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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18026A4931998-03-30030 March 1998 LER 97-007-01:on 971017,entry Into TS 3.0.3 Occurred to Allow Completion of Surveillance Testing of One Channel of Rbm.Caused by Failure of Components in LPRM Output to Rbm. Submitted TS Change Request to Extend LCO Action Statement ML18026A4891997-11-17017 November 1997 LER 97-007-00:on 971017,TS 3.0.3 Entry Voluntarily Made. Caused by Inadequate Post Maint Testing Following Earlier Work Associated W/Components.Failed Components Repaired, Replaced & Testing Completed ML18026A5961996-01-0202 January 1996 LER 95-013-00:on 951119,thermally Induced Pressure Locking of HPCI Valve Occurred Under Bonnet Pressure of 3,000-7,000 Psig.Damaged HPCI Injection Valve repaired.W/960102 Ltr ML18017A0461995-07-0707 July 1995 LER 95-008-00:on 950609,shift Average Licensed Core Thermal Power Was Exceeded.Caused by Failed Instrumentation Drift. Repaired & Recalibrated Subject Instrumentation ML18026A4261993-06-0909 June 1993 LER 90-007-01:on 900705,primary Power Supply to RPS a Power Distribution Panel Lost When One Electrical Protection Assembly (EPA) Breaker Tripped.Epa Logic Cards Reviewed & RPS Power Supply Will Be redesigned.W/930609 Ltr ML18026A4231992-11-17017 November 1992 LER 92-016-00:on 920416,discovered That Existing Analysis for Two Spent Fuel Storage Pools Did Not Reflect Current Fuel Design & Plant Operation.Caused by Failure to Modify FSAR Analysis.Fsar Will Be revised.W/921117 Ltr ML18017A0391991-07-26026 July 1991 LER 91-010-00:on 910628,RWCU Isolated on Two Occassions Due to Actuations of Steam Leak Detection Instrumentation. Caused by Design Deficiency & Elevated Ambient Penetration Room Temps.Temp Modules replaced.W/910726 Ltr ML17227A2311991-07-23023 July 1991 LER 91-009-00:on 910624,RWCU Steam Leak Detection Instrumentation Discovered to Be Inadvertently Actuated During Routine Functional Testing.Caused by Adequate Verbal Communication.Technicians briefed.W/910723 Ltr ML18026A5251991-07-0505 July 1991 LER 91-006-00:on 910608,unplanned Actuations of ESF Occurred.Caused by Unexpected Trip of Primary Power Supply EPA Breaker Losing Power.Breakers Reset & Full Power Operation Continued uninterupted.W/910705 Ltr ML20005F3401990-01-0404 January 1990 LER 89-010-01:on 890920,determined That Estimated Leakage for Main Steam Line Containment Penetrations a & B Exceeded Tech Spec Limit During Local Leak Rate Testing.Cause Not Determined.Msiv Poppet Seats & Discs lapped.W/900104 Ltr ML18040A9121988-09-23023 September 1988 LER 88-018-00:on 880824,discovered That RWCU Pump Room Ambient Temp Sensor Not Installed Per Design.Caused by Lack of Installation Detail on Design Documents for Steam Leak Detection Sys.Tech Spec Change submitted.W/880923 Ltr ML19310G9421986-04-21021 April 1986 LER 86-005-00:on 860321 Differential Pressure Condition Detected,Causing Supply Dampers to Oscillate.Caused by Open Plenum Door & Exhaust Damper Linkage Binding.Linkage Reworked & lubricated.W/860421 Ltr ML20024D9141983-07-26026 July 1983 Updated LER 83-035/03X-1:on 830228,during 4 H RCS Unidentified Leakage Test,Pump B of Drywell Sump a Continued to Operate for 4 H W/O Change in Sump Level.Caused by Clogged Pump Impeller.Pump cleaned.W/830726 Ltr ML20024E1601983-07-25025 July 1983 LER 83-098/03L-0:on 830625,position of Valve Indeterminate Due to Dual Status Indication for Suppression pool-to- Drywell Vacuum Breaker.Caused by Insufficient Limit Switch Plunger Position.Limit Switches adjusted.W/830725 Ltr ML20024D9911983-07-22022 July 1983 LER 83-096/03L-0:on 830624,RCIC Leak Detection B Power Failure Alarm Received.Undervoltage Trip Caused by Loss of Startup Transformer.Inverter Manually reset.W/830722 Ltr ML20024C2381983-06-29029 June 1983 LER 83-088/03L-0:on 830530,RCIC Pump Discharge Valve Would Not Open.Caused by Gap Between Breaker Male & Female Stab Clips.Female Clips Reworked to Allow Proper Contact. W/830629 Ltr ML20024C1001983-06-24024 June 1983 LER 83-085/03L-0:on 830525,containment Isolation Valve for Containment Atmosphere Control Sample Line Failed to Close. Cause Not Stated.Maint Personnel Verified Switch Positioning & Reconnected circuitry.W/830624 Ltr ML20024C1141983-06-24024 June 1983 LER 83-087/03L-0:on 830527,A Containment H2/02 Analyzers Found to Have Erratic Readings.Caused by Pressure Control Valve & Sample Pump Degradation to Point Where Proper Flow Not Maintained.Failed Components replaced.W/830624 Ltr ML20024C2451983-06-24024 June 1983 LER 83-086/03L-0:on 830525,reactor Bldg Door Opened While Maint Performed on Turbine Bldg Side of Air Lock to Reactor Bldg.Caused by Personnel Error.Individual W/Radio Communication Will Be posted.W/830624 Ltr ML20024A8401983-06-21021 June 1983 LER 83-082/01T-0:on 830607,main Turbine Trip on High Reactor Pressure