ML18030A123: Difference between revisions

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| issue date = 07/03/1980
| issue date = 07/03/1980
| title = Supplemental Deficiency Rept Re Pacific Check Valves. Problems W/Check Valve Operation in Unit 1 Core Spray Pump Discharge Vertical Pipe Run Will Necessitate Rework of Bonnet Stops.Final Rept Will Be Provided by Sept 1980
| title = Supplemental Deficiency Rept Re Pacific Check Valves. Problems W/Check Valve Operation in Unit 1 Core Spray Pump Discharge Vertical Pipe Run Will Necessitate Rework of Bonnet Stops.Final Rept Will Be Provided by Sept 1980
| author name = CURTIS N W
| author name = Curtis N
| author affiliation = PENNSYLVANIA POWER & LIGHT CO.
| author affiliation = PENNSYLVANIA POWER & LIGHT CO.
| addressee name =  
| addressee name =  
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=Text=
=Text=
{{#Wiki_filter:REGULATOR INFORMATION DISTRIBUTION STEM(RIDS)AUT~CURTISgN~'i'I~RECIP~NAMEACCESSION NBRt8007080213 DOC~DATE:80/07/03NOTARIZED!
{{#Wiki_filter:REGULATOR     INFORMATION DISTRIBUTION         S    TEM  (RIDS)
NOFACIL:Susquehanna SteamElectricStation<UnitirPennsylva Susquehanna SteamElectricStationrUnit2iPennsylva AUTHORAFFILIATION Pennsylvania Po~erLLightCo,RECIPIENT AFFILIATION DOCKET&#xb9;0500038705000388
ACCESSION NBRt8007080213                     DOC ~ DATE: 80/07/03 NOTARIZED! NO                  DOCKET  &#xb9; FAC IL:                 Susquehanna     Steam Electric Station< Unit ir Pennsylva              05000387 Susquehanna     Steam Electric Stationr Unit 2i Pennsylva              05000388 AUT ~                          AUTHOR  AFFILIATION CURT IS g N ~
                'i'I
                    ~          Pennsylvania Po~er L Light Co, REC IP ~ NAME                  RECIPIENT AFFILIATION


==SUBJECT:==
==SUBJECT:==
Supplcmentaldeficiency reptrePacificcheckvalves.Problemsw/checkvalveoperation inUnit1corespraypumpoischarge verticalpiperunwillnecessitate reworkofexistingbonnetstops,FinalreptwillbeprovidedbySeptDISTRIBUTION COOK:8001SCOPIESRECEIVED:1.TR QENCL+SIZE:TITLE:PSAR/FSAR AMOTSandRelatedCorr'espondence NOTESeSFA/3RECIPIENT IOCODE/NAME ACTION:AOI-lC8'h/$/A/G.LARrA<HBRoo]c',
Suppl cmental                deficiency rept re Paci f ic check valves.
WCOPIESLTTRENC11RECIPIENT LIOCODE/NAME BCyeuNr"Bc.ooo,B.PMSrWZ,8,.05COPIKSLTTRENCINTERNAL:
Problems w/check valve operation in Unit 1 core spray pump oischarge vertical pipe run will necessitate rework of existing bonnet stops, Final rept will be provided by Sept DISTRIBUTION COOK: 8001S                  COPIES RECEIVED:1.TR     QCorENCL      + SIZE:
A/DCORE8CS13AUXSYSBR18CONTSYSBROIRrHUMFACSFYEFFTRSYSBRENVENGBRGEOSCIENBR09I8CSYSBR20KIRKWOODgR~29MECHKiNGBRNRCPOR02POLYERSYSBRQABR10REACSYSBRSITANALBR271111'11111141111111111ACCIDEVALBRCHEMENGBRCOREPERFBR17DIRECTORNRREMERG.PREP 22EQUIPQUALBRHYD/GEOBR11IEE06MATLENGBRMPAOELOPROC/TSTREVBRRAOASSESSBR12REGFILE011111113111111EXTERNAL:
TITLE:     PSAR/FSAR AMOTS and Rel ated            r'espondence NOTES  e SFA/3 RECIPIENT              COPIES            RECIPIENT                COP IKS IO CODE/NAME               LTTR ENC L        IO CODE/NAME            LTTR ENC ACTION:       AO      I-l C8'h/$ /A/G.       1            BC  ye uNr" Bc.ooo, B.
ACRSNSIC30041011LPDR03JULl01980OTOTALNUMBEROFCOPIESREQUIRED:
LA RrA<HBRoo]c', W              1            PM  SrWZ,   8,. 05 INTERNAL: A/D CORE              8  CS13      1            ACCID EVAL BR                1 AUX SYS BR              18      1      1    CHEM ENG BR                  1 CONT SYS BR                      1'           CORE PERF BR 17              1 OIRr HUM FAC SFY                1      1    DIRECTOR NRR                1 EFF TR SYS BR                    1      1    EMERG.PREP         22      1 ENV ENG BR                      1      1    EQUIP QUAL BR                1 GEOSC IEN BR            09      4            HYD/GEO BR          11 I8C SYS BR              20      1      1    IEE                06      3 K IRKWOODg R ~          29      1      1    MATL ENG BR                  1 MECH KiNG BR                    1            MPA                          1 NRC        POR          02      1            OELO                        1 POLYER        SYS BR            1            PROC/TST REV BR              1 QA BR                  10      1            RAO ASSESS BR12 REAC SYS BR                      1            REG  FILE          01      1 SIT ANAL          BR  27      1                                        1 EXTERNAL: ACRS                        30      10    1      LPDR                03 NSIC                    04      1 JUL  l0  1980 O
LTTR51ENCL TWONORTHNINTHSTREET.ALLENTOWN, PA.18'101PHONE:(215)821-5151NORMANW.CURTISVicePrestrtent.Engineering
TOTAL NUMBER OF COPIES                REQUIRED: LTTR      51    ENCL
&Construction 821-5381July3,1980Mr.BoyceH.GrierDirector, RegionIU.S.NuclearRegulatory Commission 631ParkAvenueKingofPrussia,Pennsylvania 19406SUSQUEHANNA STEAMELECTRICSTATIONUPDATEINTHESTATUSOFADEFICIENCY ONPACIFICCHECKVALVESERs100450/100508 FILE840-4/900-10 PLA-502.
 
