NRC
INs) where practical, when setting goals and performing periodic evaluations under ection
50.65, "Requirements for Monitoring the Effectiveness of Maintenance at Nuclea ower
Plants," of Part 50 of Title 10 of the Code of Federal Regulations. If you have ny questions
about the information in this notice, please contact one of the technical con cts listed below or
the appropriate Office of Nuclear Reactor Regulation (NRR) project man er.
Jack W. Roe, Acting irector
Division of Reactor rogram Management
Office of Nuclea eactor Regulation
Technical contacts: Mike Kunowski, Region IlIl Joh eisler, Region IlIl
630-829-9816 63 -829-9718 E-mail: mak3@nrc.gov -mail: jhn@nrc.gov
Attachment: List of Recently Issued NRC Info tion Notices
DOCUMENT NAME: G:\NICK\REGION.IN
To receive a copy of this document, Indicate in the box C=Copy wlo attachmentenclosure E=Copy with attachmentlenclosure N = No copy
OFFICE PECB. I _ Tech Ed I _ Reg I lI _I Reg 11 l 1/E "ECB (A)D:DRPM l
NAME NFiells' { RSanders MKu owsk Jeisler ennig l l JRoe
l DATE /3/98 1SW98 17/3/98 15/3198 lH/ 48 q/l98 l I /98 OFFICIAL RECORD COPY I
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list | - Information Notice 1998-01, Thefts of Portable Gauges (15 January 1998, Topic: Shutdown Margin, Moisture Density Gauge, Stolen)
- Information Notice 1998-02, Nuclear Power Plant Cold Weather Problems and Protective Measures (21 January 1998)
- Information Notice 1998-03, Inadequate Verification of Overcurrent Trip Setpoints in Metal-Clad, Low-Voltage Circuit Breakers (21 January 1998)
- Information Notice 1998-04, 1997 Enforcement Sanctions for Deliberate Violations of NRC Employee Protection Requirements (9 February 1998)
- Information Notice 1998-05, Criminal History Record Information (11 February 1998)
- Information Notice 1998-06, Unauthorized Use of License to Obtain Radioactive Materials, and Its Implication Under the Expanded Title 18 of the U.S. Code (19 February 1998)
- Information Notice 1998-07, Offsite Power Reliability Challenges from Industry Deregulation (27 February 1998)
- Information Notice 1998-08, Information Likely to Be Requested If an Emergency is Declared (2 March 1998)
- Information Notice 1998-08, Information Likely to Be Requested If an Emergency Is Declared (2 March 1998)
- Information Notice 1998-09, Collapse of an Isocam II, Dual-Headed Nuclear Medicine Gamma Camera (5 March 1998)
- Information Notice 1998-10, Probable Misadministrations Occurring During Intravascular Brachytherapy with Novoste Beta-cath System (9 March 1998, Topic: Brachytherapy)
- Information Notice 1998-11, Cracking of Reactor Vessel Internal Baffle Former Bolts in Foreign Plants (25 March 1998, Topic: Fire Barrier, Brachytherapy)
- Information Notice 1998-12, Licensees' Responsibilities Regarding Reporting & Follow-up Requirements for Nuclear-Powered Pacemakers (3 April 1998, Topic: Fire Barrier, Brachytherapy, Stolen)
- Information Notice 1998-13, Post-Refueling Outage Reactor Pressure Vessel Leak Testing Before Core Criticality (20 April 1998, Topic: Fire Barrier, VT-2, Pressure Boundary Leakage, Brachytherapy)
- Information Notice 1998-14, Undocumented Changes to Non-Power Reactor Safety System Wiring (20 April 1998, Topic: Brachytherapy)
- Information Notice 1998-15, Integrity of Operator Licensing Examinations (20 April 1998, Topic: Fire Barrier, Job Performance Measure)
- Information Notice 1998-16, Inadequate Operational Checks of Alarm Ratemeters (30 April 1998, Topic: Brachytherapy)
- Information Notice 1998-17, Federal Bureau of Investigation'S (FBI) Awareness of National Security Issues and Response (ANSIR) Program (7 May 1998)