Vessel Level Bypassed to Clear Interlock.After Outage,Bypass Discovered Still Installed.Caused by Lack of Clear Requirement for Bypass review.W/830621 Ltr ML20024A3301983-05-27027 May 1983 LER 83-075/01T-0:on 830515,found Chlorine Detectors on Control Room Emergency Outside Air Supply May Prevent Operation in Pressurization Mode Following Loss of Power. Emergency Operation Procedures revised.W/830527 Ltr ML20024A3421983-05-27027 May 1983 LER 83-070/01T-0:on 830517,flow Rates Required to Maintain Positive Pressure in Control Structure Appeared to Exceed Tech Spec Limits.Flow Limit Inadvertently Omitted from Procedure.Procedure corrected.W/830527 Ltr ML20024A5331983-05-27027 May 1983 LER 83-067/01T-0:on 830516,reactor Mode Switch Placed in Startup Position & Half Scram Developed.Caused by Improper Functioning of Reactor Mode Switch Contacts.Switch Replaced. W/830527 Ltr ML20023D5121983-05-11011 May 1983 LER 83-063/03L-0:on 830411,main Steam Line Drain Valve Leakage Exceeded Tech Spec Limit.Cause Not Stated.Seal Ring Replaced,Outboard Valve Lapped & Valves Reassembled ML20023B8381983-04-29029 April 1983 LER 83-057/01P-0:confirms 830428 Telcon Re Incident Concerning Bypass Leakage Calculations for Feedwater Following DBA LOCA ML20028D6871983-01-10010 January 1983 LER 83-001/01P-0:confirms 830107 Telcon Re Failure to Comply W/Action Statement Requiring Grab Samples of Offgas Sys After Declaring One Train of Hydrogen Monitor Inoperable. Caused by Inadequate Shift Turnover in Chemistry Dept ML20028D3141983-01-0707 January 1983 LER 82-072/03L-0:on 821210,while Performing Surveillance, One Control Rod Would Not Indicate at One Position.Possibly Caused by Intermittent Fault on Circuit Board.Printed Circuit Board Reinstalled ML20028D2871983-01-0606 January 1983 LER 82-069/03L-0:on 821207,during Startup Testing,Hpci Sys Declared Operable Prior to Closing Out Open Equipment Release Form.Caused by Work Program Design Weakness.Present Work Practice Modified ML20028B5821982-11-19019 November 1982 Revised LER 82-026/01T-1:on 820717,review Revealed Certain Cables Discussed in Deficiency Rept 80-00-28 Not Flexed or Grounded Prior to Fuel Load.Caused by Failure to Maintain Control Over Fddr KRI-607 During Turnover of Const ML20028B0301982-11-18018 November 1982 LER 82-042/01T-0:on 821117,personnel Failed to Take Grab Samples When RHR Svc Water Sys Radiation Monitor Was Inoperable ML20028B4351982-11-18018 November 1982 LER 82-043/01T-0:on 821117,determined That Failure of Single Component Could Defeat Overload Detection & Protection Devices for Containment Penetration Carrying Power Cables for Reactor Recirculation Pumps.Cause Not Stated ML20028A9541982-11-16016 November 1982 LER 82-040/03L-0:on 821018,deluge Sys in CREOASS Initiated. Caused by Maint Personnel Bumping Fire Sys thermo-switch on Charcoal Beds.Charcoal Changed Out & Preventive Maint Procedures Modified to Valve Out Deluge Sys During Maint ML17139B0311982-09-13013 September 1982 LER 82-013/03L-0:on 820814,radiation Monitor Found Inoperable.Caused by Faulty Gm Tube & Signal Conditioner (Sensor Converter).Tube & Signal Conditioner Replaced & Monitor Returned to Svc ML20027B0571982-09-0808 September 1982 LER 82-007/01T-1:on 820825,updated Secondary Containment Vol Calculation Had Not Replaced Preliminary Analysis Utilized to Obtain Values in Fsar.Vol Based on Preliminary Calculation Which Did Not Account for Floors & Equipment ML17139A9071982-08-0202 August 1982 LER 82-001/01T-0:on 820718,unacceptable Linear Indications Found by Radiograph of A-11 Weld.Cause Not Determined.Welds Repaired Per Approved Repair Program 1998-03-30
[Table view] Category:RO)
MONTHYEARML18026A4931998-03-30030 March 1998 LER 97-007-01:on 971017,entry Into TS 3.0.3 Occurred to Allow Completion of Surveillance Testing of One Channel of Rbm.Caused by Failure of Components in LPRM Output to Rbm. Submitted TS Change Request to Extend LCO Action Statement ML18026A4891997-11-17017 November 1997 LER 97-007-00:on 971017,TS 3.0.3 Entry Voluntarily Made. Caused by Inadequate Post Maint Testing Following Earlier Work Associated W/Components.Failed Components Repaired, Replaced & Testing Completed ML18026A5961996-01-0202 January 1996 LER 95-013-00:on 951119,thermally Induced Pressure Locking of HPCI Valve Occurred Under Bonnet Pressure of 3,000-7,000 Psig.Damaged HPCI Injection Valve repaired.W/960102 Ltr ML18017A0461995-07-0707 July 1995 LER 95-008-00:on 950609,shift Average Licensed Core Thermal Power Was Exceeded.Caused by Failed Instrumentation Drift. Repaired & Recalibrated Subject Instrumentation ML18026A4261993-06-0909 June 1993 LER 90-007-01:on 900705,primary Power Supply to RPS a Power Distribution Panel Lost When One Electrical Protection Assembly (EPA) Breaker Tripped.Epa Logic Cards Reviewed & RPS Power Supply Will Be redesigned.W/930609 Ltr ML18026A4231992-11-17017 