TWO NORTH NINTH STREET. ALLENTOWN, PA. 18'101 PHONE: (215) 821-5151 NORMAN W. CURTIS Vice Prestrtent.Engineering & Construction 821-5381 July 3, 1980 Mr. Boyce H. Grier Director, Region            I U. S. Nuclear Regulatory Commission 631 Park Avenue King of Prussia, Pennsylvania 19406 SUSQUEHANNA STEAM ELECTRIC STATION UPDATE IN THE STATUS OF A DEFICIENCY ON PACIFIC CHECK VALVES ERs    100450/100508           FILE 840-4/900-10 PLA-502.


==Reference:==
==Reference:==
PLA-466  of March 31, 1980
==Dear Mr.        Grier:==


PLA-466ofMarch31,1980
This supplements the above referenced correspondence and provides an update of the information provided in our PLA-466.
Unanticipated problems with check valve operation in the Unit I Core Spray pump discharge vertical pipe run will necessitate rework of the existing bonnet stops. Bechtel NCR 5913 documents this latest discrepancy.
The original problem remains open under MCAR 1-47.
We    expect to provide a        final report to    the Commission by September,   1980.
Very      truly yours, N. W.      Curtis Vice President-Engineering            a  Construction<<Nuclear FLWsjmk Ps,a PENNSYLVANIA POWER  IL  LIGHT COMPANY 8 OOV080 zi9


==DearMr.Grier:==
Mr. Boyce H. Grier                                       June 27, 1980 cc: Mr. Victor Stello (15) copies DirectorWffice of Inspection 8    Enforcement.
Thissupplements theabovereferenced correspondence andprovidesanupdateoftheinformation providedinourPLA-466.Unanticipated problemswithcheckvalveoperation intheUnitICoreSpraypumpdischarge verticalpiperunwillnecessitate reworkoftheexistingbonnetstops.BechtelNCR5913documents thislatestdiscrepancy.
U. S. Nuclear Regulatory Commission Washington, D.C. 20555 Mr. G. McDonald, Director (1)
TheoriginalproblemremainsopenunderMCAR1-47.WeexpecttoprovideafinalreporttotheCommission bySeptember, 1980.Verytrulyyours,N.W.CurtisVicePresident-Engineering aConstruction<<Nuclear FLWsjmkPs,aPENNSYLVANIA POWERILLIGHTCOMPANY8OOV080zi9 Mr.BoyceH.GrierJune27,1980cc:Mr.VictorStello(15)copiesDirectorWffice ofInspection 8Enforcement.
Office of  Management Information & Program Control U. S. Nuclear Regulatory Commission Washington, D.C. 20555 Mr. Robert,,M. Gallo U. S. Nuclear Regulatory Commission P. O. Box 52 Shickshinny, Pennsylvania 1S655}}
U.S.NuclearRegulatory Commission Washington, D.C.20555Mr.G.McDonald, Director(1)OfficeofManagement Information
&ProgramControlU.S.NuclearRegulatory Commission Washington, D.C.20555Mr.Robert,,M.
GalloU.S.NuclearRegulatory Commission P.O.Box52Shickshinny, Pennsylvania 1S655}}

