ML20108B561

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Part 21 Rept Re Defective Engine Used for Driving Standby Power Generator at Facility.Caused by Loosened Attachments Separating Piston from Rod.Engine Will Be Repaired Prior to Installation
ML20108B561
Person / Time
Site: Susquehanna  Talen Energy icon.png
Issue date: 03/04/1985
From: Stolba F
COOPER INDUSTRIES, INC.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE)
References
REF-PT21-85-129-000 PT21-85-129, PT21-85-129-000, NUDOCS 8503070373
Download: ML20108B561 (2)


Text

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N dOOPER BESSEMER RECIPROCATING F. Bruce Stolba gy s-- - .~ v n m

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March 4, 1985 _

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Office of Inspection and Enforcement -6 g tl.S. Nuclear Regulatory Commission - z--

Washington, D.C. 20555 >M

M ATTENTION: Director of Inspection and Enforcement =dC _-

Gentlemen: M q -

In accordance with the requirements of the Nuclear Regulatory Commission ,

rules, and in particular 10CFR21, we wish to advise you of an incident g involving one of our engines used for driving a standby power generator. -

I was advised of this situation on Saturday, March 2, 1985. __

The engine in question is known as a KSV-20. The twenty cylinders of .

this diesel engine have a bore of 13.5 inches and a stroke of 16.5 inches.

It is pure turbocharged and rated at 5,000 KW at 600 RPM. It bears the _

serial number 7218. A Serial number 7218 was built in our Grove City, Pennsylvania plant and shipped to the Power Systems Division of Morrison Knudsen in Rocky Mount, North Carolina at the end of May,1984. The engine passed a routine test prior to shipment. The purpose for shipment to Rocky Mount was to allow ,

Power Systems to complete the assembly of their standby generator. This included connection of the engine to the generator and associated systems, -

and performing a series of acceptance tests. Ultimately the standby generator is to be shipped to the Susquehanna Steam Electric Station Plant of the Pennsylvania Light and Power Company at Berwick, Pennsylvania. It was during one of the test runs that a damaging incident occurred. ..

On February 26, 1985 the engine had been running for about four hours - - -

when the number six piston on the right t;dnk separated from the connecting -

_1 rod. Secondary damage occurred to the cylinder block, cylinder head, piston rod and some other parts adjacent to or part of the six right -

location. There was minor damage in evidence to control systems.

A preliminary investigation into the cause for separation of the piston

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' q-from the rod indicates that the attachments were loose or loosened. We M-are continuing to investigate all aspects of this circumstance. _.

The corrective action we propose, and which is under way, is to repair the m-engine so that it may be delivered to Berwick, Pennsylvania for installation. -

8503070373 850304 PDR ADOCK 05000387

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Page' Two March 4, 1985 Caref t.1 attention to design detail followed by years of experience attest to the fact that this is a unique incident. There is no advice or recommendation pertinent to this situation that would be of value to Therefore, we will not be other users of the nuclear standby KSV engine. .

contacting directly any Utility where KSV engines are installed. In the case of Pennsylvania Light and Power Company, any communication will be through our immediate Customer, Power Systems, a Morrison Knudsen Division .

in Rocky Mount, North Carolina.

Sincerely, b b% Nttw _

F. Bruce Stolba cc: J.W. Winstead, Manager, Purchasing, Power Systems

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