November 1992 LER 92-016-00:on 920416,discovered That Existing Analysis for Two Spent Fuel Storage Pools Did Not Reflect Current Fuel Design & Plant Operation.Caused by Failure to Modify FSAR Analysis.Fsar Will Be revised.W/921117 Ltr ML18017A0391991-07-26026 July 1991 LER 91-010-00:on 910628,RWCU Isolated on Two Occassions Due to Actuations of Steam Leak Detection Instrumentation. Caused by Design Deficiency & Elevated Ambient Penetration Room Temps.Temp Modules replaced.W/910726 Ltr ML17227A2311991-07-23023 July 1991 LER 91-009-00:on 910624,RWCU Steam Leak Detection Instrumentation Discovered to Be Inadvertently Actuated During Routine Functional Testing.Caused by Adequate Verbal Communication.Technicians briefed.W/910723 Ltr ML18026A5251991-07-0505 July 1991 LER 91-006-00:on 910608,unplanned Actuations of ESF Occurred.Caused by Unexpected Trip of Primary Power Supply EPA Breaker Losing Power.Breakers Reset & Full Power Operation Continued uninterupted.W/910705 Ltr ML20005F3401990-01-0404 January 1990 LER 89-010-01:on 890920,determined That Estimated Leakage for Main Steam Line Containment Penetrations a & B Exceeded Tech Spec Limit During Local Leak Rate Testing.Cause Not Determined.Msiv Poppet Seats & Discs lapped.W/900104 Ltr ML18040A9121988-09-23023 September 1988 LER 88-018-00:on 880824,discovered That RWCU Pump Room Ambient Temp Sensor Not Installed Per Design.Caused by Lack of Installation Detail on Design Documents for Steam Leak Detection Sys.Tech Spec Change submitted.W/880923 Ltr ML19310G9421986-04-21021 April 1986 LER 86-005-00:on 860321 Differential Pressure Condition Detected,Causing Supply Dampers to Oscillate.Caused by Open Plenum Door & Exhaust Damper Linkage Binding.Linkage Reworked & lubricated.W/860421 Ltr ML20024D9141983-07-26026 July 1983 Updated LER 83-035/03X-1:on 830228,during 4 H RCS Unidentified Leakage Test,Pump B of Drywell Sump a Continued to Operate for 4 H W/O Change in Sump Level.Caused by Clogged Pump Impeller.Pump cleaned.W/830726 Ltr ML20024E1601983-07-25025 July 1983 LER 83-098/03L-0:on 830625,position of Valve Indeterminate Due to Dual Status Indication for Suppression pool-to- Drywell Vacuum Breaker.Caused by Insufficient Limit Switch Plunger Position.Limit Switches adjusted.W/830725 Ltr ML20024D9911983-07-22022 July 1983 LER 83-096/03L-0:on 830624,RCIC Leak Detection B Power Failure Alarm Received.Undervoltage Trip Caused by Loss of Startup Transformer.Inverter Manually reset.W/830722 Ltr ML20024C2381983-06-29029 June 1983 LER 83-088/03L-0:on 830530,RCIC Pump Discharge Valve Would Not Open.Caused by Gap Between Breaker Male & Female Stab Clips.Female Clips Reworked to Allow Proper Contact. W/830629 Ltr ML20024C1001983-06-24024 June 1983 LER 83-085/03L-0:on 830525,containment Isolation Valve for Containment Atmosphere Control Sample Line Failed to Close. Cause Not Stated.Maint Personnel Verified Switch Positioning & Reconnected circuitry.W/830624 Ltr ML20024C1141983-06-24024 June 1983 LER 83-087/03L-0:on 830527,A Containment H2/02 Analyzers Found to Have Erratic Readings.Caused by Pressure Control Valve & Sample Pump Degradation to Point Where Proper Flow Not Maintained.Failed Components replaced.W/830624 Ltr ML20024C2451983-06-24024 June 1983 LER 83-086/03L-0:on 830525,reactor Bldg Door Opened While Maint Performed on Turbine Bldg Side of Air Lock to Reactor Bldg.Caused by Personnel Error.Individual W/Radio Communication Will Be posted.W/830624 Ltr ML20024A8401983-06-21021 June 1983 LER 83-082/01T-0:on 830607,main Turbine Trip on High Reactor Pressure Vessel Level Bypassed to Clear Interlock.After Outage,Bypass Discovered Still Installed.Caused by Lack of Clear Requirement for Bypass review.W/830621 Ltr ML20024A3301983-05-27027 May 1983 LER 83-075/01T-0:on 830515,found Chlorine Detectors on Control Room Emergency Outside Air Supply May Prevent Operation in Pressurization Mode Following Loss of Power. Emergency Operation Procedures revised.W/830527 Ltr ML20024A3421983-05-27027 May 1983 LER 83-070/01T-0:on 830517,flow Rates Required to Maintain Positive Pressure in Control Structure Appeared to Exceed Tech Spec Limits.Flow Limit Inadvertently Omitted from Procedure.Procedure corrected.W/830527 Ltr ML20024A5331983-05-27027 May 1983 LER 83-067/01T-0:on 830516,reactor Mode Switch Placed in Startup Position & Half Scram Developed.Caused by Improper Functioning of Reactor Mode Switch Contacts.Switch Replaced. W/830527 Ltr ML20023D5121983-05-11011 May 1983 LER 83-063/03L-0:on 830411,main Steam Line Drain Valve Leakage Exceeded Tech Spec Limit.Cause Not Stated.Seal Ring Replaced,Outboard Valve Lapped & Valves Reassembled ML20023B8381983-04-29029 April 1983 LER 83-057/01P-0:confirms 830428 Telcon Re Incident Concerning Bypass Leakage Calculations for Feedwater Following DBA LOCA ML20028D6871983-01-10010 January 1983 LER 83-001/01P-0:confirms 