Latest revision as of 01:47, 22 October 2019

Supplemental Deficiency Rept Re Pacific Check Valves. Problems W/Check Valve Operation in Unit 1 Core Spray Pump Discharge Vertical Pipe Run Will Necessitate Rework of Bonnet Stops.Final Rept Will Be Provided by Sept 1980
ML18030A123
Person / Time
Site: Susquehanna  Talen Energy icon.png
Issue date: 07/03/1980
From: Curtis N
PENNSYLVANIA POWER & LIGHT CO.
To:
References
PLA-502, NUDOCS 8007080213
Download: ML18030A123 (3)


Text

REGULATOR INFORMATION DISTRIBUTION S TEM (RIDS)

ACCESSION NBRt8007080213 DOC ~ DATE: 80/07/03 NOTARIZED! NO DOCKET ¹ FAC IL: Susquehanna Steam Electric Station< Unit ir Pennsylva 05000387 Susquehanna Steam Electric Stationr Unit 2i Pennsylva 05000388 AUT ~ AUTHOR AFFILIATION CURT IS g N ~

'i'I

~ Pennsylvania Po~er L Light Co, REC IP ~ NAME RECIPIENT AFFILIATION

SUBJECT:

Suppl cmental deficiency rept re Paci f ic check valves.

Problems w/check valve operation in Unit 1 core spray pump oischarge vertical pipe run will necessitate rework of existing bonnet stops, Final rept will be provided by Sept DISTRIBUTION COOK: 8001S COPIES RECEIVED:1.TR QCorENCL + SIZE:

TITLE: PSAR/FSAR AMOTS and Rel ated r'espondence NOTES e SFA/3 RECIPIENT COPIES RECIPIENT COP IKS IO CODE/NAME LTTR ENC L IO CODE/NAME LTTR ENC ACTION: AO I-l C8'h/$ /A/G. 1 BC ye uNr" Bc.ooo, B.

LA RrA<HBRoo]c', W 1 PM SrWZ, 8,. 05 INTERNAL: A/D CORE 8 CS13 1 ACCID EVAL BR 1 AUX SYS BR 18 1 1 CHEM ENG BR 1 CONT SYS BR 1' CORE PERF BR 17 1 OIRr HUM FAC SFY 1 1 DIRECTOR NRR 1 EFF TR SYS BR 1 1 EMERG.PREP 22 1 ENV ENG BR 1 1 EQUIP QUAL BR 1 GEOSC IEN BR 09 4 HYD/GEO BR 11 I8C SYS BR 20 1 1 IEE 06 3 K IRKWOODg R ~ 29 1 1 MATL ENG BR 1 MECH KiNG BR 1 MPA 1 NRC POR 02 1 OELO 1 POLYER SYS BR 1 PROC/TST REV BR 1 QA BR 10 1 RAO ASSESS BR12 REAC SYS BR 1 REG FILE 01 1 SIT ANAL BR 27 1 1 EXTERNAL: ACRS 30 10 1 LPDR 03 NSIC 04 1 JUL l0 1980 O

TOTAL NUMBER OF COPIES REQUIRED: LTTR 51 ENCL

TWO NORTH NINTH STREET. ALLENTOWN, PA. 18'101 PHONE: (215) 821-5151 NORMAN W. CURTIS Vice Prestrtent.Engineering & Construction 821-5381 July 3, 1980 Mr. Boyce H. Grier Director, Region I U. S. Nuclear Regulatory Commission 631 Park Avenue King of Prussia, Pennsylvania 19406 SUSQUEHANNA STEAM ELECTRIC STATION UPDATE IN THE STATUS OF A DEFICIENCY ON PACIFIC CHECK VALVES ERs 100450/100508 FILE 840-4/900-10 PLA-502.

Reference:

PLA-466 of March 31, 1980

Dear Mr. Grier:

This supplements the above referenced correspondence and provides an update of the information provided in our PLA-466.

Unanticipated problems with check valve operation in the Unit I Core Spray pump discharge vertical pipe run will necessitate rework of the existing bonnet stops. Bechtel NCR 5913 documents this latest discrepancy.

The original problem remains open under MCAR 1-47.

We expect to provide a final report to the Commission by September, 1980.

Very truly yours, N. W. Curtis Vice President-Engineering a Construction<<Nuclear FLWsjmk Ps,a PENNSYLVANIA POWER IL LIGHT COMPANY 8 OOV080 zi9

Mr. Boyce H. Grier June 27, 1980 cc: Mr. Victor Stello (15) copies DirectorWffice of Inspection 8 Enforcement.

U. S. Nuclear Regulatory Commission Washington, D.C. 20555 Mr. G. McDonald, Director (1)

Office of Management Information & Program Control U. S. Nuclear Regulatory Commission Washington, D.C. 20555 Mr. Robert,,M. Gallo U. S. Nuclear Regulatory Commission P. O. Box 52 Shickshinny, Pennsylvania 1S655