- Information Notice 1998-17, Federal Bureau of Investigation'S (FBI) Awareness of National Security Issues and Response (Ansir) Program (7 May 1998, Topic: Brachytherapy)
- Information Notice 1998-18, Recent Contamination Incidences Resulting from Failure to Perform Adequate Surveys (13 May 1998, Topic: Brachytherapy)
- Information Notice 1998-19, Shaft Binding in General Electric Type Sbm Control Switches (3 June 1998)
- Information Notice 1998-20, Problems with Emergency Preparedness Respiratory Protection Programs (3 June 1998, Topic: Brachytherapy)
- Information Notice 1998-21, Potential Deficiency of Electrical Cable/Connection Systems (4 June 1998)
- Information Notice 1998-22, Deficiencies Identified During NRC Design Inspections (17 June 1998, Topic: Stroke time, Tornado Missile)
- Information Notice 1998-23, Crosby Relief Valve Setpoint Drift Problems Caused by Corrosion of Guide Ring (23 June 1998, Topic: Loop seal, Condition Adverse to Quality)
- Information Notice 1998-25, Loss of Inventory from Safety-Related Closed-Loop Cooling Water Systems (8 July 1998, Topic: Ultimate heat sink)
- Information Notice 1998-26, Settlement Monitoring and Inspection of Plant Structures Affected by Degradation of Porous Concrete Subfoundations (24 July 1998, Topic: Condition Adverse to Quality)
- Information Notice 1998-27, Steam Generator Tube End Cracking (24 July 1998)
- Information Notice 1998-28, Development of Systematic Sample Plan for Operator Licensing Examinations (31 July 1998)
- Information Notice 1998-29, Predicted Increase in Fuel Rod Cladding Oxidation (3 August 1998, Topic: Fuel cladding)
- Information Notice 1998-30, Effect of Year 2000 Computer Problem on NRC Licensees and Certificate Holders (12 August 1998, Topic: Brachytherapy)
- Information Notice 1998-31, Fire Protection System Design Deficiencies and Common-Mode Flooding of Emergency Core Cooling System Rooms at Washington Nuclear Project Unit 2 (18 August 1998)
- Information Notice 1998-33, NRC Regulations Prohibit Agreements That Restrict or Discourage an Employee from Participating in Protected Activities (28 August 1998, Topic: Brachytherapy)
- Information Notice 1998-34, Configuration Control Errors (28 August 1998)
- Information Notice 1998-36, Inadequate or Poorly Controlled, Non-Safety-Related Maintenance Activities Unnecessarily Challenged Safety Systems (18 September 1998)
- Information Notice 1998-37, Eligibility of Operator License Applicants (1 October 1998)
- Information Notice 1998-38, Metal-Clad Circuit Breaker Maintenance Issues Identified by NRC Inspections (15 October 1998, Topic: Overtravel)
- Information Notice 1998-39, Summary of Fitness-for-Duty Program Performance Reports for Calendar Years 1996 and 1997 (30 October 1998, Topic: Fitness for Duty)
- Information Notice 1998-40, Design Deficiencies Can Lead to Reduced ECCS Pump Net Positive Suction Head During Design-Basis Accidents (26 October 1998)
- Information Notice 1998-41, Spurious Shutdown of Emergency Diesel Generators From Design Oversight (20 November 1998)
- Information Notice 1998-41, Spurious Shutdown of Emergency Diesel Generators from Design Oversight (20 November 1998)
- Information Notice 1998-42, Implementation of 10 CFR 55.55a(g) Inservice Inspection Requirements (1 December 1998)
- Information Notice 1998-43, Leaks in Emergency Diesel Generator Lubricating Oil & Jacket Cooling Water Piping (4 December 1998)
- Information Notice 1998-44, Ten-Year Inservice Inspection (ISI) Program Update for Licensees That Intend to Implement Risk-Informed ISI of Piping (10 December 1998, Topic: Probabilistic Risk Assessment)
- Information Notice 1998-45, Cavitation Erosion of Letdown Line Orifices Resulting in Fatigue Cracking of Pipe Welds (15 December 1998)
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