830107 Telcon Re Failure to Comply W/Action Statement Requiring Grab Samples of Offgas Sys After Declaring One Train of Hydrogen Monitor Inoperable. Caused by Inadequate Shift Turnover in Chemistry Dept ML20028D3141983-01-0707 January 1983 LER 82-072/03L-0:on 821210,while Performing Surveillance, One Control Rod Would Not Indicate at One Position.Possibly Caused by Intermittent Fault on Circuit Board.Printed Circuit Board Reinstalled ML20028D2871983-01-0606 January 1983 LER 82-069/03L-0:on 821207,during Startup Testing,Hpci Sys Declared Operable Prior to Closing Out Open Equipment Release Form.Caused by Work Program Design Weakness.Present Work Practice Modified ML20028B5821982-11-19019 November 1982 Revised LER 82-026/01T-1:on 820717,review Revealed Certain Cables Discussed in Deficiency Rept 80-00-28 Not Flexed or Grounded Prior to Fuel Load.Caused by Failure to Maintain Control Over Fddr KRI-607 During Turnover of Const ML20028B0301982-11-18018 November 1982 LER 82-042/01T-0:on 821117,personnel Failed to Take Grab Samples When RHR Svc Water Sys Radiation Monitor Was Inoperable ML20028B4351982-11-18018 November 1982 LER 82-043/01T-0:on 821117,determined That Failure of Single Component Could Defeat Overload Detection & Protection Devices for Containment Penetration Carrying Power Cables for Reactor Recirculation Pumps.Cause Not Stated ML20028A9541982-11-16016 November 1982 LER 82-040/03L-0:on 821018,deluge Sys in CREOASS Initiated. Caused by Maint Personnel Bumping Fire Sys thermo-switch on Charcoal Beds.Charcoal Changed Out & Preventive Maint Procedures Modified to Valve Out Deluge Sys During Maint ML17139B0311982-09-13013 September 1982 LER 82-013/03L-0:on 820814,radiation Monitor Found Inoperable.Caused by Faulty Gm Tube & Signal Conditioner (Sensor Converter).Tube & Signal Conditioner Replaced & Monitor Returned to Svc ML20027B0571982-09-0808 September 1982 LER 82-007/01T-1:on 820825,updated Secondary Containment Vol Calculation Had Not Replaced Preliminary Analysis Utilized to Obtain Values in Fsar.Vol Based on Preliminary Calculation Which Did Not Account for Floors & Equipment ML17139A9071982-08-0202 August 1982 LER 82-001/01T-0:on 820718,unacceptable Linear Indications Found by Radiograph of A-11 Weld.Cause Not Determined.Welds Repaired Per Approved Repair Program 1998-03-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML17146B1741999-08-0303 August 1999 GL 96-06 Risk Assessment for Sses. ML20206D3331999-04-27027 April 1999 SER of Individual Plant Examination of External Events Submittal on Susquehanna Steam Electric Station,Units 1 & 2. Staff Notes That Licensee IPEEE Complete with Regard to Info Requested by Suppl 4 to GL 88-20 ML20195B2381999-03-31031 March 1999 Redacted Version for 10CFR2.790 Request for Decommissioning Status Rept for Sses,Units 1 & 2 ML17164A8451998-10-31031 October 1998 SSES Unit 1 Tenth Refueling & Insp Outage ISI Outage Summary Rept. ML20236N6751998-07-0909 July 1998 Part 21 & Deficiency Rept Re Notification of Potential Safety Hazard from Breakage of Cast Iron Suction Heads in Apkd Type Pumps.Caused by Migration of Suction Head Journal Sleeve Along Lower End of Pump Shaft.Will Inspect Pumps ML20249B9791998-06-24024 June 1998 Safety Evaluation Supporting Amends 177 & 150 to Licenses NPF-14 & NPF-22,respectively ML20217Q4891998-04-21021 April 1998 Rev 1 to Draft LDCN 2482, FSAR Chapter 13.4 & FSAR Chapter 17.2 Changes to Support ITS Implementation ML18026A4931998-03-30030 March 1998 LER 97-007-01:on 971017,entry Into TS 3.0.3 Occurred to Allow Completion of Surveillance Testing of One Channel of Rbm.Caused by Failure of Components in LPRM Output to Rbm. Submitted TS Change Request to Extend LCO Action Statement ML18026A5401998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Susquehanna Steam Electric Station.W/980313 Ltr ML18026A4891997-11-17017 November 1997 LER 97-007-00:on 971017,TS 3.0.3 Entry Voluntarily Made. Caused by Inadequate Post Maint Testing Following Earlier Work Associated W/Components.Failed Components Repaired, Replaced & Testing Completed ML18017A2921997-10-28028 October 1997 1997 Nrc/Fema Observed Exercise. ML17158C1861997-06-0505 June 1997 Proceedings of Intl Topical Meeting on Advanced Reactors Safety Vol II, on 970601-05 ML20140A9661997-05-29029 May 1997 Part 21 Rept Re Ksv Emergency Diesel Generator Power Piston Failure.Caused by Jacket Water in Combustion Chamber. Recommends That Users Verify That Crown Thickness at Valve Cutout Be 100 Minimum ML18026A4781997-03-28028 March 1997 Rev 1 to Application of Anfb to ATRIUM-10 for Susquehanna Reloads. ML20137G6261997-03-25025 March 1997 Svcs Part 21 Rept Re Emergency Generators Installed at Zion Station Which Developed Significant Drop in Crankcase Lube Oil Level.Caused by Crack in Liner Wall,Allowing Jacket Water to Enter Chamber ML20155F7661996-07-25025 July 1996 Partially Deleted Job Number 739619-96, Investigation of E Diesel Breaker Misalignment ML20155F7491996-07-24024 July 1996 Independent Safety Evaluation Svcs Project Rept 3-96, Investigation of E Diesel Generator In-Operability Event ML20117G4641996-05-14014 May 1996 Part 21 Rept Re Cooper Bessemer Reciprocating Products,Div of Cooper Cameron Corp,Issued Ltr to Define Utils/Plants Containing Similar Equipment as Supplied on Cooper Bessemer Ksv & Enterprise Dsr EDGs ML18026A5961996-01-0202 January 1996 LER 95-013-00:on 951119,thermally Induced Pressure Locking of HPCI Valve Occurred Under Bonnet Pressure of 3,000-7,000 Psig.Damaged HPCI Injection Valve repaired.W/960102 Ltr ML20095K5181995-12-18018 December 1995 Safety Evaluation Supporting Amends 155 & 126 to Licenses NPF-14 & NPF-22,respectively ML18017A0511995-11-30030 November 1995 Monthly Operating Repts for Nov 1995 for SSES Units 1 & 2. W/951215 Ltr ML20092H7641995-08-31031 August 1995 Monthly Operating Repts for Aug 1995 for Susquehanna Ses ML17158A8771995-08-15015 August 1995 Exercise Manual. ML17158A8061995-07-14014 July 1995 Books 1 & 2 of ISI Outage Summary Rept SSES Unit 1 8th Refuel Outage. ML18017A0461995-07-0707 July 1995 LER 95-008-00:on 950609,shift Average Licensed Core Thermal Power Was Exceeded.Caused by Failed Instrumentation Drift. Repaired & Recalibrated Subject Instrumentation ML17164A6631995-04-11011 April 1995 Impact of Extending T-10 AOT from 3 to 7 Days. ML17164A5871995-01-31031 January 1995 Monthly Operating Repts for Jan 1995 for Susquehanna Ses ML18026A5351994-10-31031 October 1994 SSES Unit 1 & 2 MSIV Leakage Alternate Treatment Method Seismic Evaluation. W/One Oversize Drawing ML17158A4821994-08-23023 August 1994 ISI Outage Summary Rept Unit 2 6th Refueling Outage, Books 1 & 2 of 2 ML17158A2391994-04-0505 April 1994 Books 1 & 2 of SSES Unit 1 Seventh Refueling & Insp Outage ISI Outage Summary Rept. ML18017A2701993-12-31031 December 1993 PP&L Annual Rept 1993. ML17158A2651993-12-31031 December 1993 Allegheny Electric Cooperative,Inc Annual Rept 1993. ML17158A1631993-12-0909 December 1993 Remote Indication of Spent Fuel Pool Level & Temperature. ML18026A4281993-08-16016 August 1993 PP&L Response to NRC Concerns Re Loss of Spent Fuel Pool Cooling Following Loca,Sses,Units 1 & 2. ML18026A4261993-06-0909 June 1993 LER 90-007-01:on 900705,primary Power Supply to RPS a Power Distribution Panel Lost When One Electrical Protection Assembly (EPA) Breaker Tripped.Epa Logic Cards Reviewed & RPS Power Supply Will Be redesigned.W/930609 Ltr ML17157C2441993-02-28028 February 1993 Monthly Operating Rept for Feb 1993 for Susquehanna Steam Electric Station,Units 1 & 2 ML18017A2031993-02-0101 February 1993 Books 1 & 2 of Unit 2 Fifth Refueling & Insp Outage,Isi Outage Summary Rept. ML20044C2741993-01-31031 January 1993 Corrected Monthly Operating Rept for Jan 1993 for Susquehanna Steam Electric Station,Unit 2,consisting of Info on Unit Shutdowns & Power Reductions ML17157C3691992-12-31031 December 1992 PP&L Annual Rept 1992. ML20056C3941992-12-31031 December 1992 Allegheny Electric Cooperative,Inc Annual Rept 1992 ML18017A0421992-12-14014 December 1992 Suppl to 921127 Part 21 Rept Re High Air Concentration in Reactor Bldg Making Area Uninhabitable for Retrieving Air Filters,Per NUREG-0737,Item II.F.1.Util Current Position Re Fuel Pool Cooling Issues Contrary to Reg Guide 1.3 ML18026A2481992-11-27027 November 1992 Part 21 Rept Re Substantial Safety Hazard in Design of Facility for Loss of Normal Spent Fuel Pool Cooling ML18026A4231992-11-17017 November 1992 LER 92-016-00:on 920416,discovered That Existing Analysis for Two Spent Fuel Storage Pools Did Not Reflect Current Fuel Design & Plant Operation.Caused by Failure to Modify FSAR Analysis.Fsar Will Be revised.W/921117 Ltr ML17157C1421992-10-21021 October 1992 Engineering Assessment of Fuel Pool Cooling Piping EDR-G20020. ML17157C1411992-08-31031 August 1992 Loss of Fuel Pool Cooling Event Evaluation. ML17157C1401992-08-31031 August 1992 Review of Fuel Pool Cooling During Postulated Off-Normal & Accident Events SSES Units 1 & 2. ML20082C4941992-08-14014 August 1992 Evaluation of Unit 1 & Unit 2 Derating of Power Cables in Raceways Wrapped W/Thermo-Lag Matl ML17157C1381992-07-27027 July 1992 Safety Consequences of Boiling Spent Fuel Pool at Susquehanna Steam Electric Station. ML17157B9331992-07-24024 July 1992 Sixth Refueling & Insp Outage Inservice Insp Outage Summary Rept, Books 1 & 2 1999-09-30
[Table view] |
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~ ACCELE D DOCUlVHKNT DISTQISUTION SYSTEM REGUL - RY INFORMATION DISTRIBUTIu.< SYSTEM (RIDS)
ACCESSION NBR:9306150200 DOC.DATE: 93/06/09 NOTARIZED: NO DOCKET ¹ FACIL:50-368 Susquehanna Steam Electric Station, Unit 2, Pennsylva 05000388 AUTH. NAME AUTHOR AFFILIATION METER,J.J. Pennsylvania Power & Light Co.
STANLEY,H.G. Pennsylvania Power & Light Co.
RECIP . NAME RECIPIENT AFFILIATION
SUBJECT:
LER 90-007-01:on 900705,primary power supply to RPS A power distribution panel lost whrn one electrical protection assembly (EPA) breakers tripped.EPA logic cards reviewed &
RPS power supply will be redesigned.W/930609 ltr.
DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE:
TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
NOTES:
RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PDl-2 LA 1 1 PD1-2 PD 1 1 CLARK,'R 1 1 INTERNAL: ACNW 2 2 ACRS 2 2 AEOD/DOA 1 1 AEOD/DSP/TPAB 1 1 AEOD/ROAB/DSP 2 2 NRR/DE/EELB 1 1 NRR/DE/EMEB 1 1 NRR/DRCH/HHFB 1 1 NRR/DRCH/HICB 1 1 NRR/DRCH/HOLB 1 1 NRR/DRIL/RPEB 1 1 NRR/DRPW/OEAB 1 1 NRR/DRSS/PRPB 2 2 198R/~DSSA SPLB 1 1 NRR/DSSA/SRXB 1 1 REG FILE- 02 '1 1 RES/DSIR/EIB 1 1 GN1 FILE 01 1 1 EXTERNAL'G&G BRYCE g J ~ H 2 2 L ST LOBBY WARD 1 1 NRC PDR 1 1 NSIC MURPHYiG.A 1 1 NSIC POOREgW. 1 1 NUDOCS FULL TXT 1 1 NOTE TO ALL"RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTETH CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT. 504-2065) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!
FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 32 ENCL 32
- Pennsylvania Power 8 Light Company Two North Ninth Street ~ Allentown, PA 18101 ~ 215/ 7705151 June 9, 1993 U.S. Nuclear Regulatory Control Desk Commission'ocument Washington, DC 20555 SUSQUEHANNA STEAM ELECTRIC STATION LICENSEE EVENT REPORT 90-007.-01 FILE R41-2 PLAS 566 Docket No. 50-388 License No. NPF-22 Attached is Licensee Event Report 90-007-01 which is an update to LER 90-007-00. The event was determined reportable per 10CFR50.73(a)(2)(iv) in that unplanned actuations of Engineered Safety Features occurred due to the loss of the primary power supply to the Division 1 Reactor Protection System power distribution panel when one Electrical Protection Assembly breaker tripped.
'H.G.
~ltanley VP Nuclea Operations JJM/mjm cc: Mr. T. T. Martin Regional Administrator, Region I U.S. Nuclear Regulatory Commission 475 Allendale Road King of Prussia, PA 19406 Mr. G. S. Barber Sr. Resident Inspector U.S. Nuclear Regulatory Commission P.O. Box 35 Berwick, PA 18603-0035 X40nsa 9306150200 930609 PDR ADOCK 05000388 8 PDR
NRC FORM 386 V.S. NUCLEAR REGULATORY COMMISSION (64)9) APPAOVEO OMB NO. 31500104 EXPIRES: 4I30I92 ESTIMATED BURDEN PEA RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD L(CENSEE EVENT REPORT (LER) COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (P630), U.S. NUCLEAR REGVLATORY COMMISSION, WASHINGTON, DC 20565, AND TO THE PAPERWORK REDUCTION PROJECT (31500104), OFFICE OF MANAGEMENTAND BUDGET. WASHINGTON, OC 20503.
FACILITY NAME (I) DOCKET NUMBER (2) PAGE 3 S eharna Steam Electric Station Unit 2 p 5 p p p 3 8 81 DF TITLE (4)
ESF Actuations Doe to HPS EPA Breaker Spurious Trip EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8)
MONTH DAY YEAR YEAR ~< SSQVSNTIAL NVMSEA II8 Inslors MONTH tvVMSSII OAY YEAR FACILITYNAMES DOCKET NUMBER(SI 0 5 0 0 0 0 7 0 5 9 0 9 0 0 0 7 0 1 0 6 0 9 9 3 0 5 0 0 0 OPERATING THIS REPORT IS SUBMITTED PURSUANT T 0 THE RLOUIREMENTS OF 10 CFR (): IChectr one or more of the follovrlnpi (11 MODE (1) 20A02(S) 20.405(c) 50,73( ~ l(2) livl 73.71(II)
POWER 20A06 (4) (I ) (I) 50.38(cl(1) 60.73(el l2)(vl 73.71(c)
I EYEL 1 0 0 20A05 (4) (1) (6 I 50.38(cl(2) 60.73(s) l2)(vill OTHER ISpecily in Ahttrect helow end In Text, HRC Form 20A05(s)(1) liiil 50.73( ~ l(2)(i) 50.73(s) (2 H vi i i) (A) 366AI 20.405(s l(1) (Iv) 50.7 3(s) (2) (ii) 50.73(sl(2)(vii() (Bl 20A05(s) l1) (v) 50.73(s) (2) (iii) 50.73 (4) (2) (x I LICENSEE CONTACT FOR THIS LFR (12)
NAME TELEPHONE NUMBER AREA CODE J. J. Meter Powm Production Engineer COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBEO IN THIS REPORT (13) 717542-187 "IX X' r .%O.
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CAUSE SYSTEM COMPONENT TURER TO NPROS CAUSE SYSTEM COMPONENT TURER TO N)yv r 5 2 G 0 8 0 Y SUPPLEMENTAL REPORT EXPECTED (14) MONTH DAY YEAR EXPECTED SUBMISSION DATE I15I YES Ilf yet, complete EXPECTED SVBMISSIOH DA TEI X No ABSTRACT ILlmlt to f400 tpecer, I e., epproxlmetely fifteen sinpreepece typewritten Iinerl (18)
At 1633 on July 5, 1990, with the Unit operating at, 1004 power, the primary power supply to the "A" Reactor Protection System (RPS) power distribution panel was lost when one of its Electrical Protection .
Assembly (EPA) breakers tripped. This interruption caused the Reactor Water Cleanup system, and various other Primary Containment Isolation system components to isolate and the Standby Gas Treatment System and Control Room Emergency Outside Air Supply System to auto initiate.
plant systems and components functioned properly and as expected in All response to the event. No reactor parameters were affected and no Emergency Core Cooling Systems were actuated. EPA breaker was reset at 1640 and all isolation signals were reset byThe 1646. Full power operation of the unit continued without interruption. The cause of this EPA breaker trip as well as others at the Station have been investigated.
In general, the majority of the EPA breaker trips have been linked to a failure/anomaly of an electrical subcomponent on the EPA logic card.
Logic cards have undergone subcomponent lifetime upgrades and other RPS power supply components have been cleaned, inspected and optimized. The long term action is to modify the RPS supply systems such that the latest version of EPA logic cards willpower replace the existing models and forced cooling to the EPA cards will be provided.
NRC Form 366 (669)
(6+9)'.S.
NRC FORM 366A LICENSEE EVENT REPORT (LER)
NUCLEAR REGULATOAY COMMISSION APPROVED OMB NO. 31500104 EXP IR ESI 4/30/92 ESTIMATED BURDEN PER AESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (F430). U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (31500104), OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2)
LER NUMBER (6) PAGE (3)
YEAR SLS< SEQUENTIAL REVISION
%M NUMSER NUMSER Unit 2 Su ehanna Steam Electric Station TEXT /I/ mom Spoco /4 ntqu/Iud, uoo oddldooo//VRC FomI 36M'4/ () 7) 38890 007 0102 oF 0 5 DESCRIPTION OF EVENT At 1633 on July 5, 1990 with the Unit operating at 1004 power, the primary power supply to the "A" Reactor Protection System (RPS; EIIS Code: JC) power distribution panel 2Y201A was lost when one of its Electrical Protection Assembly (EPA) breakers, 2CB-S003A-C, tripped. This power interruption resulted in Primary Containment Isolation System (EIIS Code: JM) actuations and automatic system initiations. RPS as well as other plant systems functioned as designed in response to the event. The major actuations were as follows:
- 1) Reactor Building Isolated.
HVAC (EIIS Code: VA) Zones II and III
- 2) Reactor Water Cleanup System (EIIS Code: CE) inboard isolation valve closed.
- 3) Cooling water isolation valves to the Reactor Recirc Pumps closed (EIIS Code: CC).
- 4) "A" Standby Gas Treatment System (EIIS Code: BH) auto initiated.
- 5) "A" Control Room Emergency Outside Air Supply System (EIIS Code: BH) auto initiated.
The EPA breaker was reset at 1640, all reset by 1646, and all affected systems isolation were subsequently signals were restored. Full power operations of the Unit continued without interruption.
CAUSE OF EVENT The loss of power to the "A" RPS bus was due to an unexpected trip of the downstream primary power supply EPA breaker. The EPA logic cards monitor RPS power for conditions of undervoltage, and underfrequency and trip the EPAovervoltage, breakers when these conditions exist or when the logic card fails. EPA breakers are in series and the trip of either breaker will interrupt power to the distribution panel.
The cause of this EPA breaker trip as well as others at the Station have been investigated. In general, the majority of the EPA breaker trips at the station have been linked to a failure/anomaly of an electrical subcomponent on the EPA logic NRC F oRR 366A (64)9)
NRC FORM SSSA V.S. NUCLEAR REGULATORY COMMISSION (609( APPROVED OMB NO. 31500104 EXPIRFSI 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE EVENT REPORT ILER) INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (PJ)30), U.S, NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (31500(04), OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, OC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) (.ER NUMBER (6) PAGE (3)
SEQUENTIAL ~?' REVISION YEAR @( NUMBER '.~ NUMBER Unit 2 Susquehanna Steam Electric Station TEXT ///moIP 4F444/4 IRTII/IPd, II44 Pddir4IIM//VRC FamI 3SS/(3/ (12) o s o o o 3 8 8 9 0 0 0 7 0 l 0 3 op 05 card. A subcomponent failure such as a capacitor or a transistor would cause the logic card to fail and subsequently trip the EPA breaker.
Contributing factors to subcomponent failures were increasing subcomponent age and higher than optimum temperature of the subcomponent environment. As a subcomponent life increases, particularly capacitors, the EPA cards with subcomponents become less reliable and eventually fails. This "aging" process was found to be applicable when the EPA logic card was both in service and in storage. The higher the temperature a subcomponent is subjected to, the shorter its reliable life becomes. In May of 1991 a task team was formed to address the reliability of the RPS power supply systems at the Station.
Prior to the task team being formed and reaching its conclusions, logic cards that experienced a trip were not examined on a subcomponent basis. Failed logic cards were typically returned to the manufacturer for analysis. The manufacturer would then replace the subcomponent(s) that failed. The card would then be returned and either put into service or stored for future use.
In both instances the logic cards contained both new and used subcomponents. The temperature of the EPA. logic card environment was found to be greater than optimum. The ambient room temperature were EPA cards are located was near 90 degrees F. In addition the EPA cards were mounted in a sealed junction box which further increased subcomponent temperature.
CORRECTIVE ACTIONS As described above, in May of 1991 a task team was formed to address the reliability of the RPS power supply systems at the Station. Two main objectives were established. The first objective was short term and was to reduce the number of spurious RPS power supply trips by enhancing and better maintaining the components in the present systems. The second was long term and was to reduce spurious RPS power supply trips and increase reliability via the modification process.
In the short term, EPA logic cards were reviewed on an individual basis and subcomponents lifetime upgrades were performed so that each card could be reasonably expected not to fail within a five year lifetime. The junction boxes that house the EPA logic cards were equipped with ventilation louvers thereby reducing the ambient temperatures for the logic card subcomponents. Other short term actions included cleaning, inspecting and optimizing performance of RPS power supply components such as motor-NRC Form 366A (BBS)
NAC FORM &$6A U.S. NUCLEAR REGULATORY COMMISSION APPROVEO OMB NO. 31500104 (6P9)'
EXPIRES: 4/30/92
'ESTIMATED BURDEN PEA RESPONSE TO COMP(.Y WTH THIS LICENSEE EVENT REPORT (LER) INFOAMATION COLLECTION REOUEST: 500 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (P4)30), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, OC 20555. ANO TO THE PAPERWORK REDUCTION PROJECT (3)504)104). OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, OC 20503.
FACILITY NAME (I) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)
+~+ SEQUENTIAL 3'P REVISION YEAR NUMBER '- NUMBER Unit Susquehanna 2
Steam Electric Station TEXT /// more eoece /4 rerler)ed. Iree odd/I/one/NRC Form 3664'4/ (IT) 60o03890 007 01 0 4 oF 0 5, generator sets, regulating transformers, relays and connection panels.
The long term corrective action was to develop an RPS power supply modification that reduced spurious trips and increased reliability. After extensive analysis, modifications have been designed for the RPS power supply systems. The redesigned RPS power supply will utilize an improved version of EPA logic cards in lieu of the existing models and forced cooling to the EPA enclosures will be provided.
REPORTABILITY ANALYSIS This event. was determined to be reportable under 10CFR50.73(a)(2)(iv) in that unplanned actuations of Engineered Safety Features (ESF) occurred when the RPS EPA breaker tripped.
Since all ESF systems and components functioned properly and per design, there were no safety consequences or compromises to the health or safety of the public.
Had this event occurred with the Unit in cold shutdown or refueling, the safety significance would have been greater due to the fact that shutdown cooling could have been temporarily lost.
Even under these conditions the safety significance would be minimal since the plant is more than adequately designed to safely handle this type of event.
In accordance with the guidance provided in NUREG 1022 Supplement 1 items 14.1 and 14.10, the original submission date for this report was 8-6-90. No further updates to this report are expected.
ADDITIONAL INFORMATION Failed Component Information:
Component EPA Logic Card Model 147D8652 G001 & G003 Manufacturer General Electric A review of past Licensee Event Reports (LERs) for the station identified twelve other events where EPA breakers trips resulted in ESF actuations.
NRC Form 366A (669)
NRC FORM 366A
(&BI()
l LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION U.S. NUCLEAR AEGULATOAYCOMMISSION APPAOVED OMB NO. 31500104 EXP IR ESI 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFOAMATION COLLECTION REQUEST: 505) HAS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH IP.530), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO 1HE PAPERWOAK REDUCTION PROJECT (31500)04). OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUMBER (21 LER NUMBER (6) PAGE (3)
SEQUENTIAL v~~ REVISION YEAR g> NUMSER NUMBER Unit 2 S ehanna Steam Electric Station o s o o o 3 8 8 9 0 0 0 7 0105 OF 0 5:
TEXT /ffmoro Snooo ir ooqo/rod, Irro odd/)/ono/HRC Form 36(/4'4/(11)
UNIT 1 (Docket No. 50-387/License No. NPF-14)
LER 92-007 LER 87-024 LER 92-001 LER 86-029 LER 91-006 LER 86-023 LER 91-004 LER 83-172 LER 90-005 UNIT 2 (Docket No. 50-388/Licensee No. NPF-22)
LER 91-008 LER 91-007 LER 88-005 NRC Form 366A